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 Entered dateEvent description
ENS 5340617 May 2018 14:26:00On May 17, 2018, at approximately 1045 Eastern Daylight Time (EDT), Duke Energy confirmed that one emergency notification siren (i.e., B03) located in Brunswick County was malfunctioning. The siren was making an abnormal sound, alternating between low and high pitch. At approximately 1103 EDT, the siren was deactivated. There are a total of 38 sirens located in Brunswick and New Hanover Counties. No other siren was affected. Duke Energy notified the State of North Carolina, Brunswick County, and New Hanover County of the issue. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 533197 April 2018 12:10:00

On April 7, 2018, at 0836 EDT, with Unit 1 in Mode 1 at approximately 100 percent power, the reactor automatically tripped during testing of the stator cooling system. The trip was uncomplicated with all systems responding normally. No safety-related equipment was inoperable at the time of the event. Due to the Reactor Protection System (RPS) actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B).

Operations responded using Emergency Operating Procedures and stabilized the plant in Mode 3. Reactor water level being maintained via normal feedwater system. Decay heat is being removed through the bypass valves.

Reactor water level reached low level 1 (LL1) as a result of the reactor trip. The LL1 signal causes a Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Due to the Primary Containment Isolation System (PCIS) actuation, this event is also being reported as an eight-hour, non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the PCIS. Unit 2 was not affected. There was no impact on the health and safety of the public or plant personnel. The safety significance of this event is minimal. The automatic reactor trip was not complicated and all safety-related systems operated as designed. Investigation of the cause of the Reactor Protection System actuation is in progress. The licensee notified the NRC Resident Inspector.