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05000416/LER-2017-007Grand Gulf12 December 2017Engineered Safety Feature System Actuations due to the loss 01 Engineered Safety Features Transformer 11

At approximately 0918 hours on Tuesday, December 12, 2017, while operating in MODE 1 at approximately 18 percent power, the Grand Gulf Nuclear Station (GGNS) experienced a loss of the Engineered Safety Features (ESF) Transformer 11 which was powering the Division 1 ESF bus. Subsequently, the station experienced an automatic start of the Division 1 Emergency Diesel Generator and the partial isolation of the primary and secondary containment buildings. Both of these events were expectedand as designed. The direct cause of ESF actuations was the loss of ESF Transformer 11. The cause of the transformer loss is under investigation at this time and this licensee event , report will supplemented upon completion of GGNS's causal analysis.

Additionally, GGNS experiented an unrelated isolation of the Reactor Core Isolation Cooling System upon restoration of power. The isolation of the Reactor Core Isolatigh Cooling System did not result in a loss of safety function. The cause of this isolation is under investigation and will be documented in accordance with the.GGNS corrective action program.

This event is reportable to the NRC in accordanCe with 10 CFR 50.72(b)(3)(iv) and 10 CFR 50.73(a)(2)(iv)(A) as an event or condition resulting in a valid actuation of a ESF system.

Grand Gulf Nuclear Station, Unit 1 05000 416 .

NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/3112020 (4-2017) Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Information Services Branch (T-2 so RkG,„ LICENSEE EVENT REPORT (LER)

  • r F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to y n4 CONTINUATION SHEET Infocollects.Resource@nrc.gov: and to the Desk Officer: Office of Information and .i: Regulatory Affairs, NEOB-10202. (3150-0104). Office of Management and Budoet, Washington, DC 20503: If a means used to impose an information collection does not c's, T
  • (See NUREG-1022, R.3 for instruction and guidance for completing this form display a currently valid OMB control number, the NRC may not conduct or sponsor. and a N*,......0, htto://vAmnrc.00virP-adiriq-rmidoc-collectionsinureosistaff/sr1022/r3A . person is not required to respond to, the information collection.

DESCRIPTION

At approximately 0918 hours on Tuesday, December 12, 2017, while operating in MODE 1 at approximately 18 percent power, the Grand Gulf Nuclear Station (GGNS) experienced a loss of the Engineered Safety Features (ESF) Transformer 11 (EB) which was powering the Division 1 ESF bus (EA): The transformer experienced an instantaneous ground resulting in a transformer lockout and loss of power to the ESF bus. Subsequently, the station experienced an automatic start of the Division 1 Emergency Diesel Generator (EK) and the partial isolation of the primary and secondary containment buildings. Both of the system actuations were expected responses to a loss of ESF bus and both systems responded as designed. The direct cause of ESF actuations was the loss of ESF Transformer 11.

Additionally, GGNS experienced an unrelated isolation of the Reactor Core Isolation Cooling System (BN) upon restoration of power. The' isolation of the. Reactor Core Isolation Cooling System did not result in a loss of safety function. The cause of this isolation is under investigation and will be documented in accordance with the GGNS corrective action program.

REPORTABI LITY

This event is reportable to the NRC in accordance with 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.73(a)(2)(iv)(A) as an event or condition resulting in a valid actuation of a ESF system.

The 10 CFR 50.72 reporting requirements were met with the completion of Emergency Notification System (ENS) Notificatibn 53115, at 1740 hpurs eastern standard time on December 12, 2017.

CAUSE

Direct Cause:

The direct cause of the ESF actuation was the loss of ESF Transformer 11 and the opening of the transformer feeder breaker due to an instantaneous ground.

Apparent Cause:

The most probable cause is a ground on one of the feeder cables to ESF Transformer 11.

However, the investigation and causal analysis is ongoing at this time and this licensee event report will be supplemented upon completion of the GGNS causal analysis.

NRC FORM

(6-2016) 366A U.S. NUCLEAR. REGULATORY COMMISSION LICENSEE. EVENT REPORT (LER)

  • CONTINUATION 'SHEET (See NUREG-1022, R.3 for instruction and guidance for completing this form htto://www.nrc.coWreadino-rm/doc-collectionsinureos/staff/sr1022/r3/) APPROVED BY OMB: NO. 3150-0104 EXPIRES: 3/3112020 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington. DC 20555-0001, or by e-mail to Infoccillects.Resource@nrc.gov, and to the Desk Officer. Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington. DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number. the NRC may not conduct or sponsor. and a person is not required to respond to, the information collection.

2. DOCKET 3. LER NUMBER 05000.416

CORRECTIVE ACTIONS

Spare Essential Transformer 21 was placed into service and normal power was restored.

The investigation and causal analysis is ongoing and this licensee event report will be supplemented upon completion of GGNS's causal analysis. The planned corrective actions will be included in the corrective action program and may be changed in accordance with the program.

  • .":

SAFETY SIGNIFICANCE

There were no nuclear safety consequences or radiological consequences as a result of this event.

No Technical Specification Safety Limits were violated. Upon the loss of Engineered Safety Feature Transformer 11 all required accident mitigation ESF components responded as designed.

The isolation of the Reactor Core Isolation Cooling System, although unexpected, did not adversely impact the plant's ability to respond to the event.

PREVIOUSLY SIMILAR EVENTS

Protective Relaying Circuitry on the "B" Main Transformer Transformer Wiring Entergy has reviewed the events listed in the licensee event reports (LER) documented above to determine if the corrective actions should have prevented the event documented in this LER.

Based on a preliminary evaluation it has been concluded the established corrective actions would not have prevent this event.

Entergy's investigation into the cause of this event and the development of corrective actions to preclude recurrence are ongoing. This section will be supplemented at the conclusion of this effort.

05000397/LER-2017-005Columbia12 September 2017
9 November 2017
Valve Closure Results in Momentary Increase in Secondary Containment Pressure
LER 17-005-00 for Columbia Generating Station Regarding Valve Closure Results in Momentary Increase in Secondary Containment Pressure

On September 12, 2017 at 1227 PDT, Secondary Containment became inoperable due to pressure increasing above the Technical Specification limit of -0.25 inches of water gauge. While the plant was at 100% power, a Reactor Building exhaust valve and supply valve unexpectedly lost power and closed, resulting in a loss of Secondary Containment for approximately one minute. While Technical Specification limits were exceeded for this short time period, the resulting pressure excursion was bounded by analytical results; and thus, there were no safety consequences for this condition. This event was reported under 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72 (b)(3)(v)(D) as Event Notification #52966.

The apparent cause of the event was that station personnel did not deliberately and conservatively perform work tasks. Workers failed to update work instructions when work was rescheduled, and did not verify power sources at the work site. Corrective actions for this event include conducting a workshop on management expectations of Maintenance, increased management oversight, and addressing human performance issues.

05000341/LER-2017-005Fermi3 November 2017Non-Functional Mechanical Draft Cooling Tower Fan Brakes Leads to HPCI Being Declared Inoperable and Loss of Safety Function
LER 17-005-00 for Fermi 2 Regarding Non-Functional Mechanical Draft Cooling Tower Fan Brakes Leads to HPCI Being Declared Inoperable and Loss of Safety Function

At 1000 EDT on September 9, 2017, the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to loss of output from the over speed fan brake inverter. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS) and the Emergency Equipment Cooling Water (EECW) system. The Division 2 EECW system cools the High Pressure Coolant Injection (HPCI) system room cooler. As a result, the non-functionality of the fan brakes lead to an unplanned HPCI inoperability.

Since HPCI is a single train system designed to mitigate the consequences of a loss of coolant accident (LOCA), this event could have prevented the fulfillment of a safety function. The cause of the event was the failure of the Division 2 fan brake inverter.

Corrective Actions were taken to replace the inverter and returning the MDCT fans, the UHS, EECW and HPCI to service on September 9, 2017 at 2351 EDT. A failure modes evaluation was performed by the vendor with no direct cause of the failed output determined. The fan brake system is only required for a design basis tornado and there was no credible tornado threat during this event.

The HPCI system is not required to mitigate a design basis tornado. The safety significance of this event is very low and there were no radiological releases associated with this event.

05000296/LER-2017-001Browns Ferry1 September 2017
31 October 2017
Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications
LER 17-001-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications

On September 1, 2017, at approximately 1006 Central Daylight Time (CDT), Browns Ferry Nuclear Plant (BFN) Unit 3 3A Residual Heat Removal (RHR) system pump failed to start during performance of Surveillance 3-SR-3.5.1.6 (RHR I), Quarterly RHR System Rated Flow Test Loop I. The apparent cause was the Electrical Preventive Maintenance Instruction for 4kV Wyle/Siemens Horizontal Vacuum Circuit Breaker (Type-3AF) and Compartment Maintenance was revised to include steps to secure the breaker's mounting hardware which caused internal binding of the indication flag. Binding of the indication flag prevented the closing spring of the breaker from charging and the breaker from closing on demand. As a result, automatic start of the 3A RHR pump was prevented. On September 1, 2017, at approximately 1633 CDT, the 3A RHR Pump was declared operable following lubrication and testing of the breaker's indication flag mounting bolt.

A Past Operability Evaluation concluded that the 3A RHR Pump was inoperable from July 26, 2017 to September 1, 2017, which exceeded the Technical Specification allowed outage time. During this time, the 3B, 3C, and 3D RHR pumps would have started automatically upon receipt of an Emergency Core Cooling System (ECCS) initiation signal or from an Operator manual start demand from the Control Room. Based on results from the Probability Risk Assessment and Engineering inspections, there was no significant risk to the health and safety of the public or plant personnel for this event. The Corrective Action to reduce the probability of similar events occurring in the future will be addressed by revising the Electrical Preventive Maintenance Instruction for 4kV Wyle/Siemens breakers to ensure freedom of movement of the indication flag is present during the breaker inspection.

05000387/LER-2017-005Susquehanna8 June 2017
4 October 2017
Automatic Reactor Protection System Trip on High Neutron Flux
LER 17-005-01 for Susquehanna, Unit 1 Regarding Automatic Reactor Protection System Trip on High Neutron Flux

On June 8, 2017 at 1527 hours, the reactor automatically scrammed due to a loss of Main Turbine- Electro-Hydraulic Control (EHC) logic power causing a high neutron flux, Reactor Protection System (RPS) trip. The safety systems operated as expected. Secondary Containment differential pressure lowered to 0" WG due to a trip of the normal operation of the Reactor Building Ventilation system. The differential pressure was restored by the initiation of Standby Gas Treatment System.

The scram was caused directly by a DC+ (direct current, positive) test lead (Maxi Grabber) that inadvertently contacted with the grounding screw, causing a short and momentary loss of EHC logic power.

Immediate action was taken to validate that there was no damage to the +30 VDC (volts DC) EHC logic.

The root cause for this event is an insufficient focus on the High Risk Activity of adjusting the EHC power supply, and inadequate risk mitigating actions for that activity.

The condition is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an automatic actuation of the RPS, including reactor scram. Although no safety system functional failure occurred, this event is also reportable pursuant to 10CFR 50.73(a)(2)(v)(C) as a condition that could have prevented fulfillment of a safety function. There were no actual, or potential consequences to the health and safety of the public as a result of this event.

I

05000298/LER-2016-001Cooper27 September 2017De-Energized High Pressure Coolant Injection Auxiliary Lube Oil Pump Caused by Relay Failure Results in Loss of Safety Function and a Condition Prohibited by Technical Specifications
LER 16-001-01 for Cooper Nuclear Station Regarding De-Energized High Pressure Coolant Injection Auxiliary Lube Oil Pump Caused by Relay Failure Results in Loss of Safety Function, a Condition Prohibited by Tech Specs, and a 10 CFR Part 21 Report

On April 25, 2016, while performing a walkdown of Control Room panels, it was noticed that the green indication light for High Pressure Coolant Injection (HPCI) auxiliary lube oil pump (ALOP) was not illuminated.

A non-licensed operator was dispatched to the HPCI ALOP starter and reported that the local indication lights were not illuminated. HPCI was declared inoperable at 2117 Central Daylight Time (CDT) resulting in entry into Technical Specifications (TS) Limiting Condition of Operation 3.5.1, Condition C, HPCI System Inoperable.

Investigation determined that the coil in the electrical relay for the ALOP, which had recently been replaced during a preventive maintenance window, had failed after 133 hours of service. The cause of the failure was determined to be the prior pre-installation checks performed by NuTherm on the relay were inadequate to prevent the type of infant mortality failure that occurred in this case. HPCI was declared operable at 1314 CDT on April 26, 2016, after the coil was replaced.

This event is being reported as a loss of safety function due to HPCI being a single-train safety system and as a condition prohibited by TS.

The potential safety consequences of this event were minimal due to both the limited duration the condition existed and the redundant/diverse core cooling systems which remained operable.

05000263/LER-2017-004Monticello19 June 2017
16 August 2017
High Pressure Coolant Injection Steam Stop Valve Failed to Open During Test
LER 17-004-00 for Monticello Regarding High Pressure Coolant Injection Steam Stop Valve Failed to Open During Test

On June 19, 2017 following a planned High Pressure Coolant Injection (HPCI) system maintenance, a HPCI start attempt was performed per the quarterly test procedure. HPCI failed to start during the test due to the steam stop valve HO-7 not opening caused by HO-7 oil relay not functioning properly.

Since the component was not the subject of the maintenance activity, the HPCI failure was reported to the NRC under Emergency Notification System, Event Number 52814.

The HO-7 oil relay was repaired and the HPCI system was returned to operable status at 13:30 on June 23, 2017.

05000461/LER-2017-008Clinton15 June 2017
11 August 2017
Division 3 Shutdown Service Water Pump Start Failure
LER 17-008-00 for Clinton, Unit 1 re Division 3 Shutdown Service Water Pump Start Failure
On June 15, 2017, Clinton Power Station (CPS) commenced procedure CPS 9069.01, Shutdown Service Water Operability Test. The purpose of this procedure is to verify operability of the Division 3 Shutdown Service Water (SX) System Pump 1SX01PC and selected valves per the Inservice Testing program on a quarterly basis. At 0958, SX pump 1SX01PC was started and after approximately 30 seconds, it tripped due to thermal overload. The pump was declared inoperable and operations entered Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.7.2, Condition A which requires the High Pressure Core Spray (HPCS) system to be declared inoperable and enter TS LCO 3.5.1 Condition B which requires verification by administrative means that the Reactor Core Isolation Cooling (RCIC) system is operable and within 14 days restore the HPCS system to operable status. The cause of the event is under investigation. A supplemental report will be provided when the cause has been established. An ENS notification was made at 1214 (EN 52806). Because the HPCS system is a single train safety system, this event is reportable under 10 CFR 50.73(a)(2)(v)(D) as a condition that could have prevented the fulfilment of a safety function to mitigate the consequences of an accident.
05000374/LER-2017-003Lasalle
LaSalle
11 February 2017
9 August 2017
High Pressure Core Spray System Inoperable due to Injection Valve Stem-Disc Separation
LER 17-003-01 for LaSalle County Station, Unit 2 Regarding High Pressure Core Spray System Inoperable due to Injection Valve Stem-Disc Separation

On February 11, 2017, Unit 2 was in Mode 5 for a planned refueling outage. While attempting to fill and vent the Unit 2 High Pressure Core Spray (HPCS) system, no flow was observed from the drywell vent valves or downstream of the HPCS injection valve. The HPCS system was already inoperable to support scheduled surveillances performed on February 8, 2017 in which the HPCS injection isolation valve had been cycled five times satisfactorily. Troubleshooting determined the cause of the valve malfunction was due to stem-disc separation. The valve internal components were replaced prior to restart of the unit from the refueling outage. The root cause of the valve failure was insufficient capacity of the shrink-fit stem collar, combined with multiple high-load cycles, which resulted in loosening and eventual shear failure of the wedge pin and threads.

This component failure is reported in accordance with 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented fulfillment of the safety function of structures or system that are needed to mitigate the consequences of an accident. This condition could have prevented the HPCS system, a single train safety system, from performing its design function if the valve failure occurred during an actual demand. This component failure is also reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications (TS) 3.5.1 "ECCS - Operating," since the HPCS system could have been 1 inoperable for greater than the TS 3.5.1, Required Action B.2, Completion Time of 14 days to restore HPCS system to operable status. There were minimal safety consequences associated with the condition since HPCS was not required to be operable at the time of the failure, and other required emergency safety systems remained operable. There were no actual demands for Unit 2 LHPCS, other ECCS systems, or the reactor core isolation cooling (RCIC) system during this period.

- --- ------- - NRC FORM 366 (04-2017) - 01 003 2017

05000373/LER-2017-006Lasalle
LaSalle
17 May 2017
14 July 2017
Low Pressure Core Spray Inoperable due to Minimum Flow Valve Failure in Closed Position
LER 17-006-00 for LaSalle, Unit 1, Regarding Low Pressure Core Spray Inoperable due to Minimum Flow Valve Failure in Closed Position

On May 17, 2017 at 0908 CDT, during Unit 1 full-power operations, operators received an unexpected alarm for the Low Pressure Core Spray (LPCS) pump injection high flow and automatic closure of the LPCS minimum flow valve (1E21-F011). Inspections indicated the flow switch that actively controls the LPCS minimum flow valve had a faulty diaphragm which allowed for water intrusion into the device. There were no impacts on plant operations. The required actions of Technical Specifications 3.5.1, "ECCS - Operating" and TS 3.3.5.1, "Emergency Core Cooling System (ECCS) Instrumentation" were entered. The switch was replaced and LPCS system tested, which allowed full restoration of the system on May 17, 2017 at 18:45 CDT.

This condition could have prevented the LPCS system from performing its design function. This condition is reportable in accordance with 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. There was minimal safety consequences associated with the condition since other emergency safety systems remained operable.

05000397/LER-2016-004Columbia8 June 20171 OF 3
LER 16-004-01 for Columbia Generating Station Regarding Automatic Scram Due to Off-site Load Reject

On December 18, 2016 at 11:24 hours, an automatic scram occurred due to a fault on an off-site transmission network. A reactor scram was automatically initiated by the plant response to the transient.

All rods fully inserted, Main Steam Isolation Valves (SB,V) automatically closed due to loss of pow er to both Reactor Protection Sy stem (JC) busses. All safety sy stems operated as designed. Two Safety Relief Valves (SB,V) were initially cycled automatically, then several manually to maintain Reactor Pressure Vessel (AC) pressure. Reactor water level was maintained with Reactor Core Isolation Cooling (BN), Control Rod Drive (AA) flow, and High Pressure Core Spray (BG).

The cause analysis for the loss of off-site power is being performed by the entity responsible for the off-site transmission network, Bonneville Power Administration (BPA). BPA took immediate corrective actions to restore the off-site transmission network. The root cause evaluation addressing the plant response is being performed by plant personnel. A supplemental LER will be issued when the cause analyses are completed.

05000260/LER-2017-003Browns Ferry29 March 2017
30 May 2017
Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting
LER 17-003-00 for Browns Ferry Nuclear Plant, Unit 2 Regarding Manual Reactor Scram Initiated During Startup Due to Multiple Rods Inserting

On March 29, 2017, at 1842 Central Daylight Time (CDT), during Unit 2 start-up, Operations personnel received annunciators for an Intermediate Range Monitor (IRM) Downscale and a Control Rod Withdrawal Block.

Operations personnel noticed that IRM `G' was reading downscale and adjusted the range down one position with no immediate reaction. At 1844 CDT, an upscale spike on IRM `G' caused a half scram on Reactor Protection System (RPS) 'A' trip system. After verifying that the IRM `G' High-High trip signal was cleared, Operations personnel reset the half scram on RPS 'A'. An immediate, concurrent trip signal from IRM 'F' was then received on the RPS '13' trip system, resulting in multiple rods inserting into the core. When Operations personnel identified multiple rods inserting, a manual reactor scram was inserted at 1844 CDT.

The root cause was determined to be a lack of performing electromagnetic and radio-frequency interference noise testing to detect nuclear instrumentation abnormalities.

Corrective Action to Prevent Recurrence is to perform routine pre-outage and outage-related preventive maintenance tasks for noise-induced cable tests to verify the noise has been removed.

05000293/LER-2017-002Pilgrim27 March 2017
25 May 2017
Isolation of HPCI
LER 17-002-00 for Pilgrim Regarding Isolation of HPCI

On March 27, 2017, at 1825 (EDT), with the reactor at 100 percent core thermal power and steady state conditions, plant personnel caused a High Pressure Coolant Injection (HPCI) System isolation. Pilgrim Nuclear Power Station was performing planned testing on the Reactor Core Isolation Cooling (RCIC) when the HPCI System isolated. Accordingly, the HPCI System was declared inoperable.

The Technical Specifications Limiting Condition for Operation 'Action Statement 3.5.C.2 was entered and planned troubleshooting into the cause of the HPCI isolation was started. This event is reportable under 10 CFR 50.73(a)(2)(v)(D), any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.

There was no impact to public health and safety from this condition.

05000263/LER-2016-001Monticello22 March 2016
25 May 2017
High Pressure Coolant Injection System Cracked Pipe Nipple Caused Oil Leak
LER 16-001-02 for Monticello Regarding High Pressure Coolant Injection System Cracked Pipe Nipple Caused Oil Leak

The High Pressure Coolant Injection (HPCI) system was inoperable during a pre-planned maintenance activity when a significant oil leak in HPCI system oil piping occurred because of a cracked oil pipe nipple.

The leak was of sufficient size that if it occurred outside the pre-planned maintenance, HPCI would have been declared inoperable. The equipment failure analysis concluded that the most likely cause was that HPCI pipe nipple was exposed to significant loads, sufficient to initiate a crack, likely from applied wrench torques during oil leak repair activities in 2005. With the presence of the crack and crack propagation mechanism, the engineering evaluation determined that HPCI was inoperable from January 9 through March 24, 2016, i.e. 75 days. The organizational root cause was that management and individuals were tolerant of leaks on the HPCI system. As a result, station personnel did not effectively advocate prompt repair of the HPCI oil leak.

The cracked HPCI oil pipe nipple was replaced. Results of the extent of condition review identified two other pipe nipples and two elbows with thread leakage (no crack present). The pipe nipples were replaced and the elbows were reused. The HPCI system was tested successfully after the repairs.

05000260/LER-2017-002Browns Ferry24 April 2017Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications
LER 17-002-00 for Browns Ferry, Unit 2, Regarding Inoperable Primary Containment Isolation Valve Resulting in Condition Prohibited by Technical Specifications

On February 23, 2017, radiography results for the Browns Ferry Nuclear Plant (BFN), Unit 2, Reactor Core Isolation Cooling (RCIC) system stop check valve, 2-HCV-071-0014 (71-14 valve), showed the valve to be in the fully open position.

In this position, the valve was incapable of performing its design function as a Primary Containment Isolation Valve (PCIV).

In order to isolate the affected primary containment penetration flowpath, the RCIC Steam Line Outboard Isolation Valve was closed and deactivated to secure flow through the adjacent PCIV check valve in the exhaust line in accordance with plant Technical Specifications (TS) Limiting Conditions for Operation (LCO) for Primary Containment Isolation.

It is assumed in the Past Operability Evaluation (POE) that the 71-14 valve had been inoperable from April 2015 to February 2017, in violation of TS LCO 3.6.1.3. During this time period, another check valve (upstream of the 71-14 valve) remained capable of isolating the affected penetration. The 71-14 valve was repaired during the BFN, Unit 2, Cycle 19 Refueling Outage which began on February 25, 2017.

The cause of this condition was determined to be inadequate minimum allowable internal clearances for the 71-14 valve.

The 71-14 valve internals were machined to minimum allowable material as an interim action to mitigate risks. The corrective action to prevent recurrence is to replace the 71-14 valve with a new valve design that is not susceptible to the same internal binding potential.

05000260/LER-2017-001Browns Ferry16 February 2017
14 April 2017
High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse
LER 17-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse

On February 16, 2017, the spurious failure of a fuse protecting a High Pressure Coolant Injection (HPCI) system flow controller rendered the HPCI system inoperable. Operators replaced both the line and neutral fuses, and restored HPCI availability. Following a period of monitoring the current flow through the fuse and HPCI system operation tests, Operations declared the Unit 2 HPCI system to be Operable on February 17, 2017.

Since HPCI is a single-train safety system, any period of unplanned inoperability constitutes a safety-system functional failure affecting accident mitigation, and is reportable. However, in the event of an emergency, the Reactor Core Isolation Cooling (RCIC) system remained operable, and all other Emergency Core Cooling Systems and the Automatic Depressurization System were available throughout this event to facilitate core cooling.

Failure analysis indicates that the fuse failed when its internal resistor lead and its tension/retraction spring became uncoupled at their soldered junction, as a result of age-induced solder creep. Corrective Actions include the prompt replacement of the failed fuses, determining the population of fuses on the HPCI system and RCIC system that should be replaced on a one-time basis, and to initiate work orders to replace these fuses.

05000321/LER-2017-002Hatch8 February 2017
7 April 2017
High Pressure Coolant Injection System Declared Inoperable Due to Degraded Inverter
LER 17-002-00 for Edwin I. Hatch, Unit 1, Regarding High Pressure Coolant Injection System Declared Inoperable Due to Degraded Inverter

On February 8, 2017, at 1151 EST with Unit 1 at approximately 100 percent rated thermal power, the High Pressure Coolant Injection (HPCI) suction and discharge pressure indicators were noted to be downscale during a main control room panel walk down. Upon further investigation, it was discovered that the output voltage of the DC to AC inverter was degraded. The HPCI DC to AC inverter supplies power to the HPCI flow controller and power supply. HPCI was therefore declared inoperable due to the degraded voltage condition.

The inoperable as found condition of the HPCI pressure indicators was due to degraded output voltage from the DC to AC HPCI inverter. The degraded inverter was removed and replaced and HPCI was returned to operable status. As part of an extent of condition review, the internals of the degraded inverter were inspected to determine what caused premature failure of the inverter. Based on the findings of this inspection, the preventative maintenance frequency for inverter replacement and calibration will be adjusted as necessary.

05000374/LER-2017-002Lasalle
LaSalle
30 January 2017
30 March 2017
High Pressure Core Spray System Declared Inoperable due to Cooling Water Strainer Backwash Valve Stem-Disc Separation
LER 17-002-00 for LaSalle, Unit 2, Regarding High Pressure Core Spray System Declared Inoperable due to Cooling Water Strainer Backwash Valve Stem-Disc Separation

On January 30, 2017, during routine surveillance testing of the Unit 2 Division 3 Diesel Generator Cooling Water (DGCW) system, the cooling water strainer backwash valve was unable to open. The Division 3 DGCW system was declared inoperable. Upon investigation, operators determined the cause of the valve malfunction was due to stem-disc separation. Division 3 DGCW is a support system for the Division 3 Emergency Diesel Generator and the High Pressure Core Spray (HPCS) system. The required actions of Technical Specifications (TS) 3.7.2 and 3.5.1 were entered on January 30, 2017 when the DGCW and HPCS system, respectively, were determined to be inoperable. TS 3.7.2 Required Action (RA) A.1 requires the supported system to be immediately declared inoperable. TS 3.5.1 RA B.2 requires restoration of the HPCS system to operable within 14 days. TS 3.8.1 was not applicable since a note provides that Division 3 AC electrical power sources are not required to be operable when HPCS is inoperable. The valve was replaced, and the HPCS system was returned to operable on February 2, 2017.

This condition could have prevented the HPCS system, a single train safety system, from performing its design function. This event is reportable in accordance with 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented fulfillment of the safety function of structures or system that are needed to mitigate the consequences of an accident. There were minimal safety consequences associated with the event since the other emergency safety systems remained operable, and the Division 3 DGCW system remained functional as it retained the ability to provide the required flow through the system. The apparent cause of the stem-disc separation was erosion due to the carbon-steel valve internals in a raw water system environment.

05000416/LER-2017-001Grand Gulf27 January 2017
28 March 2017
High Pressure Core Spray (HPCS) Jockey Pump Trip
LER 17-001-00 for Grand Gulf, Unit 1, Regarding High Pressure Core Spray Jockey Pump Trip

At 1808 hours on 1/27/17, Grand Gulf Nuclear Station entered into LCO 3.5.1.6 when the High Pressure Core Spray (HPCS) Jockey Pump (Component Function Identifier- P) failed and the HPCS System was declared inoperable. The Reactor Core Isolation Cooling (RCIC) System was verified operable and investigation into the cause was initiated. Under those plant conditions the Plant Technical Specifications action to restore the HPCS System to operable status allows a 14 day completion time.

No other safety systems were inoperable at the time of this event.

The decision was made to disassemble the HPCS Jockey Pump and rebuild the pump using parts from the warehouse which was completed on 1/29/17. The pump was tested to demonstrate functionality of the pump on 1/29/17 and the system was returned to service.

05000341/LER-2017-002Fermi19 January 2017
16 March 2017
High Water Level Indications at Low Reactor Pressures Causes Some Functions of High Pressure Coolant Injection System and Reactor Core Isolation Cooling System to be Inoperable
LER 17-002-00 for Fermi 2 Regarding High Water Level Indications at Low Reactor Pressures Causes Some Functions of High Pressure Coolant Injection System and Reactor Core Isolation Cooling System to be Inoperable
On January 19, 2017, a condition was identified that impacted the operability of certain functions associated with the High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems under low reactor pressure conditions. HPCI and RCIC both have automatic and manual actuation functions to inject water into the reactor vessel. HPCI and RCIC also both have an automatic function (i.e. Level 8 trip signal) to prevent injection to the reactor vessel so that water does not reach the steam lines. This Level 8 trip signal comes from instrumentation that is calibrated to be most accurate at normal operating conditions. Under low reactor pressure conditions (i.e. below 600 psig), the high drywell pressure automatic actuation of HPCI and the manual initiation of both HPCI and RCIC are prevented by a Level 8 trip signal such that the affected HPCI and RCIC functions should be considered inoperable per Technical Specifications (TS). This can cause HPCI to also be considered inoperable, which could prevent the fulfillment of a safety function since HPCI is a single train system. Fermi 2 was at a pressure above 600 psig at the time of discovery and, therefore, the condition did not exist. However, a review of past operating conditions identified twelve instances in the past three years where the condition did exist. Based on an engineering analysis, the affected HPCI and RCIC functions are not required to perform a safety function at low reactor pressures; therefore, there was no adverse impact to public health and safety or to plant employees. There were no radiological releases. The cause of the event was an inconsistency between the Fermi 2 TS and the original design and licensing basis of the HPCI and RCIC systems. For corrective actions, Fermi 2 has submitted a license amendment request to clarify the TS.
05000397/LER-2016-005Columbia18 December 2016
15 February 2017
Leak in Minimum Flow Line Makes HPCS and Primary Containment Inoperable
LER 16-005-00 for Columbia Generating Station Regarding Leak in Minimum Flow Line Makes HPCS and Primary Containment Inoperable

On December 18, 2016, during a forced plant outage reported under Licensee Event Report (LER)-2016-004, a leak was identified on the minimum flow line of the High Pressure Core Spray (HPCS) system downstream of the Primary Containment Isolation Valve.

HPCS system had been running on minimum flow after being used to maintain Reactor Pressure Vessel water level. The HPCS line leak was identified during a walk down by Operations personnel after the HPCS pump had been secured. Due to the location of the leak downstream of the Primary Containment Isolation Valve, this leak constituted a breach of Primary Containment. Both HPCS and Primary Containment were declared inoperable.

The cause of the leak was determined to be from a gasketed flange in the HPCS minimum flow piping. Corrective actions included replacing the gasket. Further evaluation is ongoing and this report will be supplemented once complete.

05000373/LER-2017-001Lasalle
LaSalle
16 December 2016
8 February 2017
Reactor Core Isolation Cooling System Inoperable Longer than Allowed by the Technical Specifications due to Low Suction Pressure Trips
LER 17-001-00 for LaSalle County, Unit 1, Regarding Reactor Core Isolation Cooling System Inoperable Longer than Allowed by the Technical Specifications due to Low Suction Pressure Trips

On October 18, 2016, the Unit 1 Reactor Core Isolation Cooling (RCIC) system tripped on low suction pressure during a normal system start following completion of scheduled maintenance activities. The system was restored to operable on October 20, 2016.

A second event involving a Unit 1 RCIC system trip on low pressure suction pressure occurred on November 17, 2016, during the system's quarterly operability surveillance. The system was restored to operable on November 20, 2016. The component failure analysis completed on December 16, 2016, determined the cause of both Unit 1 RCIC system trips was a failure of the electronic governor-remote (EG-R) hydraulic actuator.

The Unit 1 RCIC inoperable period was from the first system trip on October 18, 2016, to when full restoration was completed on November 20, 2016. This time was greater than allowed by Technical Specifications (TS) 3.5.3, "RCIC System," Condition A Completion Time of 14 days. This event is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by the plant's TS. The root cause for the low suction pressure trips was inadequate management of the EG-R preventative maintenance (PM) strategy. Corrective actions included replacement of the EG-R and a plan to implement an appropriate PM strategy for the RCIC EG-R. The safety consequences were minimal since the RCIC system is not credited in the safety analysis, and the credited High Pressure Core Spray (HPCS) system remained available to provide its safety function.

05000298/LER-2016-008Cooper8 November 2016
5 January 2017
Purchase and Installation of Incorrect Actuator Results in a Condition Prohibited by Technical Specifications
LER 16-008-00 for Cooper Nuclear Station Regarding Purchase and Installation of Incorrect Actuator Results in a Condition Prohibited by Technical Specifications

On November 8, 2016 at 11:27 hours, Cooper Nuclear Station (CNS) declared Reactor Core Isolation Cooling (RCIC) inoperable for surveillance testing and entered Technical Specification (TS) Limiting Condition for Operation (LCO) 3.5.3, Condition A. Subsequently at 11:41 hours, RCIC was declared inoperable due to a water leak from the lube oiler cooler lower flange.

During investigation it was determined that valve RCIC-AOV-PCV23, which was replaced during Refueling Outage 29, was full open causing excessive cooling water pressure to the lube oil cooler. This valve regulates cooling water to the lube oil cooler. Initial examination revealed that the actuator was purchased with a closed travel stop instead of the required open travel stop. The work order was revised to fabricate and install an open travel stop. On November 10, 2016, following valve modification, RCIC passed surveillance testing, was declared operable, and TS LCO 3.5.3, Condition A, exited.

The root cause evaluation determined that the correct air operated valve was not purchased because the material master purchase order text and associated drawing didn't detail the requirement of an open travel stop.

To prevent recurrence, CNS will revise the material master purchase order text to state that the valve includes a travel stop in the open direction to limit valve travel. In addition, the drawing will be modified to show the correct travel stop with a note emphasizing the design function of the travel stop.

05000331/LER-2016-002Duane Arnold28 April 2016
6 December 2016
Unplanned RCIC Inoperability Results in Safety System Functional Failure
LER 16-002-00 for Duane Arnold Energy Center Regarding Unplanned RCIC Inoperability Results in Safety Functional Failure
On April 28, 2016, at 1055, while operating at 100% power, with no structures, systems, or components inoperable that contributed to this event, during the performance of Surveillance Test Procedure (STP) 3.3.6.1-28, Reactor Core Isolation Cooling (RCIC) System Steam Line Flow - High Channel Functional Test, the RCIC turbine received an unplanned trip signal and subsequent turbine stop valve closure. The cause of the event was a human performance error associated with verifying the correct installation location of the relay block. The turbine trip resulted in the unplanned inoperability of RCIC, therefore, this condition meets the reporting requirements of 10CFR50.73(a)(2)(v)(D). At 1353 on April 28, 2016, the RCIC turbine was reset and RCIC was declared available. The safety significance of this event was low since all Emergency Core Cooling Systems were operable during the time the RCIC turbine was tripped.
05000298/LER-2016-004Cooper25 September 2016
22 November 2016
Closure of Multiple Main Steam Isolation Valves due to High Flow Signal
LER 16-004-00 for Cooper Nuclear Station Regarding Closure of Multiple Main Steam Isolation Valves due to High Flow Signal

On September 24, 2016, at 20:40 hours, during reactor cooldown for Refueling Outage 29, Cooper Nuclear Station control room operators closed the inboard Main Steam Isolation Valves (MSIV) to minimize steam flow to control the reactor cooldown rate. Reactor pressure was controlled using the Main Steam Line Drains; and the condensate/feed system was available for reactor water level control.

On September 25, 2016, at 01:03 hours, while equalizing pressure across the MSIVs to below 200 psid, a differential pressure of 190 psid was established. Upon opening MS-AO-80A, a Group 1 isolation was immediately received due to a Main Steam Line high flow signal. The control room operators subsequently equalized pressure and successfully opened MS-AO-80A, as well as the remaining MSIVs, at 18:52 hours.

The cause of the event was insufficient procedure guidance exists regarding limitations on opening the MSIVs. To correct this, the applicable procedure has been revised to change the differential pressure limitations for opening MSIVs from 200 psid to 80 psid.

The safety significance of the event is low and did not pose a threat to the health and safety of the public.

05000298/LER-2016-005Cooper1 October 2016Implementation of Enforcement Guidance Memorandum 11-003, Revision 3, Causes Conditions Prohibited by Technical Specifications

During Refueling Outage 29 (RE-29), Cooper Nuclear Station implemented the guidance of Enforcement Guidance Memorandum (EGM) 11-003, Revision 3, "Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel," dated January 15, 2016. Consistent with EGM 11-003, Revision 3, secondary containment operability was not maintained during Operations with a Potential for Draining the Reactor Vessel activities, and Required Action C.2 of Technical Specification (TS) 3.6.4.1 was not completed.

EGM 11-003, Revision 3, was implemented four times during RE-29. These conditions are being reported as conditions prohibited by TS.

Implementation of EGM 11-003, Revision 3, during RE-29 was a planned activity. As such, there were no root cause evaluations of the events. Consistent with the guidance provided in EGM 11-003, Revision 3, Nebraska Public Power District will submit a license amendment request to adopt a Technical Specifications Task Force (TSTF) traveler associated with generic resolution of this issue within 12 months after issuance of the Notice of Availability of the TSTF traveler.

- 005 -00 Cooper Nuclear Station 05000- 298 2016 Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

PLANT STATUS

Cooper Nuclear Station (CNS) was in Mode 5, Refueling, at 0 percent power, at the time of the events.

BACKGROUND

On January 15, 2016, the Nuclear Regulatory Commission issued Enforcement Guidance Memorandum (EGM) 11-003, Revision 3, "Dispositioning Boiling Water Reactor Licensee Noncompliance with Technical Specification Containment Requirements During Operations with a Potential for Draining the Reactor Vessel." EGM 11-003, Revision 3, provides generic enforcement discretion to allow implementation of specific interim actions as an alternative to full compliance with plant technical specifications related to Secondary Containment operability during Mode 5 Operations with a Potential for Draining the Reactor Vessel (OPDRV) activities. To ensure compliance with interim actions specified in the EGM, CNS added guidance to plant Procedure 0.50.5, "Outage Shutdown Safety.

EVENT DESCRIPTION

During Refueling Outage 29 (RE-29), CNS implemented the guidance of EGM 11-003, Revision 3, four times. Consistent with EGM 11-003, Revision 3, Secondary Containment operability was not maintained during OPDRV activities, and Required Action C.2 of Technical Specification (TS) 3.6.4.1 was not completed.

The following provides the dates which EGM 11-003 was implemented:

1. On October 1 and 2, 2016, the EGM was utilized to allow work on Reactor Recirculation Pump A (RR-P-A) and RR-P-B without the jet pump plugs installed while performing Surveillance Procedure 6.1SGT.401, "SGT A Fan Capacity Test, SGT B Cooling Flow Test and Check Valve 1ST (Div 1).

2. From October 2-5, 2016, the EGM was utilized to allow work on RR-P-A, RR-P-B, Control Rod Drive (CRD) withdrawal/bypass operations and Hydraulic Control Unit (HCU) 42-31 during repairs to Main Steam Air Operated Valve 86B.

3. On October 6, 2016, the EGM was utilized to work on RR-P-A and RR-P-B without the jet pump plugs installed while draining Reactor Core Isolation Cooling 12 Relief Valve and flushing Main Steam Isolation Valves (MSIV).

4. From October 19-25, 2016, the EGM was utilized to work on RR-P-A. While using the EGM, work was also performed on CRD-V-113s (freeze seal), CRD Drive Venting, and CRD-V-105 (10-43) (freeze seal). These OPDRVs were in progress while Secondary Containment was inoperable for MSIV 86A and 86B repair, Reactor Building (RB) personnel airlock seal repair, shift of RB ventilation, Service Water Valve 531 draining and Residual Heat Removal Valve 57/67 draining.

Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

05000- 298 Cooper Nuclear Station 2016 - 005 - 00

3. LER NUMBER

BASIS FOR REPORT

These events are reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as conditions prohibited by CNS TS 3.6.4.1, which prohibits performing activities identified as OPDRVs in MODE 5 while secondary containment is inoperable.

SAFETY SIGNIFICANCE

As discussed in EGM 11-003, Revision 3, enforcement discretion is appropriate because the issues have low safety significance since licensees must implement compensatory measures to provide an adequate level of safety when using the discretion. To ensure compliance with the interim actions specified in the EGM, CNS added guidance to plant Procedure 0.50.5. This procedure was implemented for the OPDRV activities during which Secondary Containment was not operable.

CAUSE

Implementation of EGM 11-003, Revision 3, during RE-29 was a planned activity. As such, there were no root cause evaluations of the events.

CORRECTIVE ACTIONS

CNS will submit a license amendment request to adopt the Technical Specifications Task Force (TSTF) traveler associated with generic resolution of this issue, within 12 months after issuance of the Notice of Availability of the TSTF traveler.

PREVIOUS EVENTS

During RE-28, CNS implemented EGM 11-003, Revision 2, seven times. These events were reported under one License Event Report, LER 2014-004-00.

05000260/LER-2016-002Browns Ferry19 March 2016
13 September 2016
High Pressure Coolant Injection System Failure Due To Stuck Contactor
LER 16-002-00 for Browns Ferry Nuclear Plant, Unit 2, Regarding High Pressure Coolant Injection System Failure Due To Stuck Contactor

On March 19, 2016, at approximately 1024 Central Daylight Time (CDT), the Unit 2 High Pressure Coolant Injection System (HPCI) Steam Admission Valve failed to stroke due to a stuck contactor in the valve motor breaker. This rendered the Unit 2 HPCI inoperable, resulting in a Safety System Functional Failure; however the system had previously been declared inoperable for maintenance and the Unit 2 Reactor Core Isolation Cooling System had been verified as operable in accordance with Technical Specifications Limiting Conditions for Operation 3.5.1. On March 20, 2016, at approximately 1103 CDT, Maintenance personnel commenced work to repair the Unit 2 HPCI steam admission valve motor breaker. On March 21, 2016, at approximately 0245 CDT, Unit 2 HPCI was declared operable following completion of all required PMTS.

The cause of the stuck contactor was accelerated cyclic fatigue due to overheating of the motor starter during packing consolidation and MOVATS testing. Corrective actions were to replace the stuck contactor, to clean contactors in similar HPCI valve motor breakers for Units 1 and 3, to determine an allowable maximum number of valve cycles within a given time period , and to revise plant procedures based on the determined cycle limit in order to prevent contactors from sticking due to accelerated cyclic fatigue.

Subsequent review determined the identified condition to be reportable.

05000260/LER-2016-001Browns Ferry16 August 2016High Pressure Coolant Injection Safety System Functional Failure due to a Blown Fuse and a Failed Relay
LER 16-001-00 for Browns Ferry, Unit 2, Regarding High Pressure Coolant Injection Safety System Functional Failure Due to a Blown Fuse and a Failed Relay

On June 17, 2016, while performing a High Pressure Coolant Injection (HPCI) Time Delay Relay Calibration surveillance, an abnormal indication of no voltage to the Time Delay Relay coil was received. The electricians backed out of the procedure and informed Operations. Later that day, upon performing procedure step 7.3(17), fuse BFN-2-FU2-073-0039B cleared and a HPCI Logic Power Failure alarm was received. The loss of logic power rendered Unit 2 HPCI system inoperable. The most likely cause of the blown fuse was an equipment ground induced by the TM200 timer used in the calibration procedure for timing pick-up of the time delay relays. While the HPCI Time Delay Relay calibration was being performed, there was already a known ground on Battery Board 2. The corrective action is to revise the calibration procedures to reconfigure the setup of the test equipment to reduce the probability and consequences of a ground induced by the test equipment.

During troubleshooting of the blown fuse, relay 2-RLY-073-23A-K43 was replaced. It was later identified during bench testing that this relay was faulty as the result of normal breakdown of the coil insulation over time. This breakdown was attributed to end-of-life failure. The immediate corrective action to address the relay failure was replacement of the relay. To address the end of life failure of this relay, a preventative maintenance (PM) task was created to replace this relay every 16 years.

05000296/LER-2016-006Browns Ferry8 June 2016
5 August 2016
1 OF 8
LER 16-006-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding High Pressure Coolant Injection System Found to be Inoperable During Testing

During a surveillance test on June 8, 2016, the BFN, Unit 3, High Pressure Coolant Injection (HPCI) Turbine Stop Valve Mechanical Trip Valve behaved erratically upon turbine start. Troubleshooting and maintenance on the valve led to discovery of a condition that could have resulted in the HPCI system being unable to perform its required safety function in a Mode where HPCI Operability was required.

The inoperability was caused by the HPCI Turbine Stop Valve Mechanical Trip Valve's Reset Spring, which was deformed and weakened from years of continuous compression. The spring was replaced and the system was returned to service on June 10, 2016.

Corrective actions to prevent recurrence include revising preventive maintenance procedures to specify replacement of the Trip Tappet, Piston, and Reset Spring on a defined periodicity. Additionally, procedures will be revised to require testing the as-left breakaway force a minimum of three times to ensure repeatability.

Preventative maintenance procedures will also be revised to clarify that lift force checks after spring compression adjustments shall be conducted with the auxiliary oil pump running.

05000324/LER-2016-002Brunswick2 May 2016
5 July 2016
High Pressure Coolant Injection System Inoperable due to Failed Relay Coil
LER 16-002-00 for Brunswick Steam Electric Plant (BSEP), Units 1 and 2, Regarding Emergency Diesel Generator 3 Inoperable Due to Failure to Auto-Start

On July 5, 2016, at 1640 Eastern Daylight Time (EDT), the Unit 2 High Pressure Coolant Injection (HPCI) system was declared inoperable due to apparent failure of the HPCI Auxiliary Oil Pump. The HPCI Auxiliary Oil Pump provides hydraulic pressure required to open the HPCI Turbine Stop Valve and the HPCI Turbine Control Valve during initial HPCI startup. Failure of the HPCI Auxiliary Oil Pump prevents the HPCI system from performing its safety function.

This condition is being reported in accordance with 10 CFR 50.73(a)(2)(v)(D), as an event or condition that could have prevented the fulfillment of the safety function of a system that is needed to mitigate the consequences of an accident.

The HPCI system inoperability was due to loss of control power for the Auxiliary Oil Pump. The loss of control power was caused by a failed motor overload alarm relay coil; which caused current flow in excess of the control power fuse rating. The HPCI system was restored on July 6, 2016, at 1050 EDT. The alarm relay coil failure was age related.

The corrective actions include creation of preventive maintenance tasks to replace the Unit 1 and 2 HPCI motor overload alarm relay coils on an appropriate frequency.

05000298/LER-2016-002Cooper26 April 2016
27 June 2016
De-Energized High Pressure Coolant Injection Auxiliary Lube Oil Pump Caused By Light Bulb Failure Results in Loss of Safety Function
LER 16-002-00 for Cooper Regarding De-Energized High Pressure Coolant Injection Auxiliary Lube Oil Pump Caused By Light Bulb Failure Results in Loss of Safety Function

On April 26, 2016, it was noted that the green off light for High Pressure Coolant Injection (HPCI) auxiliary lube oil pump (ALOP) in the Control Room, was not illuminated. A non-licensed operator was dispatched to the HPCI ALOP starter and reported the green bulb appeared to have shattered in the socket. HPCI was declared inoperable at 1754 Central Daylight Time (CDT) resulting in entry into Technical Specifications Limiting Condition of Operation 3.5.1, Condition C, HPCI System Inoperable.

Investigation found the 125 volts direct current fuse open circuited and the local indication green light and socket were damaged. The cause of the failure was determined to be a lack of engineering knowledge which led to a design change in 1984 in the HPCI ALOP starter circuitry that diminished the robustness of the circuit with respect to a specific failure modality; direct short circuiting within the indication bulb itself. The HPCI system was restored to operable status on April 28, 2016, at 1245 CDT.

This event is being reported as a loss of safety function due to HPCI being a single-train safety system.

The potential safety consequences of this event were minimal due to the limited duration the condition existed and the redundant/diverse core cooling systems which remained operable.

3. LER NUMBER 2. DOCKET NUMBER 05000- 298 Cooper Nuclear Station 2016 - 002 - 00

05000440/LER-2016-002Perry8 February 2016
8 April 2016
Manual Reactor SCRAM Due to Spurious Opening of Safety Relief Valves
LER 16-002-00 for Perry Regarding Manual Reactor SCRAM Due to Spurious Opening of Safety Relief Valve

On February 8, 2016, at 1503 hours, control room operators initiated a manual reactor protection system (RPS) actuation in response to rising temperature in the suppression pool. All control rods full inserted. Prior to the RPS actuation the plant was in mode 1 at approximately 96 percent rated thermal power. At 1500 hours, multiple safety relief valves (SRVs) partially opened due to an invalid reactor pressure vessel (RPV) pressure signal. Control room indications showed two SRVs remained open resulting in a suppression pool temperature rise. Suppression pool cooling was initiated and a plant cooldown to Mode 4 was initiated.

The direct cause of the event was a momentary pressure perturbation limited to the RPV B reference leg that caused the connected transmitters to sense RPV pressure and level changes that resulted in SRV actuation. Corrective actions include revision to plant procedures for operation of the RPV reference legs and associated purge panels, and changes to the time constants for the affected RPV transmitters.

The safety significance of this event is considered to be very small. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event or condition that resulted in a manual actuation of the RPS.

05000325/LER-2016-001Brunswick7 February 2016
6 April 2016
Electriqal Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
LER 16-001-00 for Brunswick, Unit 1, Regarding Electrical Bus Fault Results in Lockout of Startup Auxiliary Transformer and Loss of Offsite Power
On February 7, 2016, at 1312 Eastern Standard Time (EST), Unit 1 was in Mode 1 (i.e., Run) at 88 percent of rated power in end-of-cycle coastdown. At that time, an electrical fault occurred on a balance of plant 4160-volt bus, resulting in a lockout of the Startup Auxiliary Transformer (SAT) and a loss of both Reactor Recirculation pumps. Licensed personnel inserted a manual scram per procedure. Emergency Diesel Generators supplied emergency electrical busses until offsite power was restored at 1628 EST. The loss of power and reactor water level changes resulted in automatic closures of various Primary Containment Isolation Valves (PCIVs). The electrical fault resulted in an electrical explosion; therefore, an Alert was declared at 1326 EDT. The immediate cause of this event was a fault in a non-segregated electrical bus connected to the SAT. The root causes were insufficient detail in applicable maintenance instructions for inspecting the non-segregated bus housing and inadequate instructions for terminating electrical cables in a circuit breaker cubicle. Corrective actions include repairing equipment damaged by the electrical fault and revising the procedures and work instructions.