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 Entered dateEvent description
ENS 5591526 May 2022 10:34:00The following information was provided by the licensee via phone and email: On May 26, 2022, at 0753 CDT, the Grand Gulf Nuclear Station was notified of a spurious actuation of a single Alert Notification System siren in Tensas Parish, Louisiana. The actuation occurred during siren testing conducted at approximately 0630 CDT - no emergency conditions are present at Grand Gulf Nuclear Station. A press release from Entergy is not planned at this time. This condition is reportable under 10 CFR 50.72(b)(2)(xi) as a notification of an offsite government agency. The NRC Senior Resident Inspector has been notified.
ENS 550567 January 2021 03:18:00

An Unusual Event was declared at Grand Gulf Nuclear Station at 0124 (CST) on 01/07/2021 due to Unidentified Drywell Leakage exceeding 10 GPM for 15 minutes. Unidentified leakage has reduced to less than 0.44 GPM as of 0213 CST on 01/07/2021. The cause of the increase leakage rate is under investigation. The licensee notified the NRC Resident Inspector. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE ON 01/07/21 AT 0619 EST FROM LEROY PURDY TO BRIAN LIN * * *

At 0356 CST, Grand Gulf Nuclear Station terminated the Unusual Event following plant parameters returning to normal. The current leakage rate is 0.3 gallons per minute and stable. The NRC Resident Inspector has been notified. Notified R4DO (Kozal), IRD MOC (Gott), NRR EO (Felts), DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

ENS 5490824 September 2020 06:31:00On September 24, 2020, at 0258 CDT, Grand Gulf Nuclear Station (GGNS) was notified that one Emergency Notification Siren located on US Hwy 61 had actuated. Claiborne County was informed that no emergency exists at GGNS. The alarming siren has since been secured. Notification is being provided to the NRC in regards to the potential for media inquiry. The licensee informed the NRC Resident Inspector.
ENS 5472525 May 2020 08:44:00An (automatic) reactor SCRAM occurred at 0433 CDT, on 05/25/2020, from 66 percent core thermal power. The cause of the SCRAM was due to a Main Turbine Trip. The cause of the Turbine Trip is under investigation. All systems responded as designed. No loss of offsite power or (Emergency Safety Feature) (ESF) power occurred. No (Emergency Core Cooling System) (ECCS) or Emergency Diesel Generator initiations occurred. Main Steam Isolation valves remained open and no radioactive release occurred due to this event. The plant is stable in mode 3. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS), when the reactor is critical. The NRC Resident Inspector has been notified. Decay heat removal is through the Feedwater and Condensate System.
ENS 5292123 August 2017 10:51:00

At approximately 0340 CDT on Wednesday, August 23, 2017, Grand Gulf Nuclear Station was notified by the Entergy System Dispatcher that the NRC had called them and told them that the NRC could not contact Grand Gulf on the Emergency Notification System (ENS) line nor commercial telephone. Control Room personnel immediately tested several offsite lines including the NRC ENS line and found the lines were non-functional. Offsite prompt Public Warning Sirens were available at all times. State and Local notification capability was available via UHF radio communication. GGN Emergency Response Organization notification capability was available at all times via satellite phone activation of group paging. GGN site Emergency Response Facility intercommunications were available at all times via site internal telephones. In-plant and offsite team communications were available at all times via UHF radio. This event is being reported (8-hour notification) as an event or condition that adversely impacted offsite communications in accordance with 10 CFR 50.72(b)(3)(xiii), specifically the loss of the NRC Emergency Notification System (ENS). The phone company has been contacted and actions are being taken to restore normal communications capability at this time. The NRC Resident Inspector has been notified.

  • * * UPDATE AT 1701 EDT ON 08/23/17 FROM LEROY PURDY TO JEFF HERRERA * * *

At 1701 EDT on 8/23/17 the phone systems at Grand Gulf have been restored. The licensee will be notifying the NRC Resident Inspector. Notified the R4DO (Farnholtz)

ENS 4788030 April 2012 22:34:00Grand Gulf Nuclear Station is currently in Mode 4 (less than 200 degrees F) executing Refueling Outage 18 (RF-18) including in-service inspections. General Electric notified Entergy of a weld indication that was detected by automated ultrasonic testing. The indication is in the weld root area of N06B-KB Reactor Coolant System Pressure Boundary weld. The N06B nozzle connects Residual Heat Removal System 'C' to the Reactor Pressure Vessel. The dimension of the indication is approximately 0.9 inches in length, approximately 0.5 inches in depth and with no discernible width. Nominal wall thickness is 1.3 inches. The indication does not penetrate the entire thickness of the pipe wall and there is no leakage at the indication. There has been no release of radioactive material due to the indication. No systems were actuated due to this event. There are currently no other systems affected. The cause is under investigation and corrective action plans are being explored. The weld defect has been evaluated by Entergy Engineering and determined to meet the criteria for reporting identified in NUREG-1022: Welding or material defects in the primary coolant system that cannot be found acceptable under ASME Section XI, IWB-3600, 'Analytical Evaluation of Flaws,' or ASME Section XI, Table IWB-3410-1, 'Acceptable Standards'. The NRC Resident Inspector has been informed.