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 Entered dateEvent description
ENS 5354812 August 2018 02:58:00

EN Revision Text: TECHNICAL SPECIFICATION REQUIRED SHUTDOWN - LOSS OF 480 VOLTAGE EMERGENCY BUS On 8-12-18 at 0158 EDT, Beaver Valley Unit 2 experienced a loss of 480 Volt 2P Emergency Bus. This resulted in a Loss of Safety Function due to the 2-2 Emergency Diesel Generator (EDG) being Inoperable coincident with the Residual Heat Release Valve (2SVS-HCV104). A Technical Specification shutdown is required per LCO 3.0.3. The Licensee also stated they were in an unanalyzed condition due to the EDG and Residual Heat Release Valve being inoperable at the same time. The Licensee is shutting down to Mode 5 (Cold Shutdown). The Licensee is notifying the Resident Inspector. The Licensee will be making a Press Release about the unplanned shutdown.

  • * * UPDATE ON 08/16/2018 AT 1424 EDT FROM BLASE BARTKO TO KEN MOTT * * *

On 8-12-18 at 0158 (EDT) Beaver Valley Unit 2 experienced a loss of 480 Volt 2P Emergency Bus. Per operational guidance, this was determined to be a Loss of Safety Function due to the Unit 2 Emergency Diesel Generator (EDG) being INOPERABLE coincident with the Residual Heat Release Valve (2SVS-HCV104) 10 CFR 50.72(b)(3)(v)(B) and (D). This was also reported as an Unanalyzed Condition 10 CFR 50.72(b)(3)(ii)(b). No Press Release was performed for this event. The NRC Resident Inspector was notified. At 0410 (EDT) a Technical Specification Shutdown was commenced 10 CFR 50.72(b)(2)(i). At 2011 (EDT) the 480 Volt 2P Emergency Bus was restored and energized. Further evaluation of the event has determined that this event was not an Unanalyzed Condition and did not result in a Loss of Safety Function. The classifications of Unanalyzed Condition and Loss of Safety Function are being retracted. The accuracy of the existing guidance relative to Safety Function has been entered in the Corrective Action Program and interim actions have been taken to provide accurate guidance. Notified R1DO (Young) via email.

ENS 530567 November 2017 08:29:00On November 7, at 0504 (EST), BVPS (Beaver Valley Power Station) Unit 1 experienced an automatic reactor trip due to Main Unit Generator over current. The Auxiliary Feedwater system activated and remains in service. Offsite power supply is available. Normal and Emergency busses are being supplied by Offsite power. One Source Range channel failed to energize due to its corresponding Intermediate Range instrument being under compensated. It was manually energized and is not indicating as expected. The second Source Range instrument energized but is reading erratically. Both Source Range instruments have been declared inoperable and the appropriate Technical Specification has been complied with by making the Control Rods not capable of withdrawal and isolating all dilution flow paths. Plant trip response was as expected without complications, and all control rods fully inserted in the core. The plant is currently stable in Mode 3. This event is being reported as an actuation of the Reactor Protection system 10 CFR 50.72(b)(2)(iv)(B) and a Specified System Actuation (Auxiliary Feedwater System) 10 CFR 50.72(b)(3)(iv)(A). BVPS Unit 2 is unaffected by this event and remains at 100% power in Mode 1. The NRC Resident Inspector has been notified.
ENS 530587 November 2017 14:19:00It was determined that a licensed employee was not placed in an additional Fitness-For-Duty (FFD) testing program as directed by the MRO (Medical Review Officer). Upon discovery, the individual was subsequently tested . . . and determined Fit-For-Duty per 10 CFR 26 requirements. This event is being reported pursuant to 10 CFR 26.719(b)(4). The NRC Resident Inspector has been notified.