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ENS 568849 December 2023 00:49:00The following information was provided by Utah Department of Environmental Quality, Division of Waste Management (the Division) and Radiation Control, via email: On December 8, 2023 at 1550 MST, the RSO (radiation safety officer) for IHC Health Services, Inc. DBA Utah Valley Hospital called the Division to report an incident. This was a preliminary report made by the licensee's RSO who was not on-site at the time. The licensee was exchanging a Bracco Cardiogen Generator at their facility, but when they went to make the exchange, the licensee found approximately one half inch of liquid in the well. The licensee has notified the manufacturer of the incident and is working with them to mitigate the situation. This is the second generator of this type that has been found leaking at the licensee's facility. The licensee's RSO does not have all of the necessary information at this time and will contact the Division with the additional information as soon as possible. An update to this report will be provided when the information is received. Utah Event Report ID No.: UT23-0009
ENS 5685716 November 2023 08:11:00

The following information was provided by the licensee via phone conservation: An NRC licensee lost a portable moisture density gauge while in transit to a testing site. The licensee inadvertently drove to the work location with a Troxler gauge on the work vehicle tailgate. The gauge was last known to be in possession by the licensee at the intersection of Kentucky and Diamond Avenues in Evansville, Indiana. The Troxler Model 3400, SN 20494, contained 9 mCi, Cs-137 and 1320 mCi, Am-241/Be. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

  • * * UPDATE ON 12/11/23 AT 1104 EST FROM KYLE BAUER TO ERIC SIMPSON * * *

The following is a synopsis of information that was provided by the licensee via email: The site radiation safety officer received a call on Friday, November 17, 2023, from the job site informing them that the gauge was returned. The licensee returned to the job site, retrieved the gauge, performed leak tests, and notified the NRC Region III Office (Jason Draper). Notified R3DO (McCraw), NMSS Events, and ILTAB via email. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 5684710 November 2023 10:02:00

The following was received from the South Carolina Department of Health and Environmental Control (Department) via phone and email: The South Carolina Department of Health and Environmental Control was notified via telephone at approximately 0930 EST on 11/10/23 that a medical event had been discovered by the licensee on 11/09/23 at approximately 1700 EST. The Medical University of South Carolina (MUSC) reported an underdose to a patient's liver during a Y-90 microsphere procedure by 45 percent of the prescribed 500 Gray (Gy) dose. MUSC estimates that the patient received 276 Gy of the intended 500 Gy dose. The licensee reported that the total dose or activity delivered differs from the prescribed dose or activity, as documented in the written directive, by 20 percent or more. The licensee reports no immediate or ongoing concerns to public health and safety. Department inspectors will be dispatched to the facility to investigate this event. This event is still under investigation by the South Carolina Department of Health and Environmental Control. A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.

  • * * UPDATE ON 3/19/24 AT 1508 EDT FROM KORINA KOCI TO OSSY FONT * * *

The following update was received from the South Carolina Department of Health and Environmental Control (Department) via phone and email: The licensee provided their 15-day written report dated 11/17/23, which was received on 11/18/23. The written report indicated that at the time of the Y-90 radioembolization procedure no leaking was present, and after three flushes were performed the dose vial (originally containing the TheraSpheres) was measured again. Surveys of the vial and procedure room indicated radiation doses to be at background levels. Additionally, the licensee reported that measurements of the Nalgene container contents demonstrated high levels of residual activity and based on these readings the licensee ascertained that 55 percent of the prescribed dose was administered to the patient. Upon further investigation, the licensee stated that the microcatheter passing through the Y-fitting ruptured allowing the TheraSpheres to escape and collect in the fitting. The licensee's corrective actions included: communicating the details of this event with the manufacturer and inquire on whether this event has previously occurred, and requested from the manufacturer to provide refresher training to staff on the set-up of administration lines. Finally, the licensee reported that no adverse effects to the patient are expected to occur as a result of this event, since only 55 percent of the intended dose was delivered. Department inspectors were dispatched to the facility on 12/06/23. The details of the event were consistent with the licensee's 15-day written report. This event and investigation are considered closed. Notified R1DO (Ford) and NMSS Events Notification via email.

ENS 568459 November 2023 15:55:00The following is a summary of information provided by the licensee via email: A controlled substance was found in the protected area. The NRC Resident Inspector has been notified.
ENS 568439 November 2023 13:45:00

The following information was provided by the Texas Department of State Health Services (the Department) via phone and email: On November 9, 2023, the Department was notified by the licensee that a shipment of 960 millicuries of iridium - 192 Zero Wash had not arrived at its Alice, Texas, location. The licensee stated the shipment was scheduled to arrive in Alice, Texas on October 31, 2023. The licensee stated that the carrier used often misses the arrival date by as much as a week, so they did not start looking for the shipment until November 7, 2023. The licensee contacted the shipping company and the last know location of the shipment is Abilene, Texas. The shipper is searching that location for the material. The licensee stated the material was shipped inside a 55 gallon drum. It is currently believed that it is not likely that any individual would exceed any exposure limits. Additional information will be provided as it is received in accordance with SA-300. Texas Incident Number 10065 Texas NMED Number: TX230051

  • * * UPDATE ON 11/9/23 AT 1529 EST FROM ART TUCKER TO KERBY SCALES * * *

The following update was provided by the Texas Department of State Health Services via email: On November 9, 2023, the licensee reported they had located the missing shipment of 960 millicuries of iridium - 192 Zero Wash. The licensee had placed two orders for the materials for two separate locations and the shipping company had inadvertently delivered both shipments to the same location. Notified R4DO (Warnick), and NMSS Event Notifications, ILTAB, and CSNS Mexico via email. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 567733 October 2023 11:01:00The following information was provided by the New Mexico Radiation Control Bureau via phone: On October 2, 2023, at 1430 MDT, a radiography camera source became disconnected from its cable while still inside the guide tube during operations at a fabrication facility in Loving, NM. The device was described as a QSA D880 Model A424-9 camera with a 79.7 Ci iridium-192 source, serial number: 76167M. The licensee reconnected the source and secured the source inside the device in the shielded position by 2100 MDT. There were no public or occupational overexposure related to the source being disconnected from its control cable.
ENS 566512 August 2023 14:14:00The following information was received from Elkhart Clinic via telephone: A 300 micro-curie germanium-68 (Ge-68) phantom source was sent from Elkhart Clinic of Elkhart, Indiana, in Siemens Medical Solutions in Knoxville, Tennessee, via (common carrier) on November 22, 2022. The radioactive source never arrived at its destination and was subsequently declared lost by (common carrier). Ge-68 is used as a quality control source for positron emission tomography (PET) studies. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdfNON-
ENS 5660430 June 2023 19:27:00

The following information was provided by the New Mexico Environment Department via phone and email: Acuren Inspection, Inc., New Mexico Radioactive Materials License IR-448, reported a missing source of licensed material, a lost gamma camera for industrial radiography with an unknown total quantity of radioactivity. The device was lost between the cities of Carlsbad and Jal, New Mexico on Highway 128 around mile marker 38 on June 30, 2023, at approximately 1550 MDT. Crews are actively looking for the missing device. The licensee is licensed for gamma cameras with sources of iridium-192 not to exceed 150 curies and selenium-75 not to exceed 100 curies. A request for further information from the licensee as events develop has been made. Notified external: DHS SWO, FEMA Ops Center, USDA Ops Center, HHS Ops Center, DOE Ops Center, DHS CISA Central, and EPA EOC and via E-mail: FDA EOC, Nuclear SSA, FEMA National Watch Center, and CWMD Watch Desk.

      • UPDATE ON 7/7/2023 at 1238 EDT FROM ROBERT BICKNELL TO SAMUEL COLVARD ***

The device was recovered in Kermit, Texas on July 3, 2023, and reported to the State of New Mexico at approximately 1220 (MDT). Notified internal: R4DO (Drake), NMSS (email), NMSS (Williams), ILTAB (email), ILTAB (MacDonald), IRMOC (Crouch), INES (Smith), CNSNS (Mexico) (email). Notified external: DHS SWO, FEMA Ops Center, USDA Ops Center, HHS Ops Center, DOE Ops Center, DHS CISA Central, and EPA EOC and via E-mail: FDA EOC, Nuclear SSA, FEMA National Watch Center, and CWMD Watch Desk. THIS MATERIAL EVENT CONTAINS A 'Category 2' LEVEL OF RADIOACTIVE MATERIAL Category 2 sources, if not safely managed or securely protected, could cause permanent injury to a person who handled them, or were otherwise in contact with them, for a short time (minutes to hours). It could possibly be fatal to be close to this amount of unshielded radioactive material for a period of hours to days. These sources are typically used in practices such as industrial gamma radiography, high dose rate brachytherapy and medium dose rate brachytherapy. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 5660130 June 2023 12:15:00The following information was provided by the licensee via phone and followed up with an email: Yesterday, June 29, 2023, from 1201 to 1314 CDT, a Therasphere procedure was performed on a patient. The prescribed dose was for 14.58 mCi of Yttrium-90 (Y-90) to the left lobe of the liver. The authorized user (AU) stated that everything seemed to go normally other than they remembered afterwards a little more resistance than usual while performing the injection. The patient was sent for imaging and it was discovered shortly after 1500 that there was no dose in the patient. This was investigated, and the dose was found to be in the tubing. It is believed that the radioactive particles got clogged within the catheter. The AU stated that the catheter used was a model Trinav 120 cm length catheter, which is a special catheter with anti-reflux basket to prevent reflux and specially designed for Y-90 delivery. The AU stated that they would inform the patient of the medical event on the morning of June 30, 2023 (today). Additional details will be provided in the 15-day written report. A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
ENS 5660030 June 2023 11:33:00

The following information was provided by the Oklahoma Department of Environmental Quality (DEQ) via email: On June 26, 2023, a referring physician ordered 300 microcuries for an I-123 thyroid and uptake scan. Instead, outpatient scheduling ordered a 21.1 millicuries Tc-99m sestamibi parathyroid exam. Neither the registration nor the nuclear medicine department reviewed the physician's order, and the Tc-99m sestamibi was administered. Using the nuclear medicine dose tool, the radiation dose estimates provided by the licensee for the I-123 uptake and scan would have been an approximate effective dose equivalent of 0.24 rem with the thyroid being the critical organ receiving 5.20 rad. Using the nuclear medicine dose tool, the radiation dose estimates provided by the licensee for the Tc-99m sestamibi parathyroid exam was an approximate effective dose equivalent of 0.62 rem with the gallbladder being the critical organ receiving 3.83 rad. In his email, the radiation safety officer stated that their local steps after this incident will be: to have in-depth conversations with techs and outpatient scheduling manager; initiate an incident report (internal and misadministration form); make notifications to the patient and attending physician; and engage the risk management and internal sentinel event process. The incident will be documented and reviewed in the July radiation safety meeting. It will also be reviewed during the daily facility safety meeting with C-Suites and all facility directors/managers. Additional updates will be made as they are received according to SA-300. DEQ Event #1278

  • * * RETRACTION ON 07/05/23 AT 1022 EDT FROM JULIA ROBERTS TO KERBY SCALES * * *

The following is a summary of information provided by DEQ via email: The event was not a reportable medical event due to not meeting the threshold for reporting under 10 CR 35.3045(a)(1)(ii)(A). Notified R4DO (Drake) and NMSS Events Notification (email). A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.

ENS 5660230 June 2023 14:10:00The following information is a summary provided by the licensee via phone and email: The University of New Mexico reported a violation of its non-power reactor technical specification (TS) 1.1.36(c) required alarm testing frequency. The alarm testing requirement requires that the site alarms be tested on a semi-annual basis, not to exceed 7.5 months. According to the licensee, the last successful test of the New Mexico non-power reactor alarm system occurred on October 27, 2022, which is in excess of the 7.5 month requirement. The reactor was at zero percent power when the TS violation was discovered and continues to be at zero percent power. Reactor operations are suspended until the issue is resolved.
ENS 5660330 June 2023 17:09:00The following is a summary of the information provided by Engine Systems, Inc. (ESI) via fax: Copper bus bars are used at rectifier diode pigtail connections CR1, CR2, CR3, CR4, and CR7 to provide a common connection point for associated wiring to minimize the number of conductors on a single fastener. It is intended for the conductors to clamp directly to the bus bar, thereby maintaining a low resistance conduction path between components. ESI has determined the bus bars were installed incorrectly whereby the conductors are not clamped in direct contact, resulting in current now passing through the stainless steel fasteners. This configuration is undesired and will result in unnecessary heat generation which may lead to failure of the connection and therefore failure of the automatic voltage regulator (AVR) assembly. The AVR is relied upon to automatically regulate emergency diesel generator (EDG) terminal voltage. Failure of the AVR would impact the ability of the EDG to perform its safety-related function and therefore may impact the nuclear plant's ability to manage safety-related loads during an emergency event. This Part 21 applies to the bus bar installation for part numbers 72-12300-100-ESI, 72-14200-100-ESI, and 72-14000-100-6020. These part numbers impact Constellation Energy - Nine Mile Point, Avaltec/CFE - Laguna Verde (Div III), and Avaltec/CFE - Laguna Verde (Div II), respectively. Corrective Actions: Voltage regulator installed: Bus bar installation should be corrected immediately by restacking the components to ensure direct contact with all conductors. Voltage regulators in inventory (not installed): The bus bar installation should be corrected prior to installation. If desired, the customer may perform on site or the voltage regulator chassis may be returned to ESI for rework.
ENS 5643829 March 2023 17:00:00The following report was received from the Washington State Department of Health (WA State) via email: WA State received a licensee report of a stuck radiography source incident at 1606 (PDT) on March 28, 2023. The incident took place at the licensee's facility in Tacoma. The source guide tube was crimped, preventing the source drive cable from retracting into the device's shielded enclosure. A two milli-Roentgen per hour, radiation boundary was established, and the facility operations location/entrance was secured. No overexposures or spread of contamination occurred due to the event. Source retrieval/recovery actions have been completed. WA State was notified that the source was fully retracted into the shielded exposure device today, March 29, 2023, at 0430 (PDT). WA Incident No.: WA-23-006
ENS 5643729 March 2023 11:36:00The following report was received from the Texas Department of State Health Services (the Agency) via email: On March 29, 2023, the licensee reported to the Agency that on March 28, 2023, one of its technicians was performing routine shutter checks, and the shutter on one of their Vega SHF-2 gauges, containing a 50 millicurie cesium-137 source, was stuck in the open position. Open is the normal operating position for the gauge. The gauge is mounted 10-12 feet above the ground on the side of a tank with no direct access so there is no risk of exposure to individuals The licensee will contact a service company to make repairs. An investigation into this event is ongoing. More information will be provided as it is obtained in accordance with SA-300. Texas Incident No.: 10002 Texas NMED No.: TX230013
ENS 5643426 March 2023 19:41:00The following information was provided by the licensee via email: On 03/26/2023 at 1603 EDT, while performing Appendix J local leak rate testing, it was determined that the Secondary Containment Bypass Leakage (SCBL) limit had been exceeded for Unit 2. During performance of the leak rate test, SE-259-027 for X-9B penetration, it was determined that the combined SCBL limit of 15 standard cubic feet per hour for the as-found minimum pathway was exceeded, as specified in Technical Specification, Surveillance Requirement 3.6.1.3.11. This event is being reported pursuant to 10CFR50.72(b)(3)(ii). The Resident Inspector has been notified.
ENS 5637319 February 2023 08:56:00The following information was provided by the licensee via fax or email: At 0105 EST on February 19, 2023, with the James A. FitzPatrick Nuclear Power Plant (JAF) at 100 percent power, a valid high main steam line radiation signal was received. An actuation of a fire protection foam system caused migration of high conductivity water into a low conductivity sump. Organic compounds were introduced into the primary coolant and resulted in a temporary increase in nitrogen-16 which was detected by main steam line radiation monitors and actuated primary containment isolation signals in more than one system. The reactor water recirculation sample system isolated. The signal also went to the normally isolated main steam line drain system and condenser air removal system. The event is reportable in accordance with 10 CFR 50.72(b)(3)(iv)(A). The elevated radiation condition no longer exists. Health and safety of the public was not impacted by this event. The NRC Resident Inspector was notified.
ENS 5637118 February 2023 11:25:00The following information was provided by the licensee via email: On February 17, 2023 during the planned U2R22 outage on Browns Ferry Nuclear Plant Unit 2, personnel entered the Unit 2 drywell for leak identification. Personnel discovered a cracked weld on the 2A recirculation pump discharge isolation valve drain line. At 0439 CST on February 18, 2023, following engineering evaluation, this drain line was determined to be ASME Code Class 1 piping. This constitutes an 8-hour NRC notification in accordance with 10 CFR 50.72(b)(3)(ii)(A) - Any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. The NRC Resident Inspector has been notified.
ENS 5636616 February 2023 11:33:00The following information was provided by the licensee via email: On February 16, 2023 at 0859 EST, a contract worker at McGuire was transported off-site for treatment at an off-site medical facility. Upon arrival at the off-site medical facility, medical personnel declared the individual deceased at 0915 EST. The fatality was not work-related and the individual was inside the Radiologically Controlled Area. An on-site survey confirmed that neither the individual nor the individual's clothing were contaminated. A notification will be made to the Occupational Safety and Health Administration. This is a four-hour notification, non-emergency for an on-site fatality and notification of other government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). The NRC Resident Inspector has been notified.
ENS 561992 November 2022 11:12:00

The following is a synopsis of information provided by the licensee via email: Uranium Recovery and Recycle Services (URRS) personnel were offloading ash on 11/1/22 that they had received in 2003 from the decommissioned Hematite site at Dock 3. The operators opened the Type A drum and from an inner canister pulled out the bag of Hematite ash. The bag had a tag indicating enrichment levels in excess of their license limits. Upon discovery, the operators contacted criticality safety engineering and the safeguards coordinator. The operators were instructed to replace the bag in the canister and drum and to segregate the drums that contained material potentially greater than license limits in accordance with generally accepted guidance for criticality safety. An extent of condition was performed using materials control and accounting records of the received material. It was discovered that several drums potentially contain material in excess of license enrichment limits. The plant is in a safe condition and the steps taken in response to this event are considered to be conservative. This report is being made per 10 CFR 70 Appendix A (b)(1). This event resulted in the facility being in a state that was not analyzed in their Integrated Safety Analysis Report and resulted in a failure to meet the performance requirements of 10 CFR 70.61, specifically there were no controls in place due to it being an unanalyzed condition. Westinghouse is unable to open, sample, and test the ash to determine enrichment until the proposed process has been analyzed with documented controls in place. This issue has been entered into the licensee's corrective action program as IR-2022-9728.

  • * * UPDATE ON 09/13/23 AT 1219 EDT FROM STEPHANE SUBOSITS TO THOMAS HERRITY * * *

The following is a synopsis of information provided by the licensee via email: On 9/12/2023, while offloading additional barrels of Hematite Ash from the the 2003 shipment, A URRS operator identified that the tag for a drum showed the contents have a higher enrichment than that which is recorded in the Chemical Area Manufacturing and Process System (ChAMPS) and on the original paperwork provided by Hematite Fuel Operations. The unloading activity was stopped, and URRS Management and Nuclear Criticality Safety were notified. The unopened pail was placed back in the drum and the drum was segregated from other items in the area. Environmental Health and Safety requested that the remaining seven drums be opened and the contents tag for each be checked against the information in ChAMPS and the original paperwork from Hematite Fuel Operations. This was done. This report is conservatively being made as an update to Event Notification 56199 under reporting criterion 10 CFR 70 Appendix A (b)(1) as an event that resulted in the facility being in a state that was not analyzed in the Integrated Safety Analysis, and resulted in a failure to meet the performance requirements of 10 CFR70.61 similar to the 9 drums of Hematite Ash that were discovered in November 2022 due to it being an unanalyzed condition. Westinghouse believes it is likely that the enrichment listed on the tag of the drum is inaccurate. The issue has been entered into the corrective action program as IR-2023-8953. Notified R2DO (Endress) and NMSS_EVENTS via email.

ENS 551757 April 2021 10:45:00The following was received from the Illinois Emergency Management Agency (the Agency) via email: The Agency was contacted on 4/6/21 by the Radiation Safety Officer (RSO) for Howell Asphalt Company to report a damaged Troxler Gauge. The incident occurred at approximately 1500 CDT at a temporary job site on Locust Street in Centralia, IL. The RSO for Howell Asphalt Company called to report that a Troxler 3440 gauge was run over by a vehicle and was stuck under a car. Reportedly, the driver of the vehicle dismissed the barriers and entered the construction zone. Emergency response personnel arrived on site to isolate and assist in moving the vehicle off the gauge. At the time of the accident, the gauge was in use for backscatter measurements and therefore, all sources were in the shielded position. The RSO responded to the site and reported that both the Cs-137 and the Am-241 sources appeared to be shielded and that only the gauge housing was damaged. At 1555 CDT, the RSO called to provide an update. The RSO reported that both sources were undamaged and had been retrieved. The RSO has secured the gauge and is returning it to the Effingham office for disposal through Troxler. The gauge will be transported in its Troxler case which was undamaged. Source and gauge serial numbers are pending and the report will be updated once available. Agency staff will continue to track this matter pending receipt of leak tests and confirmation of disposal Illinois Incident Number: IL210007
ENS 543726 November 2019 09:12:00The following information was received via fax: On November 4, 2019 the licensee was performing a mask treatment with the Elekta Gamma Knife Icon containing Cobalt 60. The treatment was interrupted when the High Definition Motion Management tracking system lost communication with 1 minute and 29 seconds remaining from shot B6, (planned for 2 minutes 13 seconds) and 2 minutes 36 seconds remaining for B3 (No treatment was delivered from this shot). The sources safely retracted into their home position and the software message prompted the user to reinitiate the Gamma Knife system; however, an error message occurred on each attempt to reinitiate. The system was then rebooted; however, the same error occurred again. The patient was removed from the treatment vault and a service call was made to Elekta. The onsite service engineer arrived that same day to troubleshoot and new parts were ordered and arrived on November 5, 2019. The intent is to complete the remaining treatment on November 5, 2019 once the Gamma knife repair and subsequent QA is completed. The doctor and patient were informed immediately. No overdose to anyone has occurred and no harm is expected to the patient. The (PA Bureau of Radiation Protection) will update this event as soon as more information is provided. Pennsylvania Event Report ID No: PA190025 A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
ENS 4845730 October 2012 04:10:00

This report if being made under the requirements of 10 CFR 50.72(b)(2)(iv)(B), Actuation of the Reactor Protection System While Critical, except preplanned, and under the requirements of 10 CFR 50.72(b)(3)(iv)(A), Valid Actuation of Listed System, except preplanned. Salem Unit 1 was operating at 100% reactor power when a loss of 4 condenser circulators required a manual reactor trip in accordance with station procedures. The cause of the 4 circulators being removed from service was due to a combination of high river level and detritus from Hurricane Sandy's transit. All control rods inserted. A subsequent loss of the 2 remaining circulators required transition of decay heat removal from condenser steam dumps to the 11-14 MS10s (atmospheric steam dump). Decay heat removal is from the 11/12 Aux Feed Pumps to all 4 steam generators via the 11-14 MS10s. 11/12/13 AFW pumps started due to low level on all steam generators due to shrink from full power operation (this is a normal response). All safety related equipment functioned as expected. No one has been injured. As an additional note, Hurricane Sandy had recently moved past artificial island. Salem Unit 1 is currently in Mode 3. Salem Unit 2 reactor is currently in its 2R19 refueling outage and is shutdown and defueled with no fuel movement in progress. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE ON 10/30/12 AT 0835 EDT FROM JOHN OSBORNE TO DAN LIVERMORE * * *

At 0513, following (a) Unit 1 manual (reactor) trip due to loss of condenser cooling, a manual steam line isolation was initiated due to a high condenser back pressure. All main steamline isolation valves responded as expected. The high condenser back pressure resulted in the #11 low pressure turbine rupture disc relieving. Unit 1 remains in mode 3 with Reactor Coolant System temperature at 549 (degrees) and stable. Reactor Coolant System pressure is 2235 psig and in automatic control. Pressurizer level is on program at 26 percent level and in automatic control. Core cooling is via aux feed water and the steam generator levels are on program. There were no (personnel) injuries. The licensee has notified the NRC Resident Inspector. Notified R1DO (Caruso).

ENS 4845530 October 2012 03:20:00

Peach Bottom Atomic Power Station Control Room was notified of a loss of greater than 25% of sirens after severe storms in the area associated with Hurricane Sandy. Thirty-one (31) of 97 Emergency Planning Zone (EPZ) sirens are currently unavailable in Lancaster, York, Cecil and Harford Counties. Actions are currently being taken to restore unavailable sirens. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 0515 EDT ON 10/31/12 FROM SCOTT RUCKER TO S. SANDIN * * *

Currently 12 of 97 sirens remain inoperable. The licensee will inform state and local agencies and the NRC Resident Inspector. Notified R1DO (Caruso).

ENS 4845430 October 2012 00:30:00On October 29, 2012, at 2241EDT, the Reactor Protection System automatically actuated at 100% reactor power due to a direct electrical trip to the Unit 3 Main Turbine Generator. The generator trip resulted in a turbine/reactor trip. All control rods fully inserted on the reactor trip. All plant equipment responded normally to the unit trip. This is reportable under 10 CFR 50.72(b)(2)(iv)(B). The plant is stable in Mode 3 at this time. The Auxiliary Feedwater System actuated following the automatic trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A). The Emergency Diesel Generators did not start as offsite power remained available and stable. The unit remains on offsite power and all electrical loads are stable. No primary or secondary relief valves lifted. The plant is in Hot Standby at normal operating temperature and pressure with decay heat removal using auxiliary feedwater to the steam generators and normal heat removal through the condenser via condenser steam dumps. There was no radiation released. Indian Point Unit 2 was not affected by this event and remains at 100% power. A post trip investigation is in progress. The licensee notified the NRC Resident Inspector.
ENS 4845630 October 2012 03:35:00On October 29, 2012 at 2100 EDT, Nine Mile Point Unit 2 experienced an automatic initiation of the Division 1 Emergency Diesel Generator due to a loss of line 5. Line 5 is one of the 115KV offsite power sources. Line 5 was lost due to a lightening arrestor falling onto electrical components in the Scriba switchyard during high winds. During the electrical transient, Nine Mile Point Unit 2 also experienced a feedwater level control lockup, requiring manual control. No Emergency Core Cooling Systems actuated and feedwater level control was returned to automatic. Nine Mile Point Unit 2 remained at 100% power during the loss of line 5. The off-site power source, line 5, was restored on October 30, 2012 at 0326 EDT. The licensee notified the NRC Resident Inspector.
ENS 4845329 October 2012 21:58:00On October 29, 2012 at 2100 EDT, Nine Mile Point Unit 1 experienced an automatic reactor scram due to a generator load reject. The cause of the load reject is currently under investigation. All control rods fully inserted and all plant systems responded per design following the scram. Following the automatic scram, the High Pressure Coolant Injection (HPCI) System automatically initiated as expected. At Nine Mile Point Unit 1, a HPCI System actuation signal on low Reactor Pressure Vessel (RPV) level is normally received following a reactor scram, due to level shrink. HPCI is a flow control mode of the normal feedwater systems, and is not an Emergency Core Cooling System. At 2101 EDT, RPV level was restored above the HPCI System low level actuation set point and the HPCI System initiation signal was reset. Pressure control was established on the Turbine Bypass Valves, the preferred system. Three Electromatic Relief Valves actuated due to this scram and re-closed automatically. Nine Mile Point Unit 1 is currently in Hot Shutdown, with reactor water level and pressure maintained within normal bands. Decay heat is being removed via steam to the main condenser using bypass valves. Both Reserve Station Transformers are in service and being supplied by their normal power sources. Both Emergency Diesel Generators are operable and in standby. The unit is currently implementing post scram recovery procedures. The licensee has notified the NRC Resident Inspector. Notified R1DO (Caruso).
ENS 4803820 June 2012 15:30:00

It was discovered at approximately 1700 EDT on 6/19/2012 that the moderation control in the gadolinia pellet press operation had been degraded. An operator error allowed a can containing approximately 14 kg of uranium powder to be processed without the required material move transaction, a process control that ensures the container and material type are allowed at the designated location. This resulted in a temporary degraded item relied on for safety (IROFS) condition involving a criticality control. The press moderation control is one of four IROFS to prevent a criticality accident. The gadolinia press station material control system functioned as designed and prompted the operator of an error. The other criticality controls on geometry were maintained at all times. At no time was an unsafe condition present. The gadolinia pellet press operation has been shut down and additional corrective actions, extent of condition, and extent of cause are being evaluated. This event is being conservatively reported pursuant to 10 CFR 70, Appendix A (b) (2).

  • * * RETRACTION FROM SCOTT MURRAY TO HOWIE CROUCH AT 1359 EDT ON 7/11/12 * * *

On 6/20/12, GNF-A conservatively made a 24 hour event notification (EN 48038) due to a single missed Fuel Business System (FBS) transaction on 6/19/12 at the gadolinia press operation. After further review of the identified condition, it has been determined to be not reportable to NRC and the event notification can be retracted. Notified R2DO (Blamey) and NMSS EO (Silva).

ENS 4785119 April 2012 13:30:00

At approximately 1345 EDT on 4/18/12, during routine testing on an outdoor Criticality Accident Alarm System (CAAS) Data Acquisition Module (DAM #22), the local alarm horn in the Wilmington Field Services Center (WFSC) building #3 inspection records area was found to be inaudible. The cause and extent of the condition is under investigation. Personnel were removed from the inspection records area until compensatory measures were established. There are no active fissile material operations impacted by this discovery, thus no unsafe condition existed. This event is being reported pursuant to the requirements of 10CFR70.50 (b)(2). The licensee notified the NC Division of Radiation Protection and the New Hanover County Emergency Response Center.

  • * * RETRACTION FROM SCOTT MURRAY TO JOHN SHOEMAKER ON 05/17/2012 AT 1641 EDT * * *

Upon further review, GNF-A has determined that the reported condition (EN 47851) was not required to be reported by the plain letter of the regulation (10 CFR 70.50(b)(2)) and the filing of the report was inconsistent with industry practice. As such, this report is being retracted. GNF-A has entered the condition identified in the course of the monthly tests (i.e., areas where audibility of the CAAS should be enhanced) into its corrective action program and is addressing them accordingly. The licensee will notify NRC Region II (Thomas). Notified R2DO (Shaeffer) and NMSS (Stablein).

ENS 4766415 February 2012 12:25:00At 0825 CDT on 2/15/2012, the Monticello Nuclear Power Generating Plant (MNGP) received a report from the Sherburne County Sheriff Dispatcher that there had been an inadvertent manual initiation of Emergency Preparedness sirens in the county while performing siren testing. All plant conditions/parameters are normal. A total of 48 emergency sirens were on for approximately one minute before being secured. All sirens are currently functional. Sherburne County and the site NRC Resident Inspector have been notified The licensee also notified the Wright County offices.
ENS 4803519 June 2012 15:19:00The following information was obtained from the Commonwealth of Massachusetts via email: The licensee is a manufacturer of beta gauges used to measure the thickness and weight of materials. This event was discovered when a hired decommissioning consultant found evidence of contamination in the source storage room of the facility. Their intention was to decontaminate the storage room and release it as part of an office relocation project within the same building. The leaking sources in this event were apparently caused by the licensee by the improper application of PVC tape to the source window upon packaging. The licensee claims that this is not a current practice, but is the likely cause of source leakage prior to November of 2009. One or more historical sources could have been involved. The licensee claims that they were sent to Thermo Fisher Scientific in Germany in 2009. The sealed sources installed in the licensee's devices contain Strontium-90, Krypton-85, and Americium-241 (1.85E-10 TBq each). Wipe tests were conducted on all available sources on January 19, 2012 by the licensee. None were found to be leaking. The Massachusetts Radiation Control Program has initiated an investigation of this incident and will subsequently provide a report of the findings.
ENS 4766615 February 2012 15:39:00Groundwater Analytical Company, Massachusetts radioactive materials licensee G0046, underwent bankruptcy proceedings. Their assets were subsequently seized in a bank action and auctioned off by The Branford Group. Among the items auctioned were 13 Ni-63 sources associated with gas chromatograph devices. This auction took place on 11/2/2011. The Massachusetts Radiation Control Program (Agency) discovered this event on 2/15/2012 and has opened an investigation to find the missing radioactive sources. The auction house which handled the transfer of the gas chromatographs has indicated that they have records of the individuals who purchased the items and will be providing that information to the Agency by the end of the week. The Agency continues the investigation into this matter and this item remains open. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 4719725 August 2011 11:50:00At 0917 EDT on 8/25/11, Integrity Testlab received a facsimile notification from Integrity Testlab's dosimeter processor, Landauer, that an assistant radiographer's July 2011 dosimeter had received/recorded 9.587 R. According to the assistant radiographer, his dosimeter had come off his work clothes during radiographic operations on 7/29/11. When he discovered that his film badge was not on his work clothes, he looked for and found the dosimeter near the exposure device. He believes that his dosimeter had 4 or 5 exposures during the time the dosimeter was near the exposure device. The exposure time for each exposure was about 40 seconds in length. On 8/2/11, the assistant radiographer informed the RSO what had occurred on 7/29/11. The RSO instructed the assistant to complete a statement on what transpired on that date. The RSO verified the assistant's statement with the radiographer. The RSO verbally instructed the assistant how to best secure the dosimeter on the rate alarm meter pouch and to periodically check that all required dosimetry remains on his person during radiographic operations. The RSO reviewed all daily pocket dosimeter readings recorded for the month of July. He determined that the assistant had performed radiography for a total of 9 days in July. The RSO also noticed that he had performed radiography with the same radiographer 8 of those 9 days. The radiographer's pocket dosimeter reading recorded 200 mR, while his assistant's daily readings totaled 201 Mr. The RSO contacted Landauer in order to get the radiographer's July recorded dosimeter results and Landauer verbally informed the RSO that the total was 87mR for the month of July for the radiographer. After reviewing all documentation, the RSO believes that the assistant's dosimeter was accidently exposed to excessive radiation and that this was not an actual overexposure. Furthermore, the RSO intends to inform all personnel involved in Integrity Testlab's Radiation Safety Program about this event and to instruct the personnel on the importance of securing their dosimetry on their person. An 880 Sigma device was involved during this occurrence and it had contained Ir -192, 55.5 Ci.
ENS 4718223 August 2011 14:30:00The licensee declared a Notification of Unusual Event due to seismic activity. Equipment walkdowns performed. The licensee also terminated the event at the time of notification.
ENS 4718023 August 2011 14:05:00

The licensee declared a Notification of Unusual Event due to seismic activity. The reactor was not operating at the time of the earthquake. Facility walkdown is in progress.

  • * * UPDATE FROM MOHAMMED AL-SHEIKILY TO HOWIE CROUCH AT 1415 EDT ON 8/23/11 * * *

The licensee exited the NOUE. Notified R1DO (Krohn) and NRR (Thorp).

ENS 4718623 August 2011 14:58:00

At 1355 hrs. EDT, an event was recorded by the seismic monitoring system. The seismic monitoring system classified the event as less than Operating Basis Earthquake (OBE) and less than Safe Shutdown Earthquake (SSE). The seismic monitoring system additionally classified the event as Seismic: NO At 1405 hrs., SSES (Susquehanna Steam Electric Station) declared an Unusual Event (under EAL OU5) after confirmation by outside agencies that an actual seismic event had occurred and reports from numerous personnel that they had detected ground motion. At time of transmittal there is no indication of equipment damage, personnel injuries and no automatic initiations of any ECCS or ESF systems or RPS actuations occurred. Assessment of any equipment damage is ongoing. The licensee has notified the NRC Resident Inspector and state and local authorities.

  • * * UPDATE FROM FRITZ OHLSEN TO JOHN KNOKE AT 2110 EDT ON 8/23/11 * * *

The licensee has terminated the Notification of Unusual Event. The licensee has notified the NRC Resident Inspector and state and local authorities. Notified R1DO (Krohn), IRD (Morris), DHS (Bean) and FEMA (Via).

ENS 4718823 August 2011 14:35:00

License declared an Unusual Event based on seismic activity.

  • * * UPDATE AT 1801 EDT ON 08/23/11 FROM LISA SWEENEY TO JOHN SHOEMAKER * * *

Oyster Creek has terminated from the Unusual Event for seismic activity. Engineering walk downs of reactor building, turbine building, switchyard, emergency diesel generators, intake structure, dilution structure, ISFSI (Independent Spent Fuel Storage Installation), and fire pond were completed and no problems noted. All plant conditions remain stable. Licensee notified the NRC Resident Inspector and applicable state and local authorities. A press release is planned. Notified R1 IRC (Dentil), IRD (Gott), DHS (Bean), FEMA (Via), USDA (Kraus), and DOE (Turner).

ENS 4718123 August 2011 14:24:00

At 1403 hrs. EDT, North Anna Power Station declared an Alert due to significant seismic activity onsite. The Alert was declared under EAL HA6.1. Both units experienced automatic reactor trips from 100% power and are currently stable in Mode 3. All offsite electrical power to the site was lost. All four emergency diesel generators (EDG) automatically started and loaded and provided power to the emergency buses. While operating, the 2H EDG developed a coolant leak and was shutdown. As a result, the licensee added EAL SA1.1 to their declaration. All control rods inserted into the core. Decay heat is being removed via the steam dumps to atmosphere. No personnel injuries were reported.

  • * * UPDATE FROM ROBERT RINK TO HOWIE CROUCH AT 1116 EDT ON 8/24/11 * * *

The licensee has downgraded the Alert to a Notification of Unusual Event based on equipment alignments and inspection results. The licensee notified R2 IRC. Notified IRD (Marshall), NRR (Thorp), FEMA (Hollis), DHS (Inzer), USDA (Ferezan), HHS (Willis) and DOE (Parsons).

  • * * UPDATE FROM ROBERT RINK TO HOWIE CROUCH AT 1317 EDT ON 8/24/11 * * *

The licensee has exited the Notification of Unusual Event at 1315 EDT. The exit criteria was that all inspections and walkdowns were completed and plant conditions no longer meet the criteria for a NOUE. Notified R2DO (Widmann), IRD (Marshall), NRR (Thorp), FEMA (Hollis), DHS (Inzer), USDA (Ferezan), HHS (Willis) and DOE (Jackson).

  • * * UPDATE FROM DON TAYLOR TO DONALD NORWOOD AT 1405 EDT ON 8/26/11 * * *

This notification is to report new information identified post event that a condition existed which met the emergency plan criteria but was not declared. On August 23 at 1403 EDT, North Anna Power Station declared an Alert due to seismic activity onsite. The Alert was declared under Emergency Action Level (EAL) HA6.1 "Other conditions existing which in the judgment of the SM warrant declaration of an alert. Initial review of seismic response data from the earthquake on 8/23/11 (1348 hours) indicates that design spectrum input assumptions (i.e. Design Basis Earthquake (DBE) limits) may have been exceeded above 5 HZ. This would have resulted in classification of an Alert under EAL HA1.1. No significant equipment damage to safety related systems (including class I structures) has been identified through site walk-downs nor has equipment degradation been detected through plant performance and surveillance testing following the earthquake. The licensee notified the NRC Resident Inspector. The licensee also plans on notifying the State Emergency Operations Center and the Louisa County County Administrator. Notified R2DO (Widmann) and NRR EO (Bahadur).

ENS 4719023 August 2011 14:23:00

At 1401 hrs. EDT on 8/23/11, TMI (Three Mile Island) declared an Unusual Event due to a threshold seismic condition (HU5) earthquake. The earthquake was felt at the plant. No equipment damage has been identified. No personnel injuries were reported. The licensee has notified the NRC Resident Inspector and state and local authorities.

  • * * UPDATE FROM JOE SHUFFNER TO JOHN SHOEMAKER AT 1744 EDT ON 8/23/11 * * *

The Unusual Event declared at 1401 EDT due to the ground motion felt at the site has been terminated at 1730 EDT. Walkdowns have been performed and no equipment damage has been identified. The plant remains in a stable condition at 100% power. Offsite power and diesel generators were verified to be unaffected by the event. The licensee has notified the NRC Resident Inspector and state and local authorities. Notified R1 IRC (Dentil), IRD (Gott), DHS (Bean), FEMA (Via), USDA (Kraus), and DOE (Turner).

ENS 471326 August 2011 17:44:00

The following information was obtained from the State of California via email: At 0530 PDT on 8/6/2011, a Model 4640 Troxler material density gauge belonging to Pavement Engineering of Redding, CA was lost at a construction site between McAllen Road and Olivehurst on Highway 70 south of Yuba City, CA. The operator set the gauge down by the side of the road and returned to find it missing. It was reported missing at 1105 PDT on 8/6/2011 to the California Emergency Management Agency who contacted the California Department of Public Health, Radiological Health Branch (RHB) at 1126 PDT. Sutter County Sheriff's office has responded and is investigating. Also contacted was Sutter County Fire Dept. A health physicist has been deployed from RHB to assist in the search with a variety of radiation survey instruments in case the gauge was misplaced by the side of the road. The gauge contains 9 mCi of Cs-137.

  • * * UPDATE ON 08/06/2011 AT 1936 PDT FROM JOHN FASSELL (VIA EMAIL) TO ERIC SIMPSON * * *

A survey by RHB staff over 0.6 miles of highway margin assisted by licensee personnel failed to recover the gauge. A reward will be posted by the licensee. Notified R4DO (Hagar) and FSME EO (McKenney) via email. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 469183 June 2011 11:20:00A non-licensed supervisory contractor admitted to attempting to subvert a Fitness for Duty test. The contractor's access to the site has been suspended. The NRC Resident Inspector was notified. Contact the Headquarters Operations Officer for additional details.
ENS 469152 June 2011 14:50:00An employee was treated in the site dispensary for irritation to the eye. The employee's coveralls, knee area, and boots were surveyed and determined to be contaminated (coveralls 2,643 dpm per 100 cm2 (centimeters-squared), boots 3,126 dpm per 100 cm2). Employee stated that they were cleaning out the bottom of the cone on A1 HF filter bowl from the top of the filter when something entered their eye. The individual stated that they saw a small amount of dust in the bottom of the filter bowl, but did not actually see dust near their eye. Other employees were present at the time but, did not notice what had occurred and the affected employee did not tell them what had happened. The individual returned to work after treatment. The licensee will be making a notification to NRC Region II.
ENS 469071 June 2011 11:08:00The Technical Support Center (TSC) has been rendered non-functional due to a malfunctioning TSC ventilation system. Investigation into the cause of elevated TSC room temperature led to the discovery of a malfunctioning condensing unit compressor. Repairs to the ventilation system were immediately initiated with high priority. Compensatory measures per FNP-0-EIP-6.0 (TSC Setup and Activation) for maintaining emergency assessment, off-site response, and off-site communication capabilities are being put in place. These measures include the conditional relocation of the TSC staff in the event of a declared emergency if the Emergency Director deems the TSC to be uninhabitable. The NRC Resident Inspector has been notified.
ENS 477195 March 2012 16:17:00

At the request of NRC Region I, Camden-Clark Memorial Hospital reassessed records from a prostate radioactive seed implantation procedure that had been performed on February 25, 2011. The record review indicated that the patient had received roughly 80 percent of the prescribed dose. The effect on the patient has been minimal as the desired response was achieved. The long term effect will be under constant follow-up. The entire implant process will be reviewed with special attention to real time seed placement and subsequent thirty day image evaluation with respect to NRC regulatory guidelines. The attending physician, based on medical judgment, felt that notifying the patient would be harmful. The patient is under the care of oncologic physicians and will be followed appropriately as per his disease type.

  • * * UPDATE AT 1636 EST ON 12/03/12 FROM DAN BERKLEY TO S. SANDIN * * *

The licensee is updating the report with the following information: That (1) the dose received by the target was less than 80% of the prescribed dose and (2) a small volume of tissue outside of, and adjacent to, the treatment site received a dose that was greater than 10 Gy and more than 50% greater than the prescribed dose to that location." The licensee discussed this update with R1 (Weidner). Notified R1DO (Jackson) and FSME Events Resource via email. A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.

ENS 464533 December 2010 15:39:00The following information was received via email from the State of Colorado: At approximately 1600 MST, 12/2/10, the Colorado Department of Public Health and Environment received a report of a possible misadministration at the Prostate Seed Center, a Colorado radioactive materials licensee. Additional information was received on 12/3/10 that there was indeed a misadministration of I-125 in seed form. An excess dose of 27 to 32% was administered above the prescribed dose. There was an apparent miscommunication between the supplier and the Prostate Seed Center about the units of dose the seeds were to contain. Apparently, Air Kerma units were ordered and milliCuries were delivered. An investigation as to the cause of the misadministration is being performed. A written report on the incident is required by the Department within 30 days. The excess dose was delivered to the patient's prostate. A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
ENS 464462 December 2010 16:25:00

A Troxler moisture density gauge being used at Fort Meade (Maryland) was found to be stolen along with other industrial equipment at 1400 on 12/2/10. The Troxler gauge was last seen on Monday afternoon, 11/29/10, when it was secured in a temporary storage location inside a lock-box and chained to a sea container. Other items stolen included crane mats, a generator and miscellaneous tools. The nuclear gauge is a Troxler Model 3430, S/N 37672, which contains two radioactive sources. One source is 44 mCi of Am-241/Be (S/N 78-2430). The other source is 9 mCi of Cs-137 (S/N 77-4907). The licensee will notify base police to begin an investigation into the theft. The licensee has notified the State of Maryland of the theft.

  • * * UPDATE FROM DREW THOMAS TO JOE O'HARA AT 0948 ON 12/14/10 * * *

On 12/10/10, FT. Meade U.S. Army base police officers informed the licensee that the stolen container had been "dumped" back onto the jobsite. The licensee responded to the site and discovered the missing gauge inside the container. The source was in the locked and shielded position inside the gauge and the gauge doesn't appear to have been damaged. The gauge has been recovered and is now in the custody of the licensee. A leak test of the gauge is scheduled to be performed. Notified R1DO(Holody), FSME(Reis) and ILTAB. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 464523 December 2010 11:18:00

The following was received via email from the State of Arkansas: The Arkansas Department of Health, Radioactive Materials Program, was notified at 1315 CST on December 2, 2010 by licensee Grubbs, Hoskyn, Barton, and Wyatt, Inc. (ARK-0456-03121) of a missing Troxler moisture/density gauge. The gauge was being transported between their office in Little Rock, Arkansas and a job-site in Bryant, Arkansas. The authorized user observed the gauge was missing at approximately 1230 CST. The gauge had apparently fallen from the transport vehicle. The Troxler gauge is a Model 3430 (SN 63492) containing 40 mCi Am-241:Be and 8 mCi Cs-137. It appears that the gauge was not properly secured in the vehicle. The Arkansas Department of Health is investigating the circumstances surrounding this event. The Arkansas Department of Health prepared a press release concerning this event. Arkansas Department of Health also notified the Police Departments of Little Rock and Bryant, the Sheriff's Offices of Saline and Pulaski Counties, the Arkansas State Police, and the Arkansas Department of Emergency Management. Arkansas has assigned event report ID number AR-12-10-02.

  • * * UPDATE AT 1147 EDT ON 9/6/11 FROM PEMBERTON TO HUFFMAN VIA E-MAIL * * *

On August 30, 2011, the Arkansas Department of Health, Radioactive Material Division was informed by (the) Radiation Safety Officer for Grubbs, Hoskyn, Barton and Wyatt, that the Troxler 3430 Moisture/Density Gauge, SN#63492, lost on December 2, 2010, had been recovered. A Departmental investigation confirmed that the gauge recovered on August 30, 2011, was in fact the device lost on December 2, 2010. The Department considers this incident to be closed. The State Department of Health Representative indicated that the gauge was returned to the licensee by a private citizen who wished to remain anonymous. R4DO (Drake) and FSME (McIntosh) notified. ILTAB notified via e-mail. THIS MATERIAL EVENT CONTAINS A "LESS THAN CAT 3" LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 464431 December 2010 15:14:00

Oyster Creek has declared an Unusual Event (MU7) due to Reactor Coolant System leakage greater than 10 gpm. Leakage has been determined to be from the 'B' reactor recirculation pump seals. The 'B' Reactor Recirculation Loop was isolated and leakage stopped. The plant remained in the normal electrical lineup and no safety systems actuated during this evolution. The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM ERIC SWAIN TO ERIC SIMPSON AT 1548 ON 12/1/10 * * *

At 1537 EST, "Oyster Creek has terminated from an Unusual Event. Event terminated due to isolating leakage from the 'B' Reactor Coolant Loop. The licensee notified the NRC Resident Inspector. Notified R1DO (Schmidt), IRD (Gott), NRR EO (Nelson), DHS and FEMA.

ENS 464451 December 2010 17:40:00

On 12/01/10, at 1359 EST, Peach Bottom Atomic Power Station reported a petroleum product spill in the discharge canal. Total quantity of substance is less than 1 quart. Lewis Environmental agency has been contacted to aid in containment and cleanup of the spill. This report is being submitted pursuant to 10 CFR 50.72(b)(2)(xi) and 10 CFR 72.75(b)(2). The spill did not reach Comprehensive Environmental Response Compensation and Liability Act (CERCLA) reportable quantities. The licensee notified the Pennsylvania Department of Environmental Protection, United States Coast Guard, and EPA Region 3. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM E. WRIGHT TO V. KLCO ON 12/2/10 AT 1354 EST * * *

The licensee is retracting the event due to the quantity of substance released to the environment is less than the reportable quantity. The licensee will notify the NRC Resident Inspector. Notified R1DO (Schmidt).

ENS 4635322 October 2010 16:52:00

On 10/22/10, at 1058 EDT, a troubleshooting of Independent Spent Fuel Storage Installation (ISFSI) Cask TN-50-A indicated that a leak existed in the cask lid sealing area at a rate greater than allowed by ISFSI Cask Technical Specification (TS) Section 3.1.3, Cask Helium Leak Rate. TS 3.1.3 limits the Cask Helium Leak Rate to 1.0 E-05 ref-cc/sec. The cask is currently in unloading operations and is located within the Peach Bottom Atomic Power Station Unit 3 containment building. Preliminary review indicates that a leak exists at the weld plug that provides sealing of the drilled interseal passageway associated with the drain port penetration of the cask lid. This leak effectively provides a bypass of the main lid outer confinement seal. This report if being submitted pursuant to 10CFR72.75(c)(1) as a result of a material defect in a weld in the cask main lid. This report is also being submitted pursuant to 10CFR72.75 (c) (2) as a result of a resolution in the effectiveness of the cask confinement system. The Certificate of Compliance for this cask is 1027 (Amendment 1). The NRC Resident Inspector has been informed of this notification.

  • * * UPDATE AT 1515 EDT ON 10/27/10 FROM JEREMY HITE TO DONG PARK * * *

On 10/27/10, at 1107 (EDT), troubleshooting of Independent Spent Fuel Storage Installation (ISFSI) Cask TN-68-01 identified that a helium leak exists in the cask lid sealing area at a leak rate greater than allowed by ISFSI Cask Technical Specification Section 3.1.3, Cask Helium Leak Rate. TS 3.1.3 limits the Cask Helium Leak Rate to 1.0 E-O5 ref-cc/sec. The cask was in LOADING OPERATIONS and is currently located within the (Peach Bottom Atomic Power Station) PBAPS Unit 2 containment building. Preliminary review indicates that a leak exists in the Cask Main Lid Outer Closure Seal. The cask will be repaired and tested prior to returning the cask to the Independent Spent Fuel Storage Installation (ISFSI). No release of radiation occurred as a result of this issue. This report is being submitted pursuant to 10CFR 72.75(c)(2) as a result of a reduction in the effectiveness of the cask confinement system. The Certificate of Compliance for this cask is 1027 (Amendment 0). The NRC Resident Inspector has been informed. Notified R1DO (Caruso), NRR EO (Thorp), NMSS EO (Lorson), and IRD (Grant).

ENS 4635222 October 2010 09:46:00On 10/22/2010 at 0636 hours, North Anna Unit-1 reactor was manually tripped during physics testing and 1-E-0 was entered due to problems with the Rod Control In Hold Out Switch. The out direction of the switch was not functioning properly and the reactor was tripped to put the plant in a condition to perform maintenance. All control rods fully inserted into the reactor core. This was an uncomplicated reactor trip with no automatic ESF actuation required. Unit 1 is currently stable at normal operating temperature and pressure in MODE 3 (Hot Standby). The plant electrical line-up is normal. Decay heat removal is via the steam dumps. Notification will be made to the local county administrator's office. The NRC Resident Inspector has been notified.