Semantic search

Jump to navigation Jump to search
 Entered dateEvent description
ENS 530607 November 2017 22:32:00

On 11/7/2017 at 1957 (EST), VC Summer Nuclear Station automatically tripped due to a turbine trip. The cause of the turbine trip is under investigation at this time. All systems responded as expected. All Control Rods fully inserted and all Emergency Feedwater pumps started as required. The plant is stable in Mode 3. This event is reportable per 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The unit is currently stable in Mode 3 with decay heat removal via the Main Steam to the Main Condenser. The NRC Resident Inspector has been notified. The licensee will notify the South Carolina State Emergency Management Division, the Fairfield, Richland, Lexington and Newberry Counties.

  • * * UPDATE FROM BETH DALICK TO VINCE KLCO ON 11/8/17 AT 1409 EST * * *

All systems responded as expected, with the exception of 'B' Steam Generator Feedwater Isolation Valve XVG1611 B-FW. This valve did not appear to automatically close and was slow to indicate closed from the Main Control Board. All Control Rods fully inserted and all Emergency Feedwater pumps started as required. The plant is stable in Mode 3. Notified the R2DO (Musser).

ENS 523579 November 2016 14:58:00At approximately 1008 (EST) on 11/9/16, site personnel discovered a sanitary lift station overflowing in the protected area. The overflow entered a nearby storm drain that discharges into Outfall 13. The estimated release volume is approximately 10 gallons. The release has been stopped. At 1339 an initial notification was made to SCDHEC (South Carolina Department of Health and Environmental Control). The cause of the overflow is still under investigation. Functionality of the lift pump has been restored and cleanup is complete. The NRC Senior Resident has been notified.