ENS 50625: Difference between revisions

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| event date = 11/18/2014 19:00 CST
| event date = 11/18/2014 19:00 CST
| last update date = 11/19/2014
| last update date = 11/19/2014
| title = Unanalyzed Condition Due To All Four Safety Injection Accumulators Inoperable
| title = Unanalyzed Condition Due to All Four Safety Injection Accumulators Inoperable
| event text = Following shift turnover from days to nights on 11/18/2014, it was discovered that all (4) of the Safety Injection (SI) Accumulator Outlet Isolation Valve breakers were unlocked and closed.  At the time of discovery, 3 of the safety injection accumulator valves were open and 1 was closed for testing.  At that time the plant was in MODE 3 at normal operating pressure and temperature.  The plant had been performing RCS pressure isolation valve testing prior to shift turnover.  The condition was discovered during testing of valves associated with the 'C' safety injection accumulator.   
| event text = Following shift turnover from days to nights on 11/18/2014, it was discovered that all (4) of the Safety Injection (SI) Accumulator Outlet Isolation Valve breakers were unlocked and closed.  At the time of discovery, 3 of the safety injection accumulator valves were open and 1 was closed for testing.  At that time the plant was in MODE 3 at normal operating pressure and temperature.  The plant had been performing RCS pressure isolation valve testing prior to shift turnover.  The condition was discovered during testing of valves associated with the 'C' safety injection accumulator.   
After discovery of the condition, Operations directed that the 'A', 'B', and 'D' SI Accumulator Outlet Isolation Valve breakers be opened and locked.  This action was completed by approximately 1930 [CST] on 11/18/2014.
After discovery of the condition, Operations directed that the 'A', 'B', and 'D' SI Accumulator Outlet Isolation Valve breakers be opened and locked.  This action was completed by approximately 1930 [CST] on 11/18/2014.

Latest revision as of 21:49, 1 March 2018

ENS 50625 +/-
Where
Callaway Ameren icon.png
Missouri (NRC Region 4)
Reporting
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition

10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Time - Person (Reporting Time:+2.65 h0.11 days <br />0.0158 weeks <br />0.00363 months <br />)
Opened: Tim Holland
03:39 Nov 19, 2014
NRC Officer: Howie Crouch
Last Updated: Nov 19, 2014
50625 - NRC Website