| Site | Start date | Title | Description |
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ENS 57004 | Nine Mile Point | 4 March 2024 00:42:00 | Automatic Reactor Scram Due to Main Turbine Trip on LOW Condenser Vacuum | The following information was provided by the licensee via email:
On 3/3/24 at 1942 EST, while performing a plant shutdown in preparation for a refuel outage, Nine Mile Point Unit 2 experienced a reactor scram due to a main turbine trip on low condenser vacuum. The plant was at approximately 55 percent power at the time of the reactor scram.
Additionally, following the scram a low RPV (reactor pressure vessel) level scram and containment isolation signal on level 3 was received, as expected. The containment isolation signal impacted RHR (residual heat removal) shutdown cooling, RHR letdown to radwaste, and RHR sampling. All impacted valves were closed at the time the isolation occurred.
All control rods were fully inserted. Plant response was as expected. Post scram, the main turbine bypass valves are being used to control decay heat, and normal post scram level control is via the feed / condensate system.
This is being report under 10 CFR 50.72(b)(2)(iv)(B), 'RPS Actuation', and 10 CFR 50.72(b)(3)(iv)(A), 'Specified System Actuation'.
Unit 1 is not affected. There was no impact on the health and safety of the public or plant personnel.
The NRC Resident Inspector has been notified.
The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance:
The cause of the low condenser vacuum was a momentary loss of sealing steam. The condenser remained viable for decay heat removal. All safety equipment is available. The grid is stable with the plant in its normal shutdown electrical configuration. |
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