05000251/LER-1978-009-03, /03L-0 on 780831:20 Safety Related Hydraulic Snubbers Failed Functional Tests Due to Control Block Poppet Valve & Relief Valve Malfunctions & Excessive Main Cylinder Wear.Hydraulic Type Replaced W/Mechanical Type Snubbers

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/03L-0 on 780831:20 Safety Related Hydraulic Snubbers Failed Functional Tests Due to Control Block Poppet Valve & Relief Valve Malfunctions & Excessive Main Cylinder Wear.Hydraulic Type Replaced W/Mechanical Type Snubbers
ML17338A204
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 09/30/1978
From: Schoppman M
FLORIDA POWER & LIGHT CO.
To:
Shared Package
ML17338A200 List:
References
LER-78-009-03L-01, LER-78-9-3L-1, NUDOCS 7810120052
Download: ML17338A204 (2)


LER-1978-009, /03L-0 on 780831:20 Safety Related Hydraulic Snubbers Failed Functional Tests Due to Control Block Poppet Valve & Relief Valve Malfunctions & Excessive Main Cylinder Wear.Hydraulic Type Replaced W/Mechanical Type Snubbers
Event date:
Report date:
2511978009R03 - NRC Website

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