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05000296/LER-2017-001Browns Ferry1 September 2017
31 October 2017
Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications
LER 17-001-00 for Browns Ferry Nuclear Plant, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications

On September 1, 2017, at approximately 1006 Central Daylight Time (CDT), Browns Ferry Nuclear Plant (BFN) Unit 3 3A Residual Heat Removal (RHR) system pump failed to start during performance of Surveillance 3-SR-3.5.1.6 (RHR I), Quarterly RHR System Rated Flow Test Loop I. The apparent cause was the Electrical Preventive Maintenance Instruction for 4kV Wyle/Siemens Horizontal Vacuum Circuit Breaker (Type-3AF) and Compartment Maintenance was revised to include steps to secure the breaker's mounting hardware which caused internal binding of the indication flag. Binding of the indication flag prevented the closing spring of the breaker from charging and the breaker from closing on demand. As a result, automatic start of the 3A RHR pump was prevented. On September 1, 2017, at approximately 1633 CDT, the 3A RHR Pump was declared operable following lubrication and testing of the breaker's indication flag mounting bolt.

A Past Operability Evaluation concluded that the 3A RHR Pump was inoperable from July 26, 2017 to September 1, 2017, which exceeded the Technical Specification allowed outage time. During this time, the 3B, 3C, and 3D RHR pumps would have started automatically upon receipt of an Emergency Core Cooling System (ECCS) initiation signal or from an Operator manual start demand from the Control Room. Based on results from the Probability Risk Assessment and Engineering inspections, there was no significant risk to the health and safety of the public or plant personnel for this event. The Corrective Action to reduce the probability of similar events occurring in the future will be addressed by revising the Electrical Preventive Maintenance Instruction for 4kV Wyle/Siemens breakers to ensure freedom of movement of the indication flag is present during the breaker inspection.

05000293/LER-2017-001Pilgrim16 January 2017
17 July 2017
Reactor Building Isolation Dampers Failed to Isolate
LER 17-001-01 for Pilgrim Nuclear Power Station Regarding Reactor Building Isolation Dampers Failed to Isolate

Station (PNPS) was performing surveillance testing of secondary containment isolation dampers when dampers AO-N-82 and AO-N-83, refueling floor supply isolation dampers, failed to fully close when the control switches were taken to close.

The failure of dampers AO-N-82 and AO-N-83 to fully close resulted in a loss of safety function for secondary containment, causing immediate entry into Limiting Condition for Operation (LCO) Action Statement (AS) 3.7.C.2.a, at 1155 hours. This LCO AS was exited at 1206 hours when the dampers were verified closed.

An 8-hour non-emergency notification was made in accordance with 10 CFR 50.72(b)(3)(v), any event or condition that at the time discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident. In addition, this notification is being conservatively made by PNPS in accordance with 10 CFR 50.73(a)(2)(i)(B), as a condition that was prohibited by Technical Specifications.

The reactor building isolation dampers were cleaned, lubricated and post-work tested. PNPS has returned the dampers to operable status. Planned action to prevent recurrence is to revise the preventive maintenance strategy.

There was no impact to public health and safety from this condition.

05000374/LER-2017-002Lasalle
LaSalle
30 January 2017
30 March 2017
High Pressure Core Spray System Declared Inoperable due to Cooling Water Strainer Backwash Valve Stem-Disc Separation
LER 17-002-00 for LaSalle, Unit 2, Regarding High Pressure Core Spray System Declared Inoperable due to Cooling Water Strainer Backwash Valve Stem-Disc Separation

On January 30, 2017, during routine surveillance testing of the Unit 2 Division 3 Diesel Generator Cooling Water (DGCW) system, the cooling water strainer backwash valve was unable to open. The Division 3 DGCW system was declared inoperable. Upon investigation, operators determined the cause of the valve malfunction was due to stem-disc separation. Division 3 DGCW is a support system for the Division 3 Emergency Diesel Generator and the High Pressure Core Spray (HPCS) system. The required actions of Technical Specifications (TS) 3.7.2 and 3.5.1 were entered on January 30, 2017 when the DGCW and HPCS system, respectively, were determined to be inoperable. TS 3.7.2 Required Action (RA) A.1 requires the supported system to be immediately declared inoperable. TS 3.5.1 RA B.2 requires restoration of the HPCS system to operable within 14 days. TS 3.8.1 was not applicable since a note provides that Division 3 AC electrical power sources are not required to be operable when HPCS is inoperable. The valve was replaced, and the HPCS system was returned to operable on February 2, 2017.

This condition could have prevented the HPCS system, a single train safety system, from performing its design function. This event is reportable in accordance with 10 CFR 50.73(a)(2)(v)(D) as an event or condition that could have prevented fulfillment of the safety function of structures or system that are needed to mitigate the consequences of an accident. There were minimal safety consequences associated with the event since the other emergency safety systems remained operable, and the Division 3 DGCW system remained functional as it retained the ability to provide the required flow through the system. The apparent cause of the stem-disc separation was erosion due to the carbon-steel valve internals in a raw water system environment.

05000296/LER-2016-001Browns Ferry19 January 2016
21 March 2016
Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure
LER 16-001-00 for Browns Ferry, Unit 3, Regarding Inoperable Residual Heat Removal Pump Results in Condition Prohibited by Technical Specifications and Safety System Functional Failure

On January 19, 2016, at approximately 1100 Central Standard Time (CST), during troubleshooting of the Main Control Room (MCR) green light indication on the 3A Residual Heat Removal (RHR) Pump Motor Breaker Transfer Switch (MBTS), it was discovered that the 3A RHR Pump MBTS had malfunctioned, potentially preventing the pump from starting from the MCR. The 3A RHR Pump was declared inoperable.

On January 20, 2016, at approximately 0030 CST, the 3A RHR Pump was declared operable following replacement of the 3A RHR Pump MBTS.

A Past Operability Evaluation concluded that the 3A RHR Pump was inoperable from January 9 to January 20, 2016, exceeding the Technical Specification allowed outage time. During this time, the 3B and 3D RHR Pumps were also inoperable on January 14, 2016, from 0127 to 0215 CST, resulting in a Safety System Function Failure. A Probabilistic Risk Assessment determined there was a negligible increase in risk.

The cause of this event was failure of the transfer switch to fully latch due to binding resulting from the MBTS being installed greater than its twenty-one year service life with no Preventative Maintenance (PM) performed. Corrective actions include verifying similar transfer switches are latched in the NORMAL positon on BFN, Units 1, 2, and 3, and creating a PM activity with a replacement schedule for these switches.

05000260/LER-2015-001Browns Ferry17 June 2015Failure of the 2A RHR Pump To Manually Start from the Control Room Due To A Loose Fastener

On June 17, 2015, at approximately 1015 Central Daylight Time (CDT), Browns Ferry Nuclear Plant (BFN) Operations personnel attempted to place BFN, Unit 2, Residual Heat Removal (RHR) Loop 1 into Suppression Pool Cooling (SPC). Upon actuating Hand Switch 2-HS-74-5A from the Control Room, Operations personnel observed that 2A RHR pump failed to start, and declared RHR Loop I inoperable.

On June 18, 2015, at 1710 CDT, the pump was started and stopped after completion of troubleshooting, and the RHR Loop I was declared operable.

Troubleshooting discovered a loose terminal wire which intermittently prevented 2A RHR from being manually started from the Control Room. An investigation determined the cause to be human performance errors. RHR Loop 1 was inoperable from March 20, 2015, to June 18, 2015, longer than allowed by BFN, Unit 2, Technical Specifications. This loose terminal wire made the pump vulnerable to failure during a seismic event and, therefore, not in compliance with the design basis for the RHR system. This event did not prevent the 2A RHR Pump from manually starting, from the pump breaker, for SPC in the event of an emergency. Both the SPC manual start and the automatic start response to an Emergency Core Cooling System initiation signal were unaffected by this condition.

Corrective Actions for this event were to discipline the individuals responsible, to tighten the loose fastener, and to revise maintenance instructions to reduce the probability of recurrence.

05000293/LER-2015-002Pilgrim12 March 2015Main Steam Safety Relief Valves Determined to be Inoperable Following Evaluation

On March 12, 2015, after further evaluation of system performance of SRV-3A and SRV-3C, along with results of valve internal conditions identified during physical inspection, the valves were determined to have been inoperable for an indeterminate period during the last operating cycle. Specifically, SRV-3C was determined to be inoperable based on its on-demand performance at low reactor pressures, as well as the visual conditions that were identified during the inspection process. SRV-3A was considered inoperable based on it having similar internal indications as SRV-C when it was disassembled and inspected. SRV-3A Was installed in May 2011 and SRV-3C was installed in October 2013.

Additionally, during an extent of condition review of historical SRV performance, the review identified on March 13, 2015 that SRV-3A had failed to open in response to three manual actuation demands on February 9, 2013.

At the time the valves were declared inoperable the reactor was at 100% power. The valves had been replaced in February 2015 during the forced outage relating to winter storm Juno. This event posed no threat to public health and safety.

05000296/LER-2015-001Browns Ferry11 February 2015High Pressure Coolant Injection and Reactor Core Isolation Cooling Inoperable Due To No Suction Source Aligned

On February 11, 2015, at 0820 Central Standard Time, Brown's Ferry Nuclear Plant (BFN), Unit 3, declared the High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems inoperable due to no suction source aligned. During surveillance testing, the Condensate Storage Tank (CST) emergency discharge isolation valve energized and closed when the breaker was closed, isolating both systems from their suction source. It was subsequently determined that contacts on the local hand switch were stuck closed following performance of a previous maintenance task. Operations personnel re-opened the isolation valve using the hand switch in the Control Room, restoring operability to the HPCI and RCIC systems.

The apparent cause of this event was inadequate design review of a 2010 plant modification which allowed latent design vulnerabilities to be introduced into the plant.

The corrective actions to reduce the probability of a similar event occurring in the future were to remove thermal overload heaters from the affected breakers, preventing valve closure when these breakers are closed; to review a sample of recent engineering change packages for quality of Design Review; to repair a faulty hand switch; and to implement a design change for the CST isolation valves for all three BFN units to prevent spurious operation of the isolation valve when the associated breaker is closed.

05000293/LER-2014-001Pilgrim6 May 2014Condition Prohibited By Technical Specifications

On May 6, 2014, with Pilgrim Nuclear Power Station (PNPS) in the RUN Mode operating at 100 percent power, the NRC Resident Inspector raised a concern about the PNPS method of complying with PNPS Technical Specification (TS) Limiting Condition for Operation (LCO) 3.7.A.2.b when a Primary Containment Isolation Valve is inoperable. TS LCO 3.7.A.2.b.requires that at least one containment isolation valve in each line having an inoperable valve shall be deactivated in the isolated condition. Deactivation means to electrically or pneumatically disarm, or otherwise secure the valve. PNPS interpretation and practice had been that a "Danger" tag on the control switch meets this requirement for a fail-closed valve with no automatic valve opening signal. At the time, Primary Containment Isolation Valves AO- 5042A and AO-5044A were inoperable in the isolated position but were not deactivated.

The apparent cause of this event is failure to properly revise procedures and practices when LCO TS 3.7.A.2.b was revised in 1988 to permit periodic opening of the deactivated valve in the line under administrative controls.

This event was not risk significant and had no adverse impact on the health and safety of the public.

05000373/LER-2014-002Lasalle29 March 2014Unit 1 Division 3 Ventilation Failure

On March 29, 2014, Unit 1 was in Mode 1 at 100% power. At 1620 hours CDT, the Division 3 Core Standby Cooling System (CSCS) Pump Room, Switchgear Room, and Battery Room Ventilation failed in such a manner that heat could not be removed from the rooms. Due to the lack of ventilation in the Division 3 switchgear room the High Pressure Core Spray (HPCS) system was declared inoperable and Condition B of Technical Specification (TS) 3.5.1 was entered.

The cause of the event was a failure of the hydramotor pump bearing for the 1VD19Y, Division 3 CSCS Ventilation Return Fan Outlet Damper. Loss of hydraulic pressure in the hydramotor resulted in 1VD19Y failing in the closed position. The corrective action for the event was replacement of the hydramotor for the 1VD19Y damper.

05000293/LER-2013-010Pilgrim19 October 2013Automatic Group I Primary Containment Isolation Actuation During Plant Startup Due to Reactor High Water Level

On Saturday, October 19, 2013 at 0330 (EDT) with the reactor critical at 1% core thermal power (CTP), and the mode switch in START UP, a high reactor water level condition (+55") resulted in a valid Group I primary containment isolation signal and resultant closure of the main steam isolation valves (MSIV), MSIV drain line valves, and reactor recirculation system sample line valves. The plant was in the process of starting up with reactor pressure at approximately 290 psig with a corresponding reactor coolant temperature for that pressure. Reactor startup was suspended and control rods were manually reinserted. Reactor water level was recovered and maintained within normal bands. Plant systems responded as designed to the Group I containment isolation signal.

The direct cause of MSIV isolation was automatic actuation of the Group I containment isolation signal due to high reactor high water level with the mode switch in START UP. The cause of the high reactor water level was due to unexpected rapid opening of three turbine steam bypass valves. The reason the bypass valves rapidly opened was due to a malfunction of the mechanical pressure regulator (MPR). The MPR malfunctioned because an increased error signal between turbine steam pressure and the MPR setpoint due to friction between the MPR pilot valve and the pilot valve bushing resulting from lack of rotation of the pilot valve bushing. Corrective action was taken to flush the needle valve that controls oil flow to the pilot valve bushing and exercise of the pilot valve bushing to restore proper rotation.

This event posed no threat to public health and safety.

05000293/LER-2013-008Pilgrim22 August 2013Manual Scram - Reactor Feed Pump Trip

On Thursday, August 22, 2013 at 0755 (EDT) with the reactor critical at 98% core thermal power (CTP), and the mode switch in RUN, the Pilgrim Nuclear Power Station (PNPS) was manually scrammed due to lowering reactor water level resulting from a trip of the reactor feed pumps. The reactor feed pumps tripped due to a loss of power to the pump seal cooling water flow switch relays and resultant automatic actuation of the feed pump trip circuit.

The direct cause of the reactor feed pump trip was an automatic actuation of the feed pump trip circuitry. The feed pump trip circuits actuated as designed in response to a loss of power to the pump seal cooling water flow switch relays. The seal cooling water flow switch relays lost power as a result of a 120V AC breaker trip resulting from a short-to-ground fault in the associated circuits fed by the breaker. Corrective action was taken to repair the ground fault in the associated circuits fed by the 120V AC breaker and to revise reactor feed pump trip circuit design to remove the loss of seal water trip function.

This event posed no threat to public health and safety.

05000293/LER-2013-001Pilgrim10 January 2013Inadvertent Trip of Both Recirculation Pumps and Subsequent Manual Scram

On Thursday, January 10, 2013 at 1534 hour (EST), with the reactor at 100% core thermal power, both reactor recirculation pumps unexpectedly tripped and a manual reactor scram was inserted as required by station procedures. Following the reactor scram, all rods were verified to be fully inserted and the Primary Containment Isolation System Group II (Reactor Building) and Group VI (Reactor Water Cleanup System) actuations occurred as designed due to the expected reactor water level shrink associated with the scram signal. All other plant systems responded as designed. The scram was uncomplicated and decay heat was released to the main condenser via the turbine by-pass valves.

The cause of the two reactor recirculation pumps tripping was due to the inadvertent seal-in of a relay (pump trip interlock) in the Low Pressure Coolant Injection (LPCI) Loop Select Logic circuitry within the Residual Heat Removal (RHR) System during surveillance testing. When the logic was reset at completion of testing, a normally open relay contact (which was inadvertently closed) interlocked with the recirculation pumps circuit, sent a trip signal to their drive motor breakers.

Corrective action has been taken to revise the subject surveillance procedure with steps to reinstall relay covers and added a verifier to observe relay status/ state prior to resetting the relay logic circuit.

This event had no impact on the health and/or safety of the public.

05000293/LER-2011-006Pilgrim30 November 2011HPCI Turbine Governor Control Valve Failure

On November 30, 2011, at 1747 hours, with the reactor at 100% core thermal power and steady state conditions, Pilgrim Nuclear Power Station (PNPS) declared the High Pressure Coolant Injection (HPCI) system inoperable due to the HPCI turbine governor control valve (HO-2301-24) failing to open during planned post-maintenance testing. The governor control valve is a hydraulically operated valve and its normal position is closed. The valve has a safety function to open on a demand signal during certain event mitigation scenarios requiring the HPCI system operation.

The governor control valve failed to open during the post-maintenance testing from the Alternate Shutdown Panel (ASP) and subsequently from the Main Control Room. The HPCI system was declared inoperable and the Limiting Condition for Operation (LCO) for Technical Specification (TS) 3.5.C.2 was entered.

This event had no impact on the health_ and/ or safety of the public.

05000293/LER-2011-001Pilgrim20 February 2011Technical Specification (TS) Required Shutdown - RBCCW 'B' Declared inoperable

At 0055 hours on Sunday, February 20, 2011, the Pilgrim Nuclear Power Station (PNPS) commenced a controlled shutdown of the reactor due to the 'B' train of Reactor Building Closed Cooling Water (RBCCW) being declared inoperable and expected to exceed its 72-hour Limiting Condition for Operability (LCO) as required by TS prior to return to operable status.

With the plant operating at 100% power, leakage of Salt Service Water (SSW) was detected in the RBCCW system due to high chloride levels and increased inventory in the system. An investigation into the event determined that the source of the SSW was isolated to the 'B' RBCCW heat exchanger which is designed to cool RBCCW under normal and post-accident conditions. The quantity of the leakage was determined to exceed the design limits established to ensure post-accident operation of the system and the 'B' train of RBCCW was subsequently declared inoperable.

The leak detection and repair activities identified a single tube leak resulting from an improperly modified tube sleeve (shortened and incorrect bevel) which accelerated wear on the parent tube.

This event had no impact on the health and/or safety of the public.

05000271/LER-2010-002Docket Number25 October 2010Inoperability of Main Steam Safety Relief Valves due to Degraded Thread Seals

During the 2010 refueling outage, the pneumatic actuators for the four main steam safety relief valves (RV), RV- 2-71-A, B, C & D, were tested and leakage was identified through the shaft to piston thread seal on three of the four RVs. This leakage, when combined with the RV accumulator leakage, caused two of the four RVs to not meet design actuation requirements and therefore be considered inoperable. Technical Specification (TS) 3.6.D requires at least three of the four RVs to be operable for overpressure protection of the Reactor Coolant System and TS 3.5.F requires all four RVs to be operable to support the Automatic Depressurization System (ADS) function of the Core Standby Cooling System. Since inoperability of two valves could constitute an operation or condition prohibited by TS, a cause analysis was performed. On October 25, 2010, based on a review of the analysis, it was determined that there was firm evidence that the condition may have existed for a period of time greater than allowed by the TS. Therefore, this event is reportable in accordance with 10CFR50.73(a)(2)(i)(B) as an operation or condition prohibited by TS. Subsequent material testing of a seal from the same batch lot determined that the apparent cause of the thread seal condition was thermal degradation. The thread seals were replaced and tested on all four RVs prior to start up from the 2010 outage with new seals and will be disassembled for inspection, modified and tested during the next refueling outage.

This event did not affect the automatic function of the RVs to provide overpressure protection and due to redundancy in the RV design and available nitrogen supplies, adequate relief capacity for ADS existed at all times. Therefore, this event did not pose a threat to public health and safety.

05000293/LER-2005-003Docket Number11 May 2005

On May 11, 2005, Pilgrim Station was notified that three Target Rock relief valve pilot assemblies exceeded the Technical Specification (TS) tolerance limit of 1115 psig ± 11 psi (± 1%) during routine testing at the Wyle Laboratories test facility. Certified replacement relief valve pilot assemblies were installed in the plant at the time of the notification.

The most probable cause of the as-found initial popping pressures exceeding the TS tolerance limit was corrosion bonding of the pilot valve assembly disk and seat. The corrosion bonding most likely developed while the pilot valve assemblies were in service. Poor fitting insulation was also identified as a contributing cause.

Corrective action taken includes replacing the pilot valves with certified tested replacements.

Engineering is evaluating options for resolving the high popping pressure reliability concern.

The condition posed no threat to public health and safety.

05000293/LER-2005-002Docket Number14 April 2005

On April 16, 2005 at 0955 hours, one drywell pressure transmitter was found isolated (valved out of service) and therefore, inoperable. The transmitter is part of one of two Division 'B' instrument channels that function to initiate safety systems in the event of a high-pressure condition inside the drywell. The transmitter was mistakenly isolated at 0905 hours on April 14, 2005. The Division 'A' pressure transmitters and related instrument channels that provide a similar function were not impacted. The condition existed during reactor power operation for a period longer than allowed by technical specifications.

The root cause of the condition was licensed operator error. The operator mistakenly closed the isolation valve of the pressure transmitter instead of another valve. The error was the result of inadequate use of human performance error prevention tools, i.e. self-checking and a questioning attitude. Corrective actions taken included opening the isolation valve and walk-downs to ensure other instrumentation was correctly configured.

The condition posed no threat to public health and safety.

NRC FORM 368

05000293/LER-2004-003Docket Number6 May 2004

On May 6, 2004, Pilgrim Station was notified of test results for the pilot valves of two main steam relief valves that had exceeded the Technical Specification limit of 1115 +/-11 psig during testing at the Wyle Laboratories test facility. Certified replacement relief valve pilot assemblies were installed in the plant at the time of the notification.

The root cause evaluation identified the most probable cause of initial high as-found popping pressures exceeding the tolerance limit was corrosion bonding of the pilot valve disc and seat. The corrosion bonding most likely developed while the pilot valves were in service. The root cause evaluation identified poor fitting insulation as a contributing cause.

Corrective action taken and planned includes replacing the pilot valves with certification tested pilot valves, reworking the insulation, overhauling the pilot valves, and purchasing new insulation.

The condition posed no threat to public health and safety.

05000293/LER-2003-0056 September 2003

On September 6, 2003 at 1151 hours, the safety-related train 'A' 480-volt load center and the related motor control centers (MCCs) powered from the load center de-energized. The event resulted in several systems including the high pressure coolant injection and the reactor core isolation cooling systems becoming inoperable. The train '8' 480-volt load center and related MCCs were unaffected.

The affected load center and related MCCs were re-energized by 0022 hours and the affected systems were returned to service by 1000 hours on September 7, 2003.

The direct cause of the event was the unplanned trip of the circuit breaker that powers the load center.

The root cause investigation revealed the circuit breaker tripped due to a malfunction of one of the breaker's three current transformers.

Corrective action included the replacement of the circuit breaker. Corrective action planned includes analysis of the current transformer malfunction and related actions to preclude recurrence.

The event posed no threat to public health and safety.

05000293/LER-2003-0031 June 2003

On June 1, 2003 an unplanned automatic scram occurred while at 100% reactor power. The scram was the result of a load rejection. Automatic responses included the insertion of all withdrawn control rods, transfer of the source of electrical power for Pilgrim's 4.16 kV auxiliary power distribution system (APDS), closure of the turbine steam control and stop valves, trip of the turbine, opening of the turbine steam bypass valves, and opening of main steam relief valves for pressure relief.

The direct cause of the scram was the automatic dosing of the turbine control valves. The direct cause of the event was an electrical fault in the unit auxiliary transformer (UAT) that was powering the APDS at the time of the event. The fault was the result of the failure of a conductor within the low voltage portion of the UAT (X-winding).

Corrective actions taken included a temporary alteration for powering the APDS during power operation.

Corrective actions planned include the repair or replacement of the unit auxiliary transformer.

The event posed no threat to public health and safety.

05000293/LER-2002-0017 July 2002

On July 7, 2002, the High Pressure Coolant Injection (HPCI) system was declared inoperable for 30 minutes.

The cause was a failed fuse that is part of the control power circuitry for the circuit breaker of a normally closed motor-operated valve in the HPCI system injection piping. Inspection of the failed fuse identified a separation that had occurred at an internal solder connection between the fuse end cap and the fusible link. The fusible link was intact. The fuse was replaced and the system was returned to operable status on July 7, 2002.

The event occurred at 100 percent reactor power with the reactor mode selector switch in the RUN position. The reactor vessel pressure was approximately 1035 psig with the water temperature at the saturation temperature for that pressure. This event posed no threat to public health and safety.

05000259/LER-1983-015, Forwards LER 83-015/03L-0Browns Ferry7 April 1983Forwards LER 83-015/03L-0
05000296/LER-1982-021, Forwards LER 82-021/03L-0Browns Ferry18 June 1982Forwards LER 82-021/03L-0