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 Start dateReporting criterionEvent description
05000339/LER-2016-00130 July 2016
21 September 2016
On July 29, 2016, with Unit 1 and Unit 2 at 100 percent power in mode 1, Unit 2 Reactor Coolant System (RCS) unidentified leakage was noted to take a 0.05 gallons per minute step increase coincident with a similar increase in Unit 2 containment sump in-leakage. Subsequent containment entries identified a through wall leak existed in the controlled bleed-off piping associated with the Reactor Coolant Pump seal for 2-RC-P-1C. Due to the pressure boundary leakage, this event was reported at 1517 hours on July 30, 2016, in accordance with 10 CFR 50.72(b)(2)(i), for "The initiation of any nuclear plant shutdown required by the plant's Technical Specifications" and 10 CFR 50.72(b)(3)(ii)(A) for "Any event or condition that results in the condition of the nuclear power plant including its principle safety barriers, being seriously degraded." While in Mode 5, the controlled bleed-off piping associated with the RCP seal for 2-RC-P-1C was replaced. The health and safety of the public were not affected by this event.
05000339/LER-2015-0017 October 2015On October 7, 2015, at approximately 2147 hours, with Unit 2 operating at 100 percent power Mode 1, a high energy line break (HELB) door between the Unit 1 Turbine Building (TB) and the safety related Unit 2 Emergency Switchgear Room (ESGR) was determined to be slightly open and unlatched. The door was immediately latched closed. Investigation determined the door was unlatched for approximately 46 minutes. On October 8, 2015, at approximately 1647 hours, the Unit 2 ESGR was determined to be outside of the design analysis for a Unit 1 High Energy Line Break. At 1823 hours, an 8-hour Non-Emergency Report was made to the NRC in accordance with 10 CFR 50.72(b)(3)(ii)(B) as an unanalyzed condition and in accordance with 10 CFR 50.72(b)(3)(v)(A) & (D) as a condition that could have prevented the fulfillment of safety functions to shutdown the reactor and maintain it in a safe shutdown condition and mitigate the consequences of an accident. The health and safety of the public were not affected by this event.
05000339/LER-2014-00215 September 2014

On September 15, 2014, with Unit 2 defueled, debris that had the potential to be fuel fragments was located on the core plate directly below the B11 core location, where fuel assembly 4Z9 resided during Cycle 23.

Video inspection of fuel assembly 4Z9 identified that the top springs of two fuel pins were dislodged. Due to the fact that the fuel damage exceeded expected conditions, at 1454 on September 15, 2014, this event was reported as an eight hour report as per 10 CFR 50.72(b)(3)(ii)(A), any event or condition that results in the condition of the nuclear plant, including its principle safety barriers, being seriously degraded. Detailed video inspections estimated that 15 fuel pellets were dislodged from fuel assembly 4Z9. During efforts to identify and recover the fuel pellets, 7 fuel pellets worth of material were not found and have already or are expected to granulate into fine particles that will dissolve in low flow areas of the primary plant systems, or be removed by normal purification processes. Since the specific location of the 7 fuel pellets is undesignated and because those pellets contain licensed material in a quantity greater than 10 times the quantity specified in App. C of 10 CFR 20, a report was made at 1227 on September 30, 2014, pursuant to 10 CFR 74.11(a) and to 10 CFR 20.2201(a)(ii). The health and safety of the public were not affected by this event.

05000339/LER-2014-0012 February 2014

At 0859 on February 2, 2014, with Unit 2 operating at 100% power, the "A" Math Feedwater (MFW) Pump, 2-FW- P-1A, had a motor lead connection that grounded and caused the power supply breakers for 2-FW-P-1A to trip open. The standby MFW pump, 2-FW-P-1C, auto started, as designed. The Reactor Operator (RO) believed the standby pump did not auto start, since one of the Control Room indicating lights did not illuminate as expected.

The RO believed that only one MFW pump was running with two required for operation greater than 70% power. Based on this indication and the perceived loss of MFW, the RO initiated a manual reactor trip as directed in 2-AP-31. Although the remaining control room team members were aware that the standby pump had auto- started, they were unable to intervene in time to prevent the manual trip. Following the manual reactor trip, the unit was stabilized in Mode 3 at normal reactor coolant temperature and pressure. This event was reportable per 10CFR50.72(b)(2)(iv)(B) for actuation of the reactor protection system. Following the reactor trip, the Auxiliary Feedwater pumps automatically started as designed and provided makeup flow to the steam generators. This event was reportable per 10CFR50.72(b)(3)(iv)(A) for actuation of an Engineered Safety Feature (ESF) system. The health and safety of the public were not affected by this event.

05000339/LER-2013-0034 July 201310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

annunciator, 2G-B5 "Station Service Busses 2A-2B-2C UV Relay Trouble" alarmed and locked in. Troubleshooting indicated that the under voltage (UV) relay monitoring B-C phase for Station Service Bus 2A had actuated. The 2A UV channel was placed into trip on July 3, 2013, per Technical Specification 3.3.1 Condition L, but the 2A under frequency (UF) channel was not placed into trip. On July 3, 2013, a multidiscipline team, including the vendor, determined that the UF relay would remain operable with the degraded voltage. An Operability Determination was developed and approved to document the conclusion. However, on July 10, 2013, it was revealed through additional testing that the operability determination contained inaccurate information and the 2A UF relay would not operate within the required time frame. The 2A UF relay channel was subsequently placed in trip on July 10, 2013. A potential transformer blown fuse was replaced and the UV and UF channels were restored to operable on July 22, 2013.

This event is reportable pursuant to 10CFR50.73(a)(2)(i)(B) for a condition prohibited by Technical Specifications (TS) when the inoperable UF channel was not placed into trip within the time limits of TS. The health and safety of the public were not affected by the event.

05000339/LER-2013-00210 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation
' On May 28, 2013, at 1507 hours with Unit 2 operating at 98 percent power (Mode 1), a manual reactor trip was initiated due to a main feedwater system transient. The main feedwater system transient resulted from the spurious closure of the "C" Main Feedwater Pump Discharge Motor- Operated Valve, 2-FW-MOV-250C, that subsequently resulted in the tripping of "A" Main Feedwater pump on low suction pressure. The cause of the spurious closure of 2-FW-MOV- 250C was a loss of conductivity in the upper cell switch of breaker 2-EP-BRK-25C5 which indicated that one motor on 2-FW-P-1C had tripped. At 1809 hours, a 4 hour report was made to the NRC in accordance with 10CFR50.72(b)(2)(iv)(B) for a Reactor Protection System (RPS) actuation and a 8 hour report in accordance with 10CFR50.72(b)(3)(iv)(A) for a Auxiliary Feedwater system actuation. The event is reportable pursuant to 10CFR50.73(a)(2)(iv)(A) for a condition that resulted in the automatic actuation of the RPS and AFW Systems. The health and safety of the public were not affected by the event.
05000339/LER-2011-00128 September 201110 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

On August 23, 2011, at 1440 hours with Units 1 and 2 offline, as a result of the Central Virgirfa earthquake, the Unit 2 "H" (2H) emergency diesel generator (EDG) was manually tripped due to a coolant system leak forty-nine minutes after its demand start due to a loss of offsite power. A Root Cause Evaluation determined the 2H EDG could have developed a coolant leak during its next operation (i.e., post maintenance or periodic testing or a demand start). On September 28, 2011 a completed prior operability evaluation determined the 2H EDG gasket failure resulted in fault exposure unavailable hours totaling 337.6 hours. During the fault exposure unavailable hours, approximately fourteen days, the limiting action of TS 3.8.1.b was entered three times.

Had a demand start of the 2H EDG occurred during any of these times the gasket failure could have occurred resulting in more than one inoperable EDG. This event is reportable pursuant to 10 CFR 50.73(a)(2)(v)(A), 50.73(a)(2)(v)(B), and 50.73(a)(2)(v)(D) for a condition that could have prevented fulfillment of the safety function of a system required to maintain the reactor in a safe shutdown condition, remove residual heat, and mitigate the consequences of an accident.

The event posed no significant safety implications and the health and safety of the public were not affected by the event.

05000339/LER-2010-00328 May 201010 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On May 28, 2010, at 0004 hours North Anna Unit 2 experienced an automatic Reactor trip from 100 percent power following a lightning strike in the switchyard.DAt 0014 to 0027 hours a primary grade make-up to the blender was performed.DSubsequently, it was determined that the surveillance requirement to ensure valves in the affected flow path are secured closed was not performed.DAt 0104 hours the primary grade (PG) supply valve was secured closed.

DHowever, the fifteen minute isolation requirement of Technical Specifications (TS) 3.1.8 was not met.DDue to the high volume of activities associated with the automatic reactor trip and loss of power Operations personnel failed to secure the PG supply valve within the required time.DThis event is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B) for a condition prohibited by TS.DThis event posed no significant safety implications since the dilution flow path was isolated. Therefore, the health and safety of the public were not affected by this event.

05000339/LER-2010-00210 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 28, 2010, at 0004 hours North Anna Unit 2 experienced an automatic Reactor trip from 100 percent power following a lightning strike in the switchyard. A combination of events precluded the transfer of the "B" Station Service (SS) bus to the "B" Reserve Station Service Transformer (RSST), 'resulting in the "B" SS bus being de-energized and a consequential loss of power to Unit 2 reactor coolant pump 1B (2-RC-P-1B). Unit 2 tripped on low flow in the "B" RCS loop. All available Engineered Safety Feature equipment responded as designed. A non-emergency 4-hour report was made to the NRC Operations Center at 0323 hours on May 28, 2010, in accordance with 10 CFR 50.72(b)(2)(iv)(B). An 8-hour report was also made in accordance with 10 CFR 50.72(b)(3)(iv)(A) due to actuation of the Auxiliary Feedwater System (AFW). This event is reportable pursuant to 10 CFR 50.73(a)(2)(iv)(A) for a condition that resulted in automatic actuation of the reactor protection system and the AFW system. This event posed no significant safety implications since the reactor protection system functioned to trip the reactor. Therefore, the health and safety of the public were not affected by this event.

05000339/LER-2010-00110 CFR 50.73(a)(2)(iv)(A), System Actuation

On April 27, 2010 at 1637 hours, with Unit 2 in Mode 1 at 74% power during recovery from a refueling outage, an automatic reactor trip occurred while testing a new digital automatic voltage regulator (AVR). A turbine trip due to a generator lockout caused the automatic reactor trip. The direct cause of the generator lockout protective relay actuation was the incorrect operability curve set points derived from the voltage regulator Minimum Excitation Level (MEL) tuning software.

Following the reactor trip, all control rods inserted into the core and decay heat was removed using the normal steam dump system. The Auxiliary Feedwater (AFW) Pumps received an automatic start signal due to low/low level in the steam generators following the reactor trip. Following the automatic start of the Turbine Driven AFW (TDAFW) pump, the Control Room received annunciator alarm (F-D8). This was an AFW Pump Trouble or Lube Oil Trouble alarm. An operator was dispatched and reported that oil was spraying from the pump bearings and reservoir. The TDAFW pump was secured and declared inoperable.

This event is reportable per 10 CFR 50.73(a)(2)(iv)(A) for the automatic actuation of the Reactor Protection System and AFW System. No significant safety consequences resulted from this event. Steam Generator inventory was restored to the normal operating level. Therefore, the health and safety of the public were not affected by this event.

D

05000339/LER-2008-0018 February 2008

On February 8, 2008, Unit 2 was in Mode 3, zero percent power, preparing for restart following a planned maintenance outage. At 1759 hours, a rod control urgent failure alarm was received while withdrawing the "A" Shutdown Bank control rods. Rod withdrawal was stopped and it was noted that the Group Step Counters deviated by three steps.A As a result, at 1812 hours a manual reactor trip was initiated by opening the reactor trip breakers in accordance with Technical Requirement 3.1.3. This is a valid actuation of the Reactor Protection System. Four suspect cards were replaced in Power Cabinet 2AC.

Following card replacement the reactor trip breakers were closed.A Shutdown Banks "A" and "B" were fully withdrawn with no concerns. On February 8, 2008, at 1959 hours, a non- emergency 8-hour report was made in accordance with 10 CFR 50.72(b)(3)(iv)(A) due to actuation of the Reactor Protection System. This event is reportable pursuant to 10 CFR 50.73A (a)(2)(iv)(A) for aA condition thatA resulted inAA manualA actuationA of theA Reactor Protection System. This event posed no significant safety implications because the reactor was subcritical when the reactor trip breakers were opened. Compliance with all Technical Requirements was maintained. Therefore, the health and safety of the public were not affected by this event.

A

05000339/LER-2007-00127 February 200710 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

On February 27, 2007, at 1620 hours, with North Anna Unit 2 operating at 100% power (Mode 1), Unit 2 Safeguards exhaust bypass dampers 2-HV-AOD-228-1 and 2-HV-AOD-228-2 were found to have leak-by during the performance of Periodic Test (PT) 0-PT-77.14A, Emergency Core Cooling System (ECCS) Pump Room Exhaust Air Cleanup System (PREACS) Train A Filter In-Place Test (1-HV-FL-3A). This condition rendered both trains of Safeguards exhaust inoperable. This placed Unit 2 in Technical Specification (TS) Limiting Condition of Operation (LCO) 3.0.3. Operations personnel began a unit ramp-down at 1947 hours and a 4-hour Non- Emergency Report was made to the NRC at 2215 hours, in accordance with 10 CFR 50.72(b)(2)(i), for the initiation of any nuclear plant shutdown required by the plant's Technical Specifications. At 2220 hours, with Unit 2 at 32% power, the TS action was cleared after installation of a temporary modification that restored the system to OPERABLE. The cause of the event was improper linkage adjustment and actuator preload that resulted in less than full damper closure.) This event is reportable pursuant to 10 CFR 50.73(a)(2)(i)(B), 10 CFR 50.73(a)(2)(v)(C), and 10 CFR 50.73 (a)(2)(vii). No significant safety implications existed because the ECCS PREACS ventilation filters were not called upon to perform their safety function and the unfiltered ECCS leakage limit was not being challenged.

)

05000339/LER-1998-004, Forwards LER 98-004-00,IAW 10CFR50.73.Commitments Made by Util,Listed6 October 1998
05000339/LER-1998-002, Forwards LER 98-002-00,applicable to North Anna Unit 2.Rept Has Been Reviewed by Station Nuclear Safety Operating Committee & Will Be Forwarded to Mgt Safety Review Committee for Review6 May 1998
05000339/LER-1998-001, Forwards LER 98-001-00,reviewed by Station Nuclear Safety Operating Committee & Will Be Forwarded to Mgt Safety Review Committee for Review30 April 1998
05000339/LER-1995-002, Forwards LER 95-002 Re Missed Surveillance on Individual Rod Position Indication20 July 1995
05000339/LER-1995-001, Forwards LER 95-001 Re Main Steam & Pressurizer Safety Valve Setpoints Out of Tolerance Due to Setpoint Drift27 April 1995
05000339/LER-1993-0054 October 1993
05000339/LER-1993-00212 August 1993
05000339/LER-1989-003, Advises of Change in Reportability for LER 89-003-00 Re 10 Containment Isolation Valves W/Excessive Leak Rates14 November 1990
05000339/LER-1983-031, Forwards LER 83-031/03L-05 May 1983
05000339/LER-1983-030, Forwards LER 83-030/03L-029 April 1983
05000339/LER-1983-028, Forwards LER 83-028/03L-029 April 1983
05000339/LER-1983-027, Forwards LER 83-027/03L-021 April 1983
05000339/LER-1983-026, Forwards LER 83-026/03L-020 April 1983
05000339/LER-1983-025, Forwards LER 83-025/03L-020 April 1983
05000339/LER-1983-024, Forwards LER 83-024/03L-014 April 1983
05000339/LER-1983-023, Forwards LER 83-023/03L-05 May 1983
05000339/LER-1983-022, Forwards LER 83-022/03L-023 March 1983
05000339/LER-1983-021, Forwards LER 83-021/03L-023 March 1983
05000339/LER-1983-020, Forwards LER 83-020/03L-030 March 1983
05000339/LER-1983-019, Forwards LER 83-019/03L-023 March 1983
05000339/LER-1983-018, Forwards LER 83-018/03L-023 March 1983
05000339/LER-1983-017, Forwards LER 83-017/03L-010 March 1983
05000339/LER-1983-015, Forwards LER 83-015/03L-028 February 1983
05000339/LER-1983-014, Forwards LER 83-014/03L-09 February 1983
05000339/LER-1983-013, Forwards LER 83-013/03L-031 January 1983
05000339/LER-1983-012, Forwards LER 83-012/03L-011 February 1983
05000339/LER-1983-010, Forwards LER 83-010/03L-031 January 1983
05000339/LER-1983-009, Forwards LER 83-009/03L-031 January 1983
05000339/LER-1983-007, Forwards LER 83-007/03L-028 February 1983
05000339/LER-1983-006, Forwards LER 83-006/03L-02 February 1983
05000339/LER-1983-005, Forwards LER 83-005/03L-01 February 1983
05000339/LER-1983-004, Forwards LER 83-004/03L-019 January 1983
05000339/LER-1983-003, Forwards LER 83-003/03L-019 January 1983
05000339/LER-1983-001, Forwards LER 83-001/03L-018 February 1983
05000339/LER-1982-086, Forwards LER 82-086/03L-017 January 1983
05000339/LER-1982-082, Forwards LER 82-082/03L-022 December 1982
05000339/LER-1982-081, Forwards LER 82-081/03L-015 December 1982
05000339/LER-1982-080, Forwards LER 82-080/03L-022 December 1982