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 Entered dateEvent description
ENS 5438212 November 2019 10:32:00

On November 12, 2019, the Central Emergency Control Center (CECC) was removed from service for a planned facility upgrade project. The CECC is a common Emergency Operations Facility (EOF) for the TVA Nuclear sites (Browns Ferry / Sequoyah / Watts Bar). The duration of the upgrade project is approximately 75 days. If an emergency is declared requiring CECC activation during this period, an alternate CECC will be used. During this period, the alternate CECC will be staffed and activated using existing emergency procedures. This is an eight-hour, non-emergency notification for a Loss of Emergency Assessment Capability. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii) because the CECC will be unavailable for more than 72 hours. The Emergency Response Organization has been notified that the CECC will be unavailable during the upgrade project and to report to the alternate CECC in the event of an emergency. There is no impact on the health and safety of the public or plant employees. The NRC Resident Inspector has been notified.

  • * * UPDATE AT 1316 EST ON 11/14/19 FROM BARUCH CALKIN TO JEFF HERRERA * * *

The event information was updated to indicate that the event occurred at 0700 EST. The NRC Resident Inspector has been notified. Notified the R2DO(Musser).

  • * * UPDATE FROM ALAN PRUCHA TO KERBY SCALES AT 1526 EST ON 1/31/2020 * * *

The CECC facility upgrade project is sufficiently complete such that the CECC was returned to a functional status at 1350 CST on January 31, 2020. The NRC Resident Inspector has been notified. Notified R2DO (Baptist).

ENS 5375022 November 2018 03:56:00

EN Revision Text: HPCI UNEXPECTEDLY TRANSFERRED TO ALTERNATE SUCTION SOURCE DURING TESTING At 2125 (CST) on 11/21/2018, it was discovered that U1 High Pressure Coolant Injection System (HPCI) was inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. During performance of a routine surveillance, HPCI automatically transferred from its normal suction source to the alternate suction source. The control room operator then manually tripped the HPCI turbine. HPCI was already inoperable in accordance with Technical Specifications (TS) Limiting Condition for Operability (LCO) 3.5.1, ECCS Operating, Condition C during performance of the surveillance. However, this condition was not expected nor induced by the testing. There was no impact to the safety of the public or plant personnel. The NRC Resident Inspector has been notified. CR 1469109 documents this condition in the Corrective Action Program.

  • * * RETRACTION ON 12/28/18 AT 1300 EST FROM MARK MOEBES TO JEFFREY WHITED * * *

ENS Event Number 53750, made on November 22, 2018, is being retracted. NRC notification 53750 was made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72(b)(3)(v)(D) were met when the licensee discovered an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. During performance of a routine surveillance, the High Pressure Coolant Injection (HPCI) System automatically transferred from its normal suction source to the alternate suction source. As a result, Unit 1 HPCI was declared inoperable. On December 20, 2018, a Past Operability Evaluation was completed which determined that the HPCI System remained operable. The evaluation determined that the HPCI System could have performed its specified safety function of vessel injection throughout the time that the suction path was aligned to the torus. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(D). TVA's evaluation of this event is documented in the Corrective Action Program in Condition Report 1469109. The licensee has notified the NRC Resident Inspector. Notified R2DO (Desai).

ENS 5326918 March 2018 16:16:00At 1158 CDT on March 18, 2018, the Unit 1 reactor automatically scrammed due to a Reactor Protection System (RPS) signal generated from High Reactor Steam Dome Pressure in response to Turbine Control Valve Closure. The reactor had been operating at 100 percent power. Investigation is in progress. All control rods fully inserted into the core. Main Steam Isolation Valves remained open with Main Steam Relief Valves (MSRVs) operating on the initial transient as expected. Main Turbine Bypass Valves are currently controlling reactor pressure. Reactor Feedwater pumps remained in service to control reactor water level. Primary Containment Isolation Signals Groups 2, 3, 6, and 8 containment isolation and initiation signals were received. Upon receipt of these signals all required components actuated as required. All safety system operated as expected. At no time was public health and safety at risk. This event is reportable within 4 hours per 10 CFR 50.72(b)(2)(iv)(B) 'any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' It is also reportable within 8 hours per 10 CFR 50.72(b)(3)(iv)(A) 'any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) of this section, except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation' and requires an LER within 60 days per 10 CFR 50.73(a)(2)(iv)(A). The NRC Resident Inspector has been notified.