ML17331A528

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LER 80-035/03L-0:on 801206,rod Position Identification for Control Rod N-9 Did Not Respond Properly.Caused by Connector on Top of Rod Position Detector Assembly That Appeared to Have Been Stepped On.Cable Replaced
ML17331A528
Person / Time
Site: Cook American Electric Power icon.png
Issue date: 12/31/1980
From: Rischling J
INDIANA MICHIGAN POWER CO. (FORMERLY INDIANA & MICHIG
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17331A527 List:
References
LER-80-035-03L, LER-80-35-3L, NUDOCS 8101080397
Download: ML17331A528 (1)


Text

NRC FORM 366

{7-77)

~01 CONTROL BLOCK:

M I D C C I

I LlCENSEE EVENT REPORT 0

6 Q1 0 03>>z i U. S. NUCLEAR REGULATORY COMMISSION (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 04~05 14 15 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 7 8 9 LICENSEE CODE CON'T

~0 7 8 soURGE ~LQB 0 60 61 5 0 0 0 DOCKET NUMBER 3 1 6 68 Q7 1 69 2 0 6 EVENT DATE 8 0 74 Q REPORT DATE 80 QB EVENT DESCRIPTION AND PROBABLE CONSEQUENCES Q10 WHILE PULLING SHUTDOWN CONTROL RODS IN P

~03 IDENTIFICATION FOR CONTROL ROD N-9 DID NOT RESPOND PROPERLY. THE REACTOR TRIP BREAKERS WERE OPENED. THIS EVENT WAS NON-CONSERVATIVE IN SP C

~05

~06

~OB 80 7 8 SYSTEM CAUSE CAUSE COMP. VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE 011 ~E 012 ~E 013 E L E c 0 N 04 LzJ 075 Lzf 20 0"

7 8 9 10 11 12 13 18 19 SEQUENTIAL OCCURRENCE REPORT REVISION 017 LER/RO "875 "7 ACTION FUTURE EVENT YEAf3

~80 21 22 EFFECT

~

23 SHUTDOWN

~03 24 REPORT NO.

5

'26

~W 27

~03 28 ATTACHMENT CODE 29 NPRDX TYPE

~L 30 PRIME COMP.

31 NO.

32 0

COMPONENT TAKEN ACTION ON PLANT METHOD HOURS Q22 SUBMITTED FORM SUB. SUPPLIER MANUFACTURER

~A078 ~Z018 ~0025 +B027 0 0 0 7 +N023 ~Y024 ~Z025 X 5 5 5 ps 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q27 o THE PROBLEM WAS TRACED TO A CONNECTOR ON TOP OF THE ROD POSITION DETEC 0 ASSEMB Y.

THE CONNECTOR APPEARED TO HAVE BEEN STEPPED ON. A SP R ORIGINAL AND ROD POSITION INDICATION FOR ROD N-9 WAS DECLARED OPERABLE.

3 80 7 8 9 FACILITY STATUS  % POWER OTHER STATUS. Q METHOD OF DISCOVERY DISCOVERY DESCRIPTION Q32

~ls 8 9 fC 028 ~00 10 0

12 Psg 13 NA 44 45 B Q3'PERATOR OBSERVATION 46 80 7

ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITY 35 Q LOCATION OF RELEASE Q PZQ8 7 9 zQ zs 10 11 NA 44 45 NA 80 PERSONNFL EXPOSURES NUMBER TYPE DESCRIPTION Q39 7

7 8

~00 9

0 037 Z 038 11 12 13 NA 80 PERSONNEL INJURIES NUMBER DESCRIPTIONQ41

~78 LOOOOJ 045 NA 80 7 8 9 11 12 LOSS OF OR DAMAGE TO FACILITY 43 TYPE DESCRIPTION

~e Z P42 NA o o s 80 7 8 9 10 PU 8 L I CITY NRC USE ONLY ISSUED DESCRIPTION KZ L~JQ 7 8 9 10 NA 68 69 804 g 2

465- 0 NAME OF PREPARER JBCk L Rl SChl lng PHQNE 616