05000424/FIN-2017004-02
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Finding | |
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Title | Failure to Maintain NEMA Type 4 Qualification for the Nuclear Service Cooling Water Pumps |
Description | A Green, self-revealing, NCV of TS 5.4.1.a, Procedures, was identified for the licensees failure to properly implement and establish procedures to maintain watertight requirements of the nuclear service water system (NSCW) pumps motor main power cables termination box. As a result, the Unit 2 B train NSCW pump no. 4 failed due to aphase-to-ground fault caused by water and moisture intrusion into the power cable splice connections. Failure to adequately implement and establish procedures to maintain watertight requirements of the NSCW pumps motor main power cables termination box during maintenance, as required by maintenance procedures and specifications, was a performance deficiency. The licensee replaced the motor and faulted cable; and sealed all potential water and moisture intrusion enclosure locations until watertight enclosure standards are fully restored. This issue was entered into the licensees CAP as CRs10399125, 10404327, and corrective action report 270905.The performance deficiency was more than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences (e.g. core damage). Specifically, the Unit 2 NSCW pump no. 4 was rendered inoperable, adversely affecting the NSCW system reliability. The finding was determined to be of very low safety significance (Green) because it did not result in an actual loss of safety system function, and it did not represent a loss of function of one or more than one train for more than its Technical Specification (TS) allowed outage time or greater than 24 hrs. The finding was assigned a cross-cutting aspect of Resources, because procedures and/or work instructions were not available to maintenance personnel for properly verifying motor termination boxes were installed in compliance with NEMA 4 specifications. (H.1) |
Site: | Vogtle |
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Report | IR 05000424/2017004 Section 4OA2 |
Date counted | Dec 31, 2017 (2017Q4) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | M Endress A Alen R Carrion J Rivera R Pursley A Blamey |
Violation of: | Technical Specification - Procedures |
CCA | H.1, Resources |
INPO aspect | LA.1 |
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Finding - Vogtle - IR 05000424/2017004 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Vogtle) @ 2017Q4
Self-Identified List (Vogtle)
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