(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
6-29-2017 | On March 17, 2017, at approximately 1517 EDT, during refueling operations on Unit 1, power was being restored to the Open Phase system for the 1-B Reserve Auxiliary Transformer ( RAT). During restoration, a valid undervoltage actuation signal was sent to the 1-B Emergency Diesel Generator ( EDG). The EDG automatically started and tied to the safety bus.
This undervoltage condition was caused by a wiring error in the Open Phase system to the 1-B RAT.
Unit 1 was in Mode 6 at the time and remained so throughout the event. There was no change in the decay heat removal for the plant.
Because this event resulted in the automatic actuation of a system listed in 10 CFR 50.73(a)(2)(iv)(B), this event is reportable under 10 CFR 50.73(a)(2)(iv)(A). This event had no adverse effect on the health and safety of the public, and is of very low safety significance.
Unit 2 was unaffected. |
---|
LER-2017-002, Vice President
Vogtle Units 1-2
7821 River RD
Waynesboro GA, 30830
706-848-0004 tel
706-848-3321 fax
June 29, 2017
Docket No: 50-424 NL-17-1104
U.S. Nuclear Regulatory Commission
ATTN: Document Control Desk
Washington, D.C. 20555-0001
Vogtle Electric Generating Plant — Unit 1
Licensee Event Report 2017-002-01
Wiring Error results in Automatic Actuation of a Safety System
Ladies and Gentlemen:
In accordance with the requirements of 10 CFR 50.73(a)(2)(iv)(A), Southern Nuclear Operating
Company is submitting the enclosed Licensee Event Report, 2017-002-01 for Vogtle Electric
Generating Plant Unit 1. This letter contains no NRC commitments. If you have any questions,
please contact Dom Sutton at (706) 848-1428.
Respectfully sub
Darin J. M rs
Vice President — Plant ogtle Units 1&2 - SNC
DJM/KCW
Enclosure: Unit 1 Licensee Event Report 2017-002-01
Cc: Regional Administrator
NRR Project Manager — Vogtle 1 & 2
Senior Resident Inspector — Vogtle 1 & 2
RType: CVC7000
Vogtle Electric Generating Plant — Unit 1
Licensee Event Report 2017-002-01
Wiring Labeling Error results in Automatic Actuation of a Safety System
Enclosure
Unit 1 Licensee Event Report 2017-002-01
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION
(04-2017)
LICENSEE EVENT REPORT (LER) ILWa t
l,viricir (See Page 2 for required number of digits/charactersfor each block)
•••••••
(See NUREG-1022, R.3 for instruction and guidance for completing this form
http://www.nrc.qovireadincl-rmidoc-collections/nuregs/staff/sr1022/r3i)
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 0313112020
Estimated burden per response to comply with this mandatory collection request: 80 hours
Reported lessons learned are incorporated into the licensing process and fed back to industry
Send comments regarding burden estimate to the Information Services Branch (T-2 F43), US
Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Infocollects
Resource@nrc gov, and to the Desk Officer, Office of Information •and Regulatory Affairs,
NEOB-10202, (3150-0104), Office of Management and Budget, Washington. DC 20503. If a means
used to impose an information collection does not display a currently valid OMB control number,
the NRC may not conduct or sponsor, and a person is not required to respond to, the information
collection.
1. FACILITY NAME
Vogtle Electric Generating Plant
. DOCKET NUMBER 13. PAGE
17.:15000424 1 1 OF 2
4. TITLE
Mirina Error results in_AulomaticActuation_of a Safety System_Vogtle Electric Generating Plant |
Event date: |
3-17-2017 |
---|
Report date: |
6-29-2017 |
---|
Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(B), System Actuation
10 CFR 50.73(a)(2)(iv)(A), System Actuation |
---|
4242017002R01 - NRC Website |
|
|
---|
Category:Letter
MONTHYEARML24032A0252024-02-0505 February 2024 NRC Initial Test Program and Operational Programs Integrated Inspection Report 05200026-2023009 ML24010A0712024-01-31031 January 2024 Exemption from Select Requirements of 10 CFR Part 73 (Security Notifications, Reports and Recordkeeping and Suspicious Activity Reporting) ML24031A6102024-01-31031 January 2024 Cyber Security Inspection Report 05200026/2024401 - Public ML24029A0592024-01-30030 January 2024 Request for Withholding Information from Public Disclosure Responses to NRC Request for Additional Information for Refueling Outage 1R24 Steam Generator Tube Inspection Report Enclosure 2, GAE-NRCD-RF-LR-000002 P-Attachment, Rev. 0 ML24016A1132024-01-30030 January 2024 Correction of Unit 1 Amendment Nos. 96 and 190 and Unit 2 Amendment Nos. 74 and 173 Adoption of Standard Technical Specifications Westinghouse Plants NL-24-0031, Inservice Inspection Program Owner'S Activity Report (OAR-1) for Outage 2R232024-01-29029 January 2024 Inservice Inspection Program Owner'S Activity Report (OAR-1) for Outage 2R23 IR 05000424/20244032024-01-26026 January 2024 Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection 05000424/2024403; 05000425/2024403 NL-24-0020, Plan, Unit 1 Responses to NRC Request for Additional Information for Refueling Outage 1R24 Steam Generator Tube Inspection Report2024-01-22022 January 2024 Plan, Unit 1 Responses to NRC Request for Additional Information for Refueling Outage 1R24 Steam Generator Tube Inspection Report ML23347A2092024-01-17017 January 2024 Voluntary Requests for Data, Information, And/Or Observation ML23279A0042024-01-17017 January 2024 Amendment No. 194 to Remove Combined License Appendix C NL-23-0926, Correction of Technical Specification Typographical Error2024-01-12012 January 2024 Correction of Technical Specification Typographical Error ML23341A2042024-01-12012 January 2024 Request for Additional Information Exemption Requests for Physical Barriers (EPID L-2023-LLE-0018 & L-2023-LLE-0021) ML23345A1312024-01-0303 January 2024 Withholding Letter - SNC Fleet - Physical Barriers Exemption (L-2023-LLE-0018 and L-2023-LLE-0021) ML23317A2072023-12-22022 December 2023 Issuance of Amendments 223 and 206 Regarding Revision to Technical Specifications to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the COLR Consistent with WCAP-1448 ML23335A1222023-12-19019 December 2023 Safety Evaluation Regarding Implementation of Mitigating Strategies Related to Order EA-12-049 (EPID L-2023-LRQ-0002) - Letter ML23353A1702023-12-19019 December 2023 LAR-22-002, TS 3.8.3 Inverters Operating Completion Time Extension Letter ML23310A2922023-12-0707 December 2023 Issuance of Amendment for Exception to Regulatory Guide 1.163, LAR 23 007 ML23339A1812023-12-0707 December 2023 Correction Letter Regarding License Amendment Request: More Restrictive Action for Technical Specification 3.1.9 ML23338A2182023-12-0606 December 2023 Project Manager Reassignment NL-23-0878, Request for Exemption from Security Event Notification Implementation2023-11-29029 November 2023 Request for Exemption from Security Event Notification Implementation ML23289A1632023-11-28028 November 2023 Letter and Amendment 195 and 192 LAR-23-006R1 TS 3.1.9 More Restrictive Action NL-23-0827, Response to Requests for Additional Information for a License Amendment Request and a Proposed Alternative Related to TS 3.4.142023-11-17017 November 2023 Response to Requests for Additional Information for a License Amendment Request and a Proposed Alternative Related to TS 3.4.14 ML23318A4582023-11-14014 November 2023 Integrated Inspection Report 05200025/2023003 ML23312A3502023-11-14014 November 2023 Integrated Inspection Report 05200026/2023003 ML23306A3552023-11-0808 November 2023 NRC Initial Test Program and Operational Programs Integrated Inspection Report 052000/262023008 ML23268A0572023-11-0707 November 2023 Issuance of Amendments 194 & 191 Request for License Amendment Relocation of Technical Specification 3.7.9, Spent Fuel Pool Makeup Water Sources (LAR-23-003) IR 05000424/20234022023-11-0606 November 2023 Security Baseline Inspection Report 05000424/2023402 and 05000425/2023402 IR 05000424/20230032023-10-27027 October 2023 Integrated Inspection Report 05000424/2023003 and 05000425/2023003 ML23291A1512023-10-18018 October 2023 Information Request for the Cyber Security Baseline Inspection, Notification to Perform Inspection 0520026/2024401 ML23263A9852023-10-12012 October 2023 Issuance of Amendments Nos. 221 and 204, Regarding Technical Specification 5.5.11.C, Acceptance Criteria for Charcoal Filter Testing ML23283A0472023-10-0808 October 2023 Neop Letter Dated October 8, 2023 - Vogtle 3 & 4 - TS 3.7.6 License Amendment Request NL-23-0750, Response to Second Request for Additional Information Regarding License Amendment Request: Technical Specification Revision to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the Colr2023-10-0404 October 2023 Response to Second Request for Additional Information Regarding License Amendment Request: Technical Specification Revision to Adopt TSTF-339-A, Relocate Technical Specification Parameters to the Colr NL-23-0745, Refueling Outage 1R24 Steam Generator Tube Inspection Report2023-09-22022 September 2023 Refueling Outage 1R24 Steam Generator Tube Inspection Report ML23254A2032023-09-13013 September 2023 Initial Test Program and Operational Programs Inspection Report 05200025/2023013 ML23241B0212023-09-12012 September 2023 Review of Quality Assurance Topical Report ML23234A2352023-09-0808 September 2023 Request for Withholding Information from Public Disclosure Notification of Full Compliance of Required Action for NRC Order EA-12-049 Mitigation Strategies for Beyond-Design-Basis External Events IR 05000424/20230912023-09-0505 September 2023 Plan Units 1 and 2 - NRC Investigation Report 2-2022-006 and Notice of Violation - NRC Inspection Report 05000424/2023091 and 05000425/2023091 ML23234A3002023-09-0101 September 2023 NRC Integrated Inspection Report 05200026/2023003 ML23243A0092023-08-31031 August 2023 Updated Inspection Plan for Vogtle Electric Generating Plant, Units 3 & 4 (Report 05200025 2023005 & 05200026 2023005) NL-23-0695, Response to Round 2 Request for Additional Information Regarding License Amendment Request for Technical Specification 3.8.3, Inverters Operating, Completion Time Extension (LAR-22-002S2)2023-08-31031 August 2023 Response to Round 2 Request for Additional Information Regarding License Amendment Request for Technical Specification 3.8.3, Inverters Operating, Completion Time Extension (LAR-22-002S2) ML23243B0252023-08-30030 August 2023 Exam Corporate Notification Letter (210 Day) IR 05000424/20230052023-08-29029 August 2023 Updated Inspection Plan for Vogtle Electric Generating Plant, Units 1 & 2 - Report 05000424/2023005 and 05000425/2023005 NL-23-0666, License Amendment Request: Remove Combined License Appendix C (LAR 23-008)2023-08-28028 August 2023 License Amendment Request: Remove Combined License Appendix C (LAR 23-008) 2024-02-05
[Table view] Category:Licensee Event Report (LER)
MONTHYEARND-23-0439, ITAAC Closure Notification on Completion of ITAAC 2.2.05.07a.i (Index Number 265)2023-07-18018 July 2023 ITAAC Closure Notification on Completion of ITAAC 2.2.05.07a.i (Index Number 265) 05000425/LER-2017-0022017-11-17017 November 2017 Valid Undervottage Condition results in Automatic Actuation of a Safety System, LER 17-002-00 for Vogtle, Unit 2, Regarding Valid Undervoltage Condition Results in Automatic Actuation of a Safety System 05000424/LER-2017-0022017-06-29029 June 2017 Vice President Vogtle Units 1-2 7821 River RD Waynesboro GA, 30830 706-848-0004 tel 706-848-3321 fax June 29, 2017 Docket No: 50-424 NL-17-1104 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555-0001 Vogtle Electric Generating Plant — Unit 1 Licensee Event Report 2017-002-01 Wiring Error results in Automatic Actuation of a Safety System Ladies and Gentlemen: In accordance with the requirements of 10 CFR 50.73(a)(2)(iv)(A), Southern Nuclear Operating Company is submitting the enclosed Licensee Event Report, 2017-002-01 for Vogtle Electric Generating Plant Unit 1. This letter contains no NRC commitments. If you have any questions, please contact Dom Sutton at (706) 848-1428. Respectfully sub Darin J. M rs Vice President — Plant ogtle Units 1&2 - SNC DJM/KCW Enclosure: Unit 1 Licensee Event Report 2017-002-01 Cc: Regional Administrator NRR Project Manager — Vogtle 1 & 2 Senior Resident Inspector — Vogtle 1 & 2 RType: CVC7000 Vogtle Electric Generating Plant — Unit 1 Licensee Event Report 2017-002-01 Wiring Labeling Error results in Automatic Actuation of a Safety System Enclosure Unit 1 Licensee Event Report 2017-002-01 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (04-2017) LICENSEE EVENT REPORT (LER) ILWa t l,viricir (See Page 2 for required number of digits/charactersfor each block) ••••••• (See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.qovireadincl-rmidoc-collections/nuregs/staff/sr1022/r3i) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 0313112020 Estimated burden per response to comply with this mandatory collection request: 80 hours Reported lessons learned are incorporated into the licensing process and fed back to industry Send comments regarding burden estimate to the Information Services Branch (T-2 F43), US Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Infocollects Resource@nrc gov, and to the Desk Officer, Office of Information •and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington. DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME Vogtle Electric Generating Plant . DOCKET NUMBER 13. PAGE 17.:15000424 1 1 OF 2 4. TITLE Mirina Error results in_AulomaticActuation_of a Safety System_, LER 17-002-01 for Vogtle, Unit 1, Wiring Error Results in Automatic Actuation of a Safety System 05000425/LER-2017-0012017-06-29029 June 2017 1 OF 3, LER 17-001-01 for Vogtle, Unit 2, Regarding Power Supply Failure Results in Operation in a Condition Prohibited by Technical Specifications Supplement NL-10-0577, LER 10-S01-00 for Vogtle, Units 1 & 2 Regarding Supplemental Worker'S Unescorted Access Not Revoked in a Timely Manner2010-03-30030 March 2010 LER 10-S01-00 for Vogtle, Units 1 & 2 Regarding Supplemental Worker'S Unescorted Access Not Revoked in a Timely Manner 2023-07-18
[Table view] |
Infocollects Resource@nrc gov, and to the Desk Officer, Office of Information and Regulatory Affairs NEOB-10202 (3150-0104). Office of Management and Budget, Washington. DC 20503 If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor and a person is riot required to respond to the information collection.
A. Event Description
On March 17, 2017, at approximately 1517 EDT, Unit 1 was in refueling outage 1R20 with the unit in Mode 6 being prepared for fuel offload. After work had been performed on the 1-B Reserve Auxiliary Transformer (RAT) and during power restoration, a valid undervoltage actuation signal was sent to the 1-B Emergency Diesel Generator (EDG). The EDG started and automatically tied to the electrical safety bus. Once the issue was identified and understood by the operators, the EDG was secured and the electrical safety bus was transferred to the appropriate offsite power source.
The reactor was Mode 6 at the time of the event and remained so throughout the event. Decay heat was removed via the Residual Heat Removal (RHR) system, to the Component Cooling Water System, to the Nuclear Service Cooling Water system,. and finally to the atmosphere.
This report is required per 10CFR50.73(a)(2)(iv)(A) due to an automatic actuation of the Emergency AC power system.
B. Cause of Event
The cause of the event was a wiring error of the Open Phase system alarm and trip circuitry to the RAT. This resulted in a valid undervoltage actuation signal to be sent to the 1 B EDG as power was being restored to the Open Phase system. The EDG properly detected the undervoltage condition and responded per design.
C. Safety Assessment The EDG properly started and loaded the safety bus as required. At no time was decay heat removal lost to the RCS or the Spent Fuel Pool. Because all safety systems performed their safety function, the safety significance of the event is considered very low.
D. Corrective Actions
The wiring error was discovered using a continuity check during the post-event troubleshooting. The wires from the Open Phase system to the 1-B RAT were found mislabeled and landed on the wrong terminals. The wiring error was subsequently corrected and an extent of condition review was performed to verify proper labels and continuity and no other errors were found.
E. Previous Similar Events:
None -t-
|
---|
|
|
| | Reporting criterion |
---|
05000425/LER-2017-001 | 1 OF 3 LER 17-001-01 for Vogtle, Unit 2, Regarding Power Supply Failure Results in Operation in a Condition Prohibited by Technical Specifications Supplement | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000425/LER-2017-002 | Valid Undervottage Condition results in Automatic Actuation of a Safety System LER 17-002-00 for Vogtle, Unit 2, Regarding Valid Undervoltage Condition Results in Automatic Actuation of a Safety System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000424/LER-2017-002 | Vice President Vogtle Units 1-2 7821 River RD Waynesboro GA, 30830 706-848-0004 tel 706-848-3321 fax June 29, 2017 Docket No: 50-424 NL-17-1104 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D.C. 20555-0001 Vogtle Electric Generating Plant — Unit 1 Licensee Event Report 2017-002-01 Wiring Error results in Automatic Actuation of a Safety System Ladies and Gentlemen: In accordance with the requirements of 10 CFR 50.73(a)(2)(iv)(A), Southern Nuclear Operating Company is submitting the enclosed Licensee Event Report, 2017-002-01 for Vogtle Electric Generating Plant Unit 1. This letter contains no NRC commitments. If you have any questions, please contact Dom Sutton at (706) 848-1428. Respectfully sub Darin J. M rs Vice President — Plant ogtle Units 1&2 - SNC DJM/KCW Enclosure: Unit 1 Licensee Event Report 2017-002-01 Cc: Regional Administrator NRR Project Manager — Vogtle 1 & 2 Senior Resident Inspector — Vogtle 1 & 2 RType: CVC7000 Vogtle Electric Generating Plant — Unit 1 Licensee Event Report 2017-002-01 Wiring Labeling Error results in Automatic Actuation of a Safety System Enclosure Unit 1 Licensee Event Report 2017-002-01 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION (04-2017) LICENSEE EVENT REPORT (LER) ILWa t l,viricir (See Page 2 for required number of digits/charactersfor each block) ••••••• (See NUREG-1022, R.3 for instruction and guidance for completing this form http://www.nrc.qovireadincl-rmidoc-collections/nuregs/staff/sr1022/r3i) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 0313112020 Estimated burden per response to comply with this mandatory collection request: 80 hours Reported lessons learned are incorporated into the licensing process and fed back to industry Send comments regarding burden estimate to the Information Services Branch (T-2 F43), US Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Infocollects Resource@nrc gov, and to the Desk Officer, Office of Information •and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington. DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. 1. FACILITY NAME Vogtle Electric Generating Plant . DOCKET NUMBER 13. PAGE 17.:15000424 1 1 OF 2 4. TITLE Mirina Error results in_AulomaticActuation_of a Safety System_ LER 17-002-01 for Vogtle, Unit 1, Wiring Error Results in Automatic Actuation of a Safety System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
|