NL-03-069, Steam Generator Tube Inspection - Technical Specification 5.6.8 Report on Tubes Plugged

From kanterella
(Redirected from ML031200250)
Jump to navigation Jump to search
Steam Generator Tube Inspection - Technical Specification 5.6.8 Report on Tubes Plugged
ML031200250
Person / Time
Site: Indian Point Entergy icon.png
Issue date: 04/25/2003
From: Dacimo F
Entergy Nuclear Northeast
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
NL-03-069
Download: ML031200250 (2)


Text

Entergy Nuclear Northeast Indian Point Energy Center 295 Broadway, Suite 1 PRO. Box 249 tnIile Buchanan, NY 10511-0249 Entffl Tel 914 734 5340 Fax 914 734 5718 Fred Dacimo Vice President, Operations April 25, 2003 NL-03-069 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Stop O-Pl-17 Washington, D.C. 20555

Subject:

Indian Point 3 Nuclear Power Plant Docket No. 50-286 License No. DPR-64 Steam Generator Tube Inspection -Technical Specification 5.6.8 Report On Tubes Plugged

Dear Sir:

Entergy Nuclear Operations, Inc. (ENO) is reporting, pursuant to Technical Specification 5.6.8, the Steam Generator (SG) tubes plugged following the Refuel Outage 12 Inservice Inspection (0SI) of SG at Indian Point 3 Nuclear Power Plant. The ISI, completed April 12, 2003, identified twelve tubes that were plugged. The SG Tube Inspection Report will provide additional details on the extent of inspection, each indication of an imperfection, and plugging/repair. The following table identifies the indication (PVN is permeability variation and VOL is volumetric wear) and, where applicable, the through wall (TW) wear for the twelve tubes plugged:

SG Tube Location Indication Percent TW SG31 R28 C29

-4.96 to 5.04 PVN SG32 R41 C28 TSH +0.15 VOL 34%

SG32 R40 C29 TSH +0.0 VOL 32%

SG32 R41 C29 TSH +0.05 VOL 24%

SG32 RI C85 TSH +16.70 VOL 23%

SG32 RI C9 TSC +16.01 VOL 20%

SG32 RI C66 TSC +18.16 VOL 28%

SG33 RI C66 TSH +15.62 VOL 47%

SG33 RI C27 TSH +18.04 VOL 32%

SG33 RI C27 TSC +17.86 VOL 26%

SG33 RI C8 TSC +16.51 VOL 20%

SG34 RI C8 TSH +16.69 VOL 24%

SG34 R1 C84 TSC +16.92 VOL 25%

b,4-7

Docket No. 50-286 NL-03-069 Page 2 of 2 There are no new commitments made by ENO in this submittal. If you have any questions regarding this submittal, please contact Mr. K. Kingsley at (914) 734-5581.

Very truly yours, R. Dacimo Vice President, Operations Indian Point Energy Center cc:

Regional Administrator U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Resident Inspectors Office Indian Point Unit 3 U.S. Nuclear Regulatory Commission 295 Broadway, Suite 3 P.O. Box 337 Buchanan, NY 10511-0308 Mr. Paul Eddy NYS Department of Public Service 3 Empire Plaza Albany, NY 12223 Mr. William M. Flynn New York State Energy Research and Development Authority Corporate Plaza West 286 Washington Avenue Extension Albany, NY 12203-6399 Mr. Patrick Milano, Project Manager Project Directorate I Division of Reactor Projects 1/l1 U.S. Nuclear Regulatory Commission Mail Stop 0-8C2 Washington, DC 20555