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 Start dateReport dateSiteReporting criterionSystemEvent description
05000446/LER-2017-00325 November 2017
22 January 2018
22 January 2018Comanche Peak
Comanche Peak Nuclear Power Plant, Unit 2
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Steam Generator
Feedwater
Reactor Protection System
Auxiliary Feedwater
Main Turbine

On November 25, 2017 Comanche Peak, Unit 2 received alarms indicating a trip of both main feedwater pumps. After confirming a decreasing water level in all four steam generators, the control room initiated a manual reactor trip. All safety systems responded as designed including the automatic start of the auxiliary feedwater system. The cause of the trip of both main feedwater pumps could not be positively identified. Causal analysis indicates that a prior plant modification maintained power to abandoned relays in the Solid State Protection System that may have caused both main feedwater pumps to trip. Subsequent actions were taken to remove the fuses that provided power to the abandoned relays on both Unit 1 and Unit 2 to eliminate recurrence from this possible source. Additional corrective actions have been entered into the Comanche Peak Corrective Action Program.

All times below are in Central Standard Time (CST).

05000263/LER-2017-00614 November 2017
12 January 2018
12 January 2018Monticello10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Reactor Coolant System
Reactor Protection System
Main Steam Isolation Valve
Main Steam Line
Main Steam

On November 14, 2017, it was identified that the use of the Reactor Protection System (RPS) test fixture described in some operations procedures would result in the loss of two RPS reactor Scram functions. Technical Specification 3.3.1.1 requires that RPS Instrumentation for Table 3.3.1.1-1 Function 5, Main Steam Isolation Valve-Closure and Function 8, Turbine Stop Valve-Closure, remain operable. It was concluded that a closure of three of four Main Steam Lines or Turbine Stop Valves would not necessarily have resulted in a full Scram during testing depending on the combination of closed valves occurring during the bypass condition. Operations procedures were revised to incorporate the use of the test fixture in December, 2008 for the Turbine Stop Valve Closure Scram Test Procedure and February, 2009 for the Main Steam Isolation Valve Closure Scram Test Procedure. The operations procedures were inappropriately revised to allow use of the test fixture on all RPS functions to prevent a half Scram.

The operations procedures were quarantined until revisions were issued in December, 2017 that removed use of the test fixture.

05000364/LER-2017-0053 January 2017
11 January 2018
11 January 2018Farley
Joseph M Farley Nuclear Plant, Unit 2
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)
10 CFR 50.73(a)(2)()

During a reactor startup on November 13, 2017 at 0136, while at approximately 1.5°o power (MODE 2), an Excore Power Range Nuclear Instrument (N-42) was declared inoperable due to lower than expected detector amps and indicated power. N-42 was reading approximately 0.4°0 lower power than the other three Power Range instruments. The malfunction was determined to be the result of a failed High Voltage (HV) cable center pin connector to N-42. The HV cable connector was installed during N-42 rescahng on November 10, 2017 in preparation for startup physics testing. N-42 provides an input signal to Channel 2 of the Over Temperature Delta Temperature (OTDT) Reactor Trip Signal. Prior to the discovery of the N-42 failure, Channel 3 of OTDT had also been declared inoperable and associated bistables tripped due to a failed Pressurizer Pressure transmitter. Therefore, it was determined that two channels of OTDT were inoperable longer than allowed by Technical Specification (TS) 3.0.3. This condition is reportable per 10CFR50.73(a)(2X1)(B).

The HV cable connector was repaired and all channels were OPERABLE on November 14, 2017 at 1000. The installation of the HV cable connector with the faulty center pin was attributed to human error. Corrective actions include procedure changes, training, and departmental communications related to maintenance fundamentals.

05000364/LER-2017-00219 December 2017Farley10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Steam Generator
Reactor Coolant System
Main Steam Safety Valve
Main Condenser
Main Steam

On November 1, 2017, while in Mode 6 and at 0% power level, one of the C Loop Main Steam Safety Valves (MSSV) as-found lift pressure did not meet the acceptance criteria of +/- 3% of the setpoint (1129 psig) as required by Technical Specifications (TS) Surveillance Requirement (SR) 3.7.1.1. The MSSV lifted at 1171 psig which is 9 psig outside of its acceptance range of 1096 to 1162 psig and 3.72°o above its setpoint. The apparent cause of exceeding the MSSV upper acceptance limit is degradation of the valve spring and/or valve spindle compression screw. The as-found settings remained within analytical bounds; therefore, operation of the facility in this condition had no impact on the health and safety of the public.

TS Limiting Condition for Operation (LCO) 3.7.1, IvISSVs, requires five MSSVs per steam generator to be operable in Modes 1, 2, and 3. Since the failure affected the lift pressure over a period of time, it is assumed that the C Loop MSSV was inoperable for a time greater than allowed by TS. Therefore, this occurrence is considered reportable per 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

The C Loop MSSV was replaced on November 5, 2017, while in Mode 5.

05000446/LER-2017-00111 August 2017
5 October 2017
22 January 2018Comanche Peak10 CFR 50.73(a)(2)(v), Loss of Safety FunctionSteam Generator
Feedwater
Auxiliary Feedwater

At 1124 Central Daylight Time on August 11, 2017, Comanche Peak Nuclear Power Plant (CPNPP) Unit 2 experienced an automatic Auxiliary Feedwater System actuation during a Turbine trip. The plant was stabilized at 3 percent reactor power with the Auxiliary Feedwater System feeding all Steam Generators with all levels within their normal bands. The cause of the Turbine trip was high water level in Steam Generator 2-02 related to the mechanical malfunction of a Steam Generator 2-02 flow control bypass valve. The valve '.

malfunctioned due to a loose locknut on the valve hand wheel. Corrective actions included repair of the Steam Generator 2-02 flow control bypass valve. All times in this report are approximate and Central Daylight Time unless noted otherwise.

05000323/LER-2017-0013 October 2017Diablo Canyon10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Steam Generator
Reactor Coolant System
Feedwater
Emergency Core Cooling System

During an investigation of a nitrogen leak inside the Unit 2 containment, Nitrogen Accumulator Relief Valve (RV) RV-355 was found to be leaking. The leak caused the pressure in the back up nitrogen accumulator supply to Power Operated Relief Valve (PORV) PCV-455C to decrease to a level that made the PORV inoperable. Based on a review of the ti-end data for nitrogen usage in the containment, it is conservatively assumed that RV-355 had been degraded since December 1, 2016, rendering the PORV inoperable for longer than permitted by Technical Specifications.

The presumptive cause was inadequate instructions provided in plant procedures for placing a new nitrogen bottle in service. These instructions did not provide a sequence that assures system pressure transients are mitigated. This may have caused excessive pressure excursions resulting in multiple lifts of RV-355 which resulted in damage to the RV 0-ring seat and a nitrogen leak path.

Corrective actions include replacing RV-355 and revising procedures to provide instructions on placing nitrogen supply bottles in service to maintain back pressure and minimize pressure transients on the nitrogen system.

This event did not affect the health and safety of the public.

05000298/LER-2016-00127 September 2017Cooper10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Service water
High Pressure Coolant Injection
Reactor Core Isolation Cooling
Core Spray
Automatic Depressurization System
Emergency Core Cooling System
Low Pressure Coolant Injection

On April 25, 2016, while performing a walkdown of Control Room panels, it was noticed that the green indication light for High Pressure Coolant Injection (HPCI) auxiliary lube oil pump (ALOP) was not illuminated.

A non-licensed operator was dispatched to the HPCI ALOP starter and reported that the local indication lights were not illuminated. HPCI was declared inoperable at 2117 Central Daylight Time (CDT) resulting in entry into Technical Specifications (TS) Limiting Condition of Operation 3.5.1, Condition C, HPCI System Inoperable.

Investigation determined that the coil in the electrical relay for the ALOP, which had recently been replaced during a preventive maintenance window, had failed after 133 hours of service. The cause of the failure was determined to be the prior pre-installation checks performed by NuTherm on the relay were inadequate to prevent the type of infant mortality failure that occurred in this case. HPCI was declared operable at 1314 CDT on April 26, 2016, after the coil was replaced.

This event is being reported as a loss of safety function due to HPCI being a single-train safety system and as a condition prohibited by TS.

The potential safety consequences of this event were minimal due to both the limited duration the condition existed and the redundant/diverse core cooling systems which remained operable.

05000346/LER-2017-00120 July 2017
18 September 2017
18 September 2017Davis Besse10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Emergency Diesel Generator

On July 20, 2017, with the Davis-Besse Nuclear Power Station (DBNPS) operating at approximately 100 percent power, it was identified that the Emergency Diesel Generator (EDG) fuel oil storage tank vents were not adequately protected from potential tornado-generated missiles. If a missile crimped the vent it could disable the transfer pump or tank, potentially impacting the seven-day fuel supply for the affected train(s) of EDG. While the storage tanks were protected from tornado missiles when installed, the vents were not provided with any such protection. Compensatory measures were established to ensure a vent path remained following a tornado event, and actions will be taken to ensure the vents for each EDG fuel oil storage tank are adequately protected from tornado missiles.

This issue is being reported in accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition that significantly degraded plant safety, in accordance with 10 CFR 50.73(a)(2)(v) as a condition that could have prevented the fulfillment of the safety function, in accordance with 10 CFR 50.73(a)(2)(vii) as an event where a single cause or condition caused two independent trains to become inoperable in a single system, and in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.

05000247/LER-2015-00111 August 2015
29 August 2017
15 September 2016Indian Point10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Service water
Containment Spray

On August 11, 2015, during operator investigations inside the reactor containment building, a through wall leak was discovered on the 24 Fan Cooler Unit (FCU) motor cooler service water (SW) return line. The leak was in a 2 inch copper-nickel pipe near a brazed joint upstream of containment penetration SS. The leak was located within the ASME Section XI Code ISI Class 3 boundary and estimated to be approximately 2 gpm.

Since the pipe flaw was through wall and was located within the ASME Section XI boundary, it exceeds the flaw allowable limits provided per IWC-3000.

The weld leak was evaluated and determined to meet the structural requirements of ASME Code Case N-513-3.

The condition was determined to have no impact on SW cooling safety function or adverse impact on piping structural integrity. The pipe is considered a closed loop system inside containment and required to meet containment integrity.

An engineering evaluation was performed to determine the potential air leakage out of containment based on the observed SW leakage into containment.

This evaluation concluded that the leaking defect could result in post-LOCA air leakage out of containment in excess of that allowed by Technical Specification 3.6.1 (Containment) which requires leakage rates to comply with 10 CFR 50, Appendix J.

The direct cause was corrosion. The apparent cause was the length of time to implement a modification to replace the FCU motor cooler copper-nickel piping identified in 2009 per the SW mitigation strategy.

An engineered clamp was installed over the pipe defect. The pipe and affected elbow were replaced in accordance with the requirements of ASME Section XI Code during the spring refueling outage in 2016. A modification to replace piping will be processed for funding. The event had no significant effect on public health and safety.

05000390/LER-2017-00814 August 2017Watts Bar10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Primary containment
Auxiliary Building Gas Treatment System
Shield Building
Emergency Gas Treatment System

On June 15, 2017, at 1219 Eastern Daylight Time (EDT), Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.15 Condition B was entered for Watts Bar Nuclear Plant (WBN) Unit 1 annulus pressure not within limits, resulting in Shield Building inoperability. At 1221 EDT, the WBN Unit 1 annulus pressure returned to normal, the Shield Building was declared operable, and LCO 3.6.15 Condition B was exited. Because the shield building is a non-redundant safety system, operation outside of TS allowable limits represents an event that could have prevented fulfillment of a safety function.

The temporary loss of the Shield Building resulted from a loss of pressure control in the Auxiliary Building caused by a loss of Auxiliary Building General Ventilation due to a spurious cross zone fire alarm. The Auxiliary Building Gas Treatment System was started to maintain Auxiliary Building pressure within limits and the non-safety related Annulus Auxiliary Building ventilation supply fans were replaced.

05000286/LER-2017-00211 June 2017
9 August 2017
9 August 2017Indian Point
Docket Number
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Reactor Coolant System
Feedwater
Residual Heat Removal
Decay Heat Removal

On June 11, 2017, while at 100 percent reactor power, Operations placed Chemical and Volume Control System (CVCS) Demineralizer Diversion Valve CH-TCV-149 in DIVERT to allow the 32 Mixed Bed Demineralizer to be removed from service and align the 31 Mixed Bed Demineralizer for service. Within about two minutes after returning CH-TCV-149 to AUTO, which placed the 31 Mixed Bed Demineralizer in service, Letdown Backpressure Control Valve CH-PCV-135 demand had gone to 0 percent (full open demand) while letdown backpressure had increased, reaching 302 psig.

Operations was alerted to a leak that had developed on 32 Mixed Bed Demineralizer Inlet Isolation Valve CH-352. In an effort to isolate the leak, CH-TCV-149 was placed in DIVERT. Due to the elevated pressure at CH-TCV-149 with CH-PCV- 135 fully open, placing CH-TCV-149 in DIVERT coupled with the elevated line pressure created a pressure transient in the letdown line upstream of the CVCS Reactor Coolant Filter. Reactor Coolant Filter Inlet Isolation Valve CH-305 experienced this pressure transient, which resulted in the valve developing a significant leak at the body to bonnet joint. Abnormal Operating Procedure (AOP) 3-AOP-LEAK-1 was entered, and normal letdown was manually isolated to stop the CH-305 leak. Excess letdown was placed in service to balance reactor coolant inventory at a Pressurizer water level of 61 percent.

This exceeded the 54.3 percent limit of Technical Specification 3.4.9 Condition A, and Operations declared the Pressurizer inoperable. The inoperability of the Pressurizer is reportable as a safety system functional failure under 10 CFR 50.73(a)(2)(v). The direct cause of this event was elevated system pressure due to loading of the Reactor Coolant Filter from materials when the 31 Mixed Bed Demineralizer pathway was aligned. The elevated operating pressure in the CVCS letdown stream challenged the integrity of diaphragm valves CH-352 and CH-305, requiring the isolation of normal letdown.

05000390/LER-2017-0079 June 2017
8 August 2017
3 November 2017Watts Bar10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Reactor Coolant System
Control Room Emergency Ventilation
Shield Building
Emergency Gas Treatment System

On June 9, 2017. Watts Bar Nuclear Plant (WBN) personnel determined that the reporting requirements of 10 CFR 50.72(b)(3)(v) and 10 CFR 50.73(a)(2)(v), as clarified by guidance in NUREG-1022, Revision 3. were being incorrectly applied for certain events associated with single train safety systems. When events occurred that resulted in these systems not meeting Technical Specification (TS) Limiting Conditions for Operation (LCO). the short duration of these events relative to their required action completion time, coupled with prompt return to allowable values, were not considered a loss of safety function by Operations and Licensing personnel. As a result, multiple potential loss of safety function events were not reported as required. These events were related to Refueling Water Storage Tank (RVVST) level, Containment and Shield Building pressure, and Control Room Envelope integrity.

A review of these events indicate, when considering the actual system capability and the response of equipment and personnel. a loss of safety function capability impacting public health and safety did not occur for events associated with the RWST, Containment. Shield Building, or Control Room. Corrective actions include briefing personnel on the regulatory impact of these events, and the importance of the control room boundary.

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05000341/LER-2017-00322 May 2017
21 July 2017
21 July 2017Fermi10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Service water
Emergency Diesel Generator
Reactor Pressure Vessel
Residual Heat Removal
Residual Heat Removal Service Water

On May 22, 2017 at 05:10 am (EST), while placing Division 2 Residual Heat Removal Service Water (RHRSW) in service for biocide treatment of the Division 2 Residual Heat Removal (RI IR) Reservoir, the Division 2 RI IRSW Flow Control Valve (FCV) (El 1 50F068B) failed to fully open.

Troubleshooting discovered the direct cause was failure of the anti-rotation bushing stem key. The apparent cause was system operating conditions (high vibration) resulting in the failed tack welds. Previous troubleshooting on an indication issue on May 5, 2017 for the RHRSW FCV was inadequate, and did not identify the failure of the anti-rotation key. As a result, the RHRSW FCV was returned to service at 2:50 pm on May 7, 2017, and subsequently failed on the next on-demand stroke at 5:10 am on May 22, 2017. Seventeen similar Motor Operated Valves (MOVs) were inspected and no MOVs exhibiting the symptoms observed on the E1150F068B prior to the failure of the anti-rotation key were found, and all anti-rotation devices were found to be intact. The Past Operability determination for 131150E068B found that the MOV was unable to perform its design basis functions from May 3. 2017 at 5:48 am, when the RI IRSW FCV was last successfully stroked under dynamic conditions, through May 24. 2017 at 4:04 pun, when the RI IRSW FCV was returned to service. The Division I RI-IRSW was available throughout the event except on two occasions. Division 1 of RHRSW was declared inoperable for Mechanical Draft Cooling Tower (MDCT) Nozzle Cleaning activities on May 9, 2017 from 8:41 am to May 9, 2017 at I I :18 pm. Division I of RI IRSW was again declared inoperable for IVIDCT Nozzle Cleaning activities on May 11, 2017 at 8:35 am through May 11, 2017 at 10:01 pm. The as found condition of the Division 2 RHRSW FCV is a condition prohibited by Technical Specification 3.7.1 and reportable under 10 CFR 50.73 (a)(2)(i)(13) "Operation or Condition Prohibited by Technical Specifications," and 10 CFR 50.73(a)(2)(v)(13) "Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: Remove Residual Heat.

05000286/LER-2017-00114 May 2017
13 July 2017
13 July 2017Indian Point
Indian Point Unit 3
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
Reactor Coolant System
Residual Heat Removal
Emergency Core Cooling System

On May 14, 2017, at 0233 hrs, Indian Point Unit 3 entered Mode 4 as part of coming out of outage 3R19 and preparing for power operations. Operations test group was preparing for performance of 3-PT- CS004, Residual Heat Removal (RHR) Check Valve Testing. The team gathered for a pre job brief in accordance with the requirements of EN-HU-102, Human Performance Traps &Tools Procedure. At the time the only allowable access point to the Inner Crane Wall was through the double gate combination of Gates D and E, which require one gate to be maintained closed and secured at all times. Workers needed to enter inside of the Crane Wall to perform a portion of the valve lineup required by 3-PT-CS004. After unbolting and opening the gate, the two operators and a contract Radiation Protection (RP) Technician went through gate C despite a posted sign stating that the gate was not to be utilized in modes 1 through 4.

While the valve manipulations were in progress the NRC Resident Inspector was also conducting a tour of the Vapor Containment (VC) and identified that gate C was opened. This gate being open in this plant condition resulted in a safety system functional failure, since with the gate unsecured this made the containment sumps inoperable.

05000440/LER-2017-00326 June 2017Perry10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Primary containment
Shield Building

On April 27. 2017, at 0545 hours, with the plant in Mode 1 at 100 percent rated thermal power. while shifting Annulus Exhaust Gas Treatment System (AEGTS) from sub-system B to sub-system A, annulus differential pressure could not be maintained within the required system operating band, which caused an unplanned entry into technical specification limiting conditions of operation and a momentary loss of safety function. Sub-system B was inoperable while being shutdown to standby readiness in accordance with plant operating procedures and would not have automatically started in response to an actuation signal. Investigation determined that sub- system A was inoperable due to failed recirculation damper. Sub-system B was restarted at 0550 hours. to maintain annulus differential pressure. Annulus differential pressure was maintained above the minimum differential pressure throughout the event and the technical specification limiting conditions for operation were not exceeded.

The cause for the AEGTS sub-system A recirculation damper failure was a failure to follow procedure which resulted in the split coupling that connects the actuator to the damper not being properly tightened. The recirculation damper was repaired and AEGTS sub-system A was restored to operable status on April 28, 2017, at 2208 hours. The failure to follow procedure was addressed by the FENOC performance management process.

Since AEGTS is not a core damage mitigation system and does not mitigate large and early containment releases, the inoperability of the AEGTS is determined to be of small safety significance. This event is being reported in accordance with 10CFR50.73(a)(2)(v)(C) and 10CFR50.73(a)(2)(v)(D) as an event or condition that could have prevented the fulfilment of a safety function.

05000269/LER-2017-00116 June 20179 August 2017Oconee Nuclear Station Unit 110 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Service water

On June 16, 2017, during implementation of a modification to Keowee Hydroelectric Station Governor Actuator Cabinets 1 and 2, breakers were inadvertently repositioned in each of the governor control system for Keowee Hydroelectric Units 1 and 2 (KHU1 and KHU2), rendering both units inoperable. The condition was discovered following an unsuccessful start of KHU2 for commercial operation. The KHUs are the onsite emergency power source for the Oconee Nuclear Station.

It was concluded that this constituted a loss of safety function from the time when both KHUs were inoperable until the dedicated offsite power source was aligned to the emergency busses; a period of approximately 7 hours. This condition is reportable pursuant to 10 CFR 50.73(a)(2)(v)(A-D).

Technical Specifications (TS) were followed based on time of discovery; however, a subsequent review of computer logs provided firm evidence that both KHUs were inoperable for longer than allowed by TSs based on "past inoperability," requiring this event to be reported pursuant to 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by the plant's Technical Specifications.

The direct cause of this event was attributed to the reposition due to inadvertent contact of two 24 VDC breakers. The risk impact of this event was determined to be insignificant and corrective actions are planned to prevent recurrence.

NFtC FORM 386A (04-2017) U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES 3/3112020 (See form 366 above for burden estimate) I NUMBER NO.

2017 - 001 - 00 Oconee Nuclear Station Unit 1 5000269 am

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  • 110-Milar

BACKGROUND

At Oconee Nuclear Station (ONS), the Keowee Hydroelectric Station (KHS) (EIIS:EK) serves the emergency power function typically performed by diesel generators (EIIS: DG) at other nuclear facilities.

The KHS consists of two (2) hydroelectric turbine/generator units (KHUs) and associated support equipment and auxiliaries. Each KHU is provided with its own automatic start equipment and both KHUs undergo simultaneous automatic emergency starts during an emergency. Either KHU may be aligned to either of two emergency power paths, with the underground path being preferred if only one KHU is available. In addition to Keowee, a 100 kV transmission line from a nearby plant with dedicated combustion turbines (EllS: TUR) can provide power to the Stand-by Buss (the emergency buss that supplies emergency loads on all three Oconee units).

Governor (EIIS: 65) Actuator Cabinets (EIIS: CAB) GAC1 and GAC2 contain control circuitry and components for KHU1 and KHU2 respectively, including breakers (EIIS: 52) K1 GCS BK0001 and K2 GCS BK0001 as part of the Governor Control System for KHU1 and KHU2 respectively. These breakers are small, 'plug in' type, 10 amp breakers with the actuating power switches (EIIS: JS) protruding into an open space inside their respective cabinets. These breakers provide 24 VDC to a distributing valve (EIIS: V) assembly and shutdown solenoid valve (EIIS: SV) which are both required to actuate for Keowee to start. The shutdown solenoid is a fail-safe valve that requires energization to open during turbine operation. Without power, the solenoid valve closes.

EVENT DESCRIPTION

On June 16, 2017, at approximately 0740 hours, workers were implementing a modification to Governor Actuator Cabinets 1 and 2 located within the Keowee Hydroelectric Station. The investigation showed that at approximately 0907 hours, Operator Aid Computer (OAC) alarm (EllS: ALM) indications for K1 GCS BK0001 breaker for KHU1 Channel A and B Governor Critical Alarm were received on the OAC alarm screens located in the Keowee Control Room (KCR). These alarms were not observed by the Keowee operator since he was still on rounds and not in the KCR. Normally, when a Governor Critical Alarm is received, Stat-Alarms in both the Keowee and Oconee Unit 2 Control Rooms are generated. Additionally, a governor critical alarm condition triggers an emergency lock-out of the unit, which would also normally generate Stat-Alarms. However, in this-instance, no Stat-Alarms were generated and no emergency lock-out condition was triggered due to the failure mode design of the repositioned breaker defeating the signal sent to the Stat-Alarms. Had a Stat-Alarm been received, the protocol of Stat-Alarm management would have been followed by the Oconee Unit 2 Control Room, the Oconee Unit 2 Senior Reactor Operator and the Keowee Control operators, potentially reducing the probability for this single incident to have escalated further. At 1020 hours, similar OAC alarm indications were received in the KCR associated with the KHU2 K2 GCS BK0001 breaker.

  • At 1321 hours, while attempting to start KHU2 for commercial generation, an "incomplete start" alarm was received in the KCR. Investigation into the matter subsequently revealed that the two (2) repositioned breakers were open and both KHUs were non-functional. Each KHU was declared inoperable at 1635 hours.

In Mode 1, KHU operability is required by TS 3.8.1, "AC Sources - Operating," and TS 3.7.10, "Protected Service Water." The appropriate TS conditions were entered and the Required Actions completed within the allowed Completion Times. As required by TS Limiting Condition for Operation (LCO) 3.8.1, Condition I, due to the loss of both KHUs, Standby Buses were energized from a 1 dedicated Lee Combustion Turbine and an isolated power path at 1715 hours. An NRC Emergency Notification System (ENS) call was made at 0032 hours on June 17, 2017, pursuant to 10 CFR 50.72(b)(3)(v)(A-D), reporting the event as a loss of safety function (Ref.: EN 52812). The reporting premise for the loss of safety function was that there was a 40 minute period, between when both KHUs were declared inoperable and when the LCTs energized the standby busses, when the station was without its normal onsite emergency power sources.

Subsequent troubleshooting efforts concluded that the two KHU1 and 2 breakers were mechanically and electronically sound and operating properly, but due to work activities being performed in the vicinity of these breakers, had probably been inadvertently repositioned. Both breakers were returned to the closed position and a KHU1 functional run was conducted. KHU1 was declared operable at 2150 hours. A KHU2 functional test run was then performed, the unit declared operable at 2351 hours, and the associated TS Conditions related to this event were exited.

Based on a review of OAC data, it was subsequently determined that a loss of safety function existed between 1020 hours (the time when both KHUs were rendered inoperable due to the inadvertent breaker repositioning) and 1715 hours (when the offsite Lee Combustion Turbines were aligned to the standby busses); a period of —7 hours. A loss of safety function is reportable pursuant to 10 CFR 50.73(a)(2)(v)(A-D) as "Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are need to: (A) Shut down the reactor and maintain it in a safe shutdown condition; (B) Remove residual heat; (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident.

From the time KHU inoperability was initially declared at 1635 hours on June 16, 2017, TS LCOs 3.8.1 and 3.7.10 were appropriately entered and the Required Actions completed within the stated Completion Times. However, a review of OAC data revealed that the first KHU was actually inoperable on June 16, 2017, beginning at 0907 hours and as such, the 1-hour TS LCO 3.8.1 Required Action Completion Time (per Required Action C.1) was not satisfied. Consequently, this event is also reportable pursuant to 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by the plant's Technical Specifications.

CAUSAL FACTORS

The direct cause of this event is attributed to the two (2) 24 VDC breakers K1 GCS BK0001 and K2 GCS BK0001, being out of position and rendering both KHUs inoperable due to human error.

CORRECTIVE ACTIONS

1. Completed Verified governor control system integrity on both units which allowed restoration of KHU operability in accordance with TS LCO 3.8.1.

2. Planned a. Enhance Governor Control System (GCS) lesson plans to address this event.

b. Enhance protective measures (e.g., physical / passive / extra signage) requirements for the GCS panels as well as other KHU repositionable components that may be susceptible to a similar event.

c. Improve Work Management controls to address (1) the potential consequences of working on both KHUs at the same time and (2) limiting work on a KHU that is in service.

The planned corrective actions indicated above are NOT considered NRC Commitment items.

SAFETY ANALYSIS

A probabilistic risk assessment (PRA) evaluation was conducted for the period of KHU inoperability to determine the significance of this event. It was determined through a quantitative analysis that the event had a negligible effect on the delta Core Damage Frequency (CDF) and delta Large Early Release Fraction (LERF), resulting in an insignificant impact on the health and safety of the public. This was largely due to the sustained availability of the Lee Combustion Turbine and the Standby Shutdown Facility as well as the Protected Service Water system in a.Loss of Offsite Power situation. These additional options for preventing core damage further reduce the impact of the event on CDF and LERF.

Another major driver in the negligible risk impact was the historical lack of any threat of severe weather over the duration of the KHU unavailability. When KHU failures show up in the risk model as being significant, it is almost exclusively paired with an occurrence of a Loss of Offsite Power due to severe weather. When severe weather is not expected and does not occur, the importance of the KHUs in the risk model drops significantly. Finally, the short time frame the condition existed results in an insignificant risk impact.

ADDITIONAL INFORMATION

Similar Events:

For the preceding three (3) year period, ONS has submitted three (3) LERs which reported under either 10 CFR 50.73(a)(2)(v)(A-D) or 10 CFR 50.73(a)(2)(i)(B) criteria (but not both).

startup transformer which created a temporary loss of the power paths required by TS 3.8.1 and was reported under 10 CFR 50.73(a)(2)(v)(A-D) as a condition that could have prevented.the fulfillment of a safety function.

2. LER 287/2016-001 Revision 0: Described the discovery of a Unit 3 inoperable reactor building cooling unit in which had existed longer than the time allowed by the Technical Specifications and reported per 10 CFR 50.73(a)(2)(i)(B). It was also revealed that Unit 3 had entered the mode of applicability which with the inoperable cooling unit which is prohibited by TS 3.0.4.

3. LER 269-2016-002 Revision 0: Described the discovery of inoperable containment high range radiation monitors due to the potential effects of thermally induced currents during a HELB event in a containment penetration room. It was concluded that the inoperable condition had existed longer than the time allow by the Technical Specification and was reported under 10 CFR 50.73(a)(2)(i)(B).

A review of the aforementioned LERs did not point toward a similar cause or corrective actions that could have prevented this event.

Energy Industry Identification System (EIIS) codes are identified in the text as (XX).

This event is considered INPO Consolidated Events System (ICES) Reportable rather than EPIX reportable (refer to LER line 13 on page 1). There were no releases of radioactive materials, radiation exposures in excess of limits or personnel injuries associated with this event.

05000250/LER-2017-00118 March 2017
16 May 2017
16 May 2017Turkey Point10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
Steam Generator
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Decay Heat Removal
On March 18, 2017 at approximately 1107 hours, the Turkey Point Unit 3 reactor tripped from 100% power as a result of an electrical fault on the 3A 4kV vital bus. The Auxiliary Feed Water System actuated as expected, and the 3A Emergency Diesel Generator started but did not load, as designed, due to the lockout of the 3A 4kV bus. The 3A 4kV bus remained de-energized and the reactor was stabilized in Mode 3. Both Unit 4 High Head Safety Injection (HHSI) pumps were out of service for maintenance. The 3A HHSI pump was unable to be powered from the 3A 4kV bus resulting in a loss of the Safety Injection safety function for approximately 2.5 hours on both Units 3 and 4. The safety function is achieved by operation of two of the four pumps which are shared by both units. The loss of the 3A 4kV bus was caused by an electrical fault created by a conductive foreign material that had entered the current-limiting reactor cubicle that bridged an air gap between an uninsulated bus bar and the cubicle wall. The foreign material was a carbon fiber mesh used to reinforce a Thermo-Lag installation taking place in the 3A 4kV switchgear room. Corrective actions include: 1) The Thermo-Lag installation procedure will be revised to incorporate additional precautions for handling Thermo-Lag materials, and 2) the Engineering product risk and consequence assessment process will be revised to ensure a review is conducted of Safety Data Sheets for material being considered in the design. This event had no effect on the health and safety of the public.
05000298/LER-2017-00227 April 2017Cooper10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Main Steam Isolation Valve
Emergency Core Cooling System
Main Steam Line
Safety Relief Valve
Main Steam

In February and March 2017, three Main Steam Safety Relief Valve (SRV) body assemblies (main body and pilot assembly) and the remaining five SRV pilot assemblies were tested at National Technical Systems Laboratories (formerly Wyle Laboratories). These SRVs had been removed from Cooper Nuclear Station during Refueling Outage 29 in the Fall of 2016. One SRV pilot assembly failed the as-found lift pressure testing; another SRV pilot assembly was conservatively considered a failure due to lack of as-found lift pressure test data since it was inadvertently disassembled prior to performing the as-found lift pressure test.

There were two causes for the failures. One of the SRV pilot assemblies failed due to corrosion bonding; the other SRV pilot assembly failed due to a lack of a barrier to prevent inadvertent disassembly of the SRV pilot prior to testing.

Although the Technical Specifications limits related to the set point lift pressures of the SRV pilot valve assemblies were exceeded, an analysis indicates that the design basis pressures to ensure safety of the reactor vessel and its pressure related appurtenances were not challenged. Public safety was not at risk. Safety to plant personnel and plant equipment was not at risk.

05000327/LER-2017-00126 April 2017Sequoyah10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Secondary containment
Auxiliary Building Gas Treatment System
Shield Building
Emergency Core Cooling System

On March 3, 2017, at 2232 eastern standard time (EST), Door A212 was improperly breached to facilitate a continuous fire watch. On March 7, 2017, at 0830 EST, a senior reactor operator discovered Door A212 blocked open during a walk down of the Auxiliary Building. The open door created a breach of the auxiliary building secondary containment enclosure (ABSCE) boundary. The identified breach exceeded the allowed ABSCE breach margin. As a result, both units entered Technical Specification (TS) Limiting Condition for Operation (LCO) 3.7.12, Condition B for two trains of the Auxiliary Building Gas Treatment System (ABGTS) inoperable due to an inoperable ABSCE boundary in Mode 1, 2, 3, or 4. At 0949 EST, on March 7, the door was closed and both units exited LCO 3.7.12, Condition B. Both trains of ABGTS were inoperable longer than allowed by TS. There were no actual safety consequences as a result of this event.

An evaluation determined the cause to be a less than adequate single barrier breaching standard exists at Sequoyah Nuclear Plant. A contributing cause was an inconsistent approach to entry into the barrier breaching process. Corrective actions include revising the breaching procedure to address all possible breaches and include a matrix for doors and their associated impacts, and addressing potential knowledge deficiencies.

05000458/LER-2017-00218 February 2017
18 April 2017
18 April 2017River Bend10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Emergency Diesel Generator
HVAC
On February 18, 2017, at 3:37 p.m. CST, while a refueling outage was in progress, the operators were shifting subsystems of the main control building ventilation system. The Division 2 "B" chiller had been in service, and it was intended to start the Division 1 "C" chiller to facilitate the outage work schedule. After the swap, operators noted that the air flow was abnormally low, and within approximately four minutes, the "C" chiller tripped. The operators were unsuccessful in attempts to restore the Division 2 subsystem to service;and the abnormal operating procedures for the loss of control building ventilation were then implemented. The electrical distribution subsystems in the control building were declared inoperable due to the loss of the ventilation system. This condition is being reported in accordance with 10 CFR 50.73(a)(2)(v)(A). As described in the causal analysis, a circuit breaker manufacturing defect that violated the single failure requirements of 10 CFR 50 Appendix A, General Design Criteria, was discovered. This is being reported in accordance with 10 CFR 50.73(a)(2)(ii)(B) as an unanalyzed condition. During the restoration of the ventilation system, main control room temperature increased from approximately 73F to 81F as recorded in the operator's logs. No high temperature alarms from the electrical equipment rooms actuated. Thus, this event was of minimal significance to the health and safety of the public.
05000331/LER-2017-00126 January 2017
27 March 2017
27 March 2017Duane Arnold10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Primary containment

On January 25, 2017, at 1800 CST, while operating at 100% power, during planned surveillance testing, Drywell Vent Inboard Isolation Valve, CV4302 (System Code JM), was found to exceed its Leakage Integrity Test limits and was declared inoperable. The initial observed conditions indicated that CV4302 was the likely source of leakage and was the focus of repair efforts. After completion of repairs to CV4302, post maintenance testing showed that the Drywell Vent Line Outboard Isolation valve, CV4303, was exceeding its valve leakage limits, and therefore, was declared inoperable at 0300 CST on January 26, 2017. This resulted in a containment penetration flow path not within purge valve leakage limits and was reported in accordance with 10 CFR 50.72(b)(3)(v)(C) (reference EN#52511). Repairs were completed on CV4303 and both primary containment valves were declared operable at 1007 CST on January 26, 2017.

The cause of this event was determined to be inadequate work instructions and maintenance procedures.

This event was of low safety significance and had no impact on public health or safety. This event is reportable pursuant to 10CFR50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.

05000247/LER-2016-01028 February 2017Indian Point
Docket Number ,
10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Service water
Containment Spray

On November 21, 2016, as a result of investigating an increased level rise in the Waste Hold-Up. Tank (WHUT), Operators identified a corresponding rise in containment sump level. A containment entry was made to investigate the source of the sump level rise and determined the source was a through wall leak in a Service Water (SW) supply pipe elbow to the 24 Fan Cooler Unit (FCU). The leak constituted a breach of a closed system within containment. Technical Specification (TS) 3.6.1 (Containment) was entered and containment declared inoperable. TS 3.6.6 (Containment Spray and Fan Cooler System) was entered when the 24 FCU was secured and SW to the 24 FCU was isolated. Inspections identified a through wall leak on .a SW supply pipe elbow to one of the 24 FCU water boxes.

The leak is on a 3 inch carbon steel epoxy-lined elbow.

The pipe fitting is in an ASME ISI Code Class 3, nuclear safety related piping system.

The direct cause was failure of the interior coating allowing brackish river water to corrode the carbon steel fitting. The root cause was the maintenance coating procedure requirements for post-coating inspections were inadequate. Key corrective actions included removal of the defective elbow and weld repair, recoating and re-installation.

Maintenance procedure 0-SYS-409-GEN will be revised to mandate detailed inspections and/or testing of surface preparation and applied coatings to ensure proper coverage and adhesion. The event had no effect on public health and safety.

NO:

Indian Point 2 05000-247

05000445/LER-2016-00222 February 2017Comanche Peak10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System
Service water
Emergency Diesel Generator
Containment Spray

On September 13, 2016, and September 14, 2016, during plant walk downs by Engineering and the NRC Senior Resident inspector, pressurized fire protection piping in the Service Water Intake Structure was found to not be shielded against a Moderate Energy Line Break (MELB), resulting in inoperability of one train of Service Water for both units.

During extent of condition walk downs conducted on October 6, 2016, October 10, 2016, November 17, 2016, December 5, 2016, and December 22, 2016, additional piping in the Unit 1 and Unit 2 Safeguards and Auxiliary Buildings was found to not be shielded against a MELB, resulting in inoperability of one train of various.safety related equipment for both units. The most likely cause of this event was the methodology used to conduct the initial MELB walk downs was flawed and allowed some MELB threats to be missed.

Corrective actions include shielding the affected piping, performing a 100 percent walk down of rooms containing MELB piping identified for shielding, and revising the systems interaction program maintenance procedure. I All times in this report are approximate and Central Time unless noted otherwise.

05000341/LER-2016-0016 January 2016
23 January 2017
23 January 2017Fermi10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
Reactor Protection System

At 1514 EST on January 6, 2016, while operating at 100 percent Reactor Thermal Power (RTP), the East and West Turbine Bypass Valves (TBV) automatically opened as expected for 3 minutes and 32 seconds in response to the number one High Pressure Turbine Stop Valve (TSV) drifting from full open to 25 percent open due to an actuator malfunction.

Per Technical Specification (TS) Bases 3.3.1.1, TBVs must remain shut while RTP is at or above 29.5 percent to consider all channels of the TSV closure and Turbine Control Valve (TCV) fast closure Reactor Protection System (RPS) functions operable.

Reactor Operators lowered RTP to 91.0 percent and at 1518 EST the TBV automatically closed and the TSV closure and TCV fast closure RPS functions were no longer considered inoperable. TS 3.3.1.1 requires that the TSV closure and TCV fast closure RPS functions be operable at or above 29.5 percent RTP. In this event, during the period of time while TBVs were open, reactor power was maintained above 91 percent and the RPS functions were confirmed to be enabled.

The actuator malfunction was caused by faulty connectors within the actuator. The faulty connectors were replaced.

05000368/LER-2016-00116 September 2016
15 November 2016
15 November 2016Arkansas Nuclear10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
Emergency Diesel GeneratorOn September 28, 2016, Arkansas Nuclear One, Unit 2, initiated a plant shutdown due to the inability to restore one of the Emergency Diesel Generators (EDGs) to an operable status prior to exceeding the Limited Condition Operation action time. It was determined the EDG was inoperable due to the lack of sufficient lubrication in the inboard generator bearing leading to bearing failure. The lack of lubrication was determined to be caused by improper bearing lube oil level indication due an inverted oil sight glass. It was further determined that the insufficient bearing oil level condition had existed since the performance of maintenance activities in June of 2016. The corrective action plan addresses the root cause, contributing cause, extent of condition, and extent of cause.
05000528/LER-2016-0027 September 2016
4 November 2016
4 November 2016Palo Verde10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Reactor Coolant System
Reactor Protection System

On September 7, 2016, at 2131, with Unit 1 in Mode 1 and 100 percent power, the reactor was manually tnpped and reactor coolant pumps were secured due to a control malfunction which prevented closure of a pressurizer spray valve. This event initiated from an unsuccessful attempt to transfer a non-class 120VAC instrument power bus from its normal source to its emergency/alternate source. The transfer was attempted to facilitate an inspection of an electrical load center which was sprayed with water earlier in the day by a leaking sprinkler head following Fire Protection (FP) Department routine testing of a FP water line.

The cause of the spray valve malfunction was a failed pneumatic volume booster in the spray valve actuator system combined with a current to pressure converter (I/P) calibration offset which resulted from a voltage transient during the unsuccessful electrical transfer. These conditions caused the spray valve to stay approximately five percent open when it received a close demand from the spray valve controller. The I/P converter and pneumatic volume booster were replaced and the spray valve was returned to service. Additional corrective actions will adjust preventive maintenance frequency on the pneumatic volume boosters.

In the past three years, PVNGS has not reported a similar event to the NRC.

05000286/LER-2016-0013 November 201621 December 2017Indian Point10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Service water
Containment Spray

On November 3, 2016, as a result of a containment sump pump alarm, operations obtained from Chemistry a sample which indicated a Service Water (SW) leak due to abnormal chlorides levels.

Technical Specification (TS) 3.6.1 (Containment) was entered and containment declared inoperable.

Inspections identified a through wall leak on the 31 SW Fan Cooler Unit (FCU) from FCU coil 3 which - feeds a SW return line header. TS 3.6.6 (Containment Spay and Fan Cooler System) was entered when the 31 FCU was secured and SW to the 31 FCU was isolated. TS 3.6.1, Condition A was exited after the 31 FCU was secured and SW was isolated to the 31 FCU.

The leak is at a 3 inch butt-welded joint that is ISI Class 3, nuclear safety related.

Leak rate estimate was 0.16 gpm. The direct cause was a leak in a SW pipe due to a through-wall flaw as a result of corrosion.

The root cause is indeterminate. The specific. cause for the pipe joint defect requires the component to be removed and a metallurgical failure analysis performed. Corrective actions included installation of a leak limiting clamp. The clamp is being monitored daily and UT monitoring will be performed every 90 days until the pipe is repaired. The pipe will be replaced in the next refueling outage in 2017.

The affected pipe will be analyzed after removal. The event had no effect on public health and safety.

Indian Point 3 05000-286 APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to Note: The Energy Industry Identification System Codes are identified within the brackets ().

DESCRIPTION OF EVENT

On November 3, 2016, while at 100 percent reactor power, operations received a "Vapor Containment (VC) Sump Pump Running," alarm at approximately 00:27 hours, following a VC sump pump out. In accordance with actions of 3-ARP-009, a check of the Unit Log identified that the last sump pump out was on October 30, 2016. Receipt of this alarm was earlier than expected and a possible indicator of a leak. VC radiation monitors R-11 and R-12 (IL), VC Humidity (1,7), and Fan Cooler Unit (FCU) Weir Levels WI were normal. As a result of the early VC Sump Pump Running alarm (FQA), operations requested Chemistry to obtain a sample of the VC pump out line. Results of the sample showed approximately 149 ppm chlorides, indicating a possible Service Water (SW) (BI) leak due to abnormal chloride levels. Operations entered Technical Specification (TS) 3.6.1 (Containment), Condition A (Containment Inoperable) at 03:00 hours, due to the possibility of a loss of containment (NH) integrity. At 3:19 hours, the 31 FCU (FCU) was secured due to suspected SW FCU coil leakage and entered TS 3.6.6 (Containment Spray System and Containment Fan Cooler System), Condition C (One Containment FCU Train Inoperable). At 3:19 hours, a Safety Function Determination was performed which concluded there had been a loss of safety function and VC became inoperable when indications of a possible SW leak was identified for the 31 FCU. At 3:44 hours, TS 3.6.1, Condition A was exited after the 31 FCU was secured and SW was isolated to the 31 FCU. The leak was recorded in Indian Point Energy Center (IPEC) corrective action program (CAP) as CR-IP3-2016-03607. An 8 hour non-emergency event notification (#52344) was made under 10 CFR 50.72(b) (3)(v) for a loss of safety function.

The SW System (SWS) (BI) is designed to supply cooling water from the Hudson River to various heat loads in both the primary and secondary portions of the plant. The design ensures a continuous flow of cooling water to those systems and components necessary for plant safety during normal operation and under abnormal or accident conditions. The SWS consists of two separate, 100% capacity, safety related cooling water headers. Each header is supplied by 3 pumps to include pump strainers, with SWS heat loads designated as either essential or non-essential.

The essential SWS heat loads are those which must be supplied with cooling water immediately in the event of a Loss of Cooling Accident (LOCA) and/or Loss of Offsite Power (LOOP). The essential SWS heat loads can be cooled by any two of the three SW pumps on the essential header. Either of the two SWS headers can be aligned to supply the essential heat loads or the non-essential SWS heat loads.

A VC entry was performed and inspections identified leak indications at the 31 FCU on the 3rd coil feeding the SW return line fPSP1. To confirm the specific leak location, scaffolding was erected and insulation was removed. A through wall leak was identified on the 31 SW Fan Cooler Unit (FCU) at weld B-297, in branch line C from FCU coil 3. This is one of the 3 inch SW return branch lines from the 31 FCU cooling coils which feeds a 10 inch SW return line header 12b upstream of containment penetration Mb. Line 12b is the SW system return piping from the 31 FCU back to the river.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to 2016 - 001 - 00 The piping for the 3 inch cooling coil return line is 904L stainless steel (SS) with a nominal pipe wall thickness for Schedule 40 pipe (0.216 inches). Leak rate estimate was 0.16 gpm. The leak is at a 3 inch butt-welded joint between a 904L stainless steel elbow (PSF) and pipe IPSP1 located on approximately the 76 foot elevation in containment. The piping leak is in a moderate energy ASME ISI Code Class 3, nuclear safety related piping system. 904L SS material is susceptible to the development of corrosion pits. Pin hole leaks and weld defects in this piping have previously occurred and have been evaluated. The evaluation concluded the 904L piping does not have a general corrosion problem.. Current analysis for SW pipe failures are postulated to be limited to small through-wall leakage flaws as opposed to guillotine breaks. There is no evidence of leakage at any other location on this weld or elsewhere on the piping adjacent to it.

Code Class 3 piping systems are addressed in ASME Code Case N-513-3. This Code Case provides the requirements for demonstrating structural integrity and therefore operability of a flawed pipe section. Characterization of the weld condition was performed by conducting an ultrasonic examination (UT) on November 4, 2016. The weld was examined circumferentially in a 1/5 inch by '1 inch grid pattern and by using a bulls-eye grid pattern in '4 inch increments. These UT, (Non Destructive Examinations) NDE results were documented in an NDE report. However, due to physical obstructions presented by the FCU enclosure, two circumferential grid rows on the backside of the weld could not be reached. Due to the leak location on the bottom side of the pipe on the side opposite from the FCU enclosure, the bulls-eye grid was not obstructed, and all required readings were taken. As a result of limited access, the UT examination of weld B297 resulted in completion of only approximately 70 percent of the circumference of the weld. The remaining 30 percent (approximately 3 inches) was unable to be inspected due to space constraints between the weld and the adjacent FCU plenum wall. ASME Code Case N-513-3 requires the flaw geometry to be characterized by volumetric inspection methods or by physical measurement. It mandates that the full pipe circumference at the flaw location be inspected to characterize the length and depth of all flaws in the pipe section.

Since a full volumetric examination could not be completed, the Code Case requirements could not be met. An immediate on-line weld repair of the defect was not considered feasible due to restrictions preventing 360 degree access, time required for work prep, and the potential for excessive sump filtration loading. As such, an NRC Relief Request to deviate from the 10CFR50.55a ASME Code requirements, specifically full compliance with ASME CC-N-513-3 was required. Therefore, pursuant to 10CFR50.55a(z)(2) Entergy requested relief by letter NL-16-133 (Request IP3-ISI- RR-10, Alternative to the Full Circumferential Inspection Requirement of Code Case N- 513-3), dated November 7, 2016. The NRC approved the relief request which concluded the inability to obtain full circumference readings does not adversely impact the ability to fully characterize the weld condition vs the code case requirements.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to The approval of the relief request allowed Entergy to re-establish SW to the FCU to verify that leakage limits are met using a qualified clamp over the pinhole leak.

The leakage will be inspected daily in accordance with the Code Case requirements.

SW piping to the 31 FCU must be isolated when an allowable leakage is exceeded. The qualified clamp is an engineered clam-shell type clamp comprised on an outer metal jacket and rubber gasket. The clamp is classified as a temporary modification. The clamp will withstand post-accident containment pressure, temperature and environment, is located away from potential missiles and, pipe whip effects, is dedicated for safety-related use, and is rigidly attached to Seismic Category 1 piping. The clamp over the defect will return the system to its original containment integrity configuration and allow the 31 FCU to remain operable.

The defect in the SW return pipe from the 31 FCU was evaluated with respect to TS 5.5.15 (Containment Leak Rate Testing Program), and the Appendix J Leakage program.

TS 5.5.15 requires that the SW in-leakage into containment must be limited to less than 0.36 gpm per FCU when pressurized equal to or greater than 1.1Pa. This limit protects the internal recirculation pumps from flooding during the 12 month period of post-accident recirculation. TS 5.5.15 also implements the leakage rate testing of the containment as required by 10CFR50, Appendix J. The maximum leakage to assure that the post-accident containment leakage remains within allowable limits is 0.023 gpm. This limit is based upon an evaluation to calculate the amount of SW which can leak through this pinhole under normal system operating conditions to ensure that 10CFR50 appendix J containment leakage limits are not exceeded under any mode of operation including accident conditions. The leak does not impinge upon any safety related equipment. As a result, no damage from the leakage is expected to occur.

Based on UT measured readings from the NDE Report, a new calculation was generated (IP-CALC-16-00079 FCU 31 Leak) per the ASME CC-N-513-3 requirements. The minimum required thickness for the elbow containing the weld B297 is 0.073 inches. The minimum measured thickness was 0.117 inches. The maximum allowable axial flaw size is 4.11 inches and the maximum allowable circumferential flaw size is 3.65 inches.

The existing flaw is characterized as approximately 0.50 inches by 0.50 inches, and the uninspected arc length (approximately 3 inches) of the pipe circumference is less than the allowable circumferential flaw length. Therefore, if the entirety of the uninspected portion of the pipe were to be considered a flaw, the pipe would still retain its structural integrity as evaluated in the new calculation. The pinhole flaw is opposite the uninspected portion and the flaw sizes of the two areas are independent and not additive. Based on this information, the pipe is structurally adequate for service consistent with the requirements of ASME Code Case N-513-3. The remaining service life was calculated to be 3.3 years, which is beyond the next scheduled refueling outage in the spring 2017 when a permanent repair will be made.

An extent of condition review determined the Code Case requires five similar and susceptible locations in the SW system to be volumetrically examined. NDEs were performed on November 5, 2016, on five 31 FCU SW pipe welds and recorded in NDE reports. All five weld locations were found to be structurally acceptable and documented in CR-IP3-2016-03607, corrective action (CA-6). The additional inspections confirm the integrity of the SW piping inspected since all UT data measurements were above the 87.5 percent of pipe nominal wall thickness. Also, there was no evidence of additional leakage at any other place in the 31 FCU 3 inch return line or at any other location in the other four FCU return lines. Unit 2 does not apply as it does not have similar 904L SS FCU supply or return lines.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to

CAUSE OF EVENT

The direct cause was a SW leak associated with the 31 FCU at weld B297 in branch line C from coil 3 feeding the 10 inch SW return line 12b. The leak was from a through-wall pinhole flaw at a butt-welded joint between a 904L SS elbow and pipe in containment. The likely degradation mechanism leading to the leak was corrosion. The pipe with the flaw resulted in containment out leakage in excess of 10CFR50, Appendix J limits. The root cause is indeterminate. The specific cause for the pipe joint defect requires the component to be removed and a metallurgical failure analysis performed.

CORRECTIVE ACTIONS

The following corrective actions have been or will be performed under the Corrective Action Program (CAP) to address the causes of this event:

  • A leak-limiting engineered clam-shell type clamp was applied to the pipe flaw.
  • The clamp is being monitored daily by a special operator log for any signs of increased leakage. The maximum allowed leakage rate past the clamp is 0.023 gpm.
  • UT monitoring will be performed every 90 days until the pipe is repaired.
  • The pipe/elbow will be replaced in the next refueling outage (RO) in the spring 2017.
  • The removed pipe/elbow will be inspected and a metallurgical analysis performed by an independent vendor to determine the specific cause.
  • A volumetric inspection of a sample of 3 inch 904L SS butt-welds at the 32, 33, 34, and 35 FCUs will be performed in the spring 2017 RO.
  • The Generic Letter 89-13 Program will be revised to include a requirement to conduct a definitive number of 904L weld volumetric inspections each pre-outage interval.
  • This LER will be updated after engineering review of the metallurgical analysis and revision as necessary of the cause analysis.

EVENT ANALYSIS

The event is reportable under 10 CFR 50.73(a)(2)(v)(C). The licensee shall report any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to (C) Control the release of radioactive material. This condition meets the reporting criteria because TS 3.6.1 Containment Operability was not met.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to The pipe flaw leakage was approximately 0.16 gpm which was greater than the calculated 10 CFR 50, Appendix J allowable leak rate of 0.023 gpm. TS 3.6.1 (Containment) requires the containment to be operable in Modes 1-4. TS Surveillance Requirement (SR) 3.6.1.1 requires visual examinations and leakage rate testing in accordance with the containment Leakage Rate Testing Program specified in TS 5.5.15.

SR 3.6.1.1 leakage rate requirements comply with 10 CFR 50, Appendix J, Option B. As SW is required in an accident, the SW to the FCU would not be isolated in DBA and the piping credited as a closed system inside containment for containment integrity.

Consequently, defects discovered within the FCU SW piping may adversely affect containment integrity and the ability to control releases of radioactive material.

The condition also meets the reporting criteria of 10 CFR 50.73(a) (2)(i)(B). The licensee shall report any operation or condition which was prohibited by the plant's TS. During the previous period of operation for an unknown period of time the SW pipe contained a through wall leak that did not meet code requirements. This previously unrecognized condition required entry into TS 3.7.9 and corrective actions implemented to return the pipe to operable. Failure to comply with the TS LCO and perform required actions is a TS prohibited condition.

PAST SIMILAR EVENTS

A review of the past three years of Licensee Event Reports (LERs) for events that involved containment integrity due to flawed piping credited as a closed system inside containment. No applicable LERs were identified. There was one LER, LER-2014- 002 reporting a Technical Specification prohibited condition for a flaw discovered on a SW pipe connected to the Component Cooling Water Heat Exchanger. This LER is not similar as the impacted piping is outside containment and not credited as a closed system for containment integrity.

SAFETY SIGNIFICANCE

This condition had no effect on the health and safety of the public.

There were no actual safety consequences for the event because there were no accidents or events during the degraded condition.

There were no significant potential safety consequences of this event. The leakage from the affected SW pipe was within the capability of the SW system to provide adequate SW flow to SW loads. The degraded piping was on the discharge of the FCU therefore any failure would not prevent the SW cooling function. Current analysis for SW pipe failures are postulated to be limited to small through-wall leakage flaws as SW is defined as a moderate energy fluid system. The SW leak would eventually drain to the containment sump. The containment sumps have pumps with sufficient capacity to remove excessive leakage and instrumentation to alert operators to a degraded condition.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to The containment consists of the concrete reactor building, its steel liner, and the penetrations through the structure. The containment building is designed to contain radioactive material that might be released from the reactor following a design basis accident (DBA). The containment building steel liner and its penetrations establish the leakage limiting boundary of the containment. Maintaining the containment operable limits the leakage of fission product radioactivity from the containment to the environment. The DBA analysis assumes that the containment is operable such that, for the DBAs involving release of fission product radioactivity, release to the environment is controlled by the rate of containment leakage.

The containment was designed with an allowable leakage rate of 0.1 percent of containment air weight per day. Containment isolation valves form a part of the containment pressure boundary. Two barriers in series are provided for each penetration so that no single credible failure or malfunction of an active component can result in a loss of isolation or leakage that exceeds limits assumed in the safety analysis. One of these barriers may be a closed system such as the SW piping for the FCUs. The only time containment integrity can be affected is post accident when the FCUs safety function is being performed and SW pressure for the FCU cooling piping and coils fall below peak accident pressure. Mitigation of radiation release by the degraded SW pipe pathway can be by use of radiation monitors R-16A and R-16B which monitor containment fan cooling water for radiation indicative of a leak from the containment atmosphere into the cooling water. If radiation is detected, each FCU heat exchanger can be individually sampled to determine the leaking unit. The SW for the 31 FCU can be isolated to prevent radioactive effluent releases. During the time the FCU SW piping was degraded there was no leakage out of containment.

A risk assessment was performed to determine the overall probability of a core damage event which could cause a loss 'of containment integrity due to a SW to FCU leak assuming it would take 5 days to detect a SW leak to a FCU. The risk result was 7.8E-8 which is considered negligible in terms of both core damage and large early release.

Indian Point 3 05000-286

05000286/LER-2015-00515 June 2015
14 September 2016
14 September 2016Indian Point10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Steam Generator
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Main Transformer
Main Turbine
Control Rod
Main Steam
On June 15, 2015, an automatic reactor trip (RT) occurred due to a Main Turbine-Generator trip as a result of a direct generator trip from the Buchanan switchyard. All control rods fully inserted and all required safety systems functioned properly. The plant was stabilized in hot standby with decay heat being removed by the condenser. There was no radiation release. The emergency diesel generators did not start as offsite power remained available. The auxiliary feedwater system actuated as expected due to steam generator low level from shrink effect. Prior to the RT, Con Edison requested that Main Generator Output breaker 1 be opened to support removing 345kV feeder W97 from service for removal of a Mylar balloon on a 345kV conductor at the Millwood substation. After breaker 1 was opened, Main Generator Output breaker 3 opened initiating a direct generator trip signal due to a fault in South Ring Bus breaker 5. Direct cause of the RT was failure of 345kV breaker 5 due to an internal fault which activated protective relays that opened the remaining Main Generator Output breaker 3 which initiated a trip sequence that resulted in a RT. The root cause was Indian Point Energy Center did not provide formal notification of industry operating experience (OE) to Con Edison owner of breaker 5. The specific OE pertained to ITE Type GA breakers. Corrective actions include replacement of breaker 5. Procedure EN-0E-100 (OE Program) was revised to add a section describing how to initiate formal notification to external groups when OE related to components they own and/or control can affect generation. A new site procedure was issued (SMM-LI-126) to formalize the site process for notifying external groups of OE that can affect generation. The event had no effect on public health and safety.
05000286/LER-2015-0049 May 2015
14 September 2016
14 September 2016Indian Point10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Steam Generator
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Main Transformer
Control Rod
Main Steam

On May 9, 2015, an automatic reactor trip (RT) occurred due to a Turbine-Generator trip as a result of a failure of the 31 Main Transformer (MT). All control rods fully inserted and all required safety systems functioned properly. The plant was stabilized in hot standby with decay heat being removed by the condenser. There was no radiation release. The emergency diesel generators did not start as offsite power remained available. The auxiliary feedwater system actuated as-expected due to steam generator low level from shrink effects. Control room operators received alarms on the fire detection panel of the activation of the 31 MT and curtain wall deluge valves. Report to operators that there was an explosion and fire on the 31 MT. The plant fire brigade responded to the fire. The 31 MT had failed. Due to collateral influence from the 31 MT failure, the deluge system for the 32 MT and Unit Auxiliary transformer had also activated. In accordance with the emergency plan a Notice of Unusual Event (NUE) was declared at 1801 hours, which was terminated at 21:04 hours. The direct cause was an internal fault of the A Phase high voltage winding in the upper portion of the transformer.

The root cause was vendor design/manufacturing deficiency that caused an internal failure that resulted in a fault on the A phase HV side of the transformer and the A phase HV voltage bushing. Key corrective actions included replacement of the 31 MT with a spare transformer, associated acceptance testing, repair of the isophase bus ducting for the 31 MT, inspections, cleaning, testing of the 32 MT, the Unit Auxiliary Transformer, high voltage components, isophase buses and main generator. A 4-year PM was prepared to perform Partial Discharge testing on the Unit 2, and Unit 3 MTs, Unit 2 and Unit 3 Auxiliary Transformers and the Unit 3 GT Auto Transformer The event had no significant effect on public health and safety.

FACILITY NAME (1) DOCKET (2) LER NUMBER (6) PAGE (3)

05000286/LER-2015-0078 July 2015
6 September 2016
6 September 2016Indian Point10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(iv), System Actuation
Steam Generator
Feedwater
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Main Condenser
Control Rod
Main Steam

On July 8,2015, during surveillance testing, the Control Room received a 6.9kV motor trip alarm due to 31 Condensate Pump (CP) Motor circuit breaker trip on overcurrent. .

Operators entered Alarm Operating Procedure 3-A0P-FW-1 due to loss of the 31 CP and initiated a load reduction. During this time the Main Boiler Feedwater Pump (MBFP) suction pressure decreased to its suction pressure cutback controller pressure range and its output decreased MBFP speed control to a minimum. The 31 MBFP speed control signal locked in at this minimum speed signal due to actuation of the MBFP Lovejoy speed control system Track and Hold feature. Due to this minimum 31 MBFP condition, the 31 MBFP , recirculation valve opened causing the 31 MBFP check valve to close. With the 31 MBFP unloaded, Steam Generator (SG) water levels decreased and at 15 percent operators manually tripped the reactor. The Auxiliary Feedwater System automatically started as expected due to SG low level from shrink effect. Direct cause was the 31 MBFP entered a Hold condition erroneously due to a miss-wired Track and Hold board in the speed control system. The root cause was the procurement for the MBFP Lovejoy Track and Hold boards was at an insufficient quality level commensurate with its criticality. There was a failure to mandate functional testing and wiring verification requirements on the vendor to ensure the procurement of a quality product. Corrective actions included replacement of MBFP track and hold board and 31 CP motor. A new replacement Track and Hold circuit board for both the 31 and 32 MBFP speed control system with the miss-wiring corrected was installed. The quality levels for the Track and Hold boards were revised from Q4 to Q3.

MBFP Lovejoy speed control maintenance procedures and site vendor manuals were revised to include more detail. The event had no effect on public health and safety.

FACILITY NAME (1) DOCKET (2) LER NUMBER (6) PAGE (3)

05000346/LER-2016-00615 August 2016Davis Besse10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Emergency Diesel Generator

On June 16, 2016, the Davis-Besse Nuclear Power Station (DBNPS) was in Mode 1'and 100 percent reactor power. At 1137 hours, during review of industry operating experience, an issue was identified for the potential impact of low barometric pressure associated with a tornado on the Emergency Diesel Generators (EDGs). The EDGs are equipped with a crankcase positive pressure trip with a set point of approximately 1 inch of water. It was determined that a design basis tornado could create sufficient low pressure to potentially actuate the crankcase positive pressure trip due to different vent paths between the EDG Room and the EDG crankcase. If the crankcase pressure trip occurs before the EDG starts on an emergency signal due to the tornado, the crankcase pressure trip would cause an EDG lockout. The EDG lockout would then prevent either an EDG normal or emergency start until operators could manually reset the lockout. This condition could potentially affect both EDGs simultaneously.

This was an original EDG protective logic circuitry design issue that did not anticipate the interaction between the crankcase pressure trip and the outside atmospheric pressure. Corrective actions included temporarily disabling this trip and longer-term plant modification to make the change permanent.

This event is being reported pursuant to 10 CFR 50.73(a)(2)(i)(B), 10 CFR 50.73(a)(2)(ii)(B), and 10 CFR 50.73(a)(2)(v)(A) through (D).

05000529/LER-2016-0019 August 201610 October 2016Palo Verde10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Steam Generator
Reactor Coolant System
Feedwater
Main Steam Isolation Valve
Auxiliary Feedwater
Main Steam Safety Valve
Main Steam Line
Main Steam

On August 9, 2016, Technical Specification (TS) Limiting Condition for Operation (LCO) 3.7.2, Condition A was entered for Unit 2 main steam isolation valve SGE-UV-171 (MSIV 171) train A actuator to perform a nitrogen pre-charge check.

The check identified low nitrogen pre-charge pressure on the train A accumulator. An engineering evaluation determined that the MSIV 171 train A actuator was inoperable since July 30, 2016 due to a nitrogen leak on the accumulator. This inoperability period exceeded the 7-day required action completion time for one MSIV actuator train. The MSIV 171 train A actuator was restored to operable status and LCO 3.7.2, Condition A was exited on August 9, 2016. The accumulator leak was repaired on October 5, 2016. Insufficient monitoring, trending, and understanding of reservoir hydraulic fluid level trends in relation to the nitrogen pre-charge required for MSIV operability led to the extended inoperability period.

Operator training will be revised to improve understanding of the system and the limitations of the hydraulic fluid level alarm. Additional corrective actions will revise procedures to provide enhanced rigor for the control of operations condition monitoring thresholds for an MSIV to ensure appropriate response times. Maintenance procedures will also be revised to provide more explicit guidance to minimize the potential for leaks. In the past 3 years, PVNGS has not reported a similar event to the NRC.

05000286/LER-2015-0061 July 2015
8 August 2016
8 August 2016Indian Point10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Steam Generator
Reactor Coolant System
Reactor Protection System
Auxiliary Feedwater
Main Steam Safety Valve
Main Steam Line
Main Steam

On July 1, 2015, Engineering was notified by

  • Wyle Laboratories that two of three Pressurizer Code Safety Valves (RC-PCV-464 and RC-PCV-468) were outside their As-Found lift set point test acceptance criteria (2411 - 2559 psig).

The As-Found set pressure testing acceptance criterion for operability is 2485 +/-3%. The SVs were removed during the last refueling outage (RO) in the spring of 2015 and sent offsite for testing.

Testing was performed within one year of removal as required by the Inservice Testing Program. SV RC-PCV-464 lifted at 2573 psig and SV RC-PCV-468 lifted at 2379 psig which is outside their set pressure range. The remaining SV tested satisfactorily. All three SVs were found with zero seat leakage. During the RO all'three SVs were removed and replaced with certified pre-tested spare SVs.

The SVs installed during the RO were As- Left tested to 2485 +/-1% with zero seat leakage in accordance with procedure 3-PT-R5A.

Technical Specification (TS) 3.4.10 (Pressurizer Safety Valves), requires three pressurizer safety valves to be operable with lift settings set at greater than 2460 psig and less than 2510 psig.

TS Surveillance Requirement (SR) 3.4.10.1 requires each PSV to be verified operable in accordance with the Inservice Testing Program.

The valves were disassembled and internals inspected. The most probable cause of SV RC-PCV-464 lifting greater than 3% of its nominal setpoint was setpoint drift. The most probable cause of RC-PCV-468 lifting below 3% of its nominal set point was set point drift. Corrective actions included replacement of all three code safeties with pretested spares and disassembly and inspection of valves RC-PCV-464 and RC-PCV-468. The event had no effect on public health and safety.

05000286/LER-2014-00413 August 2014
1 August 2016
1 August 2016Indian Point10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Reactor Protection System
Emergency Diesel Generator
Auxiliary Feedwater
Main Condenser
Control Rod
Main Steam
On August 13, 2014, Instrumentation and Control (I&C) technicians started performance of an 8-hour scheduled surveillance 3-PC-OLO4A (Pressurizer Pressure Loop P-455 Channel Calibration) with Loop I in test and tripped. The test was approved by I&C and operations to be stopped for a break with the bistables still tripped, Channel I in test. During the break, an automatic reactor trip (RT) occurred as a result of meeting the trip logic for Overtemperature Delta Temperature (OTDT). All control rods fully inserted and all required safety systems functioned properly. The plant was stabilized in hot standby with decay heat being removed by the main condenser. The Auxiliary Feedwater System automatically started as expected due to SG shrink effect. No work was being performed at the time of the RT and no actual OTDT existed. The direct cause of the RT was a spurious signal spiking on channel 3 of the OTDT circuitry with another channel tripped for testing. The two possible root causes were 1) a random failure of the OTDT static gain unit (Foxboro Integrator/Converter module QM-431D), 2) loose wiring connection on distribution block DB-4 (output of static gain unit QM-431) due to workmanship issue. Corrective actions included replacement of static gain module QM- 431D and associated PR N-43 isolation amplifies NM306 and NM307, and static gain modules QM-421D, and QM-411D, replacement of three OPDT trip bistables (TC-421 A/B, TC-431 A/B, TC-441 A/B), replacement of setpoint module TM-432B (other setpoint modules had been previously replaced), and replacement of Loop 3 T(avg) E/I converter TM-432R. Procedure IP-SMM-WM-140 revised to include expectation on minimizing break times when a channel is tripped. The event had no effect on public health and safety.
05000388/LER-2016-00512 July 2016Susquehanna10 CFR 50.73(a)(2)(v), Loss of Safety FunctionFeedwater
High Pressure Coolant Injection
Reactor Pressure Vessel

On 5/13/2016 at 0055, the Unit 2 Unit Supervisor directed manually overriding High Pressure Coolant Injection HPCI (HPCI) immediately prior to a manual scram during a plant transient.

This event is being reported under 10 CFR 50.73(a)(2)(v) There were two causes of this event. First, the Unit Supervisor made a decision to prematurely override HPCI to minimize distractions later in the shutdown without procedural guidance to do so. Second, weaknesses in teamwork and oversight prevented the mistake from being corrected by the crew. Immediate corrective actions include removing qualifications from the individuals involved and communicating expectations with the remaining crews. Additional corrective actions being taken include incorporating this event into initial licensed operator training and a Human Performance Improvement Plan will be created to address gap noted in the crew's performance.

05000247/LER-2016-0096 July 20166 September 2016Indian Point10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v), Loss of Safety Function
Steam Generator
Reactor Coolant System
Reactor Protection System
Auxiliary Feedwater
Control Rod
Main Steam

On July 6, 2016,Instrument and Control (I&C) technicians were preparing to perform 2-PT-2M3A (RPS Logic Train B Actuation Logic Test and Tadot). Prior to starting the test, the I&C technicians were unable to locate key #184 that was identified in the test as associated with the reactor trip breaker B bypass key switch. Control Room staff recommended obtaining key #183 associated with reactor trip breaker A bypass key switch to use in lieu of key #184. To ensure the key would work prior to starting the test, the train B bypass key switch was positioned by an I&C technician to the Defeat position. Because reactor trip Bypass Breaker B was in the racked out position, when the key switch was taken to the Defeat position, it caused the normal Reactor Trip Breaker B to open, which initiated a reactor trip (RT) and auxiliary feedwater system actuation. The direct cause was an I&C technician turned the key interlock to defeat on switchgear Channel B Reactor Protection Logic without having the BYB Bypass breaker racked in and closed. The root cause was Indian Point personnel emphasized work culture production goals without fully recognizing the need to maintain fundamental standards and expectations for nuclear workers. Key corrective actions included site all-hands meeting discussing the event, lessons learned, reinforced expectations and the Fleet Refocus Initiative. As an interim action, all essential work that effects generation was required to have direct oversight by a superintendent or above, all work start authorizations provided by operations undergo a work challenge utilizing a new checklist from this event. Complete the actions associated with the Fleet Refocus Observation program. The event had no effect on public health and safety.

Indian Point 2 05000-2'47 APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to Note: The Energy Industry Identification System Codes are identified within the brackets (1.

DESCRIPTION OF EVENT

On July 6, 2016,while at 100 percent reactor power, preparations were in progress to commence a scheduled bi-monthly surveillance test in accordance with 2-PT-2M3A (RPS Logic Train B Actuation Logic Test and TADOT (>25% Reactor Power)). The purpose of the surveillance is to perform actuation logic testing of the Reactor Protection System (JC) logic Train B in accordance with Technical Specification (TS) 3.3.1 (Reactor Protection System Instrumentation) Table 3.3.1-1, Function 20, Surveillance Requirement 3.3.1.5. The test had been originally scheduled for June 30, 2016, but due to concerns about Battery Changer 22 grounds, the test was re-scheduled for the following week., At approximately 07:30 hours, on July 6, 2016, a pre-job briefing was held with four I&C technicians and the I&C job Supervisor. Subsequent to the briefing, the I&C technicians went to the Control Room (NA) and informed the Control Room Supervisor (CRS) of the test and what to expect. In the prerequisites section of 2-PT-2M3A, the breaker interlock key number 182, 184 or equivalent was to be obtained from operations prior to commencing the test. At approximately 9:15 hours, I&C personnel determined neither key number 182 nor key number 184 could be found in the Control Room key locker. The CRS suggested that the Train A key number 183 could be used as an equivalent because it was believed that both trains were keyed the same.

Due to concerns with the short Technical Specification (TS) 8-hour Allowed Outage Time (AOT) for the test the I&C technicians wanted to ensure the key would work prior to entering the TS Limiting Condition for Operation (LCO) and starting the test and discussed it with the CRS. The key concerns were discussed with the CRS. After a brief discussion, the I&C technicians believed that Operations gave them permission to test the key prior to starting the surveillance test. Operations believed that the I&C technicians would test the key during the surveillance.

At approximately 9:30 hours, two of the I&C technicians, one operator and two Nuclear Plant Operator (NPOs) took key number 183 (designated for Train A) to the location of the Reactor Trip Breakers (RTBs) (BKR)(Cable Spreading Room) (NA). The 8-hour TS LCO was not entered. Two non-licensed operators (NPOs) were present in the Cable Spreading Room to rack in the bypass breaker when requested by the I&C technicians.

The Field Shift Supervisor (FSS) was also there to inspect cables that were utilized with the Rod Drop Testing during the recent outage. One of the I&C technicians called the Control Room and told another I&C technician, who was staged in the Control Room, that they would receive an annunciator on Panel SK, Window 2-5. The Control Room operator acknowledged the alert of an expected alarm and the I&C technician in the Control Room relayed the acknowledgement to the I&C technician in the Cable Spreading Room containing the RTBs.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to An I&C technician signaled the other I&C technician that was at the RTBs to test the key. Without using a procedure or an approved work instruction, the other I&C technician positioned the Train B bypass key switch to defeat.. Because reactor trip Bypass Breaker B was in the racked out position, when the train B bypass key switch was taken to the Defeat position, it caused the normal Reactor Trip Breaker B to open, which initiated a reactor trip (RT) at approximately 9:38 hours.

All control rods (AA) fully inserted and all required safety systems functioned properly. The plant was stabilized in hot standby with decay heat being removed by the condenser (SG). The auxiliary feedwater system (BA) actuated as expected due to steam generator low level from shrink effect.

Normally during performance of the test, the train B bypass key switch is only positioned to Defeat after Bypass Breaker B has been closed and the Reactor Trip Breaker B- has been opened. The condition was recorded in the Indian Point Energy Center (IPEC) Corrective Action Program (CAP) in. Condition Report CR-IP2-2016-04320.

The reactor protection system (RPS) (JC) initiates a reactor shutdown, based on values of selected unit parameters, to protect against violating the core fuel design limits and reactor coolant system pressure boundary during anticipated operational occurrences and to assist the Engineered Safety Feature Systems in mitigating accidents. The RPS instrumentation is segmented into four distinct but interconnected modules one of which is reactor trip switchgear that includes the reactor trip breakers (RTBs) and Bypass Breakers. These components provide a means to interrupt power to the control rod drive mechanisms (CRDMs) and allows the rod cluster control assemblies (RCCAs) or rods to fall into the core and shut down the reactor. The bypass breakers allow testing of the RTBs at power. The control rod drive system is designed such that the control rods are held in place and are capable of being moved only when its power supply is energized. Two RTBs placed in series with the control rod drive power supply remain closed as long as their respective under-voltage coils are kept energized by the RPS logic buses. Two bypass breakers are provided to allow in service testing of either RTB. The key-interlock switch is provided such that if both bypass breakers are closed at the same time while racked in, both bypass breakers will be tripped. This interlock is defeated in the test position with the key to allow for tripping of the undervoltage device of the bypass breaker when the reactor is in operation. The key interlock switch at the Reactor Trip Switchgear is placed in the Defeat position to prevent repeated breaker operation as the logics are tripped and reset.

During normal testing of the RPS Logic, the bypass breaker is racked in and closed and the key-interlock switch would then only bring in the alarm in the Control Room supervisory annunciator. For this event the bypass breaker was not racked in (closed).

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to The bypass breakers must be manually closed and under no circumstances should both bypass breakers be racked in and closed at the same time. During normal testing of Channel B, the associated key-interlock switch would have been placed in the defeat position. This would have resulted in: 1) Illuminating a red light on the Train B cabinet, 2) Annunciating an alarm RTB & BYA Train B Defeat on the Control Room supervisory annunciator, 3) Opened up the closing circuit of RTB which is being tested, 4) Opened up the coil circuit of undervoltage trip devices for breakers RTB and BYA which is being tested and preventing the unit from tripping. In this event the key bypass switch was turned to the defeat position while the Bypass Breaker was still racked out (open) which de-energized the undervoltage coil for the B RTB which caused it to open and trip the unit.

An extent of condition (EOC) review determined the condition is bounded to only the RTBs because they are the only breakers with a key-interlocked switch such that if both bypass breakers are closed at the same time while racked in, both bypass breakers will be tripped. The test procedure for unit 2 calls for key number 182, 184 or allows for an equivalent key to be used. This is vague guidance unlike unit 3 which only has one key. The Unit 2 test procedure 2-PT-2M3A will be revised to remove "equivalent.

CAUSE OF EVENT

The direct cause of the RT was due to operating the "B" RPS bypass key out of sequence during Reactor Protection logic testing. An I&C technician turned the key interlock to defeat on switchgear Channel B Reactor Protection Logic without having the BYB Bypass Breaker racked in and closed, which opened the undervoltage tripping device of the RTB and tripped the reactor. The I&C technician turned the key without procedural guidance. The I&C technicians were testing the key with verbal guidance from operations, due to vague procedure guidance in 2-PT-2M3A, that allowed an equivalent key to be used (number 183). Due to not stopping when unsure (conservative decision making), the I&C technicians tested the key prior to starting the surveillance because of perceived time pressure.

The root cause (RC) of the event was that IPEC personnel emphasized work culture production goals for productivity, schedule adherence, and backlog reduction without fully recognizing the need to maintain fundamental standards and expectations for nuclear workers, such as procedure use and adherence and staying in process during work activities. The RC resulted in the I&C technician turning the key without procedure guidance or work instructions and tripped the plant.

CORRECTIVE ACTIONS

The following corrective actions have been or Action Program (CAP) to address the causes of

  • Site all-hands meeting was held to discuss to reinforce expectations.

will be performed under the Corrective this event:

the event, the lessons learned, and comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to

  • discuss the Fleet Refocus Initiative.
  • work that effects generation was to have direct oversight by a superintendent or above.
  • All work start authorizations provided by operations watch personnel must now undergo an additional work challenge utilizing a checklist developed in response to this event. Revised process was formalized by an Operations Standing Order.
  • The completion of corrective actions associated with the Fleet Refocus Observation Program will be documented to ensure all personnel apply the essential knowledge, skills, behaviors and practices needed to conduct work safely and reliably.
  • Procedures 2-PT-2M3, 2-PT-2M2, and 2-PT-2M2A will be revised to remove the word "equivalent" to prevent any questions on which key to use.

EVENT ANALYSIS

The event is reportable under 10CFR50.73(a)(2)(iv)(A). The licensee shall report any event or condition that resulted in manual or automatic actuation of any of the systems listed under 10CFR50.73(a)(2)(iv)(B). Systems to which the requirements of 10CFR50.73(a)(2)(iv)(A) apply for this event include the Reactor Protection System including reactor trip and AFWS actuation. This event meets the reporting criteria because an automatic reactor trip was initiated at 9:38 hours, on July 6, 2016, and the AFWS actuated as a result of the RT. On July 6, 2016, at 13:16 hours, a four hour non-emergency notification was made to the NRC (Log Number 52067) for an automatic reactor trip while critical and included the eight hour non-emergency notification for the actuation of the AFW system. Both notifications were in accordance with 10CFR50.72(b)(3)(iv)(1). The event was recorded in the Indian Point Energy Center corrective action program (CAP) as CR-IP2-2016-04320.

As all primary safety systems functioned properly there was no safety system functional failure reportable under 10CFR50.73(a)(2)(v).

PAST SIMILAR EVENTS

A review was performed of the past three years of Licensee Event Reports (LERs) for events that involved a reactor trip due to testing of the reactor protection system.

No applicable LERs were identified.

SAFETY SIGNIFICANCE

This event had no effect on the health and safety of the public.

This condition had no effect on the health and safety of the public.

There were no actual safety consequences for the event because the event was an uncomplicated reactor trip with no other transients or accidents.

  • Small Group Meetings.
  • from the Fleet Refocus Initiative.

Site All-hands meeting was held to Conducted Fleet Refocus Initiative Implemented observation activities As an interim action all essential comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Required primary safety systems performed as designed when the RT was initiated. The AFWS actuation was an expected reaction as a result of low SG water level due to SG void fraction (shrink), which occurs after a RT and main steam back pressure as a result of the rapid reduction of steam flow due to turbine control valve closure.

For this RT there was no actual condition to initiate the reactor trip breaker opening. Event was initiated by human error.

There were no significant potential safety consequences of this event. The RPS is designed to actuate .a RT for any anticipated combination of plant conditions to include low SG level. All components in the RCS were designed to withstand the effects of cyclic loads due to reactor system temperature and pressure changes. The reactor trip breakers (RTBs) are in the electrical power supply line from the control rod drive motor generator set power supply to the CRDMs. Opening of the RTBs interrupts power to the CRDMs, which allows the shutdown rods to fall into the core by gravity. Each reactor trip breaker (RTB) is equipped with a reactor trip bypass breaker (RTBB) to allow testing of the trip breaker while the unit is at power. Each RTB and RTBB is equipped with an undervoltage coil and a shunt trip coil to trip the breaker open when needed. The reactor trip signals generated by the RPS automatic trip logic cause the RTBs and associated RTBB to open and shut down the reactor.

There are two RTBs in series so that opening either will interrupt power to the rod control system and allow the control rods to fall into the core and shut down the reactor. Each RTB has a parallel RTBB that is normally open. This feature allows testing of the RTBs at power. A trip signal from RPS logic train A will trip RTB A and RTBB B; and a trip signal from logic train B will trip RTB B and RTBB A. During normal operation, both RTBs are closed and both RTBBs are open. When any one train is taken out of service for testing, the other train is capable of providing unit monitoring and protection until the testing has been completed.

For this event, rod control was in automatic and all rods inserted upon initiation of a RT. The AFWS actuated and provided required FW flow to-the SGs. RCS pressure remained below the set point for pressurizer PORV or code safety valve operation and above the set point for automatic safety injection actuation. Following the RT, the plant was stabilized in hot standby.

Indian Point 2 05000-247

05000298/LER-2016-00226 April 2016
27 June 2016
27 June 2016Cooper10 CFR 50.73(a)(2)(v), Loss of Safety FunctionService water
High Pressure Coolant Injection
Reactor Core Isolation Cooling
Core Spray
Automatic Depressurization System
Emergency Core Cooling System
Low Pressure Coolant Injection

On April 26, 2016, it was noted that the green off light for High Pressure Coolant Injection (HPCI) auxiliary lube oil pump (ALOP) in the Control Room, was not illuminated. A non-licensed operator was dispatched to the HPCI ALOP starter and reported the green bulb appeared to have shattered in the socket. HPCI was declared inoperable at 1754 Central Daylight Time (CDT) resulting in entry into Technical Specifications Limiting Condition of Operation 3.5.1, Condition C, HPCI System Inoperable.

Investigation found the 125 volts direct current fuse open circuited and the local indication green light and socket were damaged. The cause of the failure was determined to be a lack of engineering knowledge which led to a design change in 1984 in the HPCI ALOP starter circuitry that diminished the robustness of the circuit with respect to a specific failure modality; direct short circuiting within the indication bulb itself. The HPCI system was restored to operable status on April 28, 2016, at 1245 CDT.

This event is being reported as a loss of safety function due to HPCI being a single-train safety system.

The potential safety consequences of this event were minimal due to the limited duration the condition existed and the redundant/diverse core cooling systems which remained operable.

3. LER NUMBER 2. DOCKET NUMBER 05000- 298 Cooper Nuclear Station 2016 - 002 - 00

05000336/LER-2016-00127 June 2016Millstone
Docket Number
10 CFR 50.73(a)(2)(v), Loss of Safety FunctionSteam Generator
Reactor Coolant System
Feedwater
Auxiliary Feedwater

On April 27, 2016, with Millstone Power Station Unit 2 (MPS2) in MODE 1 at 100% power, plant personnel inadvertently left the door to the turbine driven auxiliary feed purnp room open. This condition existed for less than one hour.. The door is a high energy line break (HELB) barrier. With the door open there is no HELB protection for the motor driven auxiliary feedwater (AFW) pumps thus potentially rendering both trains of AFW inoperable.

The cause is human performance error. The door is conspicuously labeled on each side that it is a HELB boundary door and must be closed except for entry and exit from the room. Corrective actions are being taken in accordance with the station's corrective action program.

This condition is being reported pursuant to 10 CFR 50.73(a)(2)(v) as any event or condition that alone could have prevented the fulfillment of the safety function of structures or systems that are needed to: (B) remove residual heat; and (D) mitigate the consequences of an accident.

05000413/LER-2016-00113 December 2015
23 June 2016
23 June 2016Catawba10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Steam Generator
Reactor Coolant System
Feedwater
Emergency Diesel Generator
Residual Heat Removal
Emergency Core Cooling System
Containment Spray

On March 28, 2016, Operators did not receive the expected results from a relay while performing the 1B train Emergency Core Cooling System (ECCS) Cold Leg Recirculation interlock test. Investigation found the breaker for the residual heat removal pump's loop suction valve incorrectly positioned open. ECCS 1B was declared inoperable. Subsequently, the breaker was closed after it was verified not to have been tripped open.

The last manipulation of this breaker was determined to have been during the coordination for pressure boundary valve testing and standby readiness alignment during the previous refueling cycle (December 2015). A past Operability Evaluation concluded the breaker being open led to a condition prohibited by Technical Specifications, and also a condition that could have prevented the fulfillment of a safety function for Unit 1 ECCS while the 1A emergency diesel generator was inoperable for greater than four hours during this time period. This event was determined to be reportable on April 26, 2016.

The cause of this event is that the test procedure for pressure boundary valve testing did not contain specific procedural guidance for establishing a suction source for the 1B train residual heat removal (RHR) pump. The test procedure required coordination with another procedure to ensure the breaker for the 1B train RHR pump loop suction valve was returned to the closed position. Corrective actions include procedural revisions to these procedures.

05000247/LER-2016-00710 June 20169 August 2016Indian Point10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
Reactor Coolant System
Residual Heat Removal
Emergency Core Cooling System

On June 20, 2016, Entergy management was advised by the NRC that during a tour in containment while the unit was in Mode 4, the inspector identified two open barrier gates for the Emergency Core Cooling System (ECCS) sump.

Personnel were moving scaffolding from inside the crane wall to areas outside the crane wall through the two open barrier gates. Having both sump barrier gates open violated ECCS operability basis which requires the sump barrier system to be operable in Modes 1-4.

The inspector notified the operator touring with him of the observation. The operator subsequently coached the Radiation Protection (RP) door guard to ensure that one of the gates be closed at all times. The apparent cause was a latent organizational weakness associated with the use of procedure OAP-007 (Containment Entry and Egress) which had not been communicated well within the organization.

The failure mode was personnel not being aware of all available information.

The scaffold supervisor was not aware of his requirement to serve as containment coordinator and provide the required briefing on gate closure. The RP brief was focused on the locked high radiation requirements not gate control. Corrective actions included closing and securing one gate, briefing RP personnel on the event, the lessons learned and management expectations. This event will be included in all 3R19 supplemental supervisors qualifications required reading list. Procedure OAP- 007 will be revised to include a checklist for entry briefings to include GS-191 requirements. The event had no significant effect on public health and safety.

Indian Point 2 05000-247 APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2018 comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Note: The Energy Industry Identification System Codes are identified within the brackets ().

DESCRIPTION OF EVENT

On June 20, 2016, Indian Point management was advised by the NRC that during a tour in containment (NH) while the unit was in Mode 4, the inspector identified two open barrier gates for the Emergency Core Cooling System (ECCS) (BQ) sump. Personnel were removing disassembled scaffolding from inside the crane wall on the 46 foot elevation of containment and moving it through the ECCS sump barrier gates (GATE) to areas outside the crane wall through the two open barrier gates. Having both sump barrier gates open violated ECCS operability basis which requires the sump barrier system to be operable in Modes 1-4. The plant had entered Mode 4 on July 10, 2016, at 23:30 hours. The inspector notified the operator touring with him of the observation. The operator subsequently coached the Radiation Protection (RP) door guard to ensure that one of the gates were closed at all times. No condition report recorded the event at the time. Subsequently, on June 20, 2016, after an NRC inspector advised a site manager the condition was recorded in the Indian Point Energy Center (IPEC) Corrective Action Program (CAP) as Condition Report CR-IP2- 2016-04036. On June 21, 2016, CR-IP2-2016-04037 recorded the failure to initiate a CR at the time of the event.

For postulated breaks in the Reactor Coolant System (RCS) (AB) there are two recirculation related sumps within the containment, 1) the Recirculation Sump and, 2) the Containment Sump. Both sumps collect liquids discharged into the containment during a design basis accident. As part of the resolution of Generic Safety Issue (GSI)-191 (Assessment of Debris Accumulation on PWR Sump Performance) and Generic Letter 2004-02 (Potential Impact of Debris Blockage on Emergency Recirculation During Design Basis Accidents at Pressurized Water Reactors) various flow barrier debris interceptors were installed in the containment to channel the recirculation flow into the reactor cavity sump area, up and out of the Incore Instrumentation Tunnel, through the crane wall and containment sump labyrinth wall via specially designed openings, and into the annulus area outside the crane wall.

The recirculation flow will migrate towards the Recirculation Sump or the Containment Sump depending on which pump(s) are operating. Flow channeling barriers are installed on the Reactor Cavity Sump around the Incore Instrumentation Tunnel, on the Recirculation Sump trenches, and at the Containment Sump. Flow channeling barrier gates are installed in the northeast and northwest quadrant openings of the Crane Wall. In addition, flow channeling barrier gates are installed in the north and south entrances to the Recirculation Sump area. There is one dual access gate (gates 17 and 23) to allow access without violating the flow barrier integrity during transient through the flow barrier system.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Investigation of the event determined that the scaffold work group was the largest group within containment during the time the scaffold job on the 46 foot elevation was being worked. In accordance with procedure OAP-007 (Containment Entry and Egress) the scaffold group was to assume the role of containment coordinator and be responsible for performing a containment entry briefing. However, instead of providing a containment entry briefing, a regular or standard HU pre-job brief was given to the scaffold workers by their contractor supervisor. Because the area being worked was a radiation controlled area the scaffold workers then met with Radiation Protection (RP) personnel at the Health Physics access (HP1) for a Locked High Radiation Area (LHRA) RP pre-job brief. The RP brief included discussion that one of the ECCS barrier gates had to be closed at all times per GSI-191 and OAP-007 requirements. The job also required an RP door guard whose only function was to ensure that anyone entering into the inside crane wall had to have an HP individual with them. There was no ECCS barrier gate monitor assignment as required by OAP- 007. As work progressed the scaffold workers left both ECCS barrier gates open to enhance removal of scaffold material to storage. Although the scaffold workers were told during the RP briefing that one ECCS barrier gate must remain closed at all times, it was discovered in interviews with workers that they thought that none of the other gates could be opened while they were using their gate location to remove scaffold.

It was determined that the supplemental scaffold supervisor was not aware of a specific entry procedure that was required to be used prior to a containment entry.

A specific OAP-007 procedure containment entry brief was not given to the workers nor were they and their supervisor aware of the procedure. The supplemental scaffold group supervisor stated that in previous containment entries he and his group were never the main group going into containment so they were always briefed by operations or RP and didn't recall using OAP-007. Procedure OAP-007 is specifically written to cover many aspects of containment entries. The procedure contains sections and steps discussing the ECCS barrier gates with diagrams of the crane wall and all of the gates with their locations and numbers. If the procedure had been used in addition to a pre-job and RP brief, the requirements would have been clearer to the workers and this event most likely would not have occurred.

An extent of condition (EOC) review was performed and it determined that both units are similar and both would be vulnerable in an event if there was a direct flow path for accident debris to enter the containment/internal recirculation sump. The condition is bounded by the crane wall gates as these are the only types of gates in the containment installed in the crane wall that protect the ECCS sumps from debris.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to

CAUSE OF EVENT

The apparent cause was a latent organizational weakness associated with the use of procedure OAP-007 (Containment Entry and Egress) which had not been communicated well within the organization. The failure mode was personnel not being aware of all available information. The scaffold supervisor was not aware of his requirement to serve as containment coordinator and provide the required briefing on gate closure. The RP brief was focused on the locked high radiation requirements not gate control.

CORRECTIVE ACTIONS

The following corrective actions have been or will be performed under the Corrective Action Program (CAP) to address the causes of this event:

  • Dual gates were closed and applicable gate secured. The RP door guard was coached on requirement to have at least one gate closed and secured at all times.
  • A HU meeting was held and interviews conducted with the work crew, supervisor and RP personnel and the requirements of OAP-007 were reviewed and requirements of the ECCS barrier reinforced.
  • A Department Clock Reset/Yellow memo was prepared and the lessons learned on the event and management expectations communicated with Projects organizations, all site departments, and the Fleet.
  • The event will be included in all 3R19 supplemental supervisors qualifications required reading list.
  • Procedure OAP-007 will be revised to include a checklist for entry briefings to include GS-191 requirements.

EVENT ANALYSIS

The event is reportable under 10CFR50.73(a)(2)(v)(D) as a safety system functional failure as the condition could have prevented adequate post accident core cooling due to DBA debris blockage of the recirculation and/or the containment sump. An ECCS train is inoperable if it is not capable of delivering design flow to the RCS.

Individual components are inoperable if they are not capable of performing their design function or supporting systems are not available. Technical Specification (TS) 3.5.2 (ECCS-Operating) requires three ECCS trains to be operable in Modes 1, 2 and 3, and TS 3.5.3 (ECCS-Shutdown) requires one ECCS residual heat removal (RHR) subsystem and one ECCS recirculation subsystem to be operable in Mode 4.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Indian Point 2 05000-247 The licensing and design basis of the ECCS per UFSAR Section 6.2.2 (ECCS System Design and Operation) credits flow channeling barriers installed in containment in response to the resolution of GL-2004-02. The two flow barrier gates that were used for removing scaffolding were not closed and secured to prevent it from being forced open during a DBA. The unsecured gates were not in accordance with design and not a sufficient robust barrier to prevent debris from entering the recirculation and containment sumps had a DBA occurred while in Mode 4. The condition is also reportable under 10CFR50.73(a)(2)(vii) (common cause inoperability of independent trains or channels) as the condition caused at least one independent train or channel to become inoperable in multiple systems or two independent trains or channels to become inoperable in a single system designed to (D) mitigate the consequences of an accident. The NRC inspector tour occurred during the time the unit was in Mode 4. The unit entered Mode 4 on June 10, 2016, at 23:30 hours. However, no CR was initiated for this condition at that time. CR- IP2-2016-04037 recorded that condition that while performing a walkdown with an NRC inspector on June 11, 2016, the NRC raised a question about an activity in the field and no condition report was initiated.

PAST SIMILAR EVENTS

A review was performed of the past three years of Licensee Event Reports (LERs) for events that involved SSFFs and/or common cause inoperability of an Engineered Safety Feature System that had a similar cause. No LERs were identified at Unit 2.

A review of all reported events during the past three years at both units identified one LER at Unit 3 that was similar. Unit 3 LER-2013-002 reported on April 29, 2013, a Safety System Functional Failure and Common Cause Inoperability of the Emergency Core Cooling System due to violation of containment sump debris barrier integrity. The LER reported that on March 4, 2013, during shutdown for a refueling outage, Radiation Protection (RP) personnel entered the reactor containment building to install plastic RP fencing for the Reactor Coolant Drain Tank (RCDT). After receiving clearance at Mode 4 to enter the Inner Crane Wall (ICW) to install fencing around the RCDT and post it as a Locked High Radiation Area (LHRA). The RP work crew assumed they could enter the ICW area through any sump barrier gate for the Emergency Core Cooling System (ECCS). The RP work crew chose to use a single gate access point due to its proximity to the RCDT.

Subsequently, a RP Technician identified that personnel had not entered the area using the double access gate and had brought in plastic fencing which was inappropriate material for the sump area. The apparent causes were an inadequate pre-job brief and inadequate procedure for Containment Entry and Egress (OAP-007, 0-RP-RWP-405) due to poor change management. The pre-job brief failed to cover the requirement to use the dual sump barrier gate access point when in Modes 1-4, nor did it address the type of fencing allowed. Corrective actions included revision of Procedure OAP-007 to clearly state that within the procedure's attachments that only the sump barrier dual access gate for 46 foot Containment ICW entries shall be used in Modes 1-4.

comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to The revision specified the use of the double entry gate and that one gate is to remain shut and secured at all times. Securing the gates at unit 3 which uses a slide latch does not state the use of a gate monitor. The step for Unit 2 includes statements that the gates be secured with a padlock or nut and bolt closure from the outside. This condition requires posting of a gate monitor to allow exit.

SAFETY SIGNIFICANCE

This event had no significant effect on the health and safety of the public. There were no actual safety consequences for the event because there were no accidents or transients during the time of the event. The analysis performed in response to GL- 2004-02 included debris transport analysis conservatisms for transport of debris to both the IR sump and the Containment sump in excess of quantities that would be generated. Establishing normal RHR cooling to the RCS has RCS temperature below 350 degrees F and pressure less than 400 psig.

In Mode 4 the reactor is not critical and reactivity is stable. In Mode 4 there is significantly less energy in the RCS to generate debris. At the time the actual RCS pressure (pressurizer pressure) was approximately 355 psig. An evaluation of a LOCA during Mode 3 and 4 operation was performed by Westinghouse (WCAP-12476) that showed a direct reduction in break probability for Mode 4. The evaluation concluded that Mode 4 LOCAs are not a significant contributor to shutdown risk.

During this event the entire flow barrier was not disabled because only two debris barrier gates were unsecured and only for the time scaffold workers were allowed to perform assigned work. The exact time the gates were open cannot be determined as the barrier gates have no electronic timing devises. However, the scaffold workers were assigned three entries with stay time limitations for heat stress of 45 minutes each for a total job time of 135 minutes. The scaffold work assignment took place in Mode 4. The unit entered Mode 4 on June 10, 2016, at 23:30 hours.

For the first two of three entries, the scaffold workers had to go inside the crane wall and disassemble erected scaffolding. Per the scaffold supervisor at least one door was closed during scaffold disassembly. Therefore approximately 60 minutes were left for moving disassembled scaffolding from inside the crane wall through the open gates to the outside crane wall storage areas. Therefore most debris would have been intercepted by the flow barrier system. Also, the barrier gates swing into the crane wall so that DBA flow and forces would tend to close the gate when pressure is applied (e.g., DBA debris loads) therefore limit flow barrier bypass and sump debris loading.

05000247/LER-2016-00526 March 2016
25 May 2016
25 May 2016Indian Point10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
Steam Generator
Reactor Coolant System
Feedwater
Main Turbine

On March 26, 2016, during a refueling outage, an NRC inspector identified that the trip of the MBFPs is not tested in accordance with Technical Specification 3.7.3 (Main Feedwater System) Surveillance Requirement (SR) 3.7.3.3.

This was discovered as a result of an assessment of the failure of the Main Boiler Feedwater Pumps (MBFPs) steam stop valves to close after the reactor trip on December 5, 2015.

  • TS SR 3.7.3.3 requires testing the MBFP trip function every 24 months on an actual or simulated actuation signal.

Surveillance tests 2-PT-V024DS60 .and 2-PT-V24DS61 are performed every 24 months, but only test up to the limit switch contact that actuates the MBFP turbine.trip solenoid valves and does not include the trip of the pump. A review determined the requirement to verify the trip of the MBFPs was added to the TS during the implementation of the improved TS (ITS) conversion program in 2004 but the corresponding testing was not added to the surveillance tests.

The direct cause was human error for failure to ensure testing was established to meet new ITS„SRs. The apparent cause of the error is indeterminate due to the time passed since TS conversion by Amendment 238 on November 21, 2003. Corrective actions include revision of Surveillance tests 2-PT-V024DS60 and 2-PT-V24DS61 to test tripping of the MBFPs. The MBFPs will be tested per the revised procedures prior to startup from the. outage. The event had no significant effect on public health and safety.