Semantic search

Jump to navigation Jump to search
 Entered dateEvent description
ENS 4956521 November 2013 04:23:00On November 20, 2013 at 2240 (EST), secondary containment drawndown testing surveillance failed to meet acceptance criteria SR 3.6.4.1.5 due to maximum flow rate exceeding the allowable value. SSES (Susquehanna Steam Electric Station) previously entered SR 3.0.3 at 0900 on 11/15/2013 due to not meeting SR 3.6.4.1.4 and SR 3.6.4.1.5 because of an untested alignment of the 101 bay with ventilation aligned as a no zone during past performances of the drawdown testing surveillance. The surveillance being performed on 11/20/2013 was testing this previously unsurveilled alignment. Upon failure of the surveillance, secondary containment ventilation was realigned to the previously tested 818 hatch alignment. Upon restoration of secondary containment ventilation to a known operable alignment, secondary containment LCO 3.6.4.1 was cleared and operability restored. This event is being reported under 10 CFR 50.72(b)(3)(v)(c) and per the guidance of NUREG 1022, Rev. 3 section 3.2.7 as a loss of a Safety Function. There is no redundant Susquehanna Secondary Containment System. The licensee has placed administrative controls on the 101 bay doors to prevent loss of secondary containment during the investigation to determine the reason for the surveillance test failure. The licensee has notified the NRC Resident Inspector.
ENS 5703619 March 2024 18:19:00The following information was provided by the licensee via fax or email: While performing a planned high pressure coolant injection (HPCI) system surveillance, an isolation signal was received based upon an exhaust rupture disc high pressure signal. This resulted in an unplanned inoperability of the HPCI system. All systems responded as expected, and the event is under investigation. No other systems were affected by this condition. This event is reportable as an 8-hour non-emergency notification under 10CFR50.72(b)(3)(v) as HPCI is a single train safety system. There was no impact to plant personnel or the public as a result of this condition. The NRC resident has been notified of this condition.
ENS 5703317 March 2024 17:59:00The following information was provided by the licensee via phone and email: On March 17, 2024, at 1515 CDT, the Comanche Peak Unit 2 reactor was manually tripped due to an anticipated automatic trip due to lo-lo steam generator (SG) water levels. Prior to the trip, main feedwater pump '2B' tripped and an auto runback to 700 MW (60 percent power) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs. Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedures IPO-007B. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the '2B' main feed pump trip was due to loss of primary and redundant power to the servo control valve. The loss of power to the servo control valve is under investigation.
ENS 5703216 March 2024 18:36:00The following information was provided by the licensee via phone and email: At 1449 CDT, Waterford 3 Steam Electric Station was operating at 100 percent power when a manual reactor trip was initiated due to main feed isolation valve (FW-184B) and main steam isolation valve (MS-124B) going closed unexpectedly. Emergency feedwater (EFW) was automatically actuated. Preliminary evaluation indicates that all plant systems functioned normally after the reactor trip. The unit is currently stable in Mode 3. All control rods fully inserted as expected. This event is being reported as a 4-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the reactor protection system (RPS) when the reactor is critical and as an 8-hour nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as valid actuation of the EFW system. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Decay heat is being removed through the turbine bypass valves and the atmospheric dump valve on loop '2'. There is no primary to secondary system leakage. The cause of the isolations is still being investigated.
ENS 5702915 March 2024 12:00:00The following information was received from the Massachusetts Radiation Control Program (the Agency) via email: On 3/14/2024 at 1225 EDT, a MDS Nordion, Inc. GammaMed Plus iX high dose rate (HDR) remote afterloader device malfunctioned, leaving the source in an unshielded position. Since the quality assurance/quality control (QA/QC) checks are performed in a shielded room, no individuals received any excess dose due to this device failure. On the same day at 1630 EDT, individuals from a device manufacturer, Varian Medical Systems, Inc. (NRC License # 45-30957-01) came to the site and returned the device to a shielded position. One field agent received a dose of 0.025 mSv (2.5 mrem) during this operation. On 3/15/2024, Varian personnel performed work to repair the device. This repair work is ongoing at the time of this report. The Agency will follow up with UMass Healthcare Radiation Safety Officer (RSO) to determine event cause and corrective actions. The Agency considers this event open. The Agency will follow up with a special inspection of the licensee. Device Information: MDS Nordion, Inc. GammaMed Plus iX HDR remote afterloader (sealed source and device registry number: CA-1080-D-103-S) Source Information: MDS Nordion Inc. model GM 232, Ir-192, 4.4 Ci (sealed source and device registry number: CA-1080-S-104-S) NMED Number: TBD
ENS 5704121 March 2024 16:54:00The following information was provided by the licensee via email and phone: At 0548 CDT on March 13, 2024, during a planned (high pressure coolant injection) HPCI maintenance window, a condition was identified not associated with the planned maintenance which caused HPCI to be inoperable. Specifically, the HPCI auxiliary oil pump start stop pressure switch could not be adjusted into calibration. Further investigation found that the pressure switch was not mounted as designed. Since HPCI is a single train system, this is a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The condition was corrected prior to HPCI being declared operable on March 15, 2024. The reason for the delay in the event notification beyond 8 hours from the event time was due to not recognizing the need to report the condition while in a planned HPCI maintenance window. The NRC Senior Resident Inspector has been notified.
ENS 5702613 March 2024 02:29:00

The following information was provided by the licensee via phone and email: On March 12, 2024, at 2111 EDT, a valid containment ventilation isolation train 'A' and 'B' signal was received due to a spurious loss of power to 1EMF-38 (containment particulate radiation monitor) and 1EMF-39 (containment gas radiation monitor). The power to 1EMF-38 and 1EMF-39 was restored. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: There were no plant evolutions ongoing at the time of the event and the cause of the loss of power is under investigation. There was no impact to Unit 2.

  • * * RETRACTION ON 3/13/2024 AT 1436 EDT FROM JASON MOORE TO SAM COLVARD * * *

After further review of the event, it was determined the actuation of the associated containment ventilation isolation train 'A' and 'B' was not valid. This is due to the loss of power being associated with the control room modules for 1EMF-38 and 1EMF-39, and not a result of an actual sensed parameter or plant condition. Therefore, this event notification is being retracted. The NRC Resident Inspector has been notified. Notified R2DO (Miller)

ENS 5702713 March 2024 10:42:00The following information was received by the Minnesota Department of Health (MDH) via email: On March 12, 2024, at 1539 CDT, the licensee contacted MDH to report a gauge with a missing shutter. During their routine semiannual inventory and shutter check, the licensee discovered a Texas Nuclear model 5190 fixed gauge that was missing its shutter. The gauge contained a 100 mCi Cs-137 source (decayed to 35 mCi). The gauge was equipped with a removable shutter, and the licensee assumes that it had become loose and detached from the device due to normal operating vibration. The event was discovered at approximately 1420 on March 12, 2024. The licensee stated that they had a spare shutter and were able to install it on the gauge. The gauge was installed and operating when the missing shutter was discovered. Therefore, no abnormal radiation field or exposure occurred due to the missing shutter. At the time of the call, the licensee had not yet located the missing shutter. This gauge is used for density measurements on their tailings clarifier underflow pump. Minnesota State Event Report Number: MN240002
ENS 5702412 March 2024 12:16:00The following information was provided by the licensee via phone and email: On March 12, 2024, at 0816 CDT, Comanche Peak Unit 2 reactor automatically tripped on lo-lo level in the 2-03 steam generator (SG). Prior to the trip, main feedwater pump (MFP) 2A speed reduced and a manual runback to 700 MW (60 percent) was in progress. Both motor driven auxiliary feedwater pumps and the turbine driven auxiliary feedwater pump started due to lo-lo level in all SGs. Concurrent with the loss of speed on MFP 2A, a servo filter swap was in progress on MFP 2A. Unit 2 is being maintained in hot standby (Mode 3) in accordance with integrated plant operating procedure IPO-007A. The emergency response guideline network has been exited. Decay heat is being rejected to the main condenser via the steam dump valves. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the loss of the MFP is under investigation. Unit 1 was unaffected.
ENS 5702512 March 2024 12:29:00The following summary of information was provided by the licensee via phone and email: During an inventory which began the week of March 4, 2024, the licensee discovered one lost tritium exit sign (Isolite SLX-60, 4.4 Ci). The sign was at a location undergoing renovation. All other tritium exit signs that were on site have been accounted for. An investigation ensued to attempt to determine the disposition of the missing sign. This sign was declared lost on March 12, 2024. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5702211 March 2024 16:19:00The following information was received from the Wisconsin Department of Health Services (the State) via email: On March 11, 2024, a contracted service provider was on-site to dispose of 6 sources housed in a Kevex Model 6700 Analyst. It is a 2000 Series Spectrometer, Serial Number A011E, Bench Number 5026. The Analyst (device), has been in the possession of the scrap facility for at least a decade but was never utilized. The device was identified in November 2023, as a device which contained radioactive material. At that point the State was notified, and plans were initiated to dispose of the material. The State was unable to determine who previously possessed the device, or to whom it was initially distributed. The device should have contained 3 Cd-109 pellets of 7 mCi each, and 3 Am-241 pellets of 7 mCi, each. The source serial number indicated on the labeling is 4047, Model 0202. The assay date was December 1, 1992. When the service provider disassembled the device to reach the source housing, no sources were present within the device. The service provider performed confirmatory surveys to ensure that no sources were present. Apparently, the sources were removed prior to the scrap yard receiving the device. Without knowing the provenance of the device, it is unclear whether the sources were ever properly disposed of, therefore, it is being reported as missing material. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5702111 March 2024 15:46:00The following information was provided by the licensee via phone and email: On March 11, 2024, at 1337 EDT, with Unit 1 in Mode 1 at 35 percent power performing power ascension activities, the reactor was manually tripped due to the 'A' reactor feed pump (RFP) tripping on low suction pressure. Due to the power level at the time, the 'B' RFP had not been placed in service. Closure of containment isolation valves (CIVs) in multiple systems and actuation of high-pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) occurred as a result of reaching the actuation setpoint on reactor water level as designed. The trip was not complex, with all safety systems responding normally post-trip. Operations responded and stabilized the plant. The 'B' RFP was placed in service and is controlling reactor water level. Decay heat is being removed by discharging steam to the main condenser using turbine bypass valves. Unit 2 is not affected. Due to the emergency core cooling system (ECCS) discharging into the reactor, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). Also, the Reactor Protection System actuation while critical is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, it is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of CIVs, RCIC and HPCI. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the 'A' RFP is under investigation. The reactor electric plant remains in a normal lineup with both emergency diesel generators available. There were no temperature or pressure technical specification limits approached.
ENS 5702011 March 2024 12:13:00The following was received from the Texas Department of State Health Services (the Department) via email: On March 11, 2024, the Department was notified by the licensee's radiation safety officer (RSO) that an event at the facility resulted in molten metal being spewed out from the furnace. Some of the molten metal landed on the housing cover of a Berthold LB 300 gauge containing a 2.5 curie (original activity 3 years ago) source. The licensee was able to remove the cover and inspected the gauge. The licensee found that some of the molten metal had leaked on to the shutter operator for the gauge, preventing the shutter from closing. The RSO stated they were able to remove the gauge from the vessel and place in a storage area. The RSO stated the room has been locked and posted to prevent inadvertent entry. The RSO stated they had performed radiation surveys outside the storage room and readings obtained were less than 2 millirem per hour. The RSO stated no individual received any radiation exposure that would have exceeded any limit. The RSO stated they have contacted a service provider to repair the gauge. Additional information will be provided as it is received in accordance with SA-300. Texas Incident No.: 10094 Texas NMED No.: TX240009
ENS 5701910 March 2024 12:05:00The following information was provided by the licensee via email: On 3/9/2024 at 2126 CST, train C essential cooling water was declared inoperable due to a through-wall leak on the discharge vent line. This would also cascade and cause train C essential chilled water to be inoperable. On 3/10/2024 at 0353 CDT, train B essential chilled water was declared inoperable due to chilled water outlet temperature greater than 52 degrees F following startup of essential chiller 12B. Chilled water outlet temperature was adjusted to less than 52 degrees F at 0440 CDT, and train B essential chilled water was declared operable. This condition resulted in the inoperability of two of the three safety trains required for the accident mitigating functions including: high head safety injection, low head safety injection, containment spray, electrical auxiliary building HVAC, control room envelope HVAC, and essential chilled water. This is an 8 hour reportable condition per 10CFR50.72(b)(3)(v)(D) because it could affect the ability to mitigate the consequences of an accident. The licensee notified the NRC Resident Inspector.
ENS 570178 March 2024 13:59:00The following information was provided by the licensee via email and phone call: A non-licensed supervisor had a confirmed positive fitness for duty test. Unescorted access for the individual has been denied at all Dominion Energy sites. The NRC Senior Resident Inspector has been notified.
ENS 570147 March 2024 16:20:00The following information was provided by the licensee via phone and email: On March 7, 2024, at 1142 PST, an operator trainee operating the reactor under the direction of a licensed operator initiated a planned manual scram. Following the planned manual scram, the licensed operator did not switch the console switch to 'off' or remove the key from the console. The reactor did not meet the definition of 'reactor secured' and thus the staffing requirements of technical specification 6.1.3 were still required to be met. The licensed operator then left the control room, securing the door on their way out. At 1200 PST, a licensed senior reactor operator (SRO) entered the control room and found the key in the console with the switch in the 'operate' position. This SRO placed the switch in the 'off' position, secured the key, logged the action, and notified the Director. Throughout the duration of the event, all control rods were fully inserted. Project Manager (Wertz) will be contacted. Oregon Department of Energy and the Oregon Radiation Protection Services will be notified.
ENS 570168 March 2024 13:02:00

The following was received from the Illinois Emergency Management Agency (the Agency) via email: On March 7, 2024, the Agency was notified of equipment damage at Alton Steel in Alton, IL, that exposed two sealed radioactive sources. The licensee reported that molten steel flowed over Berthold Technologies source housings (source housing serial numbers 1197-10-21 and 601-05-12) and, despite trying to cool the steel, it damaged the source housings and exposed the sources. The Berthold Technologies sources are Co-60 and have an activity of 2.3 mCi each (source serial numbers 1200-10-21 and 600-05-12). The sources were removed from the housings by a licensed service provider and placed in secured storage. Leak tests are pending. The licensee determined there were no exposures to any personnel and that the incident does not pose a risk to any members of the public. Licensee surveys indicated no contamination, and radiation levels from these sources were comparable to those from an undamaged source. The Agency plans to conduct a reactionary inspection to verify the lack of contamination/exposure and accountability of licensed materials. This is a reportable event in accordance with 32 Ill. Adm. Code 340.1220(c)(2). Illinois Item No.: IL240008

  • * * UPDATE ON 3/13/24 AT 1625 EDT FROM GARY FORSEE TO ADAM KOZIOL * * *

(On 3/8/24), another email update was received in which Alton Steel's licensed contractor advised another portion of the source rod had been located and was actively being cut from the molten steel. A conference call was immediately scheduled and the following information noted: The incident had actually taken place on 2/22/24 with no notification to the Agency. It was stated that the licensee's authorized user removed the damaged sources using pliers and placed them in secured storage but did not follow their approved emergency procedures to cease work and rope off the area at 20 feet. The licensee contacted their consultant (R.M. Wester), and they were on-site the same day. R.M. Wester personnel surveyed the area and assumed there was no contamination because they were getting the expected radiation levels. At that time, the consultant recommended that the licensee contact the manufacturer (Berthold) to come out and further evaluate the sources and devices. The manufacturer was on-site on 3/7/24 and discovered that two source rods were damaged. The manufacturer's rep advised a call to the State was needed. He noted one source rod had been damaged to the point the internal Co-60/nickel wire was exposed. On the afternoon of 3/8/24, Alton Steel's licensed consultant surveyed the mold lid and found what they assumed to be the remaining portion of the source (exposure rate of 50 mR/hour). On 3/8/24, Alton Steel personnel used a torch to cut that portion of the source from the lid of the mold. This piece was also placed in secured storage. The lid was then surveyed by the consultant which he stated evidenced no further radioactive material. The two damaged sources, as well as the source rod fragment, are pending disposal. The Agency has requested that the lid and mold be held for surveys when Agency staff are on-site. Agency staff plan to be on-site 3/13/24 to further investigate. Leak tests from the consultant did not evidence removeable contamination in excess of 0.005 uCi. At this time, there is no indication of risk to workers or the public as all sources are in secured storage. The investigation is ongoing and updates will be provided as available. On Monday, 3/11/24, Agency staff conducted interviews with the Berthold service representative which conducted the service call. Information from that call indicated the licensee had cut through a source with a torch. At this point, Agency staff responded that morning to take surveys and interview Alton Steel staff. Survey readings were taken with a microR meter, which lacked the necessary sensitivity and were inconclusive due to (naturally occurring radioactive material) NORM and refractory material. Investigation findings indicate the licensee failed to follow emergency procedures, failed to follow operating procedures, failed to adhere to license conditions, received inadequate and incorrect training, improperly handled and manipulated sealed sources, failed to perform surveys, and failed to make timely notification to the Agency. The licensee's consultant also failed to notify the Agency, lacked sufficient knowledge of the sealed source and performed inadequate surveys. Additionally, it was discovered the licensee had used a 4 inch die grinder on one source, cut through another with an oxygen lance, had a practice of handling unshielded source assemblies and an inadequate radiation safety program. Agency staff arrived at the licensee's site again on 3/13/24 to perform additional surveys. Upon arrival, the licensee stated they had found yet another piece of the Co-60 rod source under the spray booth that washes down the cast billets. This was reportedly the area below where the source was first cut with a torch. The Agency confirmed the licensee was aware of the source when using the torch and did not perform surveys or alter operations. The second source which was found to be damaged had also been inadvertently withdrawn from its shielded housing when the molten steel overflowed atop the mold cap. However, the second source immediately fell into two pieces, apparently suffering damage within the housing. That source was reportedly burnt/melt and would not fit into the shield. A licensee gauge user then used a 4 inch angle grinder to smooth out the source so it would fit back into the shield. Agency staff investigated all areas accessible (some areas were inaccessible due to molten steel). A portable germanium spectrometer was employed to discern if elevated count rates were from NORM or Co-60 contamination. Preliminary findings indicate at least two areas adjacent to the vise (where grinding had occurred) had Co-60 contamination. Samples were collected for lab analysis and additional area surveys performed. The (Illinois Emergency Management Agency - Office of Homeland Security) IEMA-OHS lab reported on the afternoon of 3/13/24 that samples did evidence Co-60 contamination. The Agency covered the contaminated area and required it to be posted. Additional surveys will be taken once accessible, to include the wash-down water sedimentation areas. A full survey and remediation plan will be required by the end of the month. Decontamination efforts will be undertaken by a qualified contractor and the Agency will perform verification surveys to support release. Updates will be provided as they become available. Notified R3DO (Hills), IR MOC (Crouch), NMSS (Williams), NMSS Events (email) Notified DHS SWO, FEMA Ops Center, USDA Ops Center, HHS Ops Center, DOE Ops Center, CISA Central Watch Officer, EPA EOC, FDA EOC (email), Nuclear SSA (email), FEMA NWC (email), CWMD Watch Desk (email)

  • * * UPDATE ON 3/18/2024 AT 1440 EDT FROM GARY FORSEE TO SAM COLVARD * * *

On 3/15/2024, the Agency dispatched seven inspectors to perform comprehensive surveys of the facility, characterize exposures, and determine if additional fragments of the source remained unaccounted for. Inspection findings indicate that there is Co-60 contamination within a single room (mold repair room) at Alton Steel. The licensee has secured the room and implemented contamination control procedures. Updated procedures and training were implemented on Friday, March 15, 2024. Extensive Agency surveys of the facility and personnel performed on 3/15/2024 indicate that the contamination is not being carried offsite; nor was there any indication of public exposures. There is no contamination of water. Contamination of the product (steel) has not been identified; nor is it likely to be a concern resulting from this incident. Due to improper handling of sources, it is likely a gauge user received an extremity dose in excess of regulatory limits. Time-motion study will be performed to refine dose estimates and substantiate. ONS-RAM is investigating additional, chronic internal exposures to Co-60 which have likely occurred over many years. ONS-RAM will return to the site on 3/20/2024 to evaluate the efficacy of contamination control measures, determine the timeline for remediation activities and perform additional sampling/surveys to better quantify exposures and determine the appropriateness of bioassays. This report will be updated as additional information becomes available. Notified R3DO (Hills), NMSS (Williams), NMSS Events (email), NMSS Regional Coordinator (Rivera-Capella) (email) THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf

ENS 570137 March 2024 02:30:00The following information was provided by the licensee via email: On March 6, 2024, at 1635 PST, with Columbia Generating Station operating at 100 percent power in Mode 1, there was a malfunction in the halogenation/dehalogenation system. This system is used for continuous control of the biological growth in the circulating water and plant service water systems as well as to prevent discharge of halogens to the Columbia River during continuous blowdown. The result of this malfunction was exceeding the established limits of 0.1 milligrams/liter (mg/L) for total residual halogen (TRH) in the station's national pollutant discharge elimination system (NPDES) permit. At the time of discovery, the local indication for TRH was 3.20 mg/L. This was confirmed via a local grab sample. This maximum daily effluent limit is the highest allowable daily discharge, measured during a calendar day. The station NPDES permit requires notification to the Energy Facility Site Evaluation Council (EFSEC). The automatic isolation function of the system failed to isolate the continuous blowdown line as did the emergency trip push button. The system was manually secured, and the continuous blowdown line to the Columbia River was isolated. The cause of the issue is under investigation. Notification was made to EFSEC on March 6, 2024, at 2303 PST. This event is being reported as a four hour report made in accordance with 10 CFR 50.72(b)(2)(xi) due to a "News Release or Notification of Other Government Agency" related to protection of the environment. The NRC Senior Resident Inspector has been notified.
ENS 570126 March 2024 17:05:00The following is a summary of information provided by the licensee via telephone: On March 6, 2024, around 0600 CST, a technician found loose molybdenum (Mo-99) / technetium (Tc-99m) contamination inside a restricted area. Prior to the discovery, a production hot cell inside the restricted area had been deep cleaned as part of the regular maintenance program. A thorough investigation of the area was conducted which revealed additional loose contamination on the lab floor. Surveys of surrounding areas did not reveal any spread of contamination outside of the restricted lab area. Due to (1) the existing access controls, (2) personal protective equipment requirements for lab access, and (3) the absence of contamination identified by body scans of personnel exiting the lab; the licensee does not suspect any spread of contamination outside of the restricted area or personnel intake. Biological samples will be collected to confirm that no intake occurred. The highest contamination level identified was 260 mrem/hr on contact and 2.3 mrem/hr at 1 foot. The contamination has been remediated to below licensee action levels. Overall, 2.4 mCi of Mo-99 was identified outside of the production hot cell. The 10 CFR 20 Appendix B limit for Mo-99 is 1 mCi. The licensee is investigating the root cause of this event.
ENS 570157 March 2024 18:22:00The following is a synopsis of information received via email from the Alabama Department of Public Health, Office of Radiation Control: On the evening of March 6, 2024, the licensee experienced a source disconnect at a job site in Russellville, Alabama. The source connector appeared to have not been connected properly, and the source apparently disconnected from the drive cable while outside the exposure device (camera). The source was retrieved and secured in a 650L model source changer about 45 minutes later when a source retrieval team arrived on site. The two source retrieval personnel received 45 milliroentgens and 15 milliroentgens of exposure respectively. The radiography crew dosimetry had not yet been retrieved for emergency processing at the time of the report. The camera and source information is as follows: Sentinel 880D, D1120, about 78.9 curies of iridium-192 in a model A424-9 source. Alabama Incident Number: TBD
ENS 570075 March 2024 14:17:00The following information was provided by the licensee via telephone and email: At 1000 MST on 3/5/24, a 10,000 Ci Co-60 source (Model 7810) became stuck in the unshielded position during operator training. The irradiator is a J.L. Shepherd, Model SDF-34-M1, panoramic dry-source storage type. Upon determining that the source was stuck, the operator attempted to manipulate the source back into the shielded position using the emergency cable, but it came loose. Site staff have secured the irradiator facility. No personnel exposure occurred, and there are no elevated dose rates outside of the irradiator enclosure. The site has requested manufacturer support to resolve the issue. The NRC Project Manager (O'Keefe) has been notified.
ENS 570105 March 2024 19:14:00

The following information was provided by the licensee via email:

      • 8 Hour Notification was due at 1520 CST *** Follow up discussion of conditions after recovery determined that a report is required. This report restores reporting compliance.

On March 5, 2024, at 0720 CST, the X-02 118V uninterruptible power supply air conditioning (UPS A/C) unit tripped with the associated emergency fan coil units (EFCUs) shut down for planned maintenance in the area. The X-01 UPS A/C unit was declared inoperable upon discovery due to a scheduled outage of support systems (Unit 1 station service water) via the safety function determination process. This placed the site in technical specification 3.7.20 condition A, B, and C to restore the UPS A/C system within one hour. The EFCUs were restarted at 0729 which satisfied condition B and C, and X-01 UPS A/C unit was aligned to Unit 2 cooling water at 0801, exiting condition A. The condition that could have prevented the fulfillment of the safety function lasted for approximately nine minutes. Area temperatures had no notable change based on field observations during the condition. The UPS HVAC system provides temperature control for the safety related UPS and distribution rooms during all normal and accident conditions. The UPS HVAC system consists of (a) a dedicated UPS room EFCU in each safety-related UPS and distribution room, and (b) two electrically independent and redundant A/C trains either of which can support all four safety related UPS and distribution rooms; each train consists of an air conditioning unit, ductwork, dampers, and instrumentation. The NRC Resident Inspector has been notified.

ENS 570095 March 2024 17:30:00The following information was provided by the California Department of Public Health, Radiologic Health Branch via email: Isolite Corporation notified the California State Warning Center of the loss of a container containing eight tritium exit signs with a total activity of 60.8 curies of tritium (H-3). Fifty-one containers of tritium signs were to be delivered by (common carrier). Only 50 containers of tritium exit signs were delivered, leaving one container containing the eight exit signs missing. (The common carrier) is currently conducting a search to determine the status of the missing container of exit signs. Since this exceeds the amount of H-3 by greater than 1000 times the value in Appendix C of Part 20, it constitutes a less than or equal to 24-hour reportable event. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 570065 March 2024 04:14:00The following information was provided by the licensee via email: At 0132 EST, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main feedwater isolation signal which resulted in steam generator lo-level reactor trip. The reactor trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the main feedwater isolation is being investigated.
ENS 570085 March 2024 17:28:00The following information was provided by the Texas Department of State Health Services (the Department) via email: On March 5, 2024, the Department was notified by the licensee that during routine shutter testing, the shutter on a Vega SH-F2C failed to close. Open is the normal operating position for the gauge shutter. The gauge contains a 500 millicurie (original activity) cesium-137 source. The gauge is in an area that is accessed only to test the shutter as it is located 230 feet off the ground. The gauge does not present an exposure risk to any individual. The licensee has contacted a service company to repair the gauge. Additional information will be provided as it is received in accordance with SA-300. Texas Incident Number: 10093 NMED Number: TX240008
ENS 570116 March 2024 09:14:00The following information was received from the Georgia Radioactive Materials Program via email: The licensee reported on 3/5/24 about an incident at Piedmont Hospital with Y-90. They underdosed a patient when the catheter was put in the artery. There were vein convulsions which caused only about 30 percent of it to be administered. The licensee stated it did not cause stasis. A follow up with a report will be submitted to the Georgia Environmental Protection Division within 15 days. Georgia Incident Number: 79 A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.
ENS 570054 March 2024 10:25:00The following is a summary of the information provided by the Louisiana Department of Environmental Quality (LDEQ) via email: At 2152 CST on March 3, 2024, a lost source was found along Corporate Blvd., Baton Rouge, LA. The device is a Model IC-51 Calibrator with 1000 mCi of Cs-137 as of August 25, 1980. The label on the device indicates the manufacturer was Gulf Nuclear, Inc., of Webster, Texas. LDEQ took possession of the device on March 4, 2024, and has it at the time of this report. Event Report ID No.: LA20240003 THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 570043 March 2024 22:15:00The following information was provided by the licensee via email: On 3/3/24 at 1942 EST, while performing a plant shutdown in preparation for a refuel outage, Nine Mile Point Unit 2 experienced a reactor scram due to a main turbine trip on low condenser vacuum. The plant was at approximately 55 percent power at the time of the reactor scram. Additionally, following the scram a low RPV (reactor pressure vessel) level scram and containment isolation signal on level 3 was received, as expected. The containment isolation signal impacted RHR (residual heat removal) shutdown cooling, RHR letdown to radwaste, and RHR sampling. All impacted valves were closed at the time the isolation occurred. All control rods were fully inserted. Plant response was as expected. Post scram, the main turbine bypass valves are being used to control decay heat, and normal post scram level control is via the feed / condensate system. This is being report under 10 CFR 50.72(b)(2)(iv)(B), 'RPS Actuation', and 10 CFR 50.72(b)(3)(iv)(A), 'Specified System Actuation'. Unit 1 is not affected. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the low condenser vacuum was a momentary loss of sealing steam. The condenser remained viable for decay heat removal. All safety equipment is available. The grid is stable with the plant in its normal shutdown electrical configuration.
ENS 570033 March 2024 15:51:00The following information was provided by the licensee via email: At 1142 CST on 3/3/2024, with Unit 2 in Mode 1 at 29 percent power, the reactor automatically tripped due to a turbine trip caused by a loss of suction to the 22 main feedwater pump. All systems responded normally post trip. Decay heat is being removed via the auxiliary feedwater water system. Secondary steam control mechanism is the steam generator PORVs (power operated relief valves). Unit 1 remains at 100 percent power and is unaffected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The resident NRC inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The trip occurred while the licensee was returning to power operations after a refueling outage. During the trip, all rods inserted into the core. The plant is in a normal shutdown electrical lineup with offsite power available. The plant will be maintained at normal operating temperature and pressure. There is no known primary to secondary leakage. The cause of the loss of 22 main feedwater pump suction is under investigation.
ENS 570021 March 2024 17:27:00The following information was provided by the licensee via email: At 1330 CST, on March 1, 2024, an equipment vendor was coordinating with Wright County performing maintenance on an emergency siren when the county operator mistakenly sent an alarm signal instead of cancel signal, activating all Wright County emergency sirens for approximately 17 seconds. At 1345 CST, the Monticello Nuclear Generating Plant (MNGP) emergency planning coordinator received a notification from the vendor and notified the duty shift manager (of the inadvertent activation). Wright County officials are planning to make a public notification via social media to local residents. No press release by the licensee is planned at this time. This event is reportable per 10 CFR 50.72(b)(2)(xi), 'News Release or Notification of Other Government Agencies.' This is a 4-hour Reporting requirement. The NRC Resident has been notified.
ENS 570001 March 2024 12:48:00The following summary of information was provided by the Florida Bureau of Radiation Control (the Bureau) via email: On March 1, 2024, at 1121 EST, the Bureau received a call from Universal Engineering Scientists to report that a Troxler gauge (Model: 3430P, Serial: 86000, 8 mCi Cs-137, 40 mCi Am-241:Be) was run over on a work site. The Cs-137 source rod was extended 12 inches into the ground. The licensee radiation safety officer (RSO) responded and determined that the source rod could not to be retracted. The gauge was placed in a container and shielded for transport to a storage facility in Port St. Lucie where it will be held for evaluation. The Bureau inspector has been notified and will respond. Florida Incident No.: FL24-015
ENS 5699728 February 2024 17:46:00The following information was provided by the licensee via phone and email: At 1350 EST on 2/28/2024, with Calvert Cliffs Unit 1 in Mode 5 at 0 percent power and Unit 2 in Mode 1 at 65 percent power, an actuation of the '1A' and '2A' emergency diesel generators' auto-start occurred due to an undervoltage condition on the number 11 and number 21 4kV buses which are fed from the number 11 13kV bus. The '1A' and '2A' emergency diesel generators automatically started as designed when the 4kV buses' undervoltage signals were received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the '1A' and '2A' emergency diesel generators. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The undervoltage condition was caused by the feeder breaker to the number 11 13 kV bus opening during electrical maintenance.
ENS 5699528 February 2024 13:25:00The following information was provided by the licensee via fax and email: At approximately 0839 (CST) with Unit 1 in Mode 1 at 100 percent power, the reactor automatically scrammed due to the depressurization of the SCRAM air header caused by an invalid signal that (occurred) during system testing. The SCRAM was uncomplicated with all systems responding as expected. The cause and details of the event are under investigation. Containment isolation valves actuated and closed on a valid Group 2 signal. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B), and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group 2 isolation signal. Operations responded using the emergency operating procedure and stabilized the plant in Mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. State as well as Wright and Sherburne Counties will be notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The Anticipated Transient Without Scram (ATWS) circuit was being tested when an invalid signal was sent to depressurize the SCRAM air header.
ENS 5699628 February 2024 16:33:00The following information was provided by the North Dakota Department of Health (the Department) via email: On February 28, 2024, EMCOR Facilities Services, Inc. reported that nine (9) single-face tritium exit signs belonging to The Church of Jesus Christ of Latter-Day Saints were removed and improperly disposed of by an electrical subcontractor (Feininger Electric Works). The make, model, and serial numbers of these tritium exit signs are unknown. North American Signs was contracted by EMCOR Facilities Services, Inc. on November 02, 2023 to complete the scope of work on behalf of the Church. In turn, North American Signs subcontracted the work to be completed by Feininger Electric Works. North American Signs informed EMCOR Facilities Services, Inc. on February 6, 2024, that a Feininger Electric Works technician mistakenly discarded 9 tritium exit signs before they could be catalogued, packed, and shipped out for proper disposal. The signs were presumably collected from a general waste receptacle and could not be recovered. The Department is attempting to gather more specific information from the entities involved. Typically, each of these signs initially contain tritium in amounts greater than one (1) curie. As such, we are reporting this event under 10 CFR 20.2201(a)(1)(i). NMED Event Number: ND240001 THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf
ENS 5702311 March 2024 15:28:00

The following summary of information was provided by the Washington State Department of Health Office Radiation Protection (the Department) via email: On March 1, 2024, the Department was notified of a medical misadministration that occurred on February 28, 2024. The misadministration was that of Ga-68 Dotatate (5.24 millicuries) being administered instead of F-18 FDG (Fludeoxyglucose). The licensee proceeded with the scan having an incomplete scan description on an outside physician's order. The signed order received only asked for "PET-CT Scan (Base of Skull to Thigh)." An unsigned order/history form, clearly designating a Ga-68 Dotatate scan, was filled out by the outside clinic's medical staff and included with the physician's order. The licensee proceeded with scan as directed using the elaboration of the unsigned order/history form as designation of the specific scan ordered. The patient was notified of the incident and will receive the appropriate scan the following week. Investigation in to how this situation can be avoided in the future has been conducted by the licensee. WA Event Number: WA-24-0007 A Medical Event may indicate potential problems in a medical facility's use of radioactive materials. It does not necessarily result in harm to the patient.

  • * * UPDATE ON 3/14/24 AT 1538 EDT FROM BORIS TSENOV TO ADAM KOZIOL * * *

The following was provided by the Washington State Department of Health Office Radiation Protection (the Department) via email: The licensee provided a written report to the Department identifying root causes and corrective actions. The report also calculated an effective dose estimate of 498 mrem and the highest expected effective organ dose to the spleen of 5.47 rem. Notified R4DO (Werner) and NMSS Events (email)

ENS 5699929 February 2024 13:22:00The following information was provided by the Illinois Emergency Management Agency (the Agency) via phone and email: The radiation safety officer (RSO) for INspec Ethylene Oxide and Specialities (INEOS), IL-01337-01, contacted the Agency on 2/28/24, to advise that a fixed gauge was found to have a shutter stuck in the `open' position. The impacted gauge is a Ronan Engineering model X90-SA1-F37, serial number M7388 containing 40 mCi of Cs-137. The device shutter is normally in the `open' position and was only found to be `stuck' during the routine six-month shutter checks. It had likely been in this condition for at least six months. The product vessel that it faces is full of commodity and will remain full for the foreseeable future. Aside from being full of commodity, the vessel is also equipped with locking mechanisms preventing any personnel access. Agency staff will be on site in the coming weeks. NMED Item Number: IL240006
ENS 5699124 February 2024 18:08:00The following information was provided by the licensee via email: At 1546 EST, with unit 2 at 100 percent power, the reactor was manually tripped due to the '22' steam generator feed pump tripping. The trip was uncomplicated with all systems responding normally post-trip. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Operations responded using emergency operation procedure EOP-0, Post Trip Immediate Actions and EOP-1, Uncomplicated Reactor Trip and stabilized the plant in mode 3. Decay heat is removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 is not affected. ESFAS (engineered safety features actuation systems) actuation (auxiliary feedwater manual actuation) is reportable under 10 CFR 50.72(b)(3)(iv)(A) 8-hour report. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5699024 February 2024 09:27:00The following information was provided by the licensee via phone and email: At 0219 CST on February 24, 2024, Browns Ferry Unit 3 was shut down in a refueling outage, while closing 4 kV shutdown board breaker 3EB-9, the 4 kV shutdown board normal feeder breaker tripped open resulting in a valid 4 kV bus under-voltage condition. Due to the under-voltage condition, the 3B emergency diesel generator (EDG) auto started and tied to the board. The cause of the breaker tripping open is unknown and an investigation is in progress. All systems responded as expected for the loss of voltage. This event requires an 8-hour report per 10 CFR 50.72(b)(3)(iv)(A). There was no impact to the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: No other safety related equipment was affected. The 3B EDG continues to supply the shutdown board pending further investigation.
ENS 5698922 February 2024 20:02:00The following information was provided by the licensee via email: At 1103 CST on February 22, 2024, a potential through-wall steam leak was identified on the high pressure coolant injection (HPCI) steam supply 1-inch drain line. As a result, HPCI was declared inoperable. Since HPCI is a single-train system, this is a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). Reactor core isolation cooling (RCIC) and low pressure emergency core cooling systems (ECCS) remain operable. Additional investigation is in progress. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5698321 February 2024 10:33:00The following is a synopsis of information that was provided by the licensee via email and phone call: A non-licensed supervisor had a confirmed positive during a fitness for duty test. The supervisor's access to the plant has been terminated.
ENS 5698621 February 2024 21:16:00The following information was provided by the Washington State Department of Health via email: Port Townsend Paper Corporation sent an old lead-lined tank to a scrap yard. Unknown radioactivity was then detected in the tank at the scrap yard. The unknown radioactive material was wrapped in lead from the tank by workers at the scrap yard and sent back to Port Townsend Paper Corporation. The Radiation Safety Officer at Port Townsend Paper Corporation measured 0.33 mR/hour on the outside of the lead. The lead and the unknown radioactive material were temporarily stored in an area of the paper mill that is usually unoccupied. An inspector from the Washington State Department of Health plans to go to the Port Townsend Paper Corporation in a few days to investigate. It is suspected that the unknown radioactivity is likely to be naturally occurring radioactive material which can build up over time in piping, tanks, etc. at paper mill facilities. All the licensee's sealed sources are accounted for, so the unknown radioactivity is unlikely to be from one of them, but the inspector will check for that possibility. WA Event Number: WA-24-005
ENS 5698220 February 2024 16:10:00The following report was received via phone call and email from the Texas Department of State Health Services (the Department): On February 20, 2024, the Department was notified by the licensee's radiation safety officer (RSO) that a Troxler 3440 moisture/density gauge was damaged at a temporary job site. The gauge contains a 40 millicurie americium - 241 source and an 8 millicurie cesium -137 source. The gauge operator was setting the gauge up for use when they noticed that a large number of construction equipment was moving into the area. The operator decided to move their truck out of the way and while they were doing so the gauge was struck by a piece of equipment. The RSO stated the gauge case was damaged, but the sources were not damaged. The cesium source was still in the fully shielded position when the event occurred. The RSO stated the gauge was transported back to their facility and a leak test was conducted on the sources. The RSO stated they have contacted a service company and as soon as they get the leak test results back, they will dispose of the gauge. No individual received any significant exposure due to this event. Additional information will be provided as it is received in accordance with SA-300. Texas Incident Number: 10089 Texas NMED Number: TX240007
ENS 5698019 February 2024 18:44:00

The following information was provided by the licensee via email: At 1045 EST, on 2/19/2024, during a maintenance activity, a loss of all reactor building ventilation occurred on Unit 2. With no flow past the ventilation radiation monitors, the radiation monitors were inoperable to support their ability to perform primary and secondary containment isolation functions or start the standby gas treatment system. Reactor building ventilation was restored within 15 minutes. Due to this inoperability, the radiation monitor system was in a condition that could have prevented fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector will be notified.

  • * * RETRACTION ON 3/15/24 AT 1315 EDT FROM BILL LINNELL TO ADAM KOZIOL * * *

Upon further investigation, it was verified that the reactor building and the refueling floor radiation monitors are not needed to control the release of radiation for events described in chapter 14 of the updated Final Safety Analysis Report. For the analyzed loss of coolant accident (LOCA), the primary and secondary signals for this purpose were available and unaffected by this event. The radiation monitors provide a tertiary redundant method that is not credited within the station analysis. For all other analyzed accidents, the signal provided by the radiation monitors is not needed, as the secondary containment isolation function and start of the standby gas treatment system are not credited. Additionally, the fuel handling accident was not credible during the time of the event because no activities were in progress on the refueling floor. Therefore, the threshold for reporting the issue as an event or condition that could have prevented the fulfillment of a safety function was not met. The NRC Resident Inspector has been notified. Notified R1DO (Jackson)

ENS 5697819 February 2024 06:32:00The following information was provided by the licensee via phone and email: On February 19, 2024, at 0236 EST, with VC Summer Unit 1 in Mode 1 at 100 percent power, an actuation of the `B' emergency diesel generator (EDG) occurred. The reason for the `B' EDG auto-start was the trip of 1 `DB' normal incoming breaker. The `B' EDG automatically started as designed when the undervoltage signal was received. The `B' emergency feedwater pump started due to the undervoltage signal and ran for approximately 1 minute and was secured by operations per procedure. Other plant equipment and systems also responded as expected. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the `B' EDG and a valid actuation of the `B' emergency feedwater pump. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The `A' Emergency Diesel Generator was tagged out for maintenance earlier in the shift, but maintenance has not started. The plan is to restore the `A' emergency diesel generator to an operable status and investigate the cause of the 1 `DB' normal incoming breaker trip. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This event resulted in the plant entering a 12 hour limiting condition for operation (LCO) in accordance with technical specification (TS) 3.8.1.1.C. due to having one operable EDG and a loss of offsite power.
ENS 5697719 February 2024 03:34:00The following information was provided by the licensee via phone and email: At approximately 2325 EST on February 18, 2024, with Unit 1 in Mode 5 at 0 percent power and Unit 2 in Mode 1 at 100 percent power, emergency diesel generator 2 automatically started due to the unexpected loss of AC power to emergency bus E2 during a planned transfer of E2 DC control power from normal to alternate for the 1B-1 battery. In addition, the unexpected loss of AC power to E2 resulted in Unit 1 primary containment isolation system (PCIS) partial Group 2 (i.e., drywell equipment and floor drain, residual heat removal (RHR), discharge to radioactive waste, and RHR process sample), Group 6 (i.e., containment atmosphere control/dilution, containment atmosphere monitoring, and post accident sampling systems), and partial Group 10 (i.e., air isolation to the drywell) isolations. Emergency diesel generator 2 automatically started and re-energized the E2 bus as designed when the loss of E2 signal was received. The PCIS actuations were as expected for the outage plant line up on Unit 1 at the time. The cause of the loss of electrical power to emergency bus E2 is under investigation at this time. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of emergency diesel generator 2 and PCIS. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: This event will be entered into the plant's corrective action program.
ENS 5697518 February 2024 16:02:00The following is a synopsis of information was provided by the licensee via email and phone call: A non-licensed supervisor had a confirmed positive during a random fitness for duty test. The supervisor's access to the plant has been terminated.
ENS 5697618 February 2024 17:32:00The following information was provided by the licensee via email: On February 17, 2024, a Honeywell employee experienced a non-work-related medical condition that required off site medical support. The incident occurred at approximately 2140 CST in the Feed Materials Building at the Metropolis facility. Due to the nature of the employee's condition, the individual was transported to (Massac Memorial Hospital in Metropolis, IL). Honeywell health physics staff accompanied the injured employee, provided guidance to emergency room personnel, and controlled the facilities prior to decontamination. A whole-body survey of the employee and plant clothing was performed; the maximum amount of contamination present on the employee's coveralls was 65,500 disintegrations per minute (dpm) per 100 centimeters squared. All contaminated clothing was removed from the employee and an additional whole-body survey was performed; no contamination above background levels was detected. An emergency medical technician's (EMT) pants leg, boot, and the gurney wheels were found to be contaminated. The maximum amount of contamination present was 13,000 dpm per 100 centimeters squared. The EMT's pants leg, boot, and gurney were decontaminated to background levels. Following medical evaluation, hospital facilities were monitored and found to be free of contamination prior to release for unrestricted use. All contaminated materials from the hospital and injured employee were returned to the Metropolis facility. The NRC Fuel Facility Inspector has been notified." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The contamination was reported as: uranium ore concentrate. The employee had fallen unconscious. They have been released from the hospital after recovering.