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 Entered dateEvent description
ENS 564599 April 2023 04:42:00

The following information was provided by the licensee via email: The following event description is based on information currently available. If through subsequent reviews of this event additional information is identified that is pertinent to this event or alters the information being provided at this time a follow-up notification will be made via the ENS or under the reporting requirements of 10 CFR 50.73. At 2144 MST on April 8, 2023, the Unit 1 reactor automatically tripped due to the loss of reactor coolant pumps stemming from the loss of 13.8 kV power to the pumps. Prior to the reactor trip, the main turbine tripped due to a loss of hydraulic pressure. The main generator output breakers did not automatically open on the turbine trip as expected so the control room operators opened the breakers per procedural guidance. Once the breakers were opened, the two 13.8 kV electrical distribution buses failed to complete a fast bus transfer, which resulted in the loss of power to the reactor coolant pumps, initiating the reactor trip. The control room operators manually actuated a main steam isolation signal per procedure, requiring use of the atmospheric dump valves. Following the reactor trip, all control element assemblies inserted fully into the core. No automatic specified system actuation was required or occurred. No emergency plan classification was required per the Emergency Plan. Safety related buses remained powered from offsite power during the event and the offsite power grid is stable. Unit 1 is stable and in Mode 3. Decay heat is being removed by the atmospheric dump valves and the class 1E powered motor driven auxiliary feedwater pump. The loss of hydraulic pressure, the main generator output breakers failing to automatically open and the fast bus transfer not actuating are being investigated. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B). The NRC Senior Resident Inspector has been informed. Unit 2 is in a refueling outage in Mode 5 and Unit 3 is in Mode 1 at 100 percent power.

  • * * UPDATE ON 4/9/23 AT 0835 EDT FROM TANNER GOODMAN TO ADAM KOZIOL * * *

This update is being made to report the manual actuation of the B-train auxiliary feedwater pump and manual main steam isolation signal (MSIS) actuation affecting multiple main steam isolation valves (MSIVs) following the reactor trip. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and a specified system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Warnick)

  • * * UPDATE ON 5/3/23 AT 1945 EDT FROM LORRAINE WEAVER TO JOHN RUSSELL * * *

This update is intended to clarify the initial description of the event that occurred on 4/8/2023. Prior to the reactor trip, the main turbine tripped due to a loss of hydraulic pressure. The main generator output breakers did not automatically open on the turbine trip. The control room operators manually opened the breakers per procedural guidance. Once the breakers were opened, the two 13.8 kV electrical distribution buses de-energized. A fast bus transfer did not occur per design, which resulted in the loss of power to the reactor coolant pumps, initiating the reactor trip. The control room operators manually actuated a main steam isolation signal per procedure, requiring use of the atmospheric dump valves. The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Gaddy)

ENS 5612726 September 2022 21:16:00The following information was provided by the licensee via email: On September 26, 2022, at approximately 1100 Mountain Standard Time, a Reactor Operator's test results were confirmed positive for use of a controlled substance following a random Fitness For Duty (FFD) screening test and it was determined that the individual violated the station's FFD Policy. The individual's unescorted access has been terminated in accordance with station procedures. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee will conduct an investigation of the individual's work history.
ENS 559263 June 2022 20:32:00The following information was provided by the licensee via email: The following event description is based on information currently available. If, through subsequent reviews of this event, additional information is identified that is pertinent to this event or alters the information being provided at this time, a follow-up notification will be made via the ENS or under the reporting requirements of 10 CFR 50.73. This telephone notification is being made pursuant to the reporting requirements of 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to describe invalid actuations of the Palo Verde Nuclear Generating Station (PVNGS) Unit 1 B Train Auxiliary Feedwater (AF) system and Essential Spray Pond (ESP) system that occurred while in a refueling outage. On April 11, 2022, at approximately 2045 Mountain Standard Time, an automatic start of the Unit 1 B Train AF and ESP systems occurred during restoration from a surveillance test. The station was conducting a surveillance test during a Unit 1 refueling outage to verify the proper responses of the Engineered Safety Features Actuation Systems to simulated design basis events. The test portion was completed satisfactorily; however, during the restoration portion, the load sequencer inadvertently cycled between Mode 0 and Mode 1 three times in immediate succession. At the time of the system actuations, one of the actuation signals associated with this portion of the test had been reset per procedure. Another actuation signal was still in while restoration steps were ongoing, but the sequencer was not expected to cycle between Modes. The system actuations did not occur as a result of actual plant conditions or parameters and are therefore invalid. The Unit 1 B Train AF and ESP system actuations were complete and the systems started and functioned successfully. For the systems that did not actuate, the reasons are clearly understood as those systems were in an overridden condition due to test configuration. The spurious actuation was not able to be replicated and a direct cause was not identified. There were no adverse impacts to public health and safety nor to plant employees. The NRC Resident Inspectors have been informed.