L-83-248, Application for Amend to License NPF-16 Revising Requirements for Both Primary & Secondary Coolants in Steam Generator Pressure/Temp Limits & Neutron Flux Monitor Surveillance

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Application for Amend to License NPF-16 Revising Requirements for Both Primary & Secondary Coolants in Steam Generator Pressure/Temp Limits & Neutron Flux Monitor Surveillance
ML17301A034
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 04/20/1983
From: Robert E. Uhrig
FLORIDA POWER & LIGHT CO.
To: Eisenhut D
Office of Nuclear Reactor Regulation
Shared Package
ML17213B292 List:
References
L-83-248, NUDOCS 8304220165
Download: ML17301A034 (7)


Text

REGULATORY ORMATION DISTRIBUTION SYS 4 (RIDS)

ACCESSION NBR:8304220165 DOC,DATE: 83/04/20 NOTARIZED:

YES FACIL:50 389 'St ~ Lucie Planti Uni!t 2i Florida Power L Light Co.

AUTH,NAME AUTHOR AFFILIATION UHRIGiR,Ee Flor ida IPower L Light Co,

'EC IP ~ NAME RECIPIENT AFFILIATION EISENHUTiDoG Division of Licensing

SUBJECT:

Application for amend to License NPF 16 revising requirements for bath primary L secondary coolantjs in steam generator pressure/temp limi,tation 8, neutron flux monitor isurveillance.

DOCKET 05000389

,DISTRIBUTION 'CODE! 8001S

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NRR/DHFS/LQB 32'RR/DS I/AEB 26 NRR/DSI/CPS 10 NRR/DSI/ICSB 16 NRR/DSI/PSB 19 NRR/DS I/RSB 23 RGN2 EXTERNAI i ACRS 41 DMB/DSS (AMDTS)

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igllgg FLORIDAPOWER & LIGHT COMPANY April 20, l983 L-83-248 Office of Nuclear Reactor Regulation Attention:

Mr. Darrell G. Eisenhut, Director Division of Licensing U.

S. Nuclear Regulatory Commission Washington, D.

C.

20555

Dear Mr. Eisenhut:

Re:

St. Lucie Unit 2 Docket No.

50-389 Proposed License Amendment Steam Generator Pressure/Temperature Limitation and Neutron Flux Monitor Surveillance In accordance with 10 CFR 50.90, Florida Power 8 Light Company submits herewith three signed originals and forty copies of a request to amend Appendix A of Facility Operating License NPF-16.

This amendment is submitted to revise the requirement for both primary and secondary coolants in the steam generator to be greater than 100'F when the pressure ih either coolant is greater than 275 psig.

This change is necessary to allow heat up of the primary coolant with the Reactor Coolant Pumps.

Also submitted is a change to the channel functional test surveillance requirements for the Wide Range Logarithmic Neutron Flux Monitor.

As discussed in paragraph 7.2.1.1.2.2.1 of the St. Lucie Unit 2 FSAR, the signals for these channels ccme from fission chamber detectors.

As discussed with your staff on April 19, 1983, the preparation of detector plateau

curves, which are presently required, cannot be acccmplished with the installed equipment.

The proposed amendment is described below and shown on the acccmpanying Technical Specification pages.

Page 3/4 7-12 Revise Section 3.7.2 to apply only to the secondary coolant in the steam generator.

Page 3/4 3-9, 10

'he once per 18-month channel functional test for the Wide Range Logarithmic Neutron Flux Monitor and the associated footnote are removed as discussed above.

pe,at 8304220ih5 830420 PDR ADOCK 05000389 P

PDR PEOPLE... SERVING PEOPLE

0 Office of Nuclear Reac or Regulation Attention:

Mr. Oarrell G. Eisenhut Page 2

The proposed amendment has, been revi ewed by the St. Luci e Facility Review Group and the Florida Power 8 Light Ccepany Nuclear Review Board.

Very truly yours, Robert E. Uhrig Vice President Advanced Systems

& Technology REU/JEM/js Attachment cc:

J.

P. O'Reilly, Region II Harold F.

Rei s, Esquire

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U.S. NUCLEAR REGULATORY COMMISSION I, FEE FORM TYPETChecx one(

REACTOR FACILITYFEE DETERMINATION INSTRUCTIONS. Fawn hams I lhrougn Ia. ae applicable, and send the onginal copy Io lhe License Fee Management Branch.

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10. TADNUMBERAssIGNEDfffavaflaofef D/86'ATE OF ISSUANCE
11. APPROVAI.
12. NRC FEE DETERMINATION The above application has been reviewed In accordance with Section 170 22 of Part 170 and ls properly categorized.

The above application has beeregtbffewed In accordance with Section 170.22 of Part 170 and is incorrectly classitied.

Fee should be class(es):

JUSTIFICATION FOR CLASSIFICATIONOR R ECLASSIFICATION:

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6. DATE OF APPLICATION
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11. APPROVAL LET1ER ORDER AMENDMENTNUMSErerar

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DATE OF ISSUANCE 9/s~jrx The above application has been reviewed In accordance with Section 170.22 of part 170 and ls properly categorized.

The above application has been reviewed In accordance with Section 170.22 of Part 170 and Is Incorrectly classified.

Fee should be class(esi: ~

JUSTIFICATION FOR CLASSIFICATIONOR RECLASSIFICATION:

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Filed by a nonprofit educational Institution.

Filed by a Government agency and Is not fora power reactor.

For a Class I. II. or III amendment which results from an NRC request dated for the application and the amendment Is to simplify or clarify License or Technical Specifications: has only minor safety significance: and Is being Issued lor.the convenience of NRC fmust meet ell of lhe crileriei.

Other fSlele reason lhereiofi

13. SIGNA'TU RE f8ranch Chfeff PATE Ia. FINALcERTIFI Iorl: the praiimmary lee Dererminartonna beeniaassessed and Is hereby afhrmeo, SIGNATURE( rofecr anagerorerancn hfeff ga FOR LICENSE FEE MANAGEMENTBRANCH USE ONLYfAffothers do nol write below this linei'he above exemption request has been reviewed and Is iiaraby accepted as being exempt.

SIGNATURElChiaf. LFMBf DATE j~y'a.r 'tfftj DATE Records Services Brancn DL Branch Chiel, DISTRIBUTIONBY LFMB LFMBExemption File LFM8 Reactor Flic

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