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05000318/LER-2022-001, Forwards LER 2022-001-00 for Calvert Cliffs Nuclear Power Plant, Unit 2, Automatic Reactor Trip Due to High Reactor Coolant System PressureCalvert Cliffs3 March 2022Forwards LER 2022-001-00 for Calvert Cliffs Nuclear Power Plant, Unit 2, Automatic Reactor Trip Due to High Reactor Coolant System Pressure
05000281/LER-2020-001, Cancellation of LER 2020-001-00 for Surry Power Station Unit 2 Re Loss of Containment Cooling Affecting Containment Partial Pressure IndicationSurry6 November 2020Cancellation of LER 2020-001-00 for Surry Power Station Unit 2 Re Loss of Containment Cooling Affecting Containment Partial Pressure Indication
05000391/LER-2017-005Watts Bar
Watts Bar Nuclear Plant. Unit 2
25 January 2018Unplanned Emergency Core Cooling System Injection into the Reactor Coolant System due to Personnel Error
LER 17-005-00 for Watts Bar, Unit 2, Regarding Unplanned Emergency Core Cooling System Injection into the Reactor Coolant System due to Personnel Error

On November 26, 2017. at 1225 Eastern Standard Time (EST), the Watts Bar Nuclear Plant (WBN) Unit 2 experienced an unplanned Emergency Core Cooling System (ECCS) discharge to the Unit 2 Reactor Coolant System (RCS) while de-pressurized. in Mode 5. with the Pressurizer vented to the Pressurizer Relief Tank.

ECCS injection via the Boron Injection flow path occurred during planned Safety Injection system Engineered Safety Features Actuation System (ESFAS) testing. The Boron Injection flow path should have been isolated and should not have resulted in any injection flow to the Unit 2 RCS. The condition was promptly corrected by operator actions based on observed plant conditions.

The cause of this event is that an Operator improperly used a Caution Order to determine the configuration of the breaker for the Boron Injection Tank outlet valve. Correct Component Verification was not utilized as required. and the current position of the breaker in the field was not validated to support testing.

Corrective actions for this event include revising procedures to ensure the breakers associated with the boron injection flow path will be tagged open during ESFAS testing and that lessons learned related to this event are communicated to operating crews. An evaluation on the use of Caution Orders for off normal equipment positions will be performed .

NRC FORM 330604-2O'

05000263/LER-2017-006Monticello14 November 2017
12 January 2018
Loss of Reactor Protection System Scram Function During Main Steam Isolation Valve and Turbine Stop Valve Channel Functional Tests due to Use of a Test Fixture
LER 17-006-00 for Monticello Regarding Loss of Reactor Protection System Scram Function During Main Steam Isolation Valve and Turbine Stop Valve Channel Functional Tests Due to Use of a Test Fixture

On November 14, 2017, it was identified that the use of the Reactor Protection System (RPS) test fixture described in some operations procedures would result in the loss of two RPS reactor Scram functions. Technical Specification 3.3.1.1 requires that RPS Instrumentation for Table 3.3.1.1-1 Function 5, Main Steam Isolation Valve-Closure and Function 8, Turbine Stop Valve-Closure, remain operable. It was concluded that a closure of three of four Main Steam Lines or Turbine Stop Valves would not necessarily have resulted in a full Scram during testing depending on the combination of closed valves occurring during the bypass condition. Operations procedures were revised to incorporate the use of the test fixture in December, 2008 for the Turbine Stop Valve Closure Scram Test Procedure and February, 2009 for the Main Steam Isolation Valve Closure Scram Test Procedure. The operations procedures were inappropriately revised to allow use of the test fixture on all RPS functions to prevent a half Scram.

The operations procedures were quarantined until revisions were issued in December, 2017 that removed use of the test fixture.

05000272/LER-2017-001Salem9 November 2017
8 January 2018
Containment Integrity Inoperable for Longer than Allowed by Technical Specifications
LER 17-001-00 for Salem Generating Station, Unit 1 Regarding Containment Integrity Inoperable for Longer than Allowed by Technical Specifications

On November 9, 2017 at approximately 2300, Salem Unit 1 was operating in MODE 3 when operators found steam leaking into the mechanical penetration area outside containment. Operators entered S1.0P-AB.STM-0001, Excessive Steam Flow, and dispatched operators to locate and isolate the leak.

Operators determined the steam was from the 14 steam generator through normally closed valves 14GB47 and 14GB48 steam generator blowdown (WI) line nitrogen supply valves. The steam leak was isolated at 2314 when operators closed normally open manual valve 14GB3.

This report is made per 10CFR50.73(a)(2)(i)(B), Any operation or condition which was prohibited by the plants Technical Specifications.

This was caused by human performance. Procedures will be revised to assure containment integrity exceptions are tracked and open valves are closed while sampling during the sparging process.

NRC FORM 3116 (04-20171

05000364/LER-2017-004Farley
Joseph M. Farley Nuclear Plant. Unit 2
22 December 2017I OF 3
LER 17-004-00 for Joseph M. Farley Nuclear Plant, Unit 2 Regarding Turbine-Driven Auxiliary Feedwater Pump Steam Admission Valve Air Leak Resulted in a Condition Prohibited by Technical Specifications

On October 31, 2017, while in Mode 6 and at 0% power level, the Turbine-Driven Auxiliary Feedwater (TDAFW) pump B-Train steam admission valve from the 2C Steam Generator failed to meet Technical Specification ('I'S) Surveillance Requirement (SR) 3.7.5,5. This SR requires that the valve's associated air accumulator provide sufficient air to ensure operation of the TDAFW pump during a loss of power or other failure of the normal air supply.

During the performance of a flow scan analysis it was identified that the air-operated actuator piston was leaking by the actuator ' o-ring. Although the steam admission valve would stroke open, the 2-hour acceptance criteria could not be met. It is likely that the steam admission valve was inoperable longer than allowed by the Required Action Statement (7 days) following the spring 2016 refueling outage when it passed its last associated surveillance. Therefore, this condition is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

Corrective actions included actuator repair during the outage and further evaluating the preventive maintenance frequency.

NRC FORM 386 (04.2017)

05000286/LER-2017-004Indian Point3 November 2017
20 December 2017
Reactor Trip Due to Main Generator Loss of Field
LER 17-004-00 for Indian Point Unit 3, Regarding Reactor Trip Due to Main Generator Loss of Field

On November 3, 2017, at 2022 hours, with reactor power at 100 percent, Indian Point Unit 3 experienced an automatic reactor trip on a turbine trip, which was in response to a main generator trip. The main generator trip was initiated by actuation of the Generator Protection System due to a main generator loss of field.

All control rods fully inserted and all required safety systems functioned properly. The plant was stabilized in hot standby with decay heat being removed by the main condenser. The Auxiliary Feedwater System (AFWS) automatically started as expected on steam generator low level to provide feedwater flow to the steam generators. The plant was stabilized in hot standby with decay heat being removed by the main condenser. The direct cause of the loss of main generator field was a failed Thyristor Firing Module drawer which affected proper operation of the redundant Thyristor Firing Module drawer. The root cause was determined to be that the Automatic Voltage Regulator (AVR) Firing Module power supplies have a latent design vulnerability where shared common output nodes are not isolated after a failure. A plant modification is proposed that will eliminate the condition by electrically isolating the AVR Firing Module power supplies upon failure.

This event had no effect on the public health and safety. The event was reported to the Nuclear Regulatory Commission (NRC) on November 3, 2017 under 10 CFR 50.72(b)(2)(iv)(B) and 50.72(b)(3)(iv)(A) as an event that resulted in the automatic actuation of the Reactor Protection System when the reactor is critical and a valid actuation of the AFWS.

05000364/LER-2017-003Farley20 December 2017Pressurizer Safety Valve Lift Pressure Outside of Technical Specifications Limits
LER 17-003-00 for Joseph M. Farley, Unit 2, Regarding Pressurizer Safety Valve Lift Pressure Outside of Technical Specifications Limits

On October 31, 2017, while in Mode 6 at 00 0 power level, it was discovered that a Unit 2 pressurizer safety valve (PSV). which had been removed during the October 2017 refueling outage (2R25) and shipped offsite for testing, failed its as-found lift pressure test. The PSV lifted below the Technical Specification (TS) 3.4.10 allowable lift setting value. Setpoint drift of the PSV is the most likely cause of the failure.

It is likely that the PSV was outside of the TS limits longer than allowed by the Required Action Statement (15 minutes) during the previous operating cycle in all applicable modes of operation. Therefore, this condition is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

The PSV was replaced during the October 2017 refueling outage.

05000278/LER-2017-001Peach Bottom23 October 2017
20 December 2017
Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line
LER 17-001-00 for Peach Bottom Atomic Power Station (PBAPS), Unit 3 Regarding Reactor Pressure Boundary Leakage Due to Weld Failure in One-Inch Diameter Instrument Line

On 10/23/2017, during a walkdown of containment at the start of the Unit 3 refueling outage, a leak was identified in a socket weld for a 1-inch diameter instrument line. The line is connected to discharge piping for the 'B' recirculation pump and is part of the reactor coolant system pressure boundary. Because the leak was misting, the leakage rate could not be quantified. However, the reactor coolant system unidentified leakage prior to plant shutdown was 0.18 gpm. RCS pressure boundary leakage while in Mode 1 is a violation of Technical Specification 3.4.4 and is a reportable condition.

The cause of the event was a lack of fusion defect in the weld when it was done in the late 1980's. Normal vibration of the line since it was installed resulted in the crack initiating at the weld defect and propagating to the surface. The section of pipe and associated fitting were replaced, along with welds in similar sections of piping. There were no actual safety consequences as a result of this event.

05000364/LER-2017-002Farley19 December 2017Main Steam Safety Valve Lift Pressure Outside of Technical Specifications Limits
LER 17-002-00 for Joseph M. Farley, Unit 2, Regarding Main Steam Safety Valve Lift Pressure Outside of Technical Specifications Limits

On November 1, 2017, while in Mode 6 and at 0% power level, one of the C Loop Main Steam Safety Valves (MSSV) as-found lift pressure did not meet the acceptance criteria of +/- 3% of the setpoint (1129 psig) as required by Technical Specifications (TS) Surveillance Requirement (SR) 3.7.1.1. The MSSV lifted at 1171 psig which is 9 psig outside of its acceptance range of 1096 to 1162 psig and 3.72°o above its setpoint. The apparent cause of exceeding the MSSV upper acceptance limit is degradation of the valve spring and/or valve spindle compression screw. The as-found settings remained within analytical bounds; therefore, operation of the facility in this condition had no impact on the health and safety of the public.

TS Limiting Condition for Operation (LCO) 3.7.1, IvISSVs, requires five MSSVs per steam generator to be operable in Modes 1, 2, and 3. Since the failure affected the lift pressure over a period of time, it is assumed that the C Loop MSSV was inoperable for a time greater than allowed by TS. Therefore, this occurrence is considered reportable per 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

The C Loop MSSV was replaced on November 5, 2017, while in Mode 5.

05000266/LER-2017-002Point Beach29 October 2017
13 December 2017
Operation or Condition Prohibited by Technica Specifications
LER 17-002-00 for Point Beach Nuclear Plant, Unit 1, Regarding Operation or Condition Prohibited by Technical Specifications

On October 29, 2017, Unit 1 entered MODE 3 from MODE 4 without satisfying all of Technical Specification 3.7.5, Auxiliary Feedwater (AFW) Limiting Conditions for Operation (LCO) as required by LCO Applicability 3.0.4 for the Turbine Driven Auxiliary Feedwater (TDAFW) pump system.

LCO Applicability 3.0.4 does not permit entry into a MODE of applicability when an LCO is not met, unless the associated actions to be entered permit continued operation in the MODE for an unlimited time or after performance of an acceptable risk assessment and the appropriate risk management actions have been established. After entering MODE 3, it was discovered that components were not operable, contrary to LCO 3.0.4.

This event is being reported pursuant to 10 CFR 50.73(a)(2)(i)(B), for an operation or condition prohibited by Technical Specifications.

05000266/LER-2017-003Point Beach30 October 2017
13 December 2017
Degraded Condition
LER 17-003-00 for Point Beach Nuclear Plant, Unit 1, Regarding Degraded Condition

On October 30, 2017, with Unit 1 in MODE 3 for refueling activities, a boric acid indication downstream of 1CV-309B, 1P-1B Reactor Coolant Pump (RCP) Labyrinth Seal 1 DPT-124 Upper Root Valve was identified as a through-wall flaw. The flaw location on the root valve to differential pressure transmitter (DPT) instrument tubing welded joint was within the reactor coolant system (RCS) pressure boundary.

This event is being reported pursuant to 10 CFR 50.73(a)(2)(ii)(A) for material defects in the primary coolant system that were not acceptable in accordance with ASME Section XI.

05000306/LER-2017-002Prairie Island16 October 2017
11 December 2017
Reactor Coolant System Shutdown Communication Live Vent Through Wall Defect
LER 17-002-00 for Prairie Island, Unit 2, Regarding Reactor Coolant System Shutdown Communication Live Vent Through Wall Defect

On October 16, 2017, with Unit 2 shutdown for a refueling outage, investigation into a boric acid indication identified a through wall leak at the socket weld that joins a 3/4 inch line to Loop A Reactor Coolant System (RCS)(AB) shutdown communication line valve 2RC-8-37 )(VTV). The leak was isolated by closed valves that would have limited primary coolant leakage to within the capacity of the charging system when the reactor coolant system was pressurized. The quantity of dry boric acid at the location was small (estimated at 1/2 teaspoon in volume). This failure constituted a welding or material defect in the primary coolant system that was not found acceptable under ASME Section Xl and an event or condition prohibited by Technical Specifications.

The cause of the leakage was determined to be stress corrosion cracking. Valve 2RC-8-37 was replaced. In addition, Prairie Island Nuclear Generating Plant intends to perform phased array ultrasonic inspections of socket welds on similar Class 1 piping containing stagnant water during future refueling outages.

05000395/LER-2017-003Summer
Vc Summer - Unit 1
28 August 2017
26 October 2017
FAILED LIGHTNING ARRESTER ON MAIN TRANSFORMER CAUSES REACTOR TRIP
LER 17-003-00 For Virgil C. Summer Nuclear Station, Unit 1, Regarding Failed Lightning Arrester On Main Transformer Causes Reactor Trip

On August 28, 2017, at 0837, VCSNS Unit 1 automatically tripped due to a turbine trip. The turbine trip was caused by the Main Generator Differential Lockout due to a fault on the center phase, 230 kV lightning arrester, on the Main Transformer (XTF-1).

The plant trip response was normal. All control rods fully inserted. Balance of Plant (BOP) buses automatically transferred to their alternate power source, Emergency Auxiliary Transformers (XTF-31/32). Both Motor Driven (MD) Emergency Feedwater (EF) pumps and the Turbine Driven EF Pump started as designed.

The cause of this event was the failure of the center phase lightning arrester on XTF-1. The failed arrester, along with the other two lightning arresters that were in service on XTF-1 during the reactor trip, was replaced. The lightning arresters were sent to an independent lab, NEETRAC - Georgia Tech, for testing and evaluation.

The examination results indicate that the most probable cause of the arrester failure was an internal flashover of the metal oxide varistor blocks. The cause of the internal flashover is likely moisture ingress from the upper end seal.

05000390/LER-2017-012Watts Bar23 October 2017Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications
LER 17-012-00 for Watts Bar, Unit 1, Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications

On August 23. 2017. Watts Bar Nuclear Plant (WBN) identified that procedures 1-E-1 and 2-E-1, Loss of Reactor or Secondary Coolant, contained steps to manually open 1-FCV-67-458 in the event of a Train A or B power failure.

Opening 1-FCV-67-458 would result in the crosstie of Essential Raw Cooling Water (ERCW) Headers 2A and 1B, which would lead to providing flow to equipment not operating due to the loss of a train of power. On October 6. 2017.

it was determined that for certain time periods, if a design basis accident had occurred on Unit 2 with a loss of offsite power concurrent with a train failure and with 1-FCV-67-458 opened, inadequate ERCW flow would have been available to remove decay heat after transfer to cold leg recirculation. This condition only affected operability of ERCW Train A. This is reportable as a condition prohibited by Technical Specification 3.7.8.

The issue associated with this incorrect procedural step to cross-tie the ERCW trains in 1-E-1 and 2-E-1 was addressed as part of actions to resolve an ERCW design and procedure issue documented in Licensee Event Report (LER) 390-2017-009. This report, while related, identifies an issue that was not addressed in the prior LER. The cause was determined to be the incorrect application of a cross tie requirement associated with 10 CFR 50 Appendix R. Corrective action will be to include engineering in the review of procedures affected by complex design changes.

NRC FORM 355 ;:;4-217' APPROVED BY OMB: NO. 3150-0104 EXPIRES: 03/31/2020 comments regarding burden estimate to the Information Services Branch (T-2 F43), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001. or by e-mail to NEOB-10202. (3150-0104), Office of Management and Budget. Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number. the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

05000280/LER-2017-001Surry9 August 2017
6 October 2017
1 OF 3
LER 17-001-00 for Surry, Unit 1, Regarding Shutdown due to an Unisolable Leak in Reactor Coolant Pressure Boundary

On August 6, 2017, with Unit 1 at 100% power, a Reactor Coolant System (RCS) leak rate calculation determined the unidentified leak rate increased by 0.08 .gallons per minute. On August 8, a leak was obServed at an RCS hot leg.sample system valve,- and Unit 1 power level was reduced to investigate leakage indications. The. root isolation valve for the sample system valve was closed; however, leakage could not be verified as completely isolated. Further evaluation determined the leak to be through wall at the inlet of the sample system valve. Based upon the source of the leak and possible continued leakage, a Technical Specification shutdown clock was entered on August 9, at 13:38 hours. At 16:37 hours, Unit 1 was placed in Hot Shutdown.

The cause of the event was the RCS pressure boundary leakage at the tubing/socket weld area of the hot leg sample system valve. With the unit in Hot Shutdown, the leak was isolated and repaired, and Unit 1 was returned to power operation on August 11, 2017. An apparent cause evaluation is being conducted. The event was reported as a plant shutdown required by Technical Specifications pursuant to 10 CFR 50.72(b)(2)(i) and degraded condition pursuant to 10 CFR 50.72(b)(3)(ii)(A). This report is being provided pursuant to 10 CFR 50.73(a)(2)(i)(A) and 10 CFR 50.73(a)(2)(ii)(A).

05000387/LER-2017-005Susquehanna8 June 2017
4 October 2017
Automatic Reactor Protection System Trip on High Neutron Flux
LER 17-005-01 for Susquehanna, Unit 1 Regarding Automatic Reactor Protection System Trip on High Neutron Flux

On June 8, 2017 at 1527 hours, the reactor automatically scrammed due to a loss of Main Turbine- Electro-Hydraulic Control (EHC) logic power causing a high neutron flux, Reactor Protection System (RPS) trip. The safety systems operated as expected. Secondary Containment differential pressure lowered to 0" WG due to a trip of the normal operation of the Reactor Building Ventilation system. The differential pressure was restored by the initiation of Standby Gas Treatment System.

The scram was caused directly by a DC+ (direct current, positive) test lead (Maxi Grabber) that inadvertently contacted with the grounding screw, causing a short and momentary loss of EHC logic power.

Immediate action was taken to validate that there was no damage to the +30 VDC (volts DC) EHC logic.

The root cause for this event is an insufficient focus on the High Risk Activity of adjusting the EHC power supply, and inadequate risk mitigating actions for that activity.

The condition is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an automatic actuation of the RPS, including reactor scram. Although no safety system functional failure occurred, this event is also reportable pursuant to 10CFR 50.73(a)(2)(v)(C) as a condition that could have prevented fulfillment of a safety function. There were no actual, or potential consequences to the health and safety of the public as a result of this event.

I

05000323/LER-2017-001Diablo Canyon3 October 2017Relief Valve Leakage Resulting in Inoperable Pressurizer Power Operated Relief Valve
LER 17-001-00 for Diablo Canyon, Unit 2, Regarding Relief Valve Leakage Resulting in Inoperable Pressurizer Power Operated Relief Valve

During an investigation of a nitrogen leak inside the Unit 2 containment, Nitrogen Accumulator Relief Valve (RV) RV-355 was found to be leaking. The leak caused the pressure in the back up nitrogen accumulator supply to Power Operated Relief Valve (PORV) PCV-455C to decrease to a level that made the PORV inoperable. Based on a review of the ti-end data for nitrogen usage in the containment, it is conservatively assumed that RV-355 had been degraded since December 1, 2016, rendering the PORV inoperable for longer than permitted by Technical Specifications.

The presumptive cause was inadequate instructions provided in plant procedures for placing a new nitrogen bottle in service. These instructions did not provide a sequence that assures system pressure transients are mitigated. This may have caused excessive pressure excursions resulting in multiple lifts of RV-355 which resulted in damage to the RV 0-ring seat and a nitrogen leak path.

Corrective actions include replacing RV-355 and revising procedures to provide instructions on placing nitrogen supply bottles in service to maintain back pressure and minimize pressure transients on the nitrogen system.

This event did not affect the health and safety of the public.

05000382/LER-2017-002Waterford
Waterford Steam Electric Station, Unit 3
17 July 2017
18 September 2017
Automatic Reactor Scram due to the Failure of Fast Bus Transfer Relays to Automatically Transfer Station Loads to Off- Site Power on a Main Generator Trip
LER 17-002-00 for Waterford, Unit 3, Regarding Automatic Reactor Scram due to the Failure of Fast Bus Transfer Relays to Automatically Transfer Station Loads to Off-Site Power on a Main Generator Trip

On July 17, 2017, at 1606 CDT, Waterford 3 experienced an automatic reactor scram due to a loss of forced circulation, which was the result of a loss of off-site power to the safety and non-safety electrical busses. Prior to the scram, plant operators manually tripped the main turbine and generator due to overheating of the isophase bus duct due to the failure of a shunt assembly connection in the duct to Main Transformer 'B'. The automatic electrical bus transfer did not occur due to relay failures in the fast dead bus transfer system. Both 'A' and 'B' Emergency Diesel Generators started and loaded as designed to re-energize the 'A' and 'B' safety busses. The loss of off-site power caused a loss of both Main Feedwater pumps, resulting in an automatic actuation of the Emergency Feedwater system.

The Root Cause of this event was the design change procedure used for modifications to the fast dead bus transfer circuitry did not include guidance to detect the susceptibility of the relays to DC coil inductive kick. The faulty relays in the fast bus transfer circuit were replaced prior to plant startup.

An Unusual Event was declared at 1617 CDT due to loss of off-site power to safety buses for >15 minutes.

All required safety-related equipment responded as expected during this event.

05000311/LER-2015-002Salem5 August 2015
7 September 2017
P.O. Box 236, Hancocks Bridge, NJ 08038-0236
PSEG
Nadea, II,C
OCT 0 2 2015
LR-N15-0205 10 CFR 50.73
U.S. Nuclear Regulatory Commission
ATTN: Document Control Desk
Washington, DC 20555-0001
LER 311/2015-002-00
Salem Nuclear Generating Station Unit 2
Renewed Facility Operating License No. DPR-75
NRC Docket No. 50-311
SUBJECT: Licensee Event Report 311/2015-002-00
In accordance with the requirements of 10 CFR 50.73(a)(2)(iv), PSEG Nuclear LLC is
submitting the enclosed Licensee Event Report (LER) Number 2015-002-00, "Reactor
Trip Due to Loss of 4kV Non-Vital Group Bus."
There are no regulatory commitments contained in this letter.
If you have any questions or require additional information, please contact
Mr. David Lafleur of Salem Regulatory Assurance at 856-339-1754.
Sincerely,
John F. Perry
Site Vice President — alem
Attachment
OCT 0 2 2015
10 CFR 50.73
Page 2
LR-N15-0205
CC
Mr. D. Dorman, Administrator— Region 1, NRC
Mr. T. Wengert, Licensing Project Manager (acting) — Salem, NRC
Mr. P. Finney, USNRC Senior Resident Inspector, Salem (X24)
Mr. P. Mulligan, Manager IV, NJBNE
Mr. R. Braun, President and Chief Nuclear Officer — Nuclear
Mr. T. Cachaza, Salem Commitment Tracking Coordinator
Mr. L. Marabella, Corporate Commitment Tracking Coordinator
Mr. D. Lafleur, Salem Regulatory Assurance
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION
01-2014)
t, , .1

'., LICENSEE EVENT REPORT (LER)
'S ree Page 2 or required number of
digits/characters for each block)
APPROVED BY OMB: NO. 3150-0104 EXPIRES: 0113112017
Estimated burden per response to comply with this mandatory collection request: 80 hours.
Reported lessons learned are Incorporated Into the licensing process and fed back to Industry.
Send comments regarding burden estimate to the FOIA, Privacy and Information Collections
Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by
Internet e-mall to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and
Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC
20503. If a means used to Impose an information collection does not display a currentlyvaild OMB
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the information collection.
1. FACILITY NAME
Salem Generating Station - Unit 2
2. DOCKET NUMBER
05000311
3. PAGE
1 OF 4
4. TrrLE Reactor Trip Due to Loss of 4 kV Non-Vital Group Bus
LER 15-002-01 for Salem, Unit 2, Regarding Reactor Trip Due to Loss of 4 kV Non-Vital Group Bus

On 8/05/15, at 1539, Salem Unit 2 experienced an automatic reactor trip. The cause of the reactor trip was due to a trip of the 21 Reactor Coolant Pump (RCP) causing a 21 Reactor Coolant Loop low flow condition.

The 21 RCP breaker tripped as designed when the 2B Auxiliary Power Transformer (APT) infeed breaker to the 2H 4 kilovolt (kV) Non-Vital Bus opened. The root cause evaluation did not identify a definitive cause.

However the most probable cause of the 2H 4 kV Non-Vital Bus trip was due to a ground fault on the 21 Heater Drain Pump (HDP) motor that was not isolated by its associated neutral overcurrent relay. An automatic start of the Auxiliary Feedwater (AFW) system occurred as expected following the reactor trip due to low steam generator water levels.

Corrective actions include replacement of the 21 HDP motor and its neutral overcurrent relay.

This event is reportable under 10 CFR 50.73 (a)(2)(iv)(A) as an event that resulted in an automatic actuation of the reactor protection system and actuation of the AFW system.

05000247/LER-2017-001Indian Point6 February 2017
22 August 2017
Manual Reactor Trip Due to Decreasing Steam Generator Levels Caused By Main Boiler Feedwater Pump Turbine Low Pressure Governor Valves Failed Closed
LER 17-001-00 for Indian Point, Unit 2 Regarding Manual Reactor Trip Due to Decreasing Steam Generator Levels Caused By Main Boiler Feedwater Pump Turbine Low Pressure Governor Valves Failed Closed

On June 26, 2017, Operations commenced a downpower from 100 percent to 93 percent reactor power to support performance of the Main Turbine Stop and Control Valve Test. With reactor power at 94 percent, the 22 Main Boiler Feed Pump Turbine (MBFPT) speed control trouble alarm annunciated coincident with pump speed swings of 800 revolutions per minute (rpm). The operators ceased the downpower and placed the 22 Main Boiler Feedwater Pump (MBFP) in Manual speed control to control the rpm swings. This was unsuccessful, and the rpm swings continued. The 22 MBFPT low pressure (LP) governor valves were observed to be cycling from full-closed to full-open. The decision was made to take local pneumatic control of the 22 MBFP to stabilize pump speed. Two minutes after establishing local pneumatic control, the LP governor valves went to full closed. With the rapid reduction in 22 MBFP speed, the pump was no longer delivering feedwater flow to the SGs. An automatic main turbine runback signal should have been generated on a low speed signal; however, there was no turbine runback actuation. In response, the operators commenced a manual runback to reduce main turbine load, but the decreasing SG levels reached 15 percent, and at 1531 hours a manual reactor trip was initiated.

All control rods fully inserted and all required safety systems functioned properly. The plant was stabilized in hot standby with decay heat being removed by the main condenser. The direct cause of the reactor trip was that the shoulder screws used on the 22 MBFPT LP governor valve servomotor linkage had backed out and detached. This caused the LP governor valves to fail closed, shutting off the turbine steam supply. This event had no effect on the public health and safety. The event was reported to the Nuclear Regulatory Commission (NRC) on June 26, 2017 under 10 CFR 50.72(b)(2)(iv)(B), 50.72(b)(2)(xi), and 50.72(b)(3)(iv)(A).

05000335/LER-2016-003Saint Lucie21 August 2016
15 August 2017
Generator Lockout Relay Actuation During Power Ascension Results in Reactor Trip
LER 16-003-01 for St. Lucie, Unit 1, Regarding Generator Lockout Relay Actuation During Power Ascension Results in Reactor Trip

On August 21, 2016, during Unit 1 restart following a maintenance outage, an unexpected actuation of the Main Generator Inadvertent Energization Lockout Relay caused the main generator to trip, resulting in an automatic reactor trip. The generator lockout prevented the automatic transfer of station auxiliaries to the available startup transformer power, requiring the emergency diesel generators to start and power the safety related buses.

Reactor coolant pumps normally powered through the non-safety buses were deenergized, and decay heat removal was via natural circulation and Auxiliary Feedwater. The lockout relay actuation was caused by a latent error introduced during a 2013 design modification where a wire was inadvertently removed from the circuit.

Corrective actions included restoration of the affected circuit and implementation of procedure guidance to verify the inadvertent energization relay state and to reset as required following Main Generator manual synchronization.

This licensee event report is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) for system actuations of the reactor protection system, the emergency diesel generators and the auxiliary feedwater system.

This event had no effect on the health and safety of the public.

05000286/LER-2017-002Indian Point
Docket Number
11 June 2017
9 August 2017
Manual Isolation of Chemical and Volume Control System Normal Letdown to Stop a Valve Leak Resulted in an Exceedance of Technical Specification 3.4.9 Condition A Limit for Pressurizer Level
LER 17-002-00 for Indian Point, Unit 3 re Manual Isolation of Chemical and Volume Control System Normal letdown to Stop a Valve Leak Resulted in an Exceedance of Technical Specification 3.4.9 Condition A Limit for Pressurizer Level

On June 11, 2017, while at 100 percent reactor power, Operations placed Chemical and Volume Control System (CVCS) Demineralizer Diversion Valve CH-TCV-149 in DIVERT to allow the 32 Mixed Bed Demineralizer to be removed from service and align the 31 Mixed Bed Demineralizer for service. Within about two minutes after returning CH-TCV-149 to AUTO, which placed the 31 Mixed Bed Demineralizer in service, Letdown Backpressure Control Valve CH-PCV-135 demand had gone to 0 percent (full open demand) while letdown backpressure had increased, reaching 302 psig.

Operations was alerted to a leak that had developed on 32 Mixed Bed Demineralizer Inlet Isolation Valve CH-352. In an effort to isolate the leak, CH-TCV-149 was placed in DIVERT. Due to the elevated pressure at CH-TCV-149 with CH-PCV- 135 fully open, placing CH-TCV-149 in DIVERT coupled with the elevated line pressure created a pressure transient in the letdown line upstream of the CVCS Reactor Coolant Filter. Reactor Coolant Filter Inlet Isolation Valve CH-305 experienced this pressure transient, which resulted in the valve developing a significant leak at the body to bonnet joint. Abnormal Operating Procedure (AOP) 3-AOP-LEAK-1 was entered, and normal letdown was manually isolated to stop the CH-305 leak. Excess letdown was placed in service to balance reactor coolant inventory at a Pressurizer water level of 61 percent.

This exceeded the 54.3 percent limit of Technical Specification 3.4.9 Condition A, and Operations declared the Pressurizer inoperable. The inoperability of the Pressurizer is reportable as a safety system functional failure under 10 CFR 50.73(a)(2)(v). The direct cause of this event was elevated system pressure due to loading of the Reactor Coolant Filter from materials when the 31 Mixed Bed Demineralizer pathway was aligned. The elevated operating pressure in the CVCS letdown stream challenged the integrity of diaphragm valves CH-352 and CH-305, requiring the isolation of normal letdown.

05000390/LER-2017-007Watts Bar9 June 2017
8 August 2017
Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance
LER 17-007-00 for Watts Bar, Unit 1, Regarding Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance

On June 9, 2017. Watts Bar Nuclear Plant (WBN) personnel determined that the reporting requirements of 10 CFR 50.72(b)(3)(v) and 10 CFR 50.73(a)(2)(v), as clarified by guidance in NUREG-1022, Revision 3. were being incorrectly applied for certain events associated with single train safety systems. When events occurred that resulted in these systems not meeting Technical Specification (TS) Limiting Conditions for Operation (LCO). the short duration of these events relative to their required action completion time, coupled with prompt return to allowable values, were not considered a loss of safety function by Operations and Licensing personnel. As a result, multiple potential loss of safety function events were not reported as required. These events were related to Refueling Water Storage Tank (RVVST) level, Containment and Shield Building pressure, and Control Room Envelope integrity.

A review of these events indicate, when considering the actual system capability and the response of equipment and personnel. a loss of safety function capability impacting public health and safety did not occur for events associated with the RWST, Containment. Shield Building, or Control Room. Corrective actions include briefing personnel on the regulatory impact of these events, and the importance of the control room boundary.

.._ _ NRr, FORM Kri 2017:

05000293/LER-2017-010Pilgrim7 June 2017
7 August 2017
Air Accumulation Creates Small Void in Core Spray Discharge Piping
LER 17-010-00 for Pilgrim re Air Accumulation Creates Small Void in Core Spray Discharge Piping

On June 6, 2017, at 1357 (EDT) with the reactor at 100% core thermal power and steady state conditions, plant personnel were performing Ultrasonic testing (UT) examination on Core Spray A high point piping in the A Residual Heat Removal Quad to ensure this piping was water solid, when they identified that the top of this horizontal pipe had an air void internally. A high point vent line with valves is located in the area of the UT exam.

It was found that the top 2 inches of the 10 inch core spray pump discharge line had accumulated an air void within the known inverted loop in Core Spray Loop-A discharge line. The system had been drained for maintenance during the Refueling Outage.

Pilgrim Nuclear Power Station is reporting this event pursuant to 10 CFR 50.73(a)(2)(i)(B), as a condition prohibited by Technical Specifications. Although upon discovery the proper Limiting Condition for Operation Action Statement was entered and the void was filled immediately to correct the issue, it is believed that this condition existed before the time of discovery for a period of time longer than that allowed by Technical Specifications.

This event posed no threat to public health and safety.

05000324/LER-2017-003Brunswick5 June 2017
3 August 2017
1 OF 4
LER 17-003-00 for Brunswick, Unit 2, Regarding Setpoint Drift in Main Steam Line Safety/Relief Valves Results in Three Valves Inoperable,

On June 5, 2017, BSEP received the results of testing of eleven main steam line safety relief valves (SRVs) removed from Unit 2 during the spring refueling outage. Three of the eleven valves were found to have as-found lift setpoints of their pilot valves outside the +/-3 percent tolerance required by Technical Specification (TS) 3.4.3.

One SRV was 9.1 percent high. One SRV was 8.6 percent high, and one SRV was 5.0 percent high. Evaluation determined that the elevated lift pressures in two valves resulted from corrosion bonding of the SRV pilot valves which raised the breakaway force needed to open the pilot. The third valve experienced steam erosion. This event had no adverse impact on nuclear safety. Although the SRV setpoint limits required by the TS were exceeded, the plant condition was bounded by the Brunswick Unit 2 Cycle 22 Reload Safety Analysis, demonstrating that the SRVs could have performed their safety function of limiting reactor vessel overpressure. TS 3.4.3 requires ten of the eleven installed SRVs to be operable. Since less than ten SRVs were operable, this event is being reported in accordance with 10 CFR 50.73(a)(2)(i)(B) for operation prohibited by the plant's TS. The SRV pilot valves were replaced with certified spares before the startup of Unit 2. A procedure was revised to reduce corrosion bonding by improving surface preparation of SRV pilot valve discs.

05000335/LER-2017-002Saint Lucie31 July 2017Inadequate Hot Leg Injection Procedure Results in Unanalyzed Condition

On July 31, 2017, FPL determined that the proceduralized manual actions to mitigate postulated electrical single failures in the St. Lucie Unit 1 hot leg injection (HLI) flow path were inadequate. Manual actions previously developed based on failure modes and effect analysis (FMEA) failed to identify the need to override open permissive interlocks in the HLI flowpath. The procedures were revised to account for the oversight, and a detailed FMEA was performed and enhancement opportunities were identified to be evaluated under the site corrective action program.

The safety significance for the additional jumper scope was bounded by previous evaluations. Therefore, this event had no significant impact on the health and safety of the public.

Reported lessons learned are incorporated into the licensing process and fed back to industry.

Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

Description of the Event

On July 31, 2017, with St. Lucie Unit 1 in Mode 1 at 100 percent reactor power, it was determined that the proceduralized manual actions to mitigate postulated electrical single failures in the St. Lucie Unit 1 hot leg injection (HLI) flow path were inadequate. The existing procedures lacked actions to address the installation of jumpers required to defeat the reactor coolant system (RCS) pressure interlocks for valves V3481 and V3652 (EIIS:BP:V) when aligning the plant for HLI. The procedures were immediately revised to include the instructions necessary to restore power to the affected valves. The required 8-hour NRC ENS notification was completed at 1832 hours.

A more detailed failure modes and effects analysis (FMEA) was completed to assure no other issues; although enhancements to improve margin were identified, there were no further issues identified that would preclude HLI flow for all strategies.

Cause of the Event

The reason the HLI initiation procedures were inadequate was that the previous FMEA to open V3481 and V3652 to provide hot leg injection was incomplete. This cause is a legacy human performance error associated with the level of detail and rigor in the evaluation and documentation of the capability to provide hot leg injection. A contributing factor was that the control circuits for valves V3481 and V3652 are not typical; the interlocks that prevent opening the valves are not powered from the MCC for the valve actuator.

Analysis of the Event

Reporting Criteria This condition is reportable pursuant to 10 CFR 50.73(a)(2)(ii)(B) as any event or condition that resulted in the nuclear power plant being in an unanalyzed condition that potentially degraded plant safety.

Background

Long-term core cooling and boron precipitation was identified during the initial licensing of St. Lucie Unit 1. Because the St. Lucie Unit 1 original design did not provide dedicated hot leg injection paths, St. Lucie Unit 1 was licensed to develop HLI procedures that utilized the existing low pressure safety injection (LPSI) and/or high pressure safety injection (HPSI) flow paths for hot leg injection.

There are five potential paths for implementing HLI. The preferred HLI flow path is to direct the discharge of one LPSI pump (EIIS:BP:P) through the 2-inch shutdown cooling (SDC) warm-up line to the opposite pump's suction line, and "backwards" through the suction line into the hot leg. The cold leg injection is via the normal HPSI pump (EIIS:BQ:P) operation. This flow path requires the opening of two motor operated valves (MOVs) in series to be successful; each valve is powered from a different electric bus.

Valves V3481 and V3652 are the cross-train powered SDC return isolation valves for the respective 1A and 1B SDC cooling loops. Loss of power scenarios were Reported lessons learned are incorporated into the licensing process and fed back to industry.

Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

mitigated by the contingency use and installation of staged electrical jumpers to provide power for these valves from the opposite train motor control center (MCC).

However, the previous FMEA failed to identify that these valves' control circuits contain open permissive interlocks to prevent subjecting the lower pressure portion of the SDC system to the higher reactor coolant system (RCS) pressure.

The FMEA performed for the 2011 LER failed to identify the need to defeat this interlock by installation of low voltage jumpers in the control room.

This condition is not applicable to St. Lucie Unit 2 as it has a dedicated HLI flow path as part of its original design.

Analysis of Safety Significance The mechanism for potential boron precipitation is described in Unit 1 UFSAR Chapter 6 Appendix C. For a hot leg break, the injection flow passes from the cold legs, through the core, into the hot legs, and out the break. For a hot leg break, core heat removal is via forced flow of the injection water. In contrast, for a cold leg break, after the reflooding is completed, the hydraulic balance will cause most of the injection flow to spill out of the break - the only flow into the core will be that required to make-up for the boil-off in the core that removes the core decay heat. The boron problem arises only during a cold leg break; as borated injection flow enters the core, and only pure water (as steam) leaves the core, the boron concentration in the core region will continue to increase. Once the boron concentration exceeds the solubility limit the boron will precipitate and potentially challenge long-term core cooling capability. The solution to the potential problem is to achieve subcooled flow through the core:

when boron in equals boron out, the concentration will not be increasing.

St. Lucie uses simultaneous hot and cold leg injection as the method to achieve forced flow through the core for long-term post-LOCA cooling. With simultaneous hot and cold leg injection, the recirculated sump fluid is injected into the hot legs as well as the cold legs. Regardless of break location, sufficient flow is delivered to provide heat removal and flush the core to prevent the concentration of boron from reaching the solubility limit.

The operators are procedurally required to initiate HLI within four to six hours post-accident.

If the loss of an electrical bus required the use of the proceduralized jumpers, the emergency response organization (ERO) problem solving teams in the technical support center (TSC) and emergency operation facility (EOF) would most likely diagnose and mitigate the open permissive interlock and initiate HLI within the required timeframe. The 2011 LER evaluated the safety significance for the use of knowledge-based instead of rule-based jumper installation, and the additional low voltage control circuit jumper scope identified in this LER does not materially affect the conclusions of the previous LERs. Based on these considerations, this event had no significant impact on the health and safety of the public.

Reported lessons learned are incorporated into the licensing process and fed back to industry.

Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

Corrective Actions

The corrective actions listed have been entered into the site corrective action program (CAP). Any changes to the actions below will be processed in accordance with the CAP.

1. The additional jumper scope was added to the proceduralized manual actions for bypassing the de-energized interlocks for SDC suction valves.

2. A more detailed FMEA was completed and additional enhancements to improve margin were identified. These enhancements are being tracked in CAP.

Identified Failed Components None

Additional Information

St. Lucie Unit 1 LERs 2011-003-00 (ADAMs accession number ML12023A003) and 2011- 003-01 (ADAMs accession number ML12081A282) reported the use of unproceduralized manual actions to accomplish HLI.

05000286/LER-2017-001Indian Point
Indian Point Unit 3
14 May 2017
13 July 2017
Single Flow Barrier Access Point Found Unbolted
LER 17-001-00 for Indian Point, Unit 3 Regarding Single Flow Barrier Access Point Found Unbolted

On May 14, 2017, at 0233 hrs, Indian Point Unit 3 entered Mode 4 as part of coming out of outage 3R19 and preparing for power operations. Operations test group was preparing for performance of 3-PT- CS004, Residual Heat Removal (RHR) Check Valve Testing. The team gathered for a pre job brief in accordance with the requirements of EN-HU-102, Human Performance Traps &Tools Procedure. At the time the only allowable access point to the Inner Crane Wall was through the double gate combination of Gates D and E, which require one gate to be maintained closed and secured at all times. Workers needed to enter inside of the Crane Wall to perform a portion of the valve lineup required by 3-PT-CS004. After unbolting and opening the gate, the two operators and a contract Radiation Protection (RP) Technician went through gate C despite a posted sign stating that the gate was not to be utilized in modes 1 through 4.

While the valve manipulations were in progress the NRC Resident Inspector was also conducting a tour of the Vapor Containment (VC) and identified that gate C was opened. This gate being open in this plant condition resulted in a safety system functional failure, since with the gate unsecured this made the containment sumps inoperable.

05000390/LER-2017-005Watts Bar10 May 2017
10 July 2017
Isolation of the 1 B-B Safety Injection Pump Leads to Condition Prohibited by Technical Specifications
LER 17-005-00 for Watts Bar re Isolation of the 1B-B Safety Injection Pump Leads to a Condition Prohibited by Technical Specifications

On May 10, 2017, at 0907 Eastern Daylight Time (EDT), Watts Bar Nuclear Plant (WBN) Unit 1 operations personnel discovered the 1B-B Safety Injection pump discharge isolation valve (1-ISV-63-527) closed. Technical Specification (TS) 3.5.2, ECCS - Operating, Condition A was immediately entered for one or more trains of the Emergency Core Cooling System (ECCS) inoperable. TS 3.5.2 Condition A was exited at 0913 EDT when 1-ISV-63-527 was opened.

Investigation determined that the 1 B-B SI pump discharge isolation valve had been closed prior to Unit 1 entering Mode 3 on April 26, 2017, representing a condition prohibited by TS. During this time period, the 1A-A SI pump was inoperable for 21 minutes, representing a condition that could have prevented fulfillment of a safety function.

The cause of the mispositioned valve was the result of an individual failing to follow procedure use and adherence requirements during the performance of Emergency Diesel Generator (EDG) Blackout testing. The safety injection pump discharge valve was closed to support the test but was not reopened following the testing. Corrective actions for this event include personal accountability actions, revision of the EDG blackout procedures to ensure the SI pump discharge valves are reopened, and additional station focus on procedure use, particularly use of Not Applicable (N/A) in performing procedures.

05000313/LER-2017-001Arkansas Nuclear
Arkansas Nuclear One – Unit 1
26 April 2017
26 June 2017
Automatic Start of an Emergency Diesel Generator Due to the Loss of Offsite Power due to Severe Weather
LER 17-001-00 for Arkansas Nuclear One, Unit 1, Regarding Automatic Start of an Emergency Diesel Generator Due to the Loss of Offsite Power due to Severe Weather

On April 26, 2017, Arkansas Nuclear One, Unit 1 (ANO-1), was operating normally at 100% rated thermal power.

The 500kV transmission line to the substation at Pleasant Hill, Arkansas was out of service for planned maintenance.

The area around the plant was experiencing severe weather from thunderstorms and tornado warnings had been issued from the National Weather Service for the four county area.

At approximately 1002 CST switchyard breakers for 500kV lines opened on fault current. High winds had damaged the transmission towers approximately 16 miles away from ANO and caused phase to ground faults. This resulted in a loss of all offsite power lines to the 500kV bus. The autotransformer also locked out as designed when the 500kV transmission lines faulted.

The Reactor Operator initiated a manual reactor trip about 8 seconds after the 500kV lines tripped and prior to the reactor protection system initiating an automatic trip. During this time both emergency diesel generators (EDGs) (EK) started as expected. EDG #2 re-energized one Engineered Safeguards bus. EDG #1 ran unloaded until shutdown.

The plant was stabilized in Mode 3 with Emergency Feedwater (EFW) pumps supplying the steam generators, maintaining the water level at the natural circulation setpoint.

05000370/LER-2017-001Mcguire23 February 2017
26 June 2017
Technical Specification Required Shutdown Due to Reactor Coolant System Leakage
LER 17-001-01 for McGuire, Unit 2, Regarding Technical Specification Required Shutdown Due to Reactor Coolant System Leakaqe

On February 23, 2017, at 19:22 hours, with Unit 1 and Unit 2 operating at approximately 100 percent power, operators commenced a Unit 2 shutdown upon discovery of pressure boundary leakage on Unit 2 Safety Injection (NI) pipe upstream of the connection to "D" Reactor Coolant System (NC) Cold Leg. During a containment walk down inspection in Mode 3 on the next day, a pinhole pressure boundary leak was observed in the body of 2NC-30, Pressurizer Spray Bypass Valve.

The cause of the NI pipe leak is thermal fatigue damage caused by NC cross-loop flows. The cause of the 2NC-30 valve leak is a casting flaw attributed to a combination of defects during the manufacturing process that resulted in a through wall pinhole leak in the valve body. The NI pipe with the flaw and the valve with the pinhole leak could have structurally performed their design functions. Therefore, the health and safety of the public were not affected by these events.

Valve 2NC-30, the NI pipe, and leaking B-Loop NI check valves were replaced. Thermal cycling monitoring and mitigation devices were installed on Unit 2 and will be installed on Unit 1 during the next refueling outage.

05000348/LER-2016-007Farley17 November 2016
7 June 2017
Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters
LER 16-007-01 for Joseph M. Farley, Unit 1, Regarding Plant Shutdown Required by Technical Specifications due to Inoperable Steam Flow Transmitters

On 11/17/2016 at 1859 with Unit 1 in Mode 1 at 99 percent power, the plant initiated a shutdown in accordance with Limiting Condition for Operation (LCO) 3.0.3 for having no operable steam flow channels for the C Steam Generator (SG). The two steam flow channels did not meet acceptance criteria for Technical Specification (TS) 3.3.2. The shutdown was completed and the plant entered Mode 3 as required by LCO 3.0.3. This is reportable as a plant shutdown required by Technical Specifications in accordance with 10 CFR 50.73(a)(2)(i)(A). This is also reportable as an event or condition that could have prevented fulfillment of a Safety Function needed to mitigate the consequences of an accident, in accordance with 10 CFR 50.73(a)(2)(v)(D).

This condition was discovered during an engineering verification of beginning of cycle full power scaling values for steam flow normalization. New scaling data was calculated and the channels were rescaled and restored to operable status. The cause of this event has not yet been determined. A supplemental LER will be submitted upon the completion of the causal analysis, and the cause and corrective actions will be provided at that time.

05000285/LER-2017-001Fort Calhoun13 March 2017
11 May 2017
Unprotected Vital Area Barrier Due to Maintenance
LER 17-001-00 for Fort Calhoun Station, Unit 1, Regarding Unprotected Vital Area Barrier Due to Maintenance
On March 13, 2017 at 16:00 hours, an unattended opening into a room classified as a vital area was identified by Security management. The unattended opening was created when a physical barrier was removed during decommissioning work within a vital area. The cause was determined to be an inadequate procedure(s) such that this action was not recognized by station personnel as a potential breach of a vital area pathway, therefore no compensatory measures were initiated prior to main steam discharge piping elbow removal. Upon recognition, the appropriate compensatory measures were implemented and a one hour report of Reportable Safeguards Events under 10 CFR 73.71(b)(1) and 10 CFR 73.71 Appendix G Section I (EN 52609) was submitted to the NRC.
05000354/LER-2016-006Hope Creek4 May 2017LER 16-006-01 for Hope Creek, Unit 1, Regarding Mode Change Without B Channel Level Instrumentation Operable

On November 9, 2016, at 0420 with the Hope Creek reactor in Operational. Condition 2, Startup, the B channel reactor level instrumentation was found to be inoperable. The inoperable Instrumentation was discovered as reactor level was being lowered into the normal band in preparation for plant startup. Hope Creek had made a mode change from Operational Condition 4, Cold Shutdown, to Operation Condition 2, Startup, on November 9, 2016, at 0317, approximately 1 hour prior to discovering the inoperable instrumentation.

The B Channel reactor level instrumentation is required to be operable in order to enter Operational Condition 2 to support the B division of the Reactor Protection System (RPS), the Emergency Core Cooling Systems (ECCS), and the Primary Containment Isolation System (PCIS). The cause was determined to be an improperly filled reference leg for the B channel reactor level instrumentation. This report Is being made under 10 CFR 50.73(a)(2Xi)(B), as a condition which was prohibited by the plant's Technical Specifications.

05000382/LER-2017-001Waterford8 March 2017
4 May 2017
1 of 5
LER 17-001-00 for Waterford, Unit 3 Regarding Both Trains of Emergency Core Cooling System Inoperable due to Inadvertently Performing Maintenance on Train 'B' Resulting in Event or Condition that Could Have Prevented Fulfillment of a Safety Function

On March 8, 2017, at 1627 CST, it was identified that Low Pressure Safety Injection (LPSI) train ‘B' was inoperable due to SI-135B, Reactor Coolant Loop 1 Shutdown Cooling Warmup Valve, being found open, which is not the required position. At the time of discovery, LPSI train ‘A' was inoperable for maintenance and the station was in compliance with Technical Specification (TS) 3.5.2 action ‘a' which requires that an inoperable LPSI train be restored within 7 days. The shift operating crew entered TS 3.5.2 action ‘c' due to both trains of the Emergency Core Cooling System being inoperable. Action ‘c' requires that with both LPSI trains inoperable, at least one train must be restored within one hour.

SI-135B was subsequently closed and tested to verify operability. TS 3.5.2 action 'c' was exited at 1705. The station remained in compliance with TS 3.5.2 action ‘a'.

It was determined that the SI-135B valve was opened inadvertently. It was planned to perform work on SI-135A, Reactor Coolant Loop 2 Shutdown Cooling Warmup Valve. The workers incorrectly began work on SI-135B and manually opened the valve. This was caused by personnel not performing proper component verification to validate that they were on the correct component, contrary to station procedures. Corrective actions are being performed to improve station work practices related to component verification.

05000454/LER-2017-001Byron25 April 20171 OF 4
LER 17-001-00 for Byron, Unit 1, Regarding Volumetric and Surface Examinations of Reactor Pressure Vessel Head Penetration Nozzles Identify Indications Attributed to Primary Water Stress Corrosion Cracking and Minor Subsurface Void Enlargement from..

During the Byron Station, Unit 1, spring 2017, refueling outage, volumetric and surface examinations of the Reactor Vessel Head Penetration (VHP) nozzles identified recordable indications for VHP nozzles 31, 74, 76, and 77 that did not meet the applicable acceptance criteria. The unacceptable indications were identified and repaired prior to returning the reactor head to service. None of the indications were located in the Reactor Coolant System pressure boundary region.

The cause of the P-31 unacceptable indication is attributed to existing welding discontinuities/minor subsurface voids opening to the surface or enlarging due to thermal and/or pressure stresses during plant operation. The cause of the P-74, P-76 and P-77 unacceptable indications is attributed to Primary Water Stress Corrosion Cracking.

The indication in penetration 31 was removed by manual buffing. The indications in P-74, P-76 and P-77 were repaired by manual grinding with no welding required.

This event is reportable in accordance with 10 CFR 50.73(a)(2)(ii)(A) for any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.

05000318/LER-2017-001Calvert Cliffs20 February 2017
19 April 2017
Pressurizer Safety Valve As-Found Settings Outside Technical Specification Limits Due To Setpoint Drift
LER 17-001-00 For Calvert Cliffs, Unit 2 re: Pressurizer Safety Valve As-Found Settings Outside Technical Specification Limits Due to Setpoint Drift
During scheduled testing at the offsite testing facility, the as-found lift setting for the pressurizer safety valve previously installed in Unit 2 at the 2RV200 location was measured outside the Technical Specification allowable values (valve lifted low). The valve had been installed during the 2015 Unit 2 refueling outage and was removed during the 2017 Unit 2 refueling outage for scheduled testing and maintenance. As scheduled, a spare valve was installed during the 2017 refueling outage. The failed valve was disassembled and inspected at the offsite facility. The apparent cause of the pressurizer safety valve failure is due to setpoint drift. The valve was successfully re-certified for use at the plant in a future installation. Setpoint setting criteria were adjusted based on more recent operating experience (setpoint drifting low).