Semantic search

Jump to navigation Jump to search
 Entered dateEvent description
ENS 5339912 May 2018 06:58:00On 5/11/2018, at 2327 hours CDT, with the plant in Mode 5, Grand Gulf Nuclear Station was making preparations for surveillance test 06-OP-1P75-R-0003, Standby Diesel Generator 1 Functional Test. The Grand Gulf Nuclear Station experienced an auto-start of the Division 1 (Emergency) Diesel Generator (EDG) when the 15AA Bus Potential Transformer (PT) fuse drawer was racked out instead of the line PT fuse drawer for Bus 15AA feeder breaker 152-1514. This resulted in the 15AA Incoming Feeder Breaker 152-1511 from Engineered Safety Features Transformer 12 opening, de-energizing the 15AA Bus. The Division 1 EDG started and energized Bus 15AA. The Division 1 LSS SYSTEM FAIL annunciator was received and Standby Service Water A failed to start due to the 15AA Bus PT fuse drawer being racked out. Standby Gas Treatment Train B was manually initiated per the Loss Of AC Power Off Normal Emergency Procedure. Station equipment operated as expected based on the PT fuse drawer that was racked out. The Division 1 EDG was manually tripped from the Control Room because cooling from the Standby Service Water A was not available. RHR (residual heat removal) B was in Shutdown Cooling (mode) and was verified not affected The licensee has notified the NRC Resident Inspector.
ENS 5330431 March 2018 10:00:00At 0206 (CDT) on March 31, 2018, with the plant in Mode 1 at 100% rated core thermal power, Grand Gulf Nuclear Station experienced a loss of Secondary Containment. During the performance of a Standby Gas Treatment System (SGTS) drawn down test with Auxiliary Building train bay door (1A319A) as the secondary containment boundary, Grand Gulf was unable to maintain secondary containment pressure, as required by SR (surveillance requirement) 3.6.4.1.4, greater than or equal to 0.266 inches of water vacuum for 1 hour. Following initial vacuum draw down, secondary containment pressure degraded to 0.225 inches of water vacuum with operators in the field reporting air leakage from door 1A319A. The test was secured and Secondary Containment was declared inoperable and Technical Specification 3.6.1.4 A.1 was entered. Following completion of the failed surveillance test, Secondary Containment was returned to an operable status at 0315 hours on March 31, 2018, by returning the system to a previously known operable configuration by closing doors 1A310, 1A312 and 1A319. This is being report under 10 CFR 50.72(b)(3)(v)(C). The licensee has notified the NRC Resident Inspector.
ENS 5311712 December 2017 20:34:00At approximately 1330 CST on Tuesday, December 12, 2017, Grand Gulf Nuclear Station declared Division 3 'C' Battery inoperable due to questions concerning battery terminal connection continuity. Technical Specification 3.8.4, DC Sources - Operating, Condition E, Required Action E.1, requires the station to declare the High Pressure Core Spray System inoperable immediately. The Division 3 'C' Battery and High Pressure Core Spray System was declared operable and the LCOs (Limiting condition of operation) were declared met at 1731CST on Tuesday, December 12, 2017. Based on field measurements of terminal torque and resistance, the as-found and as-left terminal resistance micro-ohm readings indicated satisfactorily all times. Formal evaluation of the as-found condition of the battery is in progress. This report is to notify the NRC of a loss of safety function on the High Pressure Core Spray System. The NRC Resident Inspector was notified.