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The query [[Originated by::Zack Ford]] [[Category:ENS Notification]] was answered by the SMWSQLStore3 in 0.0067 seconds.


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 Entered dateEvent description
ENS 5399814 April 2019 03:21:00On April 14, 2019 at 0003 (EDT), Nine Mile Point Unit 1 experienced an automatic reactor scram during reactor startup. The cause of the automatic scram was due to high (Reactor Pressure Vessel) pressure following closure of the turbine stop valves. All control rods fully inserted and all plant systems responded per design following the scram. Following the automatic scram, the High Pressure Coolant Injection (HPCI) System automatically initiated as expected. At Nine Mile Point Unit 1, a HPCI System actuation signal on low Reactor Pressure Vessel (RPV) level is normally received following a reactor scram, due to level shrink. HPCI is a flow control mode of the normal feedwater systems, and is not an Emergency Core Cooling System. At 0004, RPV level was restored above the HPCI System low level actuation set point and the HPCI System initiation signal was reset. Pressure control was established on the Turbine Bypass Valves, the preferred system. No Electromatic Relief Valves actuated due to this scram. Nine Mile Point Unit 1 is currently in Hot Shutdown, with reactor water level and pressure maintained within normal bands. The offsite grid is stable with no grid restrictions or warnings in effect. The unit is currently implementing post scram recovery procedures. The NRC Resident Inspector has been notified. The Licensee will notify the State of New York.