05000364/LER-2017-004

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LER-2017-004, I OF 3
Joseph M. Farley Nuclear Plant. Unit 2
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
3642017004R00 - NRC Website
LER 17-004-00 for Joseph M. Farley Nuclear Plant, Unit 2 Regarding Turbine-Driven Auxiliary Feedwater Pump Steam Admission Valve Air Leak Resulted in a Condition Prohibited by Technical Specifications
ML17362A039
Person / Time
Site: Farley, Joseph M. Farley Nuclear Plant. Unit 2 Southern Nuclear icon.png
Issue date: 12/22/2017
From: Madison D R
Southern Nuclear Operating Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
NL-17-2123 LER 17-004-00
Download: ML17362A039 (5)


comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. fluclear- Regulatory Commission. Washington. DC 20555-0001, or by earth to !nieceHeals Resourcs@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs.

used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3. LER NUMBER

00 004 364 2017

EVENT DESCRIPTION:

On October 31, 2017, while in Mode 6 and at 0% power, with the Reactor Coolant System (RCS) at atmospheric pressure and 83 degrees Fahrenheit, the Turbine-Driven Auxiliary Feedwater (TDAFW) pump B-Train steam admission valve (EIIS:

SB/FCV) from the 2C Steam Generator failed to meet Technical Specification (TS) Surveillance Requirement (SR) 3.7.5.5.

This SR verifies that the air stored in TDAFW pump steam admission valve accumulators is sufficient to open their associated train's steam admission valves. Each steam admission valve has an air accumulator associated with it. The accumulators provide sufficient air to ensure the operation of the steam admission valves for the TDAFW pump during a loss of power or other failure of the normal air supply for a period of two hours.

During the performance of a flow scan analysis it was identified that the B-Train steam admission valve actuator was leaking by the o-ring. Although the steam admission valve would stroke open, the 2-hour acceptance criteria for using only the associated accumulator could not be met. It is likely that the steam admission valve was inoperable longer than allowed by the Required Action Statement (7 days) following the spring 2016 refueling outage when it last passed its associated surveillance..

EVENT ANALYSIS:

While performing a flow scan of the TDAFW pump steam admission valve during the fall 2017 refueling outage, the actuator piston cylinder was discovered to be leaking >10 psig per minute with acceptance criteria of An actuator rebuild was completed on November 8, 2017. The steam admission valve actuator o-ring was replaced as part of the actuator rebuild. The o-ring failure was determined to be a cause of the event.

REPORTABILITY AND SAFETY ASSESSMENT:

During the performance of a flow scan analysis it was identified that the B-Train steam admission valve actuator was leaking by the o-ring. Although the steam admission valve would stroke open, the 2-hour acceptance criteria for using only the associated accumulator could not be met. Therefore, this condition is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

The Auxiliary Feedwater (AFW) system trains are configured into two flow paths, one for the motor-driven pumps and one for the turbine-driven pump. The AFW system is considered OPERABLE when the components and flow paths providing redundant AFW flow to the steam generators are OPERABLE. In addition, the TDAFW pump is required to be OPERABLE with redundant steam supplies from each of two main steam lines upstream of the main steam isolation valves and shall be capable of supplying AFW to any of the steam generators via its associated flow path.

Although the B-Train steam admission valve accumulator was incapable of maintaining the steam admission valve open for two hours, the redundant A-Train steam admission valve was capable of performing the required function.

During the previous cycle, there were no instances where both motor-driven AFW trains were rendered INOPERABLE at the same time. To further support continued operation of AFW, both trains of steam admission valves to the TDAFW pump have emergency air compressors capable of being aligned by operations to support motive operation of the steam admission valves. With the ability to operate the TDAFW pump from the A-Train steam admission valve, and having a redundant train of AFW (motor-driven), the safety function of the AFW system was met.

comments regarding burden estimate to the Information Services Brandi (T-2 F43), U.S. Nuclear; Regulatory Commission, Washington, DC 2055541001. or by e-mai to NE013-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to Impose en information collection does not dsplay a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection.

364

3. LER NUMBER

004 05000- 2017 00

CORRECTIVE ACTIONS:

The actuator repair began on October 31, 2017, and was completed by maintenance work order on November 8, 2017.

Further investigation of the preventive maintenance (PM) for diagnostic testing and actuator rebuild of the steam admission valves identified the current PM frequency was 6 years. This PM was last completed in November 2014. Based on the failure of the actuator piston o-ring, the site is evaluating frequency changes per the PM change process.

Following repair, the valve as-left testing acceptance criteria was per ASME OM Code 2001 Edition-2003 Addenda, Section ISTC-3310, "When a valve or its control system has been replaced, repaired, or has undergone maintenance that could affect the valves performance, a new reference value shall be determined or the previous value re-confirmed." The steam admission valve was functionally tested per plant procedures and was left in the acceptable range in accordance with the In-Service Testing (1ST) program.

PREVIOUS SIMILAR EVENTS:

No similar events were identified related to the accumulators or steam admission valves.

OTHER SYSTEMS AFFECTED:

No other systems were affected, other than those listed in this LER.

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