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 Entered dateEvent description
ENS 5461125 March 2020 15:28:00At 1240 (EDT) on March 25, 2020, with the Unit in Mode 2 at approximately 0% (zero percent) power starting up from a refueling outage, the reactor was manually tripped due to a trip of two of four Reactor Coolant Pumps. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the main condenser. The cause of the Reactor Coolant Pump trips is under investigation. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5224716 September 2016 23:35:00

At 1657 Eastern Daylight Time (EDT) the plant entered Mode 4 (from Mode 5), and subsequently, at 1710 EDT, it was discovered that 480V AC essential busses E1 and F1 were being supplied from the shutdown operations transformers. The essential busses E1 and F1 are required to be aligned to the power operations transformers in Mode 4 for operability in accordance with TS 3.8.9. With both E1 and F1 essential busses aligned to the shutdown operations transformers with the plant in Mode 4, both trains of the essential electrical power distribution system were inoperable, resulting in a loss of safety function. At 1733 EDT both E1 and F1 essential busses were aligned to the power operations transformers as required by TS 3.8.9. This issue is being reported as a loss of safety function of the essential electrical busses. The NRC Resident Inspector has been notified of the event.

  • * * RETRACTION AT 1315 EST ON 11/09/2016 FROM ANDY MILLER TO JEFF HERRERA * * *

Engineering reviewed the actual conditions during the approximate 36 minutes the 480V AC essential busses were being supplied from the shutdown operations transformers. Grid voltages were higher than assumed minimum voltages, and electrical loading during Mode 4 conditions were reduced from expected full power operation loading. As a result, Engineering determined that all equipment remained capable of performing its required functions while connected to the shutdown operations transformers. Because the equipment remained capable of satisfying the requirements for Operability, no condition existed that could have prevented the fulfillment of a safety function. Therefore, no loss of safety function existed for the 480V AC essential buses, and the notification made per 10 CFR 50.72(b)(3)(v)(A-D) by the Davis-Besse Nuclear Power Station on 9/16/2016 (EN# 52247) is being retracted. The NRC Resident Inspector has been briefed on the evaluation results and informed of this retraction. Notified the R3DO (Jeffers).