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05000461/LER-2017-010Clinton9 December 2017
5 February 2018
Division 1 Transformer Failure Leads to Instrument Air Isolation to Containment Requiring a Manual Reactor Scram
LER 17-010-00 for Clinton Power Station, Unit 1 Regarding Division 1 Transformer Failure Leads to Instrument Air Isolation to Containment Requiring a Manual Reactor Scram

On December 9, 2017 at 1347 CDT the Main Control Room received annunciators that indicated a trip of a 4160V 1A1 Breaker, the 480V transformer 1A and Al feed breaker. The loss of Division 1 480V power caused the instrument air (IA) containment isolation valves to fail close as designed. The loss of IA affected various containment loads, including the scram pilot air header and containment isolation valves. Another consequence of this event was that secondary containment differential pressure became positive due to fuel building ventilation dampers failing closed by design due to the loss of power. Operations entered Emergency Operating Procedure (EOP) -08, Secondary Containment Control, and Technical Specification (TS) Limiting Condition for Operation (LCO), 3.6.4.1 Action A.1. Division 2 Standby Gas Treatment System was activated at 1350 and restored secondary containment differential pressure within allowable TS values at 1351. The TS LCO and EOP were exited when allowable TS values were restored. Due to the loss of IA, a manual reactor scram was inserted at 1353 when two control rods began drifting in as expected.

A phase to ground fault was identified on 480V transformer 1A (1AP11E). On December 14, the 480V transformer was replaced and the plant returned to Mode 1 operations on December 15. The condition described in this report was determined to be reportable under 10 CFR50.73(a)(2)(iv)(A), 10 CFR 50.73(a)(2)(v)(C) and 10 CFR 50.73 (a)(2)(ii)(B). The cause of the transformer failure is currently under investigation and will be provided in a supplemental report. This event is classified as an unplanned scram with complications due to the loss of the Division 1 480V power.

05000293/LER-2017-013Pilgrim26 November 2017
25 January 2018
1 OF 4
LER 17-013-00 for Pilgrim Nuclear Power Station Regarding Reportable Conditions Involving Standby Gas Treatment System and Secondary Containment lnoperability Not Reported During the Previous Three Years

On November 26, 2017, with the Reactor in the Run Mode at 100 percent power, while reviewing a procedure to be performed during normal scheduled testing it was determined that the test as written would cause both trains of Standby Gas Treatment System (SGTS) to be made inoperable during the test. This also made secondary containment system (SCS) inoperable. This LER is submitted to acknowledge that Pilgrim Nuclear Power Station missed providing Event Notifications and LERs for past occurrences. With both trains of SGTS and SCS inoperable while in Run, this event is reportable in accordance with Title 10 Code of Federal Regulations 50.73(a)(2)(v)(C) and 50.73(a)(2)(v)(D) as conditions that could have prevented the fulfillment of the safety function of a structure or system needed to control the release of radioactive material and mitigate the consequences of an accident. This has been determined to be a reportable condition that has not been reported during the past three years involving SGTS and secondary containment inoperability. The reportable conditions have occurred several times within the past three years during scheduled testing of SGTS.

This event had no impact on the health and/or safety of the public.

05000461/LER-2017-009Clinton
Clinton Power Station, Unit 1 .
5 November 2017
4 January 2018
Trip of Emergency Reserve Auxiliary Transformer Static VAR Compensator Causes Positive Secondary Containment Pressure Following Voltage Transient on 138 kV Offsite Source.
LER 17-009-00 for Clinton, Unit 1, Regarding Trip of Emergency Reserve Auxiliary Transformer Static VAR Compensator Causes Positive Secondary Containment Pressure Following Voltage Transient on 138 kV Offsite Source

On November 5, 2017, at approximately 1240 CDT, the Main Control Room (MCR) received numerous annunciators that indicated a trip of the Emergency Reserve Auxiliary Transformer (ERAT) Static VAR Compensator (SVC) caused by a voltage transient on the 138 kV offsite supply. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.8.1, AC Sources-Operating, Required Action A.1 and A.2 were entered. As a result of the voltage transient, the Division 1 Fuel Building ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no operating VF fans, Secondary Containment (SC) vacuum rose to slightly greater than 0 inches water gauge (WG) at 1241 CDT which exceeded the TS requirement of greater than 0.25 inches vacuum WG. The MCR entered Emergency Operating Procedure (EOP)-8, Secondary Containment Control and TS LCO 3.6.4.1, Secondary Containment, Required Action A.1. The cause of the SC differential pressure becoming positive is that the circuit design of VF is not adequately robust to withstand loss of the 138 kV feed. At the time, the Division 1 safety bus was being fed from the ERAT.

Secondary Containment vacuum was restored within TS requirements at 1242 CDT by starting the Standby Gas Treatment System. A modification will be installed to prevent tripping VF during a momentary loss of power. Installation of a 138 kV Ring Bus is scheduled that is intended to improve the reliability of the radial feed of the 138 kV line. This event is being reported as a condition that could have prevented fulfillment of a safety function under 10 CFR 50.73(a)(2)(v)(C).

05000410/LER-2017-002Nine Mile Point30 September 2017
28 November 2017
Secondary Containment Inoperable Due to Wind Conditions
LER 17-002-00 for Nine Mile Point Nuclear Station, Unit 2 Regarding Secondary Containment Inoperable Due to Wind Conditions

On September 30, 2017 at 0134, Nine Mile Point Unit 2 declared Secondary Containment inoperable due to Secondary Containment vacuum decreasing below the technical specification limit. The condition is reportable under 10 CFR 50.72 (b)(3)(v)(C) and 10 CFR 50.73(a)(2)(v)(C) as any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material. The change in Secondary Containment vacuum was the result of changing wind conditions.

Secondary Containment was declared operable at 0135 when Secondary Containment vacuum was restored to greater than 0.25 inches of vacuum water gauge.

The event described in this LER is documented in the plant's corrective action program as IR# 04057558.

05000458/LER-2017-009River Bend
Docket Number
27 September 2017
13 November 2017
Potential Loss of Safety Function of Secondary Containment due to Unsecured Personnel Door
LER 17-009-00 for River Bend, Unit 1 Regarding Potential Loss of Safety Function of Secondary Containment due to Unsecured Personnel Door

On September 27, 2017, at approximately 10:00 a.m. CDT, with the plant operating at 85 percent power, a door in the auxiliary building pressure boundary was left unsecured by an employee entering the building. The employee failed to fully close the door, and then did not properly challenge the door to confirm its security prior to leaving the area. A security officer responded to the resulting alarm, and fully closed the door approximately four minutes later. Since the worker had sufficient experience with watertight doors to know their proper operation, this event is considered a skill-based error caused by over-confidence and improper assumptions. Having successfully used such doors numerous times, the worker was confident in the ability to do so. The effort to check the door's security by pushing it failed, likely due to its heavy mass.

A briefing memorandum was issued from the general manager to site personnel. Tamper alarms were installed on all watertight doors in the secondary containment boundary to provide an audible indication that the door is open.

Administrative controls have been instituted to schedule routine battery replacements.

05000387/LER-2017-005Susquehanna8 June 2017
4 October 2017
Automatic Reactor Protection System Trip on High Neutron Flux
LER 17-005-01 for Susquehanna, Unit 1 Regarding Automatic Reactor Protection System Trip on High Neutron Flux

On June 8, 2017 at 1527 hours, the reactor automatically scrammed due to a loss of Main Turbine- Electro-Hydraulic Control (EHC) logic power causing a high neutron flux, Reactor Protection System (RPS) trip. The safety systems operated as expected. Secondary Containment differential pressure lowered to 0" WG due to a trip of the normal operation of the Reactor Building Ventilation system. The differential pressure was restored by the initiation of Standby Gas Treatment System.

The scram was caused directly by a DC+ (direct current, positive) test lead (Maxi Grabber) that inadvertently contacted with the grounding screw, causing a short and momentary loss of EHC logic power.

Immediate action was taken to validate that there was no damage to the +30 VDC (volts DC) EHC logic.

The root cause for this event is an insufficient focus on the High Risk Activity of adjusting the EHC power supply, and inadequate risk mitigating actions for that activity.

The condition is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an automatic actuation of the RPS, including reactor scram. Although no safety system functional failure occurred, this event is also reportable pursuant to 10CFR 50.73(a)(2)(v)(C) as a condition that could have prevented fulfillment of a safety function. There were no actual, or potential consequences to the health and safety of the public as a result of this event.

I

05000397/LER-2016-002Columbia27 September 20171 OF 3
LER 16-002-01 for Columbia Generating Station Regarding Valve Closure Results in Momentary Increase in Secondary Containment Pressure

On October 3, 2016 at 1008 PDT, the Secondary Containment (Reactor Building) became inoperable due to p:'essure increasing above the Technical Specification limit of -0.25 inches of water gauge (inwg). While the plant was at 100% power, a Reactor Building exhaust valve (REA-V-1) unexpectedly closed, resulting in a loss of Secondary Containment vacuum for approximately four minutes.

Operations personnel manually started the Standby Gas Treatment System A and quickly restored Secondary Containment to less than -0.25 inwg. While Technical Specification limits were exceeded for this short time period, the resulting pressure excursion was bounded by analytical results; and thus, there were no safety consequences for this condition. This event was reported under reporting criterion 10 CFR 50.72(b)(3)(v)(C) as Event Notification #52276.

The cause of the REA-V-1 closure is currently under investigation; corrective actions for this condition will be determined upon completion of the in% estigation.

NRC FORM 386 (06-2016)

05000325/LER-2017-004Brunswick Steam Electric Plant (Bsep) Unit117 September 2017Emergency Diesel Generator and Primary Containment Isolation System Actuations

On September 17, 2017, at 0938 Eastern Daylight Time (EDT), a momentary power interruption to Emergency Bus E4 occurred during planned surveillance activities involving Emergency Diesel Generator (EDG) 4. This occurred when EDG 4 was disconnected from Emergency Bus E4 and offsite power was not supplying the bus. EDG 4 automatically transferred from manual mode to automatic control and reconnected to Emergency Bus E4. Normal frequency and voltage were restored with EDG 4 in automatic control. The momentary power interruption to Emergency Bus E4 resulted in various Unit 2 Primary Containment Isolation System (PCIS) actuations. The affected equipment responded as designed.

The direct cause of this event was that Operators were not aware that, at the time of the event, Emergency Bus E4 was being supplied solely by EDG 4. As a result of a failed under-frequency relay, the incoming line and feeder breakers from Balance of Plant (BOP) Bus 2C to Emergency Bus E4 had opened during the performance of the EDG 4 surveillance, leaving only EDG 4 to power Emergency Bus E4 in the manual mode of operation.

05000293/LER-2017-011Pilgrim
A Ler Number
20 June 2017
15 August 2017
Simultaneously Opened Reactor Building Airlock Doors Caused Loss of Secondary Containment
LER 17-011-00 for Pilgrim Nuclear Power Station Regarding Simultaneously Opened Reactor Building Airlock Doors Caused Loss of Secondary Containment

On June 20, 2017, at 1444 hours (EDT), with the reactor at 100% core thermal power and steady state conditions, plant personnel notified the Main Control Room that both doors in the secondary containment airlock at the 23 foot elevation on the East Side Reactor Building (RB) Entrance were opened simultaneously.

The failure of this interlock (to prevent both doors from being opened) caused a loss of secondary containment per Technical Specification (TS) 3.7.C.1. The doors were immediately closed, and the secondary containment boundary was reestablished.

An 8-hour non-emergency notification was made in accordance with 10 CFR 50.72(b)(3)(v)(C), any event or condition that at the time discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material. The safety significance of this event was minimal given the impact on the secondary containment.

Secondary containment remained available and functional during the event since secondary containment was immediately restored by closing the doors.

05000293/LER-2017-001Pilgrim16 January 2017
17 July 2017
Reactor Building Isolation Dampers Failed to Isolate
LER 17-001-01 for Pilgrim Nuclear Power Station Regarding Reactor Building Isolation Dampers Failed to Isolate

Station (PNPS) was performing surveillance testing of secondary containment isolation dampers when dampers AO-N-82 and AO-N-83, refueling floor supply isolation dampers, failed to fully close when the control switches were taken to close.

The failure of dampers AO-N-82 and AO-N-83 to fully close resulted in a loss of safety function for secondary containment, causing immediate entry into Limiting Condition for Operation (LCO) Action Statement (AS) 3.7.C.2.a, at 1155 hours. This LCO AS was exited at 1206 hours when the dampers were verified closed.

An 8-hour non-emergency notification was made in accordance with 10 CFR 50.72(b)(3)(v), any event or condition that at the time discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident. In addition, this notification is being conservatively made by PNPS in accordance with 10 CFR 50.73(a)(2)(i)(B), as a condition that was prohibited by Technical Specifications.

The reactor building isolation dampers were cleaned, lubricated and post-work tested. PNPS has returned the dampers to operable status. Planned action to prevent recurrence is to revise the preventive maintenance strategy.

There was no impact to public health and safety from this condition.

05000293/LER-2017-004Pilgrim5 April 2017
2 June 2017
Secondary Containment Testing Led to Loss of Safety Function to Both Trains of Standby Gas Treatment System
LER 17-004-00 for Pilgrim Nuclear Power Station Regarding Secondary Containment Testing Led to Loss of Safety Function to Both Trains of Standby Gas Treatment System

On April 5, 2017, at 0030 hours (EDT) with the Reactor in the Run Mode at approximately 97 percent power, both trains of the Standby Gas Treatment System (SBGTS) were made inoperable during the performance of a surveillance test of secondary containment prior to the refueling outage, With both trains of SBGTS inoperable while in the Run mode, this event is reportable per the requirements of Title 10, Code of Federal Regulations (CFR) 50.73(a)(2)(v)(C) and 10 CFR 50.73(a)(2)(v)(D), any event that could have prevented the fulfillment of the safety functions to "control the release of radioactive material" and "mitigate the consequences of an accident.

This event had no impact on the health and/or safety of the public.

05000461/LER-2017-001Clinton24 February 2017
21 April 2017
Failure of the 138 kV Offsite Power Source Results in a Loss of Secondary Containment Vacuum
LER 17-001-00 for Clinton, Unit 1, Regarding Failure of the 138 kV Offsite Power Source Results in a Loss of Secondary Containment Vacuum
On February 24, 2017 at approximately 2239 hours (CDT), the Main Control Room (MCR) received numerous annunciators which indicated a loss of the 138 kV off-site supply to the Emergency Reserve Auxiliary Transformer (ERAT). The MCR entered Technical Specification (TS) Limiting Condition for Operation (LCO) 3.8.1, AC Sources- Operating, Required Actions A.1 and A.2. The Division 1 Fuel Building ventilation (VF) system isolation dampers closed due to the voltage transient causing a trip of the VF supply and exhaust fans and Secondary Containment (SC) vacuum to rise to slightly greater than 0 inches water gauge (WG), exceeding the TS requirement of greater than 0.25 inches vacuum WG. The MCR entered Emergency Operating Procedure (EOP)-8, Secondary Containment Control, and TS LCO 3.6.4.1, Secondary Containment, Required Action A.1. SC vacuum was restored within TS requirements at approximately 2242 hours by starting the Standby Gas Treatment (VG) system. The Transmission System Operator confirmed that the loss of the 138 kV line was due to a line fault external to the Station. The 138 kV line was successfully re-energized at 0053 hours on February 25, 2017 and the ERAT off-site source was restored and declared OPERABLE at 0300 hours. This event is reportable per 10CFR50.73(a)(2)(v)(C).
05000366/LER-2017-002Hatch16 February 2017
13 April 2017
Emergency Diesel Generator Start Due to Inadvertent Electrical Bus De-Energization
LER 17-002-00 for Edwin I. Hatch, Unit 2, Regarding Emergency Diesel Generator Start Due to Inadvertent Electrical Bus De-Energization

On February 16, 2017, at 1320 EST with Unit 2 at 0 percent rated thermal power due to being in a refueling outage, maintenance electricians were sent to the field to perform a protective relay trip test for the 2D start-up transformer (SAT). During the test setup, the 2E 4160 VAC Emergency Bus was inadvertently and momentarily de-energized, causing the 2A Emergency Diesel Generator (EDG) to autostart, secondary containment to isolate, and start of the standby gas treatment system. Subsequent investigations revealed that the cause of the event was due to a movement operated contact (MOC) switch adapter was not required to be installed on the 2D normal supply breaker in the 2E 4160 VAC bus. All systems responded appropriately.

A review of the event determined that the MOC switch adapter was not required to be installed by the procedure, but was instructed to be installed by supervision. Corrective actions were taken to cover supervisor roles and responsibilities and the need for all workers to follow plant standards for procedure use and adherence. All breaker procedures and protective relay test procedures were reviewed to determine if a MOC switch adapter needs to be installed. Continuing training will also be held to cover this event and its lessons learned.

05000254/LER-2017-001Quad Cities24 January 2017
22 March 2017
Secondary Containment Interlock Doors Opened Simultaneously
LER 17-001-00 for Quad Cities, Unit 1, Regarding Secondary Containment Interlock Doors Opened Simultaneously

On January 24, 2017, at 10:00 hours, Operations was notified that both doors in the secondary containment interlock on the 595 foot elevation between the Reactor Building (RB) and the Unit 2 Reactor Feed Pump room (located inside the Turbine Building (TB)) were opened simultaneously for approximately 3 seconds. The failure of this interlock caused a loss of secondary containment per Technical Specification (TS) 3.6.4.1, Condition A. The doors were immediately reclosed, and the secondary containment boundary was immediately reestablished. Operators verified the RB (secondary containment) differential pressure was maintained operable at greater than 0.10 inches of water vacuum.

Secondary containment remained available and functional during the event since the secondary containment interlock was immediately restored by closing the doors and since the RB differential pressure was maintained during the event. The RB is a common volume to both Units 1 and 2, and an interlock failure can impact the secondary containment for both units.

The cause of the interlock failure was due to a dirty contact that caused the interlock relay to stick. This allowed the second door to open before the first door was secured. Corrective actions included inspecting and cleaning of the interlock relay contacts. Steps will be added to the Preventative Maintenance Work Orders to perform a visual inspection and cleaning of interlock relays.

The safety significance of this event was minimal. Given the impact on the secondary containment, this report is submitted (for Units 1 and 2) in accordance with the requirements of 10 CFR 50.73 (a)(2)(v)(C), which requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material.

05000416/LER-2017-002Grand Gulf28 February 2017Loss of Secondary Containment and Inoperability of the Standby Gas Treatment Systems as a result of a damages power supply.

On March 24, 2017, it was determined that the A Standby Gas Treatment System (SGTS A) was not operating as expected. The investigation into the event revealed the Single Nest Power Supply had failed resulting in loss of flow control. It was determined the power supply had been replaced and the technical specification limiting condition for operation exited on February 23, 2017. The A SGTS was not run between replacement of the power supply and the time of discovery condition on March 24, 2017. Additionally, the B SGTS was removed from service for planned corrective and preventative maintenance on February 28, 2017 and returned to service on March 3, 2017. This condition prohibited by technical specifications in accordance with 10 CFR 50.73(a)(2)(i)(B) for the A SGTS train being inoperable for a period great than allowed by technical specifications. The cause of this event has been determined to be a power supply that could not be fully inserted due to pre-existing damage.

The damaged power supply was not appropriately corrected prior to installation due to an incorrect screening practice. The defective power supply was replaced and tested satisfactorily. Entergy established proceduralized barriers to minimize recurrence of similar errors through the establishment of pre-installation checks for the power supply as well as post maintenance testing of the replaced power supplies. There were no actual nuclear safety consequences or radiological consequences. No Technical Specification Safety Limits were violated.

(4-2017) to 366A U.S. NUCLEAR REGULATORY COMMISSION

CONTINUATION SHEET

(See NUREG-1022, R.3 for instruction and guidance for completing this form htiorAww.nrc.00vireadino-rrradoc-collectionsinureosistaff/sr1022,ra) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/31/2020 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-8001, or by e-mail to Infocollects.Resourcee nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

Grand Gulf Nuclear Station, Unit 1 05000 416

DESCRIPTION

On March 24, 2017, while operating the A Standby Gas Treatment System (SGTS A) the SGTS Flow Recorder was indicated a downscale reading. The Plant Data System computer points indicated a flow mismatch between the available indications of approximately 5000 cubic feet per minute (CFM). Due to the mismatch indications and the downscale reading the surveillance was terminated and Standby Gas "A" was returned to standby.

The investigation of the identified conditions determined the failure of the systems was the Single Nest Power Supply. Failure of this power supply would result in a loss of the associated train's flow control. The investigation revealed that the power supply was replaced and the technical specification limiting condition for operation exited on February 23, 2017. The A SGTS was not run between replacement of the power supply and the time of discovery condition on March 24, 2017.

Prior to the power supply being replaced the system had been successfully tested and therefore it was determined that this condition could only have been present since the installation of the new Power Supply was completed on February 23, 2017.

The investigation further revealed that the B SGTS was removed from service for planned corrective and preventative maintenance on February 28, 2017 and returned to service on March 3, 2017.

The above described condition rendered the A SGTS inoperable and also resulted in a period when both SGTSs were inoperable during the same time period.

REPORTABILITY

The condition is also reportable as a condition prohibited by technical specifications in accordance with 10 CFR 50.73(a)(2)(i)(B) for the A SGTS train being inoperable for a period great than allowed by technical specifications.

An engineering evaluation was performed that demonstrated the SGTS A was able to perform its safety function with the identified nonconformance. Therefore this LER supplement retracts reporting this concern as a loss of safety function under 10 CFR 50.73(a)(2)(v)(C).

CAUSE

The cause of this event has been determined to be within the control system of the Single Nest Power Supply.

The equipment failure analysis determined the power supply could not be fully inserted due to pre-existing damage. The damage to the power supply was not appropriately corrected prior to installation due to an incorrect screening of the condition report that initially identified the pre-existing condition.

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6-2016) FiEnt, LICENSEE EVENT REPORT (LER) (A 2 CONTINUATION SHEET (See NUREG-1022, R.3 for instruction and guidance for completing this form http:ilwwwnrc.govireadina-rinidcc-collectionsinureasistaffisrl 022/0) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/31/2020 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Infacollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

Grand Gulf Nuclear Station, Unit 1 05000 416

3. LER NUMBER

CORRECTIVE ACTIONS

The defective power supply was replaced and tested satisfactory.

Proceduralized barriers were established to minimize recurrence of similar errors through the establishment of pre-installation checks for the power supply as well as post maintenance testing of the replaced power supplies.

The governance was reviewed as it relates to discovery of deficient conditions on replacement parts and required actions based on classification of the part (i.e. safety related, quality part, etc.). This action was performed to determine if this issue should have been identified as a NON CONFORMING part and if it should have been tagged and segregated. This review revealed the process was not followed and follow-up actions were developed to correct the cause of the error.

SAFETY SIGNIFICANCE

There were no actual nuclear safety consequences or radiological consequences as a result of this power supply failure. No Technical Specification Safety Limits were violated.

PREVIOUSLY SIMILAR EVENTS

The identified licensee event reports were reviewed and it has been determined that the causes and corrective actions for the previously identified events were sufficiently different that they could not have predicted or prevented the occurrence of this event.

05000333/LER-2016-004FitzPatrick24 June 2016
23 August 2016
Transformer Fault Results in Manual Scram and Secondary Containment Vacuum Below Technical Specification Limit
LER 16-004-00 for James A. Fitzpatrick Regarding Transformer Fault Results in Manual Scram and Secondary Containment Vacuum Below Technical Specification Limit

On June 24, 2016, at 1205, several 600V electrical busses lost power when James A. FitzPatrick Nuclear Power Plant was Reactor Water Recirculation (RWR). The 'A' RWR pump tripped immediately causing reactor power to reduce to approximately 50%. The remaining RBCLC pump was inadequate to maintain the MG Set fluid drive oil temperature for the 'B' RWR pump so Operators initiated a manual scram at 1236. This event is reportable per 10 CFR 50.73(a)(2)(iv)(A).

The power loss also affected Reactor Building Ventilation (RBV). This system supports the requirement of Technical Specification Surveillance Requirement 3.6.4.1.1 for a differential pressure in Secondary Containment. At the loss of RBV, Secondary Containment automatically isolated and the Standby Gas Treatment system was manually initiated. However, during this short transition the differential pressure requirement was not met. This report is being submitted per 10 CFR 50.73(a)(2)(v)(C).

The apparent cause of the 71T-5 fault was inadequate preventative maintenance which allowed the transformer to remain in service beyond expected service life.

05000461/LER-2016-009Clinton22 August 2016Trip of Fuel Building Fans Due to Damper Failure Results in Loss of Secondary Containment
LER 16-009-00 for Clinton Power Station, Unit 1 Regarding Trip of Fuel Building Fans Due to Damper Failure Results in Loss of Secondary Containment
On June 24, 2016 at 1511 (CST) Clinton Power Station (CPS) was operating at 99 percent reactor power when the MCR received two Fuel Building (VF) trouble alarms. An unexpected damper closure resulted in Secondary Containment (SC) vacuum degrading, eventually exceeding the Technical Specification (TS) limit of 0.25 inch vacuum water gauge. TS Limiting Condition for Operation (LCO) 3.6:4.1, Secondary Containment, Required Action A.1 and Emergency Operating Procedure (EOP) - 08, Secondary Containment Control were entered. At 1512, SC vacuum was restored within TS limits with the auto start of VF supply fan 1VFO3CB and exhaust fan 1VFO4CB. An initial Investigation determined that the 'A' Exhaust Fan Isolation Damper 1VF11YA had failed to the closed position on loss of air due to failure of the associated air supply solenoid, 1FSVVF005. The apparent cause of this event is the failure of the ASCO solenoid valve, 1FSVVF005, due to a slightly deformed and worn core which resulted in sticking. The failed solenoid valve 1FSVVF005 was replaced and the VF system ventilation was restored. In addition, parts quality testing, and preventative maintenance programs are being established to replace VF solenoid operated valves on a periodic basis. The temporary loss of SC is reportable under 10CFR 50.73(a)(2)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material.
05000331/LER-2016-001Duane Arnold19 June 2016
18 August 2016
Two Instances of Both Doors in Secondary Containment Airlock Opened Concurrently
LER 16-001-00 for Duane Arnold Energy Center Regarding Two Instances of Both Doors in Secondary Containment Airlock Opened Concurrently

On June 19, 2016, while operating at 82% power, two secondary containment access airlock doors were briefly opened simultaneously during a surveillance test. This event was a momentary inoperability of secondary containment integrity, which is an 8 hour reportable event. The Resident Inspector was notified, and an Event Notification made pursuant to 10 CFR 50.72(b)(3)(v)(C). (Reference EN#52022). Following the event, the door controls were adjusted and verified to function properly. On June 29, 2016, at 100% power, workers opened two doors concurrently when entering a secondary containment access airlock. The individuals promptly closed their respective doors. The event was a brief inoperability of secondary containment integrity as above, notifications were made, and repairs completed. (Reference EN#52053) The root causes were determined to be inadequate procedural guidance and equipment design not being able to prevent the simultaneous opening of an inner and outer door at all times, under all possible conditions. Corrective actions include modification of the interlock tests, and replacement of key door interlock components.

These events did not result in a safety system functional failure. There were no radiological releases associated with these events.

05000333/LER-2016-003FitzPatrick7 June 2016
3 August 2016
Concurrent Opening of Reactor Building Airlock Doors
LER 16-003-00 for James A. FitzPatrick Regarding Concurrent Opening of Reactor Building Airlock Doors

On the morning of June 7, 2016, while operating at 100% power, workers opened doors concurrently when entering a secondary containment access airlock. The individuals involved each closed their respective doors upon encountering this unexpected condition; however, the result was a brief inoperability of secondary containment.

This resulted in an 8 hour reportable event. The Resident Inspector was notified, and an Event Notification was made pursuant to 10 CFR 50.72(b)(3)(v)(C) due to a condition at the time of discovery that prevented the fulfillment of the Secondary Containment safety function (Reference ENS 51985). Following the event, the doors functioned properly, and no deficiencies were noted with either door.

There were no radiological releases associated with this event.

05000458/LER-2016-006River Bend13 May 2016
12 July 2016
Potential Loss of Safety Function of Multiple Systems Due to Design Deficiency in 480-volt Circuit Breakers
LER 16-006-00 for River Bend Station re: Potential Loss of Safety Function of Multiple Systems Due to Design Deficiency in 480-volt Circuit Breakers

At 1200 CDT on May 13, 2016, while the plant was operating at 100 percent power, the shift manager was notified of a design inadequacy that could potentially prevent both divisions of the standby gas treatment system (GTS) from performing its design function.

Under certain specific conditions, the 480-volt circuit breakers supplying the GTS fans may not re-close following a trip signal. In the postulated condition in which a start signal is followed by an immediate (within 0.075 seconds) trip signal, the breaker could fail to close at the next attempt. As a result of this condition, both divisions of GTS were declared inoperable. The initial investigation of this condition determined that circuit breakers in the main control building air conditioning system (HVC) and the diesel generator building ventilation system (HVP) are also susceptible to this postulated failure mechanism. This defect has the potential to similarly cause the HVC and HVP systems to be incapable of performing their safety function. The affected circuit breakers in those systems have been modified to correct the deficiency. This condition is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) and (a)(2)(v)(D) as operations prohibited by Technical Specifications and an event that could have caused a loss of safety functions of the affected systems.

The specific scenario in which this failure mechanism could plausibly have occurred is a highly unlikely event. Additionally, standing _ orders were already in place at the time of this -event that directed the operators to take compensatory actions to preserve the safety function of the affected systems. Those orders will remain in effect until all modifications are complete. Thus, this condition does not represent a significant challenge to the health and safety of the public.

05000410/LER-2016-001Nine Mile Point7 April 2016
6 June 2016
Secondary Containment Inoperable Due to Simultaneous Opening of Airlock Doors
LER 16-001-00 for Nine Mile Point, Unit 2, Regarding Secondary Containment Inoperable Due to Simultaneous Opening of Airlock Doors
On April 7, 2016, at approximately 1730 hours, the secondary containment of the Nine Mile Point Unit 2 (NMP2) Reactor Building was breached when workers opened both inner and outer airlock doors, SA262-2 and SA262-3, simultaneously. The integrity of the airlock was re-established within 4 to 5 seconds when one of the doors was closed and latched. This resulted in a momentary loss of Secondary Containment Operability (TS 3.4.3). Secondary containment differential pressure never exceeded the minimum Technical Specification limit of 0.25 inch of vacuum water gauge. The causal analysis identified that the existing notice providing airlock door usage instructions is not effective in preventing doors being opened simultaneously in all situations. Corrective actions taken include revising the notice signage at all airlock doors to increase wait time from 5 seconds to 10 seconds to allow personnel traversing the airlock to exit. NMP2 has submitted LER 2014-007, Revision 1 for similar conditions. I
05000461/LER-2016-005Clinton
Docket-Number
2 April 2016
31 May 2016
Insulator Failure On the Reserve Auxiliary Transformer Results In A Loss of Secondary Containment Vacuum
LER 16-005-00 for Clinton Power Station, Unit 1, Regarding Insulator Failure on the Reserve Auxiliary Transformer Results in a Loss of Secondary Containment Vacuum
On April 2, 2016, at approximately 1257 CDT the Main Control Room (MCR) received numerous annunciators that indicated a trip of the Reserve Auxiliary Transformer (RAT) and associated Static VAR Compensator (SVC). The MCR entered Technical Specification (TS) Limiting Condition for Operation (LCO) 3.8.1, AC Sources-Operating, Required Actions A.1 and A.2. The Division 1 Fuel Building ventilation (VF) system isolation dampers closed due to loss of power causing a trip of VF supply and exhaust fans. With the VF fans inoperable, Secondary Containment (SC) vacuum rose to slightly greater than 0 inches water gauge (WG) which exceeded the TS requirement of greater than 0.25 inches vacuum WG. The MCR entered Emergency Operating Procedure (EOP)-8, Secondary Containment Control, and TS LCO 3.6.4.1, Secondary Containment, Required Action A.1. SC vacuum was restored within TS requirements at 1300 by starting the Standby Gas Treatment (VG) system. The RAT was successfully returned to service following replacement of the broken 'A' phase insulator stack on the 345 kV Circuit Switcher 4538. The cause of this event was identified as the failure of the 'A' phase 4538, 345 kV Circuit Switcher insulator due to a manufacturing defect. The corrective actions included performing a risk review of all Ohio Brass Insulators for potential failure impact and creating a replacement strategy to replace the high risk and critical insulators. Replacement of the remaining Ohio Brass insulators in the switchyard will be completed by the end of C1R17.
05000461/LER-2016-004Clinton30 March 2016
26 May 2016
Trip of Emergency Reserve Auxiliary Transformer Static VAR Compensator Causes Positive Secondary Containment Pressure Following Lightning Strike on 138 kV Offsite Source
LER 16-004-00 for Clinton, Unit 1, Regarding Trip of Emergency Reserve Auxiliary Transformer Static VAR Compensator Causes Positive Secondary Containment Pressure Following Lightning Strike on 138 kV Offsite Source
On March 30, 2016, at approximately 1545 CDT, the Main Control Room (MCR) received numerous annunciators that indicated a trip of the Emergency Reserve Auxiliary Transformer (ERAT) Static VAR Compensator (SVC) caused by a voltage transient on the 138 kV supply. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.8.1, AC Sources-Operating, Required Action A.1 and A.2 were entered. As a result of the voltage transient, the Division 1 Fuel Building ventilation (VF) system isolation dampers closed causing a trip of VF supply and exhaust fans. With no operating VF fans, Secondary Containment (SC) vacuum rose to slightly greater than 0 inches water gauge (WG) which exceeded the TS requirement of greater than 0.25 inches vacuum WG. The MCR entered Emergency Operating Procedure (EOP)-8, Secondary Containment Control and TS LCO 3.6.4.1, Secondary Containment, Required Action A.1. The likely cause of the voltage transient on the 138 kV line was a lightning strike that occurred during thunderstorms in the area on the day of the event. SC vacuum was restored within TS requirements at 1550 CDT by starting the Standby Gas Treatment System. Corrective actions have been initiated to improve reliability of the 138 kV source. This event is being reported as a condition that could have prevented fulfillment of a safety function under 10 CFR 50.73(a)(2)(v)(C).
05000461/LER-2016-002Clinton13 February 2016
13 April 2016
Trip of Fuel Building Ventilation Exhaust Fan Due to Moisture Formation Resulting In the Loss of Secondary Containment Vacuum
LER 16-002-00 for Clinton, Unit 1, Regarding Trip of Fuel Building Ventilation Exhaust Fan Due to Moisture Formation Resulting In the Loss of Secondary Containment Vacuum

On 02/13/2016 at 0206 (CST) the plant was at 99 percent reactor power when Fuel Building Exhaust Fan "A" (1VFO4CA) tripped due to indicated high Secondary Containment (SC) vacuum during routine venting of the drywell per plant procedures. Following the fan trip, SC vacuum degraded, eventually exceeding the Technical Specification (TS) limit of 0.25 inch vacuum water gauge. The TS Limiting Condition for Operation (LCO) 3.6.4.1 Required Action A.1 and an Emergency Operating Procedure were entered. Plant Operations subsequently started the Standby Gas Treatment System (VG) and restored Secondary Containment within TS limits. An investigation determined that ice formed in the sensing line causing an inaccurate Secondary Containment vacuum reading on the indication and control loop for 1VFO4CA. This caused 1VFO4CA to trip which in turn led to a loss of Secondary Containment vacuum. A cause evaluation established that prior instrument sensing line designs did not recognize the potential to trap water in the sensing line to the Secondary Containment pressure instrumentation. Corrective actions will include completing an engineering change to install an alternate Fuel Building Ventilation (VF) system sensing line design to prevent moisture accumulation line to ensure accurate indication and control of Secondary Containment pressure.

This event is reportable under 10 CFR 50.73(a)(2)(v)(C).

05000325/LER-2016-001Brunswick7 February 2016
6 April 2016
Electriqal Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
LER 16-001-00 for Brunswick, Unit 1, Regarding Electrical Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
On February 7, 2016, at 1312 Eastern Standard Time (EST), Unit 1 was in Mode 1 (i.e., Run) at 88 percent of rated power in end-of-cycle coastdown. At that time, an electrical fault occurred on a balance of plant 4160-volt bus, resulting in a lockout of the Startup Auxiliary Transformer (SAT) and a loss of both Reactor Recirculation pumps. Licensed personnel inserted a manual scram per procedure. Emergency Diesel Generators supplied emergency electrical busses until offsite power was restored at 1628 EST. The loss of power and reactor water level changes resulted in automatic closures of various Primary Containment Isolation Valves (PCIVs). The electrical fault resulted in an electrical explosion; therefore, an Alert was declared at 1326 EDT. The immediate cause of this event was a fault in a non-segregated electrical bus connected to the SAT. The root causes were insufficient detail in applicable maintenance instructions for inspecting the non-segregated bus housing and inadequate instructions for terminating electrical cables in a circuit breaker cubicle. Corrective actions include repairing equipment damaged by the electrical fault and revising the procedures and work instructions.
05000387/LER-2015-006Susquehanna29 September 2015
30 March 2016
Loss of Safety Function due to Inoperability of Both Trains of the Standby Gas Treatment System and a Loss of Safety Function of the Control Room Emergency Outside Air Supply System due to Air Flow Controller found in Manual
LER 15-006-01 for Susquehanna, Unit 1, Regarding Loss of Safety Function due to Inoperability of Both Trains of the Standby Gas Treatment System and a Loss of Safety Function of the Control Room Emergency Outside Air Supply System due to Air Flow...

On September 29, 2015, at 0900 hours, the 'B' train of the Standby Gas Treatment System (SGTS) was declared inoperable as part of surveillance test SE-030-002B (24-Month Control Structure Ventilation System Operability Test Div II 'B' SGTS).

During the test, personnel also commenced testing of the Unit 1 Reactor Pressure Vessel water level instrumentation per SI- 180-306 (24-Month Calibration of RWCU PCIS Secondary Containment Isolation and CREOASS Initiation of Reactor Vessel Water Level 2 and MSIV Isolation on Reactor Vessel Water Level 1 for channels LITS-B21-1N026A and B21-1N026C). At 1030 hours, level instrument LITS-B21-1N026A failed its test acceptance criteria, resulting in entry into the Action Statement for TS 3.3.6.2, Condition A. This failed instrument channel is part of the initiation logic for the 'A' train of SGTS. In accordance with TS 3.0.6, since the SGTS is a support system, a loss of safety function determination was performed and concluded the 'A' train of SGTS was inoperable. With both the 'A' and 'B' trains of SGTS inoperable, the Action Statement for TS 3.6.4.3, Condition D, was entered at 1050 hours. At 1456 hours on September 29, 2015, an 8-hour Event Notification (#51432) was made to the NRC per 10 CFR 50.72(b)(3)(v)(c) for a condition that could have prevented the fullfilment of the safety function of the SGTS. On September 30, 2015, during panel walkdowns, it was identified that the 'B' CREOAS system flow controller was still in manual and had not been restored to auto after completion of SE-030-002B on September 29, 2015. As a result, the TS 3.7.3 Action Statement for CREOAS system was entered for the 'B' train being inoperable. In accordance with 10 CFR 50.73(a)(2)(v)(C),this LER is being submitted for any event or condition that at the time of discovery, could have prevented the fulfillment of the safety function of SGTS and the CREOAS system.

Apparent cause: Loss of safety function was not recognized and mitigated when scheduling a surveillance test concurrent with the planned inoperability of the opposite division. Key corrective action: Revise surveillance procedures for instrumentation involving RPS, ECCS initiation, Primary Containment Isolation System (PCIS) and the Secondary Containment Isolation System, to include information on equipment impacts for instruments removed from service, and that redundant equipment is to be operable. There were no actual consequences to the health and safety of the public.

05000458/LER-2016-004River Bend29 January 2016
29 March 2016
Actuation of the Division 1 Emergency Diesel Generator and Primary Containment Isolation Logic Due to Partial Loss of Offsite Power
LER 16-004-00 for River Bend, Unit 1, Regarding Actuation of the Division 1 Emergency Diesel Generator and Primary Containment Isolation Logic Due to Partial Loss of Offsite Power

On January 29, 2016, at 1518 CST, with the plant in cold shutdown, power was lost on reserve station service (RSS) line no. 1. This is one of two sources of offsite power required by Technical Specifications. The power loss de-energized the Division 1 onsite AC safety.- related switchgear, causing an automatic start of the Division 1 emergency diesel generator (EDG). The Division 1 reactor protection system (RPS) bus was also de-energized, causing a half-scram signal. Approximately 8 minutes later, a full actuation of the RPS occurred due to high water level in the control rod drive hydraulic system scram discharge volume header. All reactor control rods were already fully inserted. The loss of Division 1 RPS also caused the actuation of the Division 1 primary containment isolation logic. The Division 1 isolation valves in the balance-of-plant systems closed as designed. Both trains of the standby gas treatment system actuated.

The loss of RSS No. 1 was caused when company transmission department personnel working in the local 230kV switchyard executed a deficient work instruction while modifying relay settings. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as the automatic actuation of the Division 1 EDG, the Division 1 primary containment logic, and the reactor protection system (while subcritical). At the time of the event, the shutdown cooling system was operating on the Division 2 subloop, which was unaffected.

The Division 1 EDG performed as designed. This event was, thus, of minimal significance to the health and safety of the public.

05000352/LER-2016-001Limerick25 January 2016
23 March 2016
Inoperable Reactor Enclosure Secondary Containment Integrity Due to Open Airlock
LER 16-001-00 for Limerick, Unit 1, Regarding Condition That Could Have Prevented Fulfillment of the Reactor Enclosure Secondary Containment Integrity Safety Function
Unit 1 reactor enclosure secondary containment integrity was briefly declared inoperable when both doors on a reactor enclosure 201' elevation pipe tunnel airlock were simultaneously opened. The cause of the event was a degraded closing mechanism on the airlock inboard door. The airlock doors were closed to restore reactor enclosure secondary containment integrity. The degraded inboard door closing mechanism was repaired.
05000254/LER-2016-002Quad Cities15 January 2016
14 March 2016
Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Pump Rm)
LER 16-002-00 for Quad Cities Units 1 and 2, Regarding Secondary Containment Different Pressure Momentarily Lost due to Air Failure (RWCU pump Rm)

building. The alarms occurred during an entry to the Unit 2 Reactor Water Cleanup (RWCU) pump room. A negative reactor building pressure was restored within two minutes (approximately 20:40 hours) without operator action.

Since both Units 1 and 2 share a common reactor building (RB), the loss of differential pressure impacted both Units 1 and 2 secondary containments.

The cause was a sheared air line inside the Unit 1 RB ventilation exhaust plenum which depressurized the air header supplying operating air to all three Unit 1 reactor building exhaust fan isolation dampers, causing the dampers to fail open, including the one on the standby fan.

Corrective actions included replacing the sheared air line, and the addition of a preventive maintenance task for replacement of equivalent air lines on all RB supply and exhaust fan dampers.

The safety significance of this event was minimal. Given the impact on the secondary containment, this report is submitted (for Units 1 and 2) in accordance with the requirements of 10CFR 50.73(a)(2)(v)(C), which requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material.

05000254/LER-2016-001Quad Cities12 January 2016
10 March 2016
Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Hx Rm)
LER 16-001-00 for Quad Cities, Unit 1, Regarding Secondary Containment Differential Pressure Momentarily Lost Due to Air Line Failure (RWCU Hx Rm)

building. The alarms occurred during an entry to the Unit 2 Reactor Water Cleanup (RWCU) Heat Exchanger (HX) room. A negative reactor building pressure was restored within one minute (alarm cleared at 13:41 hours) by immediately securing a reactor building supply fan. Since both Units 1 and 2 share a common reactor building (RB), the loss of differential pressure (RB pressure went positive) for approximately one (1) minute impacted both Units 1 and 2 secondary containments.

The cause was a sheared air line inside the Unit 1 RB ventilation exhaust plenum which depressurized the air header supplying operating air to all three Unit 1 reactor building exhaust fan isolation dampers and causing the dampers to fail open, including the one on the standby fan.

Corrective actions included replacing the sheared air line, and the addition of a preventive maintenance task for replacement of equivalent air lines on all RB supply and exhaust fan dampers.

The safety significance of this event was minimal. Given the impact on the secondary containment, this report is submitted (for Units 1 and 2) in accordance with the requirements of 10CFR 50.73(a)(2)(v)(C), which requires the reporting of any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material.

05000458/LER-2016-002River Bend9 January 2016
7 March 2016
Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient
LER 16-002-00 for River Bend, Unit 1, Regarding Automatic Reactor Scram and Division 2 Primary Containment Isolation Due to Offsite Grid Electrical Transient
On January 9, 2016, at approximately 2:37 a.m. CST, with the plant operating at 100 percent power, an automatic reactor scram occurred concurrent with the closure of all main steam isolation valves (MSIVs). That action was the result of an electrical transient caused by a phase-to-phase fault on a nearby 230kV transmission line. The transient caused a momentary decrease in the voltage on both reactor protection system busses, which also power the MSIV control solenoids. The Division 2 primary containment isolation logic was also actuated, causing the Division 2 valves in balance-of-plant systems to close. Both divisions of the standby gas treatment system automatically started due to the shutdown of the normal annulus pressure control system. Both reactor recirculation pumps downshifted to slow speed. The company's transmission department investigated the event. Although no definite source of the fault was found, it was concluded that a lightning strike likely caused the transient. The fault occurred on a 230kV transmission line approximately three miles from the station. The fault lasted for 5.4 cycles before it was isolated by automatic breaker action, and caused the voltage on the switchgear supplying the RPS busses to decrease to approximately 34 percent of normal. This transient was sufficient to trip the scram solenoids and the MSIV solenoids. No plant parameter limits requiring the automatic actuation of any of the emergency core cooling systems or the emergency diesel generators were exceeded. This event, thus, was of minimal significance to the health and safety of the public. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv) as an actuation of the reactor ( protection system and the primary containment isolation logic. .
05000458/LER-2016-001River Bend5 January 2016
7 March 2016
Potential Loss of Secondary Containment Safety Function Due to Failure of Auxiliary Building Ventilation System
LER 16-001-00 for River Bend, Unit 1, Regarding Potential Loss of Secondary Containment Safety Function Due to Failure of Auxiliary Building Ventilation System

On January 5, 2016, at 10:58 p.m. CST, with the plant operating at 100 percent power, the main control room alarm indicating high pressure in the auxiliary building actuated. Operators confirmed that the building pressure was out of specification. Secondary containment was declared inoperable, and the Division 2 standby gas treatment system was started. This action restored building pressure to the acceptable range, and secondary containment was declared operable at 12:27 a.m. on January 6. An inspection of the auxiliary building normal ventilation system found that discharge dampers on the exhaust fans were degraded, and the flow control damper on the supply fans was not operating correctly. In order to restore the normal ventilation system to service, the troubleshooting plan for this condition temporarily altered the operating configuration of the system to close the suction damper on the idle exhaust fan.

This prevents backflow through the idle fan, allowing the system to control building pressure within the required operating range.

Corrective maintenance is being planned to restore the material condition of the normal ventilation system. This condition is being reported in accordance with 10 CFR 50.73(a)(2)(v)(C) as an event that caused the secondary containment to be potentially incapable of performing its safety function. ,

05000333/LER-2015-006FitzPatrick22 September 2015
4 February 2016
Transitory Secondary Containment Differential Pressure Excursions
LER 15-006-01 for James A. FizPatrick Regarding Transitory Secondary Containment Differential Pressure Excursions

On September 22, 2015 at 17:03, with James A. FitzPatrick Nuclear Power Plant operating at 100 percent power, the Emergency and Plant Information Computer (EPIC) indicated a spike in Secondary Containment (SC) differential pressure (d/P) during performance of a surveillance test associated with automatic isolation of SC and initiation of the Standby Gas Treatment System. Per the plant data systems SC d/P exceeded the Technical Specification (TS) allowed value, and then immediately trended negative following auto-start of one of the trains of Standby Gas Treatment.

The time period that SC d/P was greater than the TS allowed value is reportable pursuant to 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.73(a)(2)(v)(C), as an event or condition that could have prevented fulfillment of a safety function. SC was operable following reestablishment of greater than or equal to 0.25 inches of water vacuum, and remains operable.

SC d/P excursions during transition from normal to isolation mode of the Reactor Building Ventilation (RBV) System are an expected condition, and attributable to the design of the non-safety related RBV System. The cause of the SC d/P exceeding the TS allowed value has been determined not to be associated with a component failure or equipment malfunction. Similar reportable events were identified during preparation of this report. A comprehensive listing of these occurrences is included in the report.