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 Entered dateEvent description
ENS 530523 November 2017 21:08:00

On November 3rd, 2017 at 2022 EDT, the Indian Point Unit 3 Reactor Protection system automatically actuated at 100 percent power. Annunciator first out indication was from 33 SG (Steam Generator) Low Level. This automatic reactor trip is reportable to the NRC under 10 CFR 50.72(b)(2)(iv)(B). All control rods fully inserted on the reactor trip. All safety systems responded as expected. The Auxiliary Feedwater System actuated as expected. Offsite power and plant electrical lineups are normal. All plant equipment responded normally to the unit trip. No primary or secondary code safeties lifted during the trip. The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The Emergency Diesel Generators did not start as offsite power remained available and stable. The Unit remains on offsite power and all electrical loads are stable. Unit 3 is in Hot Standby at normal operating temperature and pressure with decay heat removal using auxiliary feedwater to the steam generators and normal heat removal through the condenser via the high pressure steam dumps. Unit 2 was unaffected and remains at 100 percent power. A post trip investigation is in progress. The licensee indicated that Radiation Monitor number 14 spiked twice during the transient, however, is currently not indicating any signs of radiation. The licensee will notify the NRC Resident Inspector and the NY Public Service Commission.

  • * * UPDATE AT 1523 EST ON 11/06/17 FROM RAMIREZ OVIDIO TO JEFF HERRERA * * *

The initial notification stated that Indian Point Unit 3 Reactor Tripped on 33 SG (Steam Generator) Low Level, this is incorrect. Indian Point Unit 3 Reactor Tripped on a Turbine Trip. The Turbine Trip was caused by a Generator Back-up Lockout Relay. The Turbine Trip was the 'first' annunciator first-out but was acknowledged instead of silenced during initial operator actions. The Turbine Trip first-out being acknowledged allowed a Low Steam Generator first-out to later annunciate. A Low Steam Generator Level is an expected condition post trip. This update does not change any actions taken by the operating team or required notifications under 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). A post trip investigation remains in progress. The licensee will notify the NRC Resident Inspector and the NY Public Commission. Notified the R1DO(Cook)

ENS 5182929 March 2016 17:04:00This is a non-emergency report. Indian Point Unit 2 is shut down for a scheduled refueling outage and is performing an industry required MRP-227-A inspection of the reactor vessel internals. During this inspection, Entergy identified baffle/former bolts with either visual anomalies or ultrasonic indications. All vessel internal examinations have been successfully completed with no anomalies other than the baffle/former bolts. Entergy will be developing a repair plan that will be implemented prior to startup. The unit is in a safe and stable condition. No leakage was detected as a result of this condition. On March 29, 2016, this event was determined to be reportable pursuant to 10 CFR 50.72(b)(3)(ii)(B), since the as-found conditions were not previously analyzed. Entergy is planning a press release to communicate this condition to our stakeholders. Therefore this is also being reported under 10 CFR 50.72(b)(2)(xi) since a news release is planned. The NRC Resident Inspector has been informed. The licensee will notify State and local government agencies as appropriate.