ENS 54144
ENS Event | |
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00:00 May 10, 2019 | |
Title | 60 Day Optional Notification Due to Actuation of an Emergency Diesel Generator |
Event Description | This 60-day optional telephone notification is being made in lieu of an LER submittal, as allowed by 10 CFR 50.73(a)(1). This notification is made pursuant to the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) for an invalid actuation of one of the systems listed in 10 CFR 50.73(a)(2)(iv)(B).
At approximately 2000 EDT on May 9, 2019, an invalid actuation of emergency diesel generator (EDG) 1 occurred. At the time, EDG 1 was removed from service for planned maintenance. The invalid actuation occurred when the starting air clearance was being lifted while simultaneously performing a Post Maintenance Test (PMT) where an external DC power source was applied to a relay that provided continuity directly to the starting air solenoids. As a result, the air start solenoids were energized causing EDG 1 to start. EDG 1 started and functioned successfully. The actuation was complete; EDG 1 successfully started and ran unloaded. The actuation was not initiated in response to actual plant conditions, it was not an intentional manual initiation, and there were no parameters satisfying the requirements for initiation of the system. Therefore, this event has been determined to be an invalid actuation. This event did not result in any adverse impact to the health and safety of the public. The licensee has notified the NRC Resident Inspector. |
Where | |
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Brunswick North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1308.7 h54.529 days <br />7.79 weeks <br />1.793 months <br />) | |
Opened: | Stephen Yodersmith 12:42 Jul 3, 2019 |
NRC Officer: | Andrew Waugh |
Last Updated: | Jul 3, 2019 |
54144 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 569872024-01-02T04:33:0002 January 2024 04:33:00
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