This 60-day optional telephone notification is being made in lieu of an LER submittal, as allowed by
10 CFR 50.73(a)(1). This notification is made pursuant to the reporting requirements specified in
10 CFR 50.73(a)(2)(iv)(A) for an invalid actuation of one of the systems listed in
10 CFR 50.73(a)(2)(iv)(B).
At 0946 hrs on December 1, 2020, with unit 2 in Mode 5 at 0% power, an invalid actuation of the Emergency Diesel Generators (EDG) 'A' and 'B', 'A' Residual Heat Removal (RHR) Pump, 'A' Service Water Booster Pump (SWBP), and Auxiliary Feed Water (AFW) Pumps 'A' and 'B' occurred. The actuation was caused by a Safety Injection (SI) signal while installing simulations to support Reactor Safeguards testing. The SI signal occurred when two out of three logic was met for Low Pressurizer Pressure, which was caused by a high resistance connection to a test point from a loose test lead.
All aligned equipment, 'A' and 'B' EDGs, 'A' RHR Pump, 'A' SWBP and 'A' and 'B' AFW Pumps, responded properly to the auto-start signal and the actuation was complete. The actuation was not initiated in response to actual plant conditions, it was not an intentional manual initiation, and there were no parameters satisfying the requirements for initiation of the system. Therefore, this event has been determined to be an invalid actuation.
There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector was notified.