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 Start dateReporting criterionEvent description
05000316/LER-2017-00123 March 2017
19 May 2017
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On March 23, 2017, at 0941, Eastern Daylight Time (EDT), with Unit 2 in Mode 1 at 100% power, the Unit 2 Containment CEQ Fan #1 Backdraft Damper opening force exceeded the Technical Specification (TS) Surveillance Requirement (SR) limit.

Maintenance was performed on the damper and operability of the Unit 2 CEQ Fan #1 was restored at 1724 EDT. A past operability evaluation was performed and determined that the condition likely existed since maintenance was performed to lubricate the damper on February 24, 2017. As a result, the Unit 2 CEQ Fan #1 was inoperable longer than allowed by TS. During this time, the Unit 2 CEQ Fan #2 was declared inoperable to perform surveillance testing on March 2, 2017, from 0938 Eastern Standard Time (EST) until 1326 EST. This resulted in both trains being inoperable simultaneously for a short period of time.

The cause of the elevated force required to open the Unit 2 CEQ Fan #1 Backdraft Damper was determined to be that the lubrication Preventive Maintenance (PM) work order instructions were not adequate and did not provide adequate Post-Maintenance Testing (PMT) instruction. Corrective action is to revise model work order tasks to provide additional details and appropriate PMT. The risk significance of this condition has been determined to not constitute a significant increase in risk.

This event is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) and 10 CFR 50.73(a)(2)(v)(D).

05000316/LER-2016-00213 December 2016
9 February 2017

On December 13, 2016, the Unit 1 AB Emergency Diesel Generator (EDG) developed a fuel oil leak from a fuel injector pump Delivery Valve Holder (DVH) during a maintenance run of the diesel. On December 21, 2016, with Unit 1 in Mode 1 at 100 percent power and Unit 2 in Mode 4 during a refueling outage, it was determined that the failed DVH on the Unit 1 AB EDG was due to a design and manufacturing issue. Subsequently the Unit 1 CD EDG, Unit 2 AB EDG, and Unit 2 CD EDG were conservatively declared inoperable due to multiple affected diesel fuel pump DVHs being installed on each EDG.

The Root Cause was determined to be due to insufficient Corrective Action Program oversight by Engineering to ensure product quality and issue resolution in relation to a previous EDG DVH failure in 2013. Testing is being conducted to determine the resulting impact to associated EDGs. The affected DVHs have been replaced.

A Loss of Safety Function was reported via Event Notification 52456 for Unit 2 in accordance with 10 CFR 50.72(b)(3)(v)(D). The Loss of Safety Function is required to be reported in a Licensee Event Report in accordance with "50.73(a)(2)(v)(D) Event or Condition that Could Have Prevented Fulfillment of a Safety Function.

05000316/LER-2016-0016 July 2016
31 August 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation

On July 6, 2016, with the Donald C. Cook Nuclear Plant Unit 2 Reactor operating in Mode 1 at 100 percent power, the control room received a report of a steam leak on the Unit 2 B Right Moisture Separator Reheater (MSR)

  • crossover piping and damage to the turbine building structure. This information resulted in a decision by the crew to manually trip the Unit 2 Reactor at 0038. The cause of the steam leak was the sudden failure of the balance bellows on the Unit 2 B Right MSR crossover expansion joint, which also resulted in damage to the west wall of the turbine building.

The Root Cause was determined to be an organizational failure to recognize the risk significance of, and to adequately correct or mitigate, previously identified vibration issues with the Unit 2 B Right MSR crossover expansion joint tie rod and bellows in a timely fashion.

This event is being reported in accordance with 10CFR 50.73(a)(2)(iv)(A) as a manual actuation of the Reactor Protection System and an automatic actuation of the Auxiliary Feedwater system.

05000316/LER-2015-00123 April 2015
15 January 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

On April 23, 2015, at 0210, Donald C. Cook Nuclear Plant Unit 2 Reactor was manually tripped from approximately 2 percent of rated thermal power during plant restart following a refueling outage. Unit 2 Reactor was manually tripped due to the inability to maintain Average Reactor Coolant System Temperature above the Technical Specification (TS) required minimum Temperature for Criticality when two newly installed Steam Dump Valves failed open while being manually valved into service. The valves were subjected to, but not designed for, two phase flow.

The Root Cause has been determined to be that the modification process failed to identify and document all system operational vulnerabilities. The corrective action to preclude repetition is an enhancement of the Engineering Modifications procedure to require development and inclusion of a narrative to describe system operation, including key interfacing system operation.

The manual Reactor Protection System (RPS) actuation was reported via Event Notification 51004 in accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A), and 10 CFR 50.72(b)(2)(i). The valid RPS actuation and the completion of the plant shutdown required by TS are reportable as a Licensee Event Report in accordance with (- 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(2)(i)(A) respectively.

05000316/LER-2013-00128 July 201310 CFR 50.73(a)(2)(iv)(A), System Actuation

On July 28, 2013, the Donald C. Cook Nuclear Plant Unit 2 reactor was operating at 100 percent power. At 1018, reactor operators manually tripped the reactor when reaching a low steam generator level threshold during a secondary plant transient event.

The secondary plant transient occurred when a steam supply valve closed to the Right Moisture Separator Reheater which resulted in feedwater heater level oscillations followed by Heater Drain Pumps tripping on heater low levels. This caused feedwater pump suction pressure to lower and automatically tripped the West Main Feedwater Pump. As a result, steam generator level lowered to 23 percent on the #4 Steam Generator. The reactor operators manually tripped the reactor based on a manual trip threshold for Steam Generator levels that was established by the Unit Supervisor.

The initiating cause of the steam supply valve closure and subsequent secondary plant transient was a loss of control air to the air operated valve resulting from fretting of the control air line.

The Reactor Protection System and the specified Auxiliary Feedwater System actuation was reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The valid actuation is reportable as a Licensee Event Report (LER) in accordance with 10 CFR 50.73(a)(2)(iv)(A).

05000316/LER-2003-00530 December 2003On December 30, 2003, at approximately 1328 Eastern Standard Time, the Unit 2 reactor automatically tripped on low steam generator water level coincident with feed flow less than steam flow for Steam Generator #22. Just prior to the trip, the Control Room Instrument Distribution (CRID) IV inverter transferred to the alternate power supply. A Feedwater Isolation Relay (K666X2), powered from CRID IV, opened. The opening of the relay initiated a seal-in closure signal to Steam Generator #22 and #23 Feedwater Isolation Valves (2-FMO-202 and 2-FMO-203), resulting in a loss of feedwater flow to Steam Generators #22 and #23 and produced a low steam generator water level trip coincident with feed flow less than steam flow. Following the reactor trip, the Unit Output Breakers failed to automatically open because a Main Turbine Stop Valve position indicator failed to provide a closed indication. The Unit Output Breakers were manually opened in accordance with the reactor trip response procedure. All safety components started and performed as expected. The initiator of the reactor trip was determined to be a momentary ground on the GRID IV bus, which occurred during the conduct of instrument calibration. The ground caused the automatic transfer of CRID IV to the alternate power source. The voltage drop on the CRID IV bus caused the Feedwater Isolation Relay to open. The root cause of the event has been determined to be inattention on the part of the Instrument and Control Technician who was performing the calibration. Corrective actions include the establishment of enhanced controls for the disconnecting and connecting of electrical leads.
05000316/LER-2003-00426 April 200310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On April 26, 2003, Donald C. Cook Nuclear Plant (CNP), during the performance of a routine inspection of the ice bed within the Unit 2 ice condenser, identified that ice basket 11-7-1 weighed 1125 pounds (lbs.). Technical Specification (TS) 3.6.5.1d requires that the ice bed shall be OPERABLE with each ice basket containing at least 1144 lbs. of ice (end-of-cycle). Therefore, the weight of ice basket 11-7-1 did not meet the minimum required weight specified in TS 3:6.5.1d.

This condition is reportable pursuant 10 CFR 50.73(a) (2) (i) (B). During the extent of condition evaluation for this event, CNP discovered that during the Unit 1 2002 refueling outage ice basket 2 4 - 1 - 7 fell below the minimum TS weight limit. Ice basket 24-1-7 was emptied and refilled with 1445 lbs. of ice. This condition was not recognized as being reportable at that time. The failure to initiate an LER for ice basket 24-1-7 has been entered into the CNP corrective action program and will be reported in LER 50-315/2002-008-00.

Ice basket 11-7-1 was emptied, inspected for damage, and refilled with 1484 lbs. of borated ice. Additionally, in accordance with TS 4.6.5.1.b.2, upon discovery of the low weight in ice basket 11- 7-1, an additional 20 ice baskets within the same bay were weighed. The average weight of the 20 additional ice baskets and the discrepant basket (ice basket 11-7- 1) was greater than 1144 lbs. Additional administrative requirements will be added to the ice basket inspection procedure to ensure discrepant conditions are evaluated prior to the basket being emptied.

05000316/LER-2003-0038 March 2003

This supplemental LER is being issued to update the causal and corrective action statements. At 0400 hours on March 5, 2003, Technical Specification (TS) Limiting Condition for Operation (LCO) 3.7.1.2, Action "a" was entered to perform routine maintenance on the Unit 2 West Motor Driven Auxiliary Feedwater (MDAFW) pump. During post-maintenance testing, a loud 'buzzing" noise was heard emanating from the vicinity of the pump motor. A supporting/refuting evaluation was performed, which eliminated the pump, breaker, or system alignment as the possible source of the noise. At this point, the decision was made to replace the suspect motor. Initially, Indiana Michigan Power (I&M) had expected to complete the replacement of the West MDAFW pump motor within the allowed outage times specified in TS 3.7.1.2. However, unanticipated delays prevented the completion of this activity within the allowed outage time.

Therefore, I&M requested, and was granted, enforcement discretion on March 8, 2003. .

The apparent cause of the Unit 2 West MDAFW pump motor noise was loose air baffles due to mounting hole deformation as determined by the vendor's as found condition analysis. The cause for the failure to complete the motor replacement within the allowed outage time was inconsistent maintenance work practices and inadequate interface requirements that resulted In a lack of command and control process for short term LCO activities. Corrective actions to prevent recurrence included the establishment of administrative guidance to ensure the appropriate techniques and tools are used when performing work on critical components, and the development and satisfactory completion of coupling installation training. Also, going forward, KM established a team to respond to equipment issues that challenge short duration allowed outage time.

I&M determined that no net Increase in risk was associated with extending the TS 72-hour allowed outage time by an additional 36 hours to restore the West MDAFW pump to an operable status. Although the proposed action deviated from a requirement In TS 3.7.1.2, it did not affect any safety limits, setpoints in the TS, or other operational parameters, nor did it affect any margins assumed In the accident analyses. In addition, the redundant Unit 2 East MDAFW pump and TDAFW pump continued to be operable to perform their required design function. The Unit 2 West MDAFW pump motor was replaced with a spare motor and the pump was declared operable at 0246 hours on March 9, 2003.

05000316/LER-2002-0075 November 2002

On November 2, 2002, at 0827 hours, the Unit 2 CD Emergency Diesel Generator (EDG) , was declared inoperable and Technical Specification (TS) 3.8.1.1, Action "b", was entered in preparation for routine surveillance testing in accordance with TS 4.8.1.1.2 . a . 5 . T Within approximately 10 minutes after reaching full load of 3500 kilowatts (kW) during the surveillance test, the CD EDG load began oscillating approximately 150 kW. T The amount of time required to correct this condition exceeded the 72-hour allowed outage time requirements of TS 3.8.1.1, Action "b". T Donald C.

Cook Nuclear Plant (CNP) requested and received enforcement discretion from the Nuclear Regulatory Commission (NRC), to extend the 72-hour allowed outage time by an additional 72 hours. T The purpose of this extension was to allow sufficient time to restore the Unit 2 CD EDG to operable status and exit TS 3.8.1.1, Action "b". T CNP evaluated the described condition and determined that the risk of operating an additional 72 hours with the Unit 2 CD EDG unavailable was less than the risk associated with a plant shutdown. T The apparent cause of the load oscillations was a failure of the electronic governing module in the EDG speed governing system.

Corrective actions include replacement of the governor. T A formal root cause analysis is in progress to ensure adequate corrective actions to prevent recurrence are identified and implemented.

05000316/LER-2002-006

At 0045 hours on July 22, 2002, Unit 2 tripped due to low condenser vacuum. At the time of the trip, operators were performing a flush of the main condensers in preparation for the upcoming biocide treatment of the circulating water system. In accordance with 10 CFR 50.72 (b)(2)(iv)(B), a four-hour ENS notification (Event # 39081) was made to the NRC on July 22, 2002, at 0233 hours for an event or condition that resulted in an actuation of the reactor protection system (RPS) when the reactor is critical. As such, this LER is being submitted in accordance with the requirements of 10 CFR 50.73 (a)(2)(Iv)(A) for a condition or event that resulted in an automatic actuation of the RPS system.

The apparent cause of the event is a previously unrecognized steam side heat transfer anomaly in "C" main condenser that has resulted in "C" North water box removing significantly more heat than in "C" South water box. Corrective actions to prevent recurrence of this event will be determined by an equipment root cause investigation to be performed after the steam side of the "C" main condenser has been inspected during the next Unit 2 outage of sufficient duration. Additional corrective actions, including preventive actions, may be developed based on the results of the investigation. If significant changes are identified as a result of completion of the root cause investigation, an update to this LER will be submitted.

As a compensatory action, the main condenser water box flushing and isolation procedure has been revised to provide improved guidance for performing these activities to minimize the possibility of a unit trip The safety significance of this event was minimal. Plant systems responded per design with no significant anomalies noted. Plant procedures and operator training provided sufficient direction for control room personnel to shutdown the plant and maintain it in a safe shutdown condition. There was no impact on the health and safety of the public as a result of this event

05000316/LER-2002-00512 May 2002

At 2301 firs on May 12, 2002, Unit 2 tripped due to an instrument rack power supply failure. Specifically, the second of two redundant 24-volt direct current (VOC) power supplies to reactor control instrumentation control group cabinet 2-PS-CGC-16 failed. The failure of both power supplies caused steam generator (SG) feedwater regulating valve 2-FRV-210 to close. Unit 2 subsequently tripped on low water level in SG-21 coincident with low feedwater flow. In accordance with 10 CFR 50.72 (b)(2)(iv)(B), a four-hour ENS notification (Event #38915) was made to the NRC on May 13, 2002, at 0255 hours for an event or condition that resulted in an actuation of the reactor protection system (RPS) when the reactor is critical. As such, this LER is being submitted in accordance with the requirements of 10 CFR 50.73 (a)(2)(1v)(A) for a condition or event that resulted in an automatic actuation of the RPS system.

The preliminary cause of this event was age-related failure of components within the power supplies. A contributing factor was that no provisions existed for periodic monitoring of the power supplies.

This event had minimal safety significance since plant procedures and operator training provided sufficient direction for control room personnel to shutdown the plant and maintain it in a safe shutdown condition. The failed 24-VDC power supplies were replaced. The remaining 24-VDC control group power supplies in Unit 2 were inspected and one power supply was replaced. Routine tasks have been established to verify the availability of the 24-VDC power supplies for both Unit 1 and Unit 2.

05000316/LER-2002-00419 January 2002

At 00:01 hours on 01/19/02, in preparation for a Unit 2 refueling outage, Operations shift personnel initiated a planned manual reactor trip of Unit 2 from 22t power per Procedure 02-OHP-4021-001-003, Revision 15, T "Power Reduction." T Shortly thereafter, an automatic start of the turbine driven auxiliary feedwater pump (TDAFP) occurred as a result of a valid low-low level indication in the steam generators. T The automatic start of the TDAFP was determined to be an "unanticipated" engineered safety feature (ESF) actuation.

Steam generator levels rapidly recovered. T Operators secured the"TDAFP and throttled the flows from the motor driven auxiliary-feedwater pumps in accordance with plant procedures for reactor trip response and recovery. T Reactor coolant system cooldown and depressurization proceeded normally. T During the trip, pressurizer level shrank lower than procedurally anticipated, resulting in a reactor coolant system 'letdown isolation.

At 07:56 on 01/19/02, the Shift Manager made an eight hour, non-emergency notification to the NRC (EN# 38640) per 10 CFR 50.72(b)(3)(iv)(A) for an unanticipated ESF actuation. T The cause of this event was inadequate procedural guidance. T Corrective actions included revision of the applicable procedures to include a reduction in the planned power level trip point to reduce the potential for automatic start of the TDAFP.

05000316/LER-2002-0033 April 200210 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

During the weekly battery surveillance on April 3, 2002, a maintenance electrician identified cracks in the top cover between the post seals and the sample tubes of battery cells 27 and 102 of the 2AB 250-volt D.C. battery bank. The cracks were above the electrolyte with no indications of electrolyte leakage observed. The time of identification was 1200 on April 3, 2002. An action request was generated at 1530 on April 3, 2002, to document the deficiency. Shift manager notification was not made by the initiator or supervisor performing the approval as required by procedure. Operations became aware of the equipment deficiency at 1700 on April 4, 2002, when a deficiency tag was processed for the 2AB battery. The Shift Manager visually confirmed the cracking on cells 27 and 102, and identified, during an extent of condition inspection, that cell 35 exhibited the same cracking phenomenon. The 2AB battery was declared INOPERABLE at 1812 and Unit 2 entered technical specification (TS) action statement 3.8.2.3.b. A TS required shutdown commenced at 2114 on April 4, 2002, when the battery was not returned to an operable status.

A four-hour ENS notification, event number 38832, was made at 2330 on April 4, 2002, in accordance with 10 CFR 50.72(b)(2)(i) for an initiation of a reactor shutdown required by the plant's TS.

The TS required shutdown was terminated at 0145 on April 5, 2002, when a Notice of Enforcement Discretion (NOED) was granted by the Nuclear Regulatory Commission (NRC). In granting the NOED, the NRC would not enforce the allowed outage time in TS action 3.8.2.3.b for 13 hours, thereby providing an additional 11 hours for restoration of the 2AB battery to an OPERABLE status. The three cracked battery cells were replaced and 2AB battery was declared OPERABLE at 0755 on April 5, 2002. Unit 2 subsequently returned to full power.

05000316/LER-2002-00212 February 2002

On February 12, 2002, Technical Specification (TS) 3.9.4.c was violated when the 100 PSI Control Air to Containment Control Air Header #2 Train 'B' Containment Isolation Valve, 2-XCR-101(EllS:LKSHV), was stroked open during core alterations with open test connections on both sides of the valve, one inside containment and one outside. This configuration provided direct access from the containment atmosphere to the outside atmosphere. The apparent cause was determined to be ineffective procedural control (02-OHP-4030.STP.041). The preferred method for establishing refueling integrity for 2-CPN-74 in the procedure does not consider the possibility that the control air ring headers may be cross-tied. A contributing cause was that the installation of containment control air header cross-tie jumpers was not documented in the Proceduralized Temporary Modification Log on January 20, 2002.

Upon discovery that the preferred method used to maintain refueling integrity for 2-CPN-74 was ineffective, an alternate method was established and valve 2-XCR-101 was visually confirmed to be intact and closed. The Temporary Modification Log Index was reviewed to verify that other Temporary Modifications were logged. The containment control air cross-tie jumpers were documented in the log at that time.

The refueling integrity procedures will be revised to ensure that the methods used to establish refueling integrity for Penetrations CPN-74 and CPN-29 recognize that the Containment Control Air headers may be cross-tied. Unit 1 and Unit 2 Type B and C Leak Rate Testing procedures will be revised to ensure that steps are added for documenting the placement of the containment control air header cross tie jumpers in the Proceduralized Temporary Modification Log.

05000316/LER-2002-00126 January 2002

On January 26, 2002, during refueling outage 13, 10 CFR 50 Appendix J, Type B and C leak rate testing was being performed in accordance with procedure 02-EHP-4030-234-203, "Unit 2 B & C Leak Rate." This procedure requires root shutoff valve 2-GPX-301-V1 (ElISIK:SHV) from the nitrogen supply manifold to be in the closed position for testing.

When core alterations commenced, valve 2-GPX-301-V1 was thought to be tagged "Do Not Operate" in the closed position as required by procedure 02-OHP-4030-STP-041, "Refueling Integrity". Upon successful completion of the leak rate testing, an auxiliary equipment operator (AEO) found the root shutoff valve 2-GPX-301-V1 in the open position during the valve lineup restoration. This resulted in refueling integrity being lost while fuel movement was in progress. The control room was notified and core alterations were suspended. Based on investigation of this incident, the valve was mispositioned for approximately 10 hours. This breach of refueling integrity is prohibited by Technical Specification (TS) and is therefore reportable in accordance with 50.73(a)(2)(i)(B).

The cause of this event was failure to follow procedures. The AEO performing the initial valve lineup for testing opened valve 2-GPX-301-V1 and inappropriately pulled the "Do Not Operate" tag from the valve contrary to the requirements of plant procedures 02-EHP-4030-234-203 and 02-0HP-4030.STP.041.

Operations restored valve 2-GPX-301-V1 to the closed position, thereby re-establishing refueling integrity. A review of the completed B & C test lineups impacting refueling integrity was conducted and verified that no other loss of containment integrity had occurred during core alteration. A lessons learned memo was published and distributed to the auxiliary equipment operators. The human performance and personal accountability aspects of this issue have been appropriately addressed.

05000316/LER-2001-0047 October 2001

On October 7, 2001, a reactor trip occurred at 8 percent reactor power. The trip was the result of a loss of rod control system voltage. The cause of the loss of rod control system voltage was an open resistor at the input to the north control rod drive motor generator (CRD-MG) voltage regulator. The open resistor caused a low voltage transient when the north CRD-MG field collapsed. A protective auxiliary relay removed power from the south CRD-MG voltage regulator resulting in a loss of rod control system voltage. The loss of voltage caused all control rods to rapidly insert, thereby, initiating a Power Range, Neutron Flux, High Negative Rate trip from the reactor protection system (RPS). The RPS actuation was initiated by actual plant conditions that satisfied the requirements for the initiation of the trip, and was, therefore, a valid RPS actuation.

The failed resistor was determined to be the result of a random component failure. The resistor was original equipment and inspection revealed no evidence of overheating or manufacturing defect. The defective resistor was replaced and, as a precaution, the remaining series resistor in the north CRD-MG along with the identical resistors in the south CRD-MG were replaced.

This event was reported in accordance with 10 CFR 50.72(b)(1)(iv)(B).

05000316/LER-2001-00329 August 200110 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
This supplemental LER was issued to identify the correct the reporting requirement for submittal of the LER. No other changes were made. On August 29, 2001, Donald C. Cook Nuclear Plant (CNP) Unit 1 was in MODE 5 for a planned maintenance outage and Unit 2 was in MODE 1. Unit 2 Operations personnel were performing a routine surveillance test of the Essential Service Water (ESW) system in accordance with approved plant procedures. At approximately 2255 hours, Unit 2 Operations personnel noted low ESW flow to both of the Unit 2 Emergency Diesel Generator (EDG) heat exchangers. The Unit 1 ESW flows were also checked and it was determined that ESW flow to both Unit 1 EDG heat exchangers was low. All four EDGs were declared inoperable. Unit 2 entered Technical Specification (TS) 3.0.3, and Unit 1 entered TS 3.8.1.2. After flushing the ESW side of the associated heat exchangers both Unit 2 EDGs were declared OPERABLE at 2350 hours. Based on conservative decision making, Unit 2 was shut down on August 30, 2001, to facilitate the identification and correction of the causes for the low ESW flow conditions. The U.S. Nuclear Regulatory Commission was notified of the decision to commence a Unit 2 shutdown. A common mode failure of the EDGs was reported in accordance with 10 CFR 50.72(b)(3)(v), "Non-Emergency Events - 8-Hour Reports." The cause of the low flow conditions was pre-existing material failure of the Unit 1 East ESW strainer basket, which created a bypass flow path around the strainer. The bypass flow path allowed large debris to enter the ESW system. The cause of the EDG common mode failure was the station design and operational practices that allowed aligning the ESW supplies to each EDG from both ESW headers on the associated unit. C Corrective actions included inspection and replacement of all baskets, revision of the applicable maintenance procedures which detail installation requirements, and modification to the design and operating procedures to maintain the alternate ESW valves to the EDGs normally shut during normal and accident conditions.
05000316/LER-2001-00223 January 2001

This LER supplement is being submitted to include revised information related to the completed root cause evaluation.

This LER revision replaces the previous LER in its entirety. On January 23, 2001, during the removal of plant equipment from the Unit 2 lower containment personnel airlock, the airlock doors' interlock failed. This allowed the inadvertent opening of both the inner and outer lower containment airlock doors at the same time for approximately 5 seconds.

Technical Specification 3.6.1.3 requires both containment airlock doors to be closed; except during normal transit entry and exit through containment, then at least one airlock door shall be closed. Because both lower containment airlock doors were open at the same time, an 8-hour ENS notification was made to the NRC in accordance with 10 CFR 50.72 (b)(3)(v)(C), for a condition or event that could have prevented the fulfillment of the safety function of a system needed to control the release of radioactive material.

The root cause for the containment airlock door interlock failure was the interlock mechanism slipping out of adjustment.

The specific failure involved a gradual loosening of the setscrews that hold the interlock gears in place.

Both the inner and outer lower containment airlock doors were immediately closed to restore containment integrity. The airlock door interlock was repaired and satisfactorily tested. Preventive maintenance (PM) activities for the airlock doors were evaluated and the root cause recommendations and vendor recommendations have been incorporated into the appropriate procedures. A detailed design analysis is presently being performed and is being tracked in accordance with the site Corrective Action Program. The appropriate procedure has been revised to include directions on the operation of the containment airlock doors and the consequences of improper airlock door configuration, including radiological and industrial safety concerns. This condition is not considered to be safety significant due to the extremely low probability of a Loss of Coolant Accident or Main Steam Line Break occurring during the 5-second time interval in which both airlock doors were open. A review of plant events during the past three years did not identify any conditions in which the containment doors were opened simultaneously. Therefore, this is considered an isolated event.

FORM 366 (7-2001) �

05000316/LER-1985-043, Resubmitted LER 85-043-00:on 851227,auxiliary Bldg Ventilation Grab Sample Not Obtained within Tech Spec Time Constraints.Caused by Personnel Error.Administrative Action Taken W/Individual Involved20 March 1986
05000316/LER-1984-008, Updated LER 84-008-01:on 840419 & 24,containment Purge Isolated Due to Radiation Monitor High Alarms on Containment Area Radiation Monitor Train A.Caused by Software Error. Resolution Under Evaluation by Manufacturer31 May 1984
05000316/LER-1984-003, Updated LER 84-003-01:on 840311 & 17,upper Containment Area Radiation Monitor VRS-2201(IL) Received High Alarm.Caused by Equipment Malfunction Due to Software Problems.New Software Installed16 July 1984
05000316/LER-1983-123, Forwards LER 83-123/03L-0 & LER 83-111/03X-117 January 1984
05000316/LER-1983-081, Updated LER 83-081/03X-1:on 830822 & 25,during Normal Operation,Reactor Trips Occurred as Result of Failures of 120-volt Ac Vital Bus Inverter.Caused by Operating Temps Above Rated Design Temps.Forced Air Cooling Installed18 January 1984
05000316/LER-1983-072, Forwards Updated LER 83-072/03X-1 & LER 83-094/03L-012 October 1983
05000316/LER-1983-040, Forwards LER 83-040/03L-04 May 1983
05000316/LER-1983-039, Forwards LER 83-039/01T-022 April 1983
05000316/LER-1983-036, Forwards LER 83-036/01T-019 April 1983
05000316/LER-1983-035, Forwards LER 83-035/03L-015 April 1983
05000316/LER-1983-034, Forwards LER 83-034/03L-05 April 1983
05000316/LER-1983-027, Forwards LER 83-027/03L-024 March 1983
05000316/LER-1983-026, Forwards LER 83-026/01T-010 March 1983
05000316/LER-1983-025, Forwards LER 83-025/03L-02 March 1983
05000316/LER-1983-022, Forwards LER 83-022/03L-017 March 1983
05000316/LER-1983-018, Forwards LER 83-018/03L-016 February 1983
05000316/LER-1983-017, Forwards LER 83-017/03L-014 February 1983
05000316/LER-1983-015, Forwards LER 83-015/03L-0 & 83-016/03L-011 February 1983
05000316/LER-1983-011, Forwards LER 83-011/03L-07 February 1983
05000316/LER-1982-118, Forwards LER 82-118/03L-028 January 1983
05000316/LER-1982-116, Forwards LER 82-116/03L-0 & 82-117/01T-0.LERs Previously Submitted Using 1983 Numbers 83-001/03L-0 & 83-003/01T-0, Respectively31 January 1983
05000316/LER-1982-113, Forwards Updated LER 82-113/01X-13 February 1983
05000316/LER-1982-109, Forwards LER 82-109/03L-010 January 1983
05000316/LER-1982-106, Forwards Updated LER 82-106/03X-110 January 1983
05000316/LER-1982-096, Forwards LER 82-096/01T-015 December 1982
05000316/LER-1982-095, Forwards LER 82-095/03L-010 December 1982
05000316/LER-1982-093, Forwards Updated LER 82-093/03X-117 February 1983
05000316/LER-1982-091, Forwards LER 82-091/03L-06 December 1982
05000316/LER-1982-088, Forwards LER 82-088/03L-023 November 1982
05000316/LER-1982-085, Forwards LER 82-085/03L-012 November 1982
05000316/LER-1982-084, Forwards LER 82-084/03L-011 November 1982
05000316/LER-1982-083, Forwards LER 82-083/03L-029 October 1982