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 Start dateReporting criterionEvent description
05000443/LER-2017-00127 June 201710 CFR 50.73(a)(2)(iv)(A), System Actuation

On April 29. 2017 at 18:44. the Reactor was manually tripped by the operators at approximately 12% power in response to a feedwater isolation caused by I ugh Steam Generator (SG) Level on the 'B' SG. The feedwater isolation signal P-14 was automaticall) actuated at 18:43 when the 'B' SG level reached the setpoint 0 r 90.8?..o narrow ranue level. The plant was being started up following the major work perlbrmed for Refueling Outage 18. No adverse consequences resulted from this event.

Post-trip investigation revealed that FW-LT-502-V 1 L (the Variable leg pressure isolation for FW-LT-502) had not been restored to the required open position during routine instrument line filling and venting. On April 26. 2017. l&C' performed hacklilline of the reference legs on multiple steam generator level channels. including FW-1.T-502. the '13' SG wide range level instrument.

1:W-LT-502- VII. not being restored to the open position caused the 'B' SG wide range indication to respond slowly to level changes resulting in overfeeding the 'B' steam generator. The cause of the event was determined to be failure of the l&C technician to properly implement maintenance fundamentals during the performance of restoration of FW-LT-502. Individual perlbrmance was corrected. A contributing cause was determined to be improper characterization or SG level hack fill activity as skill-of-the-craft. Planned corrective actions include development of a maintenance procedure to provide specific step-by-step instructions.

05000443/LER-2016-0012 March 2016
26 April 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation

On March 2, 2016 at 0253 while operating at 100% power, Seabrook Station experienced an automatic reactor trip due to a turbine trip.

A failure of inverter ED-I-11 caused a voltage transient in the power supplies for the Turbine Control System (TCS). The TCS is designed with redundant inverters so that the loss of one inverter will not cause a system failure. However, during this event, the inverter failure caused a voltage increase which exceeded the voltage limits of the TCS power supplies causing them to momentarily shut down. Loss of the TCS power supplies initiated an automatic turbine trip signal, which in turn actuated an automatic reactor trip as designed. Other plant equipment functioned as expected and no adverse consequences resulted from this event.

The direct cause of the event was a failure of inverter ED-I-11 which resulted in an overvoltage condition to the turbine control system.

At this time, the cause of the failure of the inverter has not been determined. If additional troubleshooting identifies a cause, this LER will be supplemented. Immediate corrective action was implementation of a temporary modification to energize the power panel normally fed by ED-I-11 to eliminate single point vulnerability. Planned corrective actions are to continue troubleshooting and repair of inverter ED-I-11, install overvoltage protection for the TCS cabinets and upgrade the TCS power supplies to higher voltage rated units.

FnRM 2RR (11-7015)

05000443/LER-2014-0026 April 201410 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On April 6, 2014, while the plant was in refueling outage sixteen, it was determined during surveillance testing that three of four reactor coolant pump (RCP) undervoltage (UV) reactor trip channels exceeded the Technical Specification (TS) channel response time acceptance criteria of 1.5 seconds for the RCP UV reactor trip function. The condition for the RCP UV time delay relays exceeding tolerance was experienced on all four channels; however, only three of the four channels did not meet their TS required response times. Since this condition involved multiple similar components, there is evidence indicating that this condition may have arisen over time and three channels of RCP UV were inoperable concurrently. This resulted in the plant operating in a condition prohibited by the TS.

The root cause was determined to be the revisions of the Design Control Manual in 1991 and earlier did not require a failure modes and effects analysis as part of the design change packages that installed the E7022PA relays. The RCP UV time delay setting was not identified as a critical attribute and the manufacturer's recommendations for applications requiring very precise time delay settings were overlooked and not incorporated into station procedures. Corrective actions already taken include the replacement of one relay and adjustment of all relays to acceptable response times.

Planned corrective actions are to revise procedures to energize relays for at least 3 hours before performing testing, to perform rechecks at 72 hours during outages and perform additional rechecks if adjustments were made.

05000443/LER-2014-0011 April 201410 CFR 50.73(a)(2)(iv)(A), System Actuation

On April 1, 2014 at 00:26 while operating at approximately 15% power following turbine shutdown and removal of the main generator from service, Seabrook Station experienced an automatic reactor trip on reactor coolant two loop loss of flow. The loss of flow was the result of the unexpected closure of the main generator breaker (MGB) "B" phase resulting in 345KV bus 6 de-energizing to isolate the generator breaker. All buses transferred to the reserve auxiliary transformers as designed; however, a slight delay in the automatic transfer for bus 1 resulted in two reactor coolant pumps (RCP) tripping. The RCPs tripping resulted in an automatic reactor trip due to reactor coolant loop low flow. The emergency feedwater system actuated on low SG level, and plant equipment functioned as expected. No adverse consequences resulted from this event.

The root cause is inadequate procedural guidance as the procedure used for MGB operation lacked appropriate information regarding local/remote selector switch position, mitigating actions, and minimizing time with MGB protection defeated. Corrective action is to revise the procedure to add controls to communicate potential risk while switch is in the local position, ensure the use of guarded equipment controls, and minimize the time spent with the switch in local without breaker lock rods installed.

05000443/LER-2012-0057 December 201210 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On 12/7/12, with the plant in Mode 1 at 100% power, Service Water Cooling Tower level was discovered to be below the Technical Specification (TS) limit of 42.15 feet. Following discovery, a fast fill of the cooling tower was performed to restore water level above the TS limit. It was subsequently determined that cooling tower water level was below the TS limit for approximately 17 days.

adverse consequences resulted from this event and no safety system functional failure occurred since there was sufficient water in the cooling tower to maintain the cooling tower functional at all times.

No The cause of the event was failure to use diverse means to validate the accuracy of a potentially inaccurate cooling tower level indicator. Corrective actions included restoring level in the Service Water Cooling Tower and increasing the use of operator fundamentals.

05000443/LER-2012-00410 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(iv), System Actuation

On October 31, 2012, during operation at approximately 48% power, the operators manually initiated a tower actuation (TA), which transferred the cooling water source for the train-A service water (SW) loop from the ocean to the cooling tower. The Atlantic Ocean serves as the normal ultimate heat sink; however, if the normal supply of cooling water from the ocean is unavailable, a mechanical draft cooling tower serves as the ultimate heat sink. A strainer is provided in each SW train to prevent shells and mussels from fouling the heat exchangers. During this event, SW was operating on the ocean and differential pressure across the train-A SW strainer increased above the alarm setpoint of 10 psid. In response to the high differential pressure, the operators initiated a TA in accordance with station procedures to transfer train-A SW operation to the cooling tower. Train-A SW operated on the cooling tower until 0430 on November 1, 2012, when the SW train was transferred back to the ocean.

The root cause of the event is the lack of a structured process to ensure ongoing equipment monitoring following a storm for systems sensitive to changing environmental conditions. The corrective action for this event is creation of a procedure to address the affects of severe weather on the SW screens (both during the storm and after). No adverse consequences resulted from this event.

05000443/LER-2012-00225 September 201210 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On September 25, 2012 with the unit in a refueling outage and defueled, station personnel, while reviewing a design change for installation of new circuit boards in the solid state protection system, identified a deficiency in the procedure that performs response time testing of the reactor trip breakers (RTB). The RTB have two diverse trip methods: the undervoltage circuit and the shunt trip circuit. When a RTB is opened through the shunt trip circuit, two coils (STA and SH TR) must function in order to open the breaker. A review of the existing test method found that the shunt trip circuits for both RTB had not been adequately tested. Further, a review of previous revisions of the surveillance procedures concluded that the response time of the shunt trip circuit had never been adequately tested.

This event is similar to and has the same cause as the inadequate time response testing reported in LER 2012 001. The cause of both events was ineffective methods utilized in the mid 1980's to verify that surveillance test procedures ensured compliance with the TS. The corrective actions for this condition included revising the surveillance procedure and obtaining response times, which were found to be within acceptable limits. A review of the adequacy of time response testing is ongoing to address the extent of condition. No adverse consequences resulted from this event.

05000443/LER-2011-00321 December 201110 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On December 21, 2011, during operation at approximately 65% power, station personnel identified a condition that previously rendered one of the offsite AC power sources inoperable. The plant design includes two independent offsite AC sources: (1) one circuit through the unit auxiliary transformers (UAT) to both trains of emergency buses, and (2) a second source through the reserve auxiliary transformers (RAT) to both trains of emergency buses. Offsite power is normally provided through the UAT, and the RAT supply is in standby. Operability of the RAT supply is contingent on the ability of the system to perform a fast transfer to the RAT supply upon opening of a UAT supply breaker. A review of the system design determined that when the emergency diesel generator (EDG) is operating in parallel with offsite power, the fast transfer feature to the RAT supply is unavailable, rendering this offsite AC source inoperable. On at least two occasions, this previously unrecognized condition rendered the offsite AC source inoperable for a period longer than permitted by the technical specifications.

This event resulted from a failure to recognize the impact of EDG operation on the fast transfer feature.

Operations issued guidance that the offsite AC source is inoperable during parallel operation of an EDG. No adverse consequences resulted from the event.

05000443/LER-2011-0026 October 201110 CFR 50.73(a)(2)(iv)(A), System Actuation

At approximately 1226 on October 6, 2011 with the plant operating in Mode 1 at 100% power, Seabrook experienced a plant trip on low steam generator water levels following loss of an operating main feed pump. The main feed pump tripped on low suction pressure while restoring a condensate pump to service following maintenance. During restoration of the pump, air entered the condensate system and caused a drop in condensate pump discharge pressure, which resulted in a low pressure condition at the suction of the main feed pump. The trip of the main feed pump on low suction pressure initiated a turbine setback; however, with reduced feedwater flow, steam generator levels decreased to the low level reactor trip setpoint. The automatic systems functioned as designed. The emergency feedwater system automatically actuated and recovered steam generator levels. No adverse consequences resulted from this event.

The cause of this event was the lack of a procedure for restoring a condensate pump to service during operation at power. The corrective action revised the operating procedure to provide instructions for filling and venting a condensate pump following maintenance.

05000443/LER-2011-00124 March 201110 CFR 50.73(a)(2)(i)(B), Prohibited by Technical SpecificationsOn March 24, 2011 during operation in mode 1 at 100% power, station personnel, while reviewing station documents, determined that one of the two containment gaseous radioactivity monitors did not meet the qualifications for a reactor coolant system leakage detection monitor required by the technical specifications (TS). The indication provided by the backup gaseous monitor did not meet the seismic requirements of Regulatory Guide (RG) 1.45, Reactor Coolant Pressure Boundary Leakage Detection Systems, and the monitor should not have been used to satisfy TS requirements. TS 3.4.6.1 requires a containment gaseous monitor and a particulate monitor. On several occasions, the plant operated with the normal particulate and gaseous monitors out of service and relied on the backup gaseous monitor to meet TS requirements. This situation resulted in a condition prohibited by the TS when plant operation continued with two inoperable leakage detection monitors for longer than the 6 hours permitted by the TS. No adverse consequences resulted from this event. The cause of the condition was the design change that installed the backup monitor in the early 1990's did not qualify the monitor's indication to seismic requirements in accordance with RG 1.45. The condition was corrected in April 2011 by a design change that upgraded the gaseous monitor indication to meet seismic requirements.
05000443/LER-2010-00117 March 201010 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On March 15, 2010 during operation in mode 1 at 100% power, both trains of the containment enclosure emergency air cleanup system (CEEACS) were rendered inoperable due to an opening in the ventilation area boundary. For approximately five hours on March 15 and approximately 4 hours on March 17, a door in the containment enclosure boundary (CEB) was opened to support planned maintenance activities in the positive displacement charging pump room. Under accident conditions, the CEEACS maintains a negative pressure in the enclosure surrounding the containment to prevent uncontrolled releases of radioactivity into the environment.

However, the breach in the CEB created by the open door would have prevented both trains of the CEEACS from establishing the minimum required negative pressure in the enclosure. This condition placed the plant in Technical Specification (TS) 3.0.3, although it was unrecognized at the time, and resulted in a loss of safety function for the CEEACS. The causes of the event included lack of programmatic controls to ensure the control room is notified prior to propping open a CEB door and historical guidance that led the operators to believe that only TS 3.6.5.2, Containment Enclosure Boundary Integrity, applied when a CEB door was open. The planned corrective actions will strengthen an existing program to address opening CEB doors and revise the TS.

05000443/LER-2008-00110 CFR 50.73(a)(2)(iv)(A), System Actuation

At 2302 on January 19, 2008 while operating in mode 1 at 100% power, Seabrook Station experienced a turbine trip and subsequent reactor trip due to a fault on 345kV bus 3. This bus is located between the generator step-up transformer and the switchyard circuit beakers. The fault initiated a 345 kV bus lockout, which in turn tripped the main turbine and the circuit breakers associated with the unit auxiliary transformers (UAT), which normally supply the plant's 4,160 volt and 13,800 volt buses. The loss of the UATs initiated an automatic transfer of the plant buses to the alternate 345kV power source via the reserve auxiliary transformers.

The transient caused a loss of all four operating reactor coolant pumps (RCP) for approximately one hour. Due to the unavailability of presssurizer spray with all RCPs stopped, the pressurizer power-operated .relief valve automatically opened as designed to control reactor coolant system pressure. The operators restored normal pressurizer spray following the restart of one RCP at 0009 on January 20, 2008.

The cause of the 345kV bus fault was a failure of the operating shaft in the manually-operated disconnect switch for 345kV bus 3. On January 22, the plant entered mode 5. to repair 345kV bus 3 and returned to service on January 31, 2008. No adverse safety consequences resulted from this event.

05000443/LER-2007-00210 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On April 5, 2007 with the unit in Mode 1 at 100% power, Seabrook Station declared the turbine driven emergency feedwater pump (TDEFWP) inoperable because the turbine steam supply valve stroke time was outside its acceptable limit. The design basis stroke time for the steam supply valve is five to 15 seconds; however, a review of past surveillance tests revealed that the actual stroke time was less than five seconds. This condition, which rendered the TDEFWP inoperable, existed on three occasions because the surveillance test for measuring the valve's stroke time incorrectly specified a minimum stroke time of four seconds rather than five seconds.

The valve stroke time was adjusted and restored to an acceptable value. The cause of the event was a human error in 1989 that failed to identify that a design change inserted an incorrect minimum stroke time in station documents. While the technical specifications require a plant shutdown if an emergency feedwater pump is inoperable for greater than 72 hours, the plant continued to operate in Mode 1 for more than 72 hours on three occasions with the TDEFWP inoperable. Consequently, this event resulted in a condition prohibited by the technical specifications. The TDEFW pump remained functional and no adverse consequences resulted from this event.

05000443/LER-2006-001On January 31, 2006, at 1612 it was determined that a non-supervisory, station contract employee was incorrectly granted unescorted access to the protected area. A review of pre employment screening records from March 2005 related to fitness for duty records revealed that the employee's pre-access drug test revealed levels of marijuana metabolites that were higher than the allowed levels per 10 CFR 26. The test was incorrectly classified as negative by the site Medical Review Officer (MRO). A one-hour report (EN# 42297) was made to the NRC at 1'708 on January 31, 2006. The individual's site access was suspended and the Medical Review Officer was suspended.
05000443/LER-2005-00510 CFR 50.73(a)(2)(iv)(A), System Actuation

On April 13, 2005 at 0350 with the plant in Mode 6 and core reload in progress, an actuation of the reactor protection system (RPS) resulted from a low water level in steam generator (SG)-B.

While SG-B was in wet lay-up recirculation, an incorrect valve alignment resulted in an inadvertent transfer of water from SG-B to SG-D. This transfer of water lowered the level in SG-B to the low water level reactor trip setpoint, resulting in an actuation of the RPS. This valid actuation of the RPS did not actuate any other components because the reactor trip breakers were already open and the emergency feedwater system was removed from service. The cause of this event was an inadequate procedure. The procedure that controlled filling and recirculation of the SGs during shutdown did not include sufficient instructions to prevent transferring water between SGs. The corrective actions for this condition included revising the procedures to prevent cross-connecting the SG flow paths. No adverse consequences resulted from this event.

05000443/LER-2003-00110 June 200310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On June 10, 2003, due to a potential for a common mode failure found during preventive maintenance activities for the "A" Emergency Diesel Generator (EDG-1A), EDG-1B was started and run unloaded to satisfy the requirements of Technical Specification (TS) 3.8.1.1 action b.

A subsequent review conducted on June 18, 2003, determined that unloaded testing of EDG-1B did not adequately address the requirements of TS 3.8.1.1. EDG-1B was subsequently retested satisfactorily under loaded conditions.

Failure to complete the loaded run within the required action statement time constitutes noncompliance with the requirements of the action statement and is reportable as a condition prohibited by TS pursuant to 10 CFR 50.73(a)(2)(i)(B). LER 02-002-00 identified a condition where plant operators failed to start the operable EDG unit within 24 hours after discovery as required by TS 3.8.1.1 action b.

The cause of this event was the failure of Licensee personnel to understand the entire affect of a change to the Technical Specifications due to an inadequate license amendment review process and an inadequate response to TS 3.8.1.1 questions. Corrective actions include revising the TS change review process, and providing additional training for the Operations Department and personnel involved in the event.

There were no adverse safety consequences as a result of this event.

05000443/LER-2002-00210 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(b)

On July 24, 2002, with the plant operating at 100 % power, a surveillance test was performed on emergency diesel generator (EK) DG-1B (DG-1B). After approximately three hours of fully loaded operation of DG-1B, plant operators noted that the kilovolt amperage reactive (kVAR) indication was fluctuating. As a result of the fluctuation, plant operators subsequently shutdown the engine and declared DG-1B inoperable at 2302 on July 24, 2002.

Technical Specification (TS) 3.8.1.1 Action statement b. requires that when one diesel generator is inoperable, the operability of the remaining diesel must be demonstrated operable within 24 hours. TS 3.8.1.1 Action b. also identifies that the operability of the remaining diesel generator need not be verified if it has been successfully operated within the last 24 hours, or if currently operating, or if the diesel generator became inoperable due to 1.) Preplanned preventive maintenance or testing; 2.) An inoperable support system with no potential common mode failure for the remaining diesel generator, or 3.) An independently testable component with no potential common mode failure for the remaining diesel generator. Subsequent analysis of the event determined that the decision not to test DG-1A within 24 hours was not consistent with guidance provided in TS Bases section 3/4.8.1.

The failure to meet the requirements of TS 3.8.1.1 action b. is a condition prohibited by the Technical Specifications and is reportable pursuant to the requirements of 10 CFR 50.73(a)(2)(i)(B). Subsequent testing of DG-1A was satisfactorily completed at 0247on July 31, 2002. Additional corrective actions to prevent recurrence have been identified. There were no adverse safety consequences as a result of this event.

05000443/LER-2002-00128 May 200210 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 28, 2002, at 2:31 AM, with the plant in Mode 4, the Control Room Operator initiated a manual reactor trip due to the loss of indication for control rod L5 during control rod surveillance testing.

At the time of the event, control bank A was at 72 steps withdrawn; the other shutdown and control banks were fully inserted into the core. During the withdrawal of control bank A, a Digital Rod Position Indication (DRPI) urgent alarm was received indicating that the rod position indication for Control Bank A was invalid. Pursuant to Technical Specification 3.1.3.3, the reactor trip breakers were manually opened using the reactor trip switch. All rods fully inserted. All systems functioned as required. At the time of the event, reactor coolant temperature was approximately 276 degrees Fahrenheit and reactor coolant pressure was approximately 552 psig.

An eight-hour event notification to the Nuclear Regulatory Commission (NRC) was made pursuant to the requirements of 10CFR50.72(b)(3)(iv)(A). The event notification was 38947.

It was determined that DRPI rod L5 position indication card had failed in service. The failed card was replaced and the surveillance was completed satisfactorily.

This License Event Report is being submitted pursuant to the requirements of 10CFR50.73(a)(2)(iv)(A).

05000443/LER-1999-001, Forwards LER 99-001-00 for Event That Occurred at Seabrook Station on 990329.List of Commitments Made in Response to Ler,Encl28 April 1999
05000443/LER-1998-014, Forwards LER 98-014-00 for Event That Occurred at Seabrook Station on 981222.Encl 2 Is List of Util Commitments Made in Response to LER18 January 1999
05000443/LER-1998-013, Forwards LER 98-013-00 Re 981214 Discovery That Valves Were Not Included within Scope of Plant IST Program.Commitments Made by Util,Encl14 January 1999
05000443/LER-1998-008, Forwards LER 98-008-00 Re Inadvertent ESF Actuation Due to Personnel Error on 98062322 July 1998
05000443/LER-1998-006, Forwards LER 98-006-00 Re Seabrook Station 980611 Plant Shutdown Which Was Caused by Inoperability of Control Room Air Condition Subsystem10 July 1998
05000443/LER-1998-004, Forwards LER 98-004-00 Re Min Shift Crew Composition Event That Occurred on 980504.Rept Is Submitted Per Requirements of 10CFR50.73(a)(2)(i)3 June 1998
05000443/LER-1998-003, Forwards LER 98-003-00,re Class 1E 125 Vdc Battery Surveillance Testing Which Occurred on 98021719 March 1998
05000443/LER-1998-002, Re Potential Safety Injection Pump Runout Conditions Identified on 980113.LER 98-002-00 Retracted20 March 1998
05000443/LER-1998-001, Forwards LER 98-001-00 Re Inadequate ECCS Venting Surveillance for Event That Occurred on 980103.Event Being Reported,Per 10CFR50.73(a)(2)(i),10CFR50.73(a)(2)(ii), 10CFR50.73(a)(2)(v) & 10CFR50.73(a)(2)(vii)2 February 1998
05000443/LER-1997-016, Forwards LER 97-016-01 Re Event That Occurred on 971105 at Station.Ler Is Being Submitted to Retract LER 97-016-00, Which Was Determined to Be Unreportable9 February 1998
05000443/LER-1997-015, Forwards LER 97-015-00 for Seabrook Station for Event That Occurred on 971028.Event Being Reported Pursuant to 10CFR50.73(a)(2)(ii)26 November 1997
05000443/LER-1996-001, Repts That During 1996 One Challenge to Plant Pressurizer PORVs Was Identified.Description of Event in LER 96-001-00 Re Automatic Rt26 February 1997
05000443/LER-1995-001, Forwards LER 95-001 Re Inadequate Overtemperature Delta T & Overpower Delta T Channel Calibr7 July 1995
05000443/LER-1993-017, Forwards LER 93-017-00 Re Service Water Pump Discharge Check Valve Testing.Due to Administrative Error During Processing LER Not Submitted within 30 Days of Determination of Reportability as Required by 10CFR50.7318 October 1993
05000443/LER-1993-01330 August 1993
05000443/LER-1993-01226 August 1993
05000443/LER-1993-00727 August 1993
05000443/LER-1993-006, Forwards LER 93-006-00 Re Train a Svc Water Inoperability on 93040130 April 1993
05000443/LER-1992-019, Forwards LER 92-019-01 Re Delta T/Tavg Protection Channel Operational Test,Documenting Root Cause & Corrective Actions,Per Evaluation Ongoing at Time of LER 92-019-00 Submittal11 January 1993
05000443/LER-1992-013, Forwards LER 92-013-01 Re Tornado Design of Plant Doors. Submittal Documents Root Cause & Corrective Actions Ongoing at Time of LER 92-013-00 Submittal20 November 1992
05000443/LER-1992-002, Forwards License Amend Request 92-12 to License NPF-86, Changing TS to Correct Acceptance Value for Sum of RHR Sys Injection Line Flow Rates,Per LER 92-02-0022 October 1992
05000443/LER-1990-01727 July 1990
05000443/LER-1990-01624 July 1990
05000443/LER-1990-01520 July 1990
05000443/LER-1990-004, Forwards Util Commitment to Perform Visual Insp of Four Feedwater Sys Check Valves Dash Plate Capscrews During First Refueling Outage,Per LER 90-004-001 July 1991
05000443/LER-1989-006, Forwards LER 89-006-00 Re Misposition of Unborated Water Source Locked Valves.In Addition to Corrective Actions Review of Operating Experience Revealed No Specific Trends or Indications of Diminished Performance28 April 1989