05000251/LER-1978-013-03, /03L-0:on 780929,condensate Storage Tank Held Less than 185,000 Gallons for About 8 H.Caused by Leaks in Condenser Tubes,Necessitating Increased Steam Generator Blowdown.Flow Demand Exceeded Output of Treatment Plant

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/03L-0:on 780929,condensate Storage Tank Held Less than 185,000 Gallons for About 8 H.Caused by Leaks in Condenser Tubes,Necessitating Increased Steam Generator Blowdown.Flow Demand Exceeded Output of Treatment Plant
ML17338A262
Person / Time
Site: Turkey Point 
Issue date: 10/27/1978
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
Shared Package
ML17338A261 List:
References
LER-78-013-03L-01, LER-78-13-3L-1, NUDOCS 7811060163
Download: ML17338A262 (2)


LER-1978-013, /03L-0:on 780929,condensate Storage Tank Held Less than 185,000 Gallons for About 8 H.Caused by Leaks in Condenser Tubes,Necessitating Increased Steam Generator Blowdown.Flow Demand Exceeded Output of Treatment Plant
Event date:
Report date:
2511978013R03 - NRC Website

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!5 AS!QAT OATS Cp EVENT DESCRIPTION ANO IRROBABLS CONSECUE NCS S QIO For a eriod of about 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> durin unit startup, the Condensate Storage T nI

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CST contained less than the 185 000 allons required by T.S. 3.8.l.c.

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and safet was not affected.

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Durin unit startu condenser tube leaks necessitated increasing steam ow own flow.

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out ut of the water treatment lant and led to CST level decreasin to less than the T.S. 3.8.1.c limit.

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