ML20023C296

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LER 83-027/03L-0:on 830408,during Valve Insp,Grease Discovered on Seats & Discs.Caused by Maint Procedures Not Prohibiting Personnel Placing Grease on Seat & Disc.Grease Removed,Valves Repaired & Procedures Will Be Revised
ML20023C296
Person / Time
Site: Dresden Constellation icon.png
Issue date: 05/05/1983
From: Stachniak R
COMMONWEALTH EDISON CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML20023C292 List:
References
LER-83-027-03L, LER-83-27-3L, NUDOCS 8305170163
Download: ML20023C296 (3)


Text

.. NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION

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j LICENSEE EVENT REPORT

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CONTROL CLOCK: l i

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Ih (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATIONI I o I .i l. l I I uCENSEE

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7 f 3 NU".98 ER EVENT OATE 74 75 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES h 10121l While performine an insnection of valves 2-201-1B. Ic_ in AO-7-1601 nnA i 1

< I o 13 ! I 2-220-58A 58B. ernase was discovered on each valve sear nna d4=c. T.nen1 lonk l

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l o 14 l I rate tests (LLRT's) nerformed before inanectinn nn=ned. T.T nT ' e narfn-aa a f ear I lo151I crease was removed failed excent for 2-220-5HA nnd 2-701-1R. Min in n 1 offoce I l lo is I l on Public health and safety since all second isolation valves on each line  ;

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a;7l l showed minimal leakage. First occurrence of this type. I 1 o la i ! I 7 as 80 SYSTE'A CAUSE CAUSE COMP.

CODE VALV E

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9 10 11 12 13 18 19 20 SEOU E NTI A L OCCURRENCE REPCRT REVISION LER RO EVENT YEAR REPORT NO, CODE TYPE NO.

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CAUSE CESCRIPTION AND CCARECTIVE ACTIONS h

{ liloll Maintenance procedures did not prohibit personnel from placine crease on valve l Iilii i seats. Crease was placed on valves to protect seat and disc surfaces durino

} I It i2Il repair. All grease was removed, valves repaired. and LLRT tested successfully. I

] lt #3l l dxistine procedures will be reviewed and revised. A trainine module on noe l liiAi l of lubricants and sealants will be develoned. I 7 3 9 90

$A *b P0WER OTHER STA TUS 01 O ERY DISCOVERY DESCRIPTION li 151 (,,G,j@ l 0l 0l Ol@l A TivtTY CO TENT N/A l d h! Recufred NRC Tnanecefon l RELEASEo OPREtEiSE v/4AMOu~T O, ACTIVITY @ n/3 I LOCATION OF RELEASE @

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  1. ERSONNEL EXPOSURES 1

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NAME OF PREPARER . ac M ak (815) 942-2920 x529 '

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ATTACHMENT TO LICENSEE EVENT REPORT #83-27/03L-0 m COMMONWEALTH EDISON COMPANY (CWE)

DRESDEN UNIT 2 (ILDRS-2)

DOCKET # 050-237 ,

During the scheduled refueling outage, Mechanical Maintenance personnel inspected the seating surfaces of main steam isolation valves (MSIV's) 2-203-1B, 1C, and ID as the result of an anonymous allegation made to the resident NRC inspector. All three valves had recently been repaired and successfully local leak rate tested. The valves were disassembled, inspected, and Dow Corning 111 grease was- found on the disc and seat of each valve. The seating surface and disc of each valve was cleaned, the valves re-assembled, and local leak rate tests were performed. Valve 203-1B passed the local leak rate test without any further maintenance. However, valves 203-1C and ID failed successive leak rate tests. The valves were disassembled again, the seats relapped, and the valves re-assembled.

When all maintenance was completed and the valves rebuilt, both valves passed local leak rate tests. After grease had been discovered on the seating surface of each ?$IV, a list of those valves in which the l

valve seat was exposed this outage and could have been potentially greased during maintenance or repair, was prepared. A total of twenty valves forming part of the primary containment isolation boundary, including the MSIV's, were identified. After the list had been studied, it was determined that there was reason to believe that three valves had greased seats (2-220-58A and 58B and 2-1601-61) . Additionally, a sample of three of the remaining valves believed to be . free of grease were selected for k inspection to verify the condition.

  1. The six additional valves were disassembled, inspected and grease was found as expected, on three of them. These were 2-220-58A and 58B and 2-1601-61.

The seating surface of the three greased valves were cleaned and all six valves were reassembled. All six valves except 2-220-58B were successfully local

] leak rate tested without further maintenance. Valve 2-220-58B was disassembled once again, the "0" ring seating surface between the valve seat assembly and the valve body was relapped, and the "0" ring replaced. When the valve was re-assembled, it was successfully local leak rate tested.

On April 11, 1983, shortly after grease had been discovered on the seating surface of the three MSIV's, members of the NRC Regional Staff were notified of the deficiency. As a result of a telephone conference call made between D. J. Scott and D. L. Farrar of Commonwealth Edison and C.E. Norelius and other members of the NRC Regional Staff, six action items j were agreed upon and later verified by a confirmatory action letter to 3

Mr. Cordell Reed from James G. Keppler, dated April 13, 1983. A summary of the six action items agreed upon are listed as follows:

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1. A review will be conducted of other isolation valves maintained during the current Unit 2 and the previous Unit 3 re-fueling outage. This review will be

' sufficiently comprehensive to eliminate concerns about the possible inappropriate use of grease during valves re-assemblies.

2. The Quality Control Department will review the event and develop standard inspection plans for isolation valve p maintenance requiring valve disassembly and re-assembly.
3. A tailgate on the event will be prepared and presented to Mechanical Maintenance supervision in order to emphasize the critical nature of the decision to use lubricants

. where not specifically addressed in the procedure.

4. Existing maintenance procedures dealing with assembly and disassembly of valves will be reviewed and revised as necessary to ensure appropriate precautions and controls are in place as regard to the use of lubricants and sealants.
5. A training module will be prepared and incorporated into the maintenance training program dealing with the subject of the correct use of lubricants and sealants in various maintenance activities, n
6. A repair manual will be developed specifically for disassembly and re-assembly of MSIV's. ,

In addition to the committment to complete the action items listed above, (j Commonwealth Edison performed an internal audit of the incident. A committee was formed to investigate the maintenance practice of using grease during the re-assembly of valves subject to post maintenance local leak rate tests.

(Ib The goal of the committee was to investigate the particular circumstances

[j involved in the usage of grease during the re-assembly of MSIV's t'

203-1B, 1C, and ID and also to address the broader question of the implication of the maintenance practice on other critical valves at l

Dresden Station. As a result of the investigation, it was determined that the motivation behind the use of lubricants and/or grease in the re-assembly of the MSIV's and other valves was not to intentially bias the

' results of any local leak rate test, but to assist in the re-assembly of large and sometimes difficult to maintain equipment. Tracking of the six l, action items will be done via the AIR System to ensure follow-up and i

completion.

l' This incident had no effect on public health and safety since the second L isolation valve for each line affected had minimal or no leakage. This was a first occurrence of this type.

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