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ML20042D31429 December 1989LER 89-032-00:on 891210,as-left Type B & C Local Leak Rate Test Data Exceeded Tech Spec Limit of 488.452 Std Cubic Ft/H.Caused by Degradation of Telephone & Electrical Conduit Penetration Seal.Conduit Cut & capped.W/891229 Ltr
ML20024E92730 August 1983LER 83-062/01T-0:on 830819,HPCI Motor Gear Unit Observed Moving Between High & Low Speed Stops W/O Operation Action. Caused by Failure of HPCI Controller Amplifier.Amplifier replaced.W/830830 Ltr
ML20024D83428 July 1983LER 83-055/01T-0:on 830719,one 1/8 by 1/16-inch Hole Found on Bellows Seal on Torus to Drywell Vacuum Breaker Line Containing Breakers 2-1601-32A & B.Cavity Filled to Original Thickness & Surface buffed.W/830728 LtrFuel cladding
Liquid penetrant
ML20024D69927 July 1983Updated LER 83-057/03X-1:on 821224,while Performing Routine Insp,Pinhole Leak Found in 2D3 to 2C3 Feedwater Heater Normal Drain Line.Caused by Excessive Movement of 2D3 Drain Line.Mod Initiated to Add restraints.W/830727 Ltr
ML20024B64030 June 1983LER 83-044/03L-0:on 830603,review of Area X Temp Showed Increase of Approx 25 F Due to Crack in Test Tap on MSIV 2C. Caused by Fatigue Due to Improper Support of 3/4-inch Test Connection.Steam Line Cut & capped.W/830630 Ltr
ML20024B76429 June 1983LER 83-045/03L-0:on 830608,during Normal Operation,Circuit Breaker for Core Spray Injection Valve MO2-1402-25B Tripped. Caused by Incorrect Setting on Circuit Breaker,Due to Personnel Error.Breaker Set correctly.W/830629 Ltr
ML20024B67224 June 1983Updated LER 82-053/03X-1:on 821215,while Performing LPCI Valve Operability surveillance,2A LPCI HX Bypass Valve Position Identification Lost.Breaker Trip Setting Found to Be One Setting Too Low.Cause unknown.W/830624 Ltr
ML20024A5281 June 1983LER 83-019/03L-0:on 830521,MSIV 203-1B Found W/Closure Time of 2.7 Exceeding Tech Spec Limit of 3 to 5 S.Caused by Misadjustment to Timing Mechanism on MSIV-203-1B.MSIV Adjusted within Tech Spec limits.W/830608 Ltr
ML20023D83925 May 1983LER 83-035/03L-0:on 830427,low Pressure Coolant Injection HX Discharge Valve MO2-1501-3B Failed to Open.Cause Undetermined.Control Circuitry Inspected by Electrical & Instrument Maint & Found satisfactory.W/830525 Ltr
ML20023D99723 May 1983Updated LER 83-013/03X-1:on 830211,power Lead from Welding Machine Became Disconnected & Grounded to Torus Base Metal Causing Arc Strike Which Fused Copper/Brass Into Metal. Cause Considered accident.W/830523 Ltr
ML20023C2965 May 1983LER 83-027/03L-0:on 830408,during Valve Insp,Grease Discovered on Seats & Discs.Caused by Maint Procedures Not Prohibiting Personnel Placing Grease on Seat & Disc.Grease Removed,Valves Repaired & Procedures Will Be Revised
ML20023C2804 May 1983LER 83-025/03L-0:on 830409,reactor Bldg Fuel Pool Channel a High Radiation Alarm Activated,Causing Reactor Bldg Vent Sys to Trip.Caused by Burned Out Relay Coil.Relay Coil Replaced
ML20023B82726 April 1983LER 83-024/03L-0:on 830403,while Performing Core Spray Operability Test,Valve Mo 1402-4A Failed to Open.Caused by Burned Out Motor.Motor Replaced
ML20028F36019 January 1983LER 82-058/03L-0:on 821226,small Leak Found on Reactor Water Cleanup Line 2-1201B 8-inch-A Between 2-1201-135B & 98B Valves.Cause Unknown.Pipe Will Be Examined When Section Replaced During 1983 Refueling Outage
ML20028F47919 January 1983LER 83-003/03L-0:on 830108,during Surveillances Dis 1400-5 & DOS 6600-1,diesel Generator Low Water Pressure Alarm Received.Caused by Bad Low Cooling Water Pressure Switch. Switch Replaced W/Class 9012 Type GAW-5
ML20028E79118 January 1983LER 82-057/03L-0:on 821224,pin Hole Leak Found in 2D3 to 2C3 Feedwater Heater Normal Drain Line.Caused by Excessive Movement of 2D3 Feedwater Heater Normal Drain Line.Mod to Add Sys Restraints Initiated
ML20028E98514 January 1983LER 83-002/01T-0:on 830105,during Mode 1,while Performing Leak Checks,Tap Isolation Valve 3-1299-13 & Pipe Cap Found Blowing Steam.Cause Unknown.Pipe Threads Chased & New Cap Installed.Valve Will Be Replaced During Next Refueling
ML20028E24212 January 1983LER 82-056/03L-0:on 821218,rod Block Setpoint of 12.2% Found on APRM 6.Caused by Setpoint Drift.Aprm 6 Bypassed While Rod Block Setpoint Readjusted
ML20028E26810 January 1983LER 82-049/03L-0:on 821217,D-3 Diesel Generator Failed to Start on Two Successive Attempts Following Semiannual Insp. Caused by Worn Out Cylinder & Accumulation of Dust Particles Inside Air Starter.Starter Replaced
ML20028E96410 January 1983Updated LER 82-043/03X-1:on 821028,during Mode 1,w/east Scram Discharge Vol Level Switches Under Test,Magnetrol Level Switches 82D & 82F Would Not Trip on Command.Caused by Misaligned Upper Switch Contact MechanismsScram Discharge Volume
ML20028C22720 December 1982LER 82-049/03L-0:on 821128,during Quarterly Valve Timing Surveillance DOS 1600-1,torus Inert & Purge Valve 2-1601-56 Would Not auto-close.Caused by Versa Valve Leaking from Weep Hole Due to Hardening of O-ring Seal.Valve Replaced
ML20028E69517 December 1982Updated LER 82-046/03X-1:on 821112,during Routine Insp,Water Discovered Spraying from 1-inch Drain Line Off Bottom of 3A Feedwater Isolation Valve MO3-3206A.Caused by Cracked Weld. Drain/Line Removed & Refitted
ML20028C2008 December 1982Updated LER 82-030/03X-1:on 820716,3A TIP Ball Valve Failed to Reclose After Opening During Valve Exercise.Cause Unknown.Limit Switches & Ball Valve Replaced & Successfully Tested
ML20028B09618 November 1982LER 82-045/01T-0:on 821109,during Normal Operation,Diesel Generator D-3 Tripped on Low Cooling Water Pressure.Caused by Bad Low Cooling Water Pressure Switch.Switch Replaced
ML20028A1169 November 1982LER 82-042/01T-0:on 821027,excessive Water Found Leaking from Recirculation Pump Seal 3B.Caused by Recirculation Pump Seal Failure.Unit Manually Brought Down.Seals Replaced. Supplementary LER to Be Issued When Cause of Failure Known
ML20028A7184 November 1982LER 82-040/03L-0:on 821019,upscale Trip Point of Channel B Refuel Floor Area Radiation monitor,3-1705-8B,found at 130 Mrem/H.Caused by Instrument Set Point Drift.Monitor Reset to Trip at 90 Mrem/H
ML20052G5913 May 1982LER 82-018/03L-0:on 820414,closure Time of Nitrogen Inerting Stop Valve 3-1601-55 Exceeded Tech Spec Limit of 15-s.Caused by Failure of Asco Solenoid to Permit Normal bleed-off of Air Supply & Close Valve.Solenoid Replaced
ML20052E4193 May 1982LER 82-011/03L-0:on 820403,LPCI Differential Pressure Switch 2-261-34B Declared Inoperable During Monthly Surveillance Test Dis 1500-9.Caused by Wear of Contact Point in Mechanical Linkage.Switch Adjusted
ML20052E63628 April 1982LER 82-012/03L-0:on 820407,during Semiannual QA Audit,No Info Found to Verify Instrument Check Surveillance of Temp Detectors for Safety/Relief Valves.Caused by Failure to Include Requirement Change in Tech Spec Procedures
ML20052E43728 April 1982LER 82-017/03L-0:on 820407,cracked Weld Discovered on Test Tap of Condensate Booster Recirculation Line.All Leakage Contained in Turbine Bldg Floor Sumps.Cause Not Stated.Tap Cut & Capped
ML20052E88227 April 1982LER 82-019/01T-0:on 820417,while Conducting ASME Class I Hydrostatic Test During Shutdown,Water Discovered Leaking from LPCI Check Valve 3/4-inch Test Equalizing Line.Caused by Inadequate Piping SupportHydrostatic
ML20052E47627 April 1982LER 82-013/03L-0:on 820402,LPCI Differential Pressure Switch 2-261-35B Failed to Operate on Increasing Differential Pressure.Caused by Contact Point Wear in Mechanical Linkage. Pressure Switch Adjusted
ML20052C42423 April 1982LER 82-016/03L-0:on 820329,during Refueling Outage Mechanical Snubber 23 on Reactor Water Cleanup Sys Found Inoperable.Caused by Overloading Snubber During One Time Event.Snubber Replaced W/Hydraulic Snubber HSSA-10
ML20052G69022 April 1982Corrected LER 82-010/03L-0:on 820325,pilot Cell Voltage Readings Not Taken for 24/48,125 or 250-volt Dc Batteries Per Tech Specs.Caused by Broken Fluke Voltmeter.Event to Be Reviewed W/Shift Supervisors
ML20052E47322 April 1982Updated LER 80-048/03X-2:on 801223,while Testing Group 2 & 3 Isolation Circuitry,Shutdown Cooling Sys Inboard Isolation Valve Did Not Close.Caused by Dirt Buildup on Valve Stem. Thermal Overloads Adjusted & ResetTime of Discovery
ML20052B41220 April 1982LER 82-010/03L-0:on 820325,while Unit 2 Was in Normal Operation & Unit 3 in Refuel,Pilot Cell Voltage Readings Were Not Taken for Units 2 & 3 Dc Batteries.Caused by Operator Error
ML20052E71917 April 1982Updated LER 82-002/03X-1:on 820107,during Refueling Outage, Outboard MSIVs 3-203-2B & 3-203-2D Showed Leakages at Rates in Excess of Tech Specs.Caused by Packing Leakage.Valve Stem leak-off Lines Isolated & Packing Tightened
ML20052E4851 April 1982Updated LER 81-026/03X-1:on 810915,during Shutdown Process, Rod P-10 Showed Wrong Position on Rod Worth Minimizer.Caused by Diode Failure Resulting in Multiple Output Distributor Error Forcing Rod Block to Occur.Five Diodes Replaced
ML20050D47730 March 1982LER 82-014/03L-0:on 820317,crack Discovered in Head Seal Leak Detection Piping.Cause Undetermined.Leakage Located in Section of Pipe That Cannot Be Isolated.Analysis & Repairs to Be Done Following Cavity Drain Down
ML20042A5949 March 1982LER 82-007/03L-0:on 820213,during Routine Surveillance of Reactor Level Switch LIS 2-263-58B,setpoint Found to Be Above Tech Spec Limit.Caused by Instrument Setpoint Drift. Switch Adjusted
ML20042A7548 March 1982LER 82-006/03L-0:on 820210,ATWS Div II High Pressure Transmitter 2-263-20D,read Offscale High & Tripped Light on Panel 2202-70B.Caused by Faulty Capacitor in Amplifier Circuit Board.Amplifier Circuit Board Replaced
ML20041E6813 March 1982LER 82-012/03L-0:on 820204,drywell & Torus Purge Sys Valve 3-1601-21 Found to Leak.Caused by Failure of Resilient Seating Matl to Maintain Proper Seal to Valve Butterfly Disc.Valve Will Be Replaced
ML20041E7482 March 1982LER 82-011/03L-0:on 820203,during Performance of Leak Tests Per Dts 1600-1,leakage Rate of 284.84 Scfh Observed on HPCI Turbine Exhaust Check Valve 3-2301-45.Cause Not Determined. Valve Repaired & Vol Retested
ML20041E6212 March 1982LER 82-013/03L-0:on 820204,during Refueling Outage,Nitrogen Inerting Makeup Sys Supplying Nitrogen to Drywell Found to Leak at Rate of 80.39 Scfh.Caused by External Damage to Pressure Valve RV-3-8526.Valve Will Be Replaced
ML20042A65025 February 1982Updated LER 81-033/01X-1:on 810602,while Blowing Down HPCI Steam Supply Line W/Hpci Turbine on Turning Gear,Auxiliary Oil Pump Tripped & Motor Was Burned.Caused by Loose Stator Winding.Motor Rewound
ML20042C51825 February 1982Updated LER 81-025/01X-1:on 810914,during Automatic Depressurization Sys Valve Operability Surveillance,B Electromatic Relief Valve Failed to Open at Rated Pressure. Caused by Excessive Leakage on Threads
ML20049H78023 February 1982LER 82-008/03L-0:on 820126,HPCI Temp Switches 2371A,2372A, 2373B,2370C & 2370D Were Above Tech Spec Limits.Caused by Misaligned Microswitch Due to Loose Screws Which Enlarged Gap Between Actuator & Switch Plunger
ML20049H69323 February 1982LER 82-003/03L-0:on 820127,leak of Over 1% Detected Through Charcoal Filters in B Standby Gas Treatment Sys.Caused by Improper Packing of Charcoal Canisters.Charcoal Beds Replaced
ML20049H65723 February 1982LER 82-005/03L-0:on 820130,during Single Control Rod Scram Testing,Crd H-10 Failed to Scram.When Solenoid Fuses Pulled,Crd Failed to Scram.Caused by Sticking Scram Pilot Solenoid Valve.Both Valves Replaced & Tested
ML20049H60923 February 1982LER 82-004/03L-0:on 820127,after Filling Floor Drain Sample Tank A,Ci Content Found Above Tech Spec.Caused by Failure of Conductivity Recorder in Radwaste Control Room to Indicate That Carryover Was Occurring