ENS 55891
ENS Event | |
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18:59 May 10, 2022 | |
Title | Both Trains of LOW Pressure Coolant Injection (LPCI) Inop |
Event Description | The following information was provided by the licensee via fax:
At 1359 CDT on May 10, 2022, the 1B LPCI Loop Upstream Injection valve (1-1001-28B) was found to have a motor operated torque switch issue and inadequate lubrication. This issue called into question the ability of the valve to close when required. At 1746 CDT on May 10, 2022, both trains of Unit 1 LPCI were made simultaneously inoperable. TS 3.6.1.3 Condition A required de-activation of 1B LPCI Loop Downstream Injection valve (1-1001-29B) which was completed at 1746 CDT. Because of the de-activation of the 1B LPCI Loop downstream injection valve and LPCI Loop select logic, both trains of LPCI were made inoperable. Due to this inoperability, the system was in a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(V). Unit 1 HPCI and both loops of Core Spray are operable. After further engineering review, it was determined that 1B LPCI Loop Upstream injection valve condition was minor in nature and would not have affected the ability of the valve to close when required. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
The following information was provided by the licensee via phone call and email: The last sentence in the second paragraph, "After further engineering review, it was determined that 1B LPCI Loop Upstream injection valve condition was minor in nature and would not have affected the ability of the valve to close when required," has been deleted. The licensee is continuing to follow up on the issue and believes that sentence to be unclear and premature. Notified R3DO (Skokowski). |
Where | |
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Quad Cities Illinois (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat | |
Time - Person (Reporting Time:+4.72 h0.197 days <br />0.0281 weeks <br />0.00647 months <br />) | |
Opened: | Harlem - Eq Opr 23:42 May 10, 2022 |
NRC Officer: | Brian P. Smith |
Last Updated: | May 11, 2022 |
55891 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 558912022-05-10T18:59:00010 May 2022 18:59:00
[Table view]10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat Both Trains of LOW Pressure Coolant Injection (LPCI) Inop ENS 536932018-10-24T05:00:00024 October 2018 05:00:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(iv)(A), System Actuation 1/2 Edg Auto Started and Lpci/Core Spray Inoperable Due to Loss of Safety Bus ENS 415312005-03-28T01:30:00028 March 2005 01:30:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Electrical Safety Bus Trip During Quad Cities Unit 1 Refueling Outage ENS 413692005-02-04T00:19:0004 February 2005 00:19:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition 4160 Volt Relaying and Metering Single Failure Vulnerability 2022-05-10T18:59:00 | |