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 Entered dateEvent description
ENS 563894 March 2023 16:42:00The following information was provided by the licensee via email: At 0910 (CST), with Unit 2 in Mode 4 at 0 percent power, an actuation of a reactor scram on low charging water header pressure occurred during restoration from hydrostatic test conditions. All control rods were already fully inserted prior to the receipt of the scram signal. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the Unit 2 RPS system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5590520 May 2022 17:39:00The following information was provided by the licensee via email: At 0905 CST on 05/20/2022, it was discovered both trains of Control Room Area Filtration and Area Ventilation Air Conditioning Systems were simultaneously INOPERABLE. Due to this INOPERABILITY, the system was in a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5504623 December 2020 12:28:00At 0653 CST on 12/23/20, it was discovered the single train of high pressure core spray was inoperable. Due to this inoperability, the system was in a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). All other emergency core cooling systems were operable during this time. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The high pressure core spray is inoperable because the water lake pump tripped. This inoperability puts the licensee in a 14-day limiting condition for operability.
ENS 510547 May 2015 17:51:00This report is being made pursuant to 10CFR50.72(b)(2)(xi), News Release or Notification of Other Government Agency. Operations received a report from Security that a fishing boat has capsized on the station cooling lake. At 1530 (CDT) the LaSalle County Operating Department was notified that the LaSalle County Coroner confirmed that there was a fatality. The Illinois Department of Natural Resources (IDNR), LaSalle County Sheriff, Seneca Rescue Team, and NRC Senior Resident Inspector have been notified.