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 Discovered dateReporting criterionTitleEvent description
ENS 570137 March 2024 00:35:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite NotificationThe following information was provided by the licensee via email: On March 6, 2024, at 1635 PST, with Columbia Generating Station operating at 100 percent power in Mode 1, there was a malfunction in the halogenation/dehalogenation system. This system is used for continuous control of the biological growth in the circulating water and plant service water systems as well as to prevent discharge of halogens to the Columbia River during continuous blowdown. The result of this malfunction was exceeding the established limits of 0.1 milligrams/liter (mg/L) for total residual halogen (TRH) in the station's national pollutant discharge elimination system (NPDES) permit. At the time of discovery, the local indication for TRH was 3.20 mg/L. This was confirmed via a local grab sample. This maximum daily effluent limit is the highest allowable daily discharge, measured during a calendar day. The station NPDES permit requires notification to the Energy Facility Site Evaluation Council (EFSEC). The automatic isolation function of the system failed to isolate the continuous blowdown line as did the emergency trip push button. The system was manually secured, and the continuous blowdown line to the Columbia River was isolated. The cause of the issue is under investigation. Notification was made to EFSEC on March 6, 2024, at 2303 PST. This event is being reported as a four hour report made in accordance with 10 CFR 50.72(b)(2)(xi) due to a "News Release or Notification of Other Government Agency" related to protection of the environment. The NRC Senior Resident Inspector has been notified.
ENS 570105 March 2024 13:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentAccident Mitigation - Loss of UPS Cooling

The following information was provided by the licensee via email:

      • 8 Hour Notification was due at 1520 CST *** Follow up discussion of conditions after recovery determined that a report is required. This report restores reporting compliance.

On March 5, 2024, at 0720 CST, the X-02 118V uninterruptible power supply air conditioning (UPS A/C) unit tripped with the associated emergency fan coil units (EFCUs) shut down for planned maintenance in the area. The X-01 UPS A/C unit was declared inoperable upon discovery due to a scheduled outage of support systems (Unit 1 station service water) via the safety function determination process. This placed the site in technical specification 3.7.20 condition A, B, and C to restore the UPS A/C system within one hour. The EFCUs were restarted at 0729 which satisfied condition B and C, and X-01 UPS A/C unit was aligned to Unit 2 cooling water at 0801, exiting condition A. The condition that could have prevented the fulfillment of the safety function lasted for approximately nine minutes. Area temperatures had no notable change based on field observations during the condition. The UPS HVAC system provides temperature control for the safety related UPS and distribution rooms during all normal and accident conditions. The UPS HVAC system consists of (a) a dedicated UPS room EFCU in each safety-related UPS and distribution room, and (b) two electrically independent and redundant A/C trains either of which can support all four safety related UPS and distribution rooms; each train consists of an air conditioning unit, ductwork, dampers, and instrumentation. The NRC Resident Inspector has been notified.

ENS 5700127 August 2022 05:00:0010 CFR 21.21(d)(3)(i), Failure to Comply or DefectPart 21 - Service Water Booster Pump Bearing Housing Cover Oil LeakThe following information was provided by the licensee via phone and email: On August 27, 2022, while in Mode 1 at 100 percent power, Nebraska Public Power District (NPPD) Cooper Nuclear Station (CNS) identified a 3 drops per minute (dpm) oil leak from the radial (inboard) bearing housing cover on one of four residual heat removal (RHR) service water booster pumps (SWBP); specifically, SWBP-D. Subsequent analysis determined that the leak was a result of a deviation with the configuration of the labyrinth seal drain path. This deviation was due to an error introduced in a manufacturing drawing used by the vendor for the fabrication of four new replacement pumps. The bearing housing cover is a unique design to CNS for the RHR SWBPs. On March 1, 2024, NPPD completed a substantial safety hazard evaluation and determined that the manufacturing drawing error could cause a substantial safety hazard. The NRC Resident Senior Resident has been notified. This is a non-emergency notification required by 10 CFR 21.21(d)(3)(i). A written notification will be provided within 30 days. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All four SWBPs had a similar housing design. Three of the four pump housings have been replaced. No other nuclear plant is affected due to the housing design being unique to CNS.
ENS 569579 February 2024 18:22:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Condition - Inadequate Fuses for Fuel Pool Cooling

The following information was provided by the licensee via email: On 2/9/24 at 1322 EST, it was determined that the unit was in an unanalyzed condition. A review of DC feeder circuit protection schemes identified a circuit for the fuel pool cooling system is uncoordinated due to inadequate fuse sizing. This results in a concern that postulated fire damage in one area could cause a short circuit without adequate protection, leading to the unavailability of equipment credited for in 10 CFR 50 Appendix R, Fire Safe Shutdown. This condition is not bounded by existing design and licensing documents; however, it poses no impact to the health and safety of the public or plant personnel. Therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). The postulated event affects the following fire zones: fire areas 6S and 6N (within the Unit 2 reactor building). Compensatory actions for affected fire areas have been implemented. An extent of condition review is being performed. The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Fire watches have been established in the affected areas. These will be maintained until the protection scheme is revised.

  • * * UPDATE ON 03/08/24 FROM PAUL BOKUS TO TOM HERRITY * * *

The following updated information was provided by the licensee via email and phone call: On 03/08/24 at 1418, extent of condition reviews identified circuit(s) in the Units 2 and 3 Reactor Protection Systems (RPS) which are also uncoordinated due to improper fuse sizing. These circuits are not bounded by existing design and licensing documents for 10 CFR 50 Appendix R Fire Safe Shutdown and, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects the following fire areas: 32, 33, 38 and 39 (Units 2 and 3 Switchgear Rooms). In accordance with procedural requirements, compensatory actions for the affected fire areas have been implemented and will remain until the condition is resolved. The NRC Senior Resident Inspector has been notified. Notified R1DO (Arner)

  • * * UPDATE ON 3/13/2024 AT 1538 FROM TROY RALSTON TO SAM COLVARD * * *

On March 13, 2024, at 1350 EDT, extent of condition reviews identified a circuit in the Unit 2 reactor protection system (RPS) which is also uncoordinated due to improper fuse sizing. This circuit is not bounded by existing design and licensing documents for 10 CFR 50, Appendix R, Fire Safe Shutdown, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects fire area 57 (Switchgear Corridor, common to Units 2 and 3). In accordance with procedural requirements, compensatory actions for the affected fire areas have been implemented and will remain until the condition is resolved. Additionally, it was previously reported that fire area 6N contained a circuit which was not bounded by the Fire Safe Shutdown analysis; however, after further review it has been determined that compliance is maintained in this fire area and is therefore retracted from the scope of this report. The NRC Senior Resident Inspector has been notified. Notified R1DO (Jackson)

  • * * UPDATE ON 3/21/2024 AT 1525 FROM PAUL BOKUS TO IAN HOWARD * * *

The following information was provided by the licensee via email: On 03/21/24 at 1211, extent of condition reviews identified an annunciator circuit for the Unit 3 emergency service water (ESW) and high pressure service water (HPSW) pump structure heating and ventilation panel that is also uncoordinated due to improper fuse sizing. This circuit is not bounded by existing design and licensing documents for 10 CFR 50 Appendix R Fire Safe Shutdown and, therefore, this event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). This event poses no impact to the health and safety of the public or plant personnel. The postulated event affects fire area 47 (Unit 3 pump structure for `B' ESW and `3A'-`3D' HPSW pumps) and the yard fire area (Manhole 026D). In order to restore immediate compliance, the cable has been de-energized to eliminate the possibility of the event of concern. This circuit will remain de-energized or other measures will be implemented until the condition is permanently resolved. The NRC Senior Resident Inspector has been notified. Notified R1DO (Ford)

ENS 5692818 January 2024 20:04:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Residual Heat Removal Degraded Due to Service Water Leakage

The following information was provided by the licensee via email: On January 18, 2024, at 0030 PST, diesel generator 2 (DG2) was shut down following a monthly surveillance run. Subsequently, a leak was discovered in the DG2 building. Service water pump '1B' was secured at 0117, effectively stopping the leak. The leak was determined to be service water coming from a diesel generator mixed air cooling coil. Service water system 'B' and DG2 were subsequently declared inoperable at 0135. After discussion with engineering, it was identified that the amount of service water leakage from the cooling coil was assumed to be greater than the leakage allowed by the calculation to assure adequate water in the ultimate heat sink to meet the required mission time of 30 days. At 1204, it was determined that entry into Technical Specification 3.7.1 condition D was warranted since the assumed leakage from the cooling coil could exceed the calculated allowed value. At 1238, the control power fuses for service water pump '1B' were removed. DG2 and service water system 'B' were declared unavailable, and the technical specification condition for the inoperable ultimate heat sink was exited. With the control power fuses removed, the pump is kept from auto starting, effectively preventing the leak and ensuring the safety function of the ultimate heat sink is maintained while the cooling coil is repaired or replaced. Due to the leakage assumed greater than the calculated allowable value this condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) as an unanalyzed condition and per 10 CFR 50.72(b)(3)(v)(B) as an event or condition that could have prevented fulfillment of the safety function of structures or systems that are needed to remove residual heat. There was no impact to the health and safety of the public. The NRC Resident has been notified.

  • * * RETRACTION ON 3/18/24 AT 1923 FROM VALERIE LAGEN TO KAREN COTTON * * *

The following information was provided by the licensee via email: On January 18, 2024 at 2138 EST, Columbia Generating Station notified the NRC under 10 CFR 50.72(b)(3)(ii)(B) of an unanalyzed condition on the available capacity of the ultimate heat sink (UHS) and under 10 CFR 50.72(b)(3)(v)(B) of an event or condition that could have prevented fulfillment of the safety function of structures or systems needed to remove residual heat. On January 18, 2024, following monthly surveillance of the diesel generator DG2, a DG2 room cooler flow alarm was received at 0115. A leak was discovered in the diesel mixed air (DMA) air handler unit. Service Water Pump '1B' was secured and the leakage was stopped at 0117. The service water system 'B' and diesel generator system 'B' were declared inoperable at 0135. The leak was assumed to be greater than that allowed to ensure adequate water in the UHS required to meet the 30-day mission time, and the UHS was declared inoperable at 1204. Control power fuses for the service water pump '1B' were removed to fully eliminate the leakage path from the cooler, and the UHS was declared operable at 1238. Following the event, engineering performed an analysis based on the size and location of the leak, and concluded it would have taken 1.4 days to deplete the available excess water in the UHS to below the minimum technical specification required water level of the spray pond. Operations were able to secure the service water subsystem of the UHS prior to exceeding the volumetric margins in the spray ponds to ensure the 30-day mission time was met. The condition did not represent a safety significant unanalyzed condition nor a loss of safety function. The NRC Resident Inspector has been notified. Notified R4DO (Gepford).

ENS 5662012 July 2023 08:49:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual HeatECCS Potentially Inoperable

The following information was provided by the licensee via email: At 0449 (EDT) on 7/12/2023, Millstone Unit 3 declared the 'B' train of the emergency core cooling system (ECCS) inoperable due to a degraded damper associated with the ventilation support system for the 'B' charging pump. At the time of this event, the 'A' train of service water was already inoperable due to planned maintenance on a breaker that would have prevented an 'A' service water valve powered from this breaker from closing on a safety signal. This configuration resulted in the possibility that the 'A' train of ECCS would not have been available to fulfill its design function under all postulated accident conditions. This event is being reported under 10 CFR 50.72(b)(3)(v)(B), '(any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (B) remove residual heat).' Subsequently, the 'A' train of service water was restored to operable at 0548 on 7/12/2023. Repairs and investigation continue on the 'B' train ECCS damper. The NRC resident has been notified. This event did not impact Millstone Unit 2. There was no impact to the public.

  • * * RETRACTION ON 7/31/2023 AT 1400 EDT FROM JAMES KELLY TO JOHN RUSSELL* * *

The following information was provided by the licensee via email: The condition was reported to the NRC pursuant to 10 CFR 50.72(b)(3)(v)(B), via an 8-hour report as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat. A subsequent engineering review of the conditions that existed at the time determined that, based on area temperature response, any impact on ventilation flows into and out of the `B' charging pump cubicle did not generate an observable change in the temperature trend. Based on this, it is concluded with reasonable assurance that the functional requirement of the support system was maintained and the `B' charging pump would have continued to perform its safety function until the `A' train of service water was restored to operable and as a result safety function was not lost. Therefore, this condition is not reportable and NRC Event Number 56620 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector." Notified R1DO (Bicket).

ENS 5654225 May 2023 04:00:0010 CFR 21.21(a)(2), Interim Report for Comply or Defect in ComponentPart 21 Interim Evaluation - Mechanical Draft Cooling Tower Fan Brakes Design FlawThe following is a summary of the information provided by the licensee via email: As previously reported under Fermi LER 2023-001-00, submitted on May 22, 2023, at 1145 EDT on March 23, 2023, it was determined that all mechanical draft cooling tower (MDCT) fan brakes would not perform their design function during a tornado due to the speed switch not functioning over its published voltage and frequency ranges. The MDCT fan brakes are required to prevent fan overspeed from a design basis tornado. On May 25, 2023, Fermi completed its 10 CFR Part 21 discovery process and determined the need to perform a 10 CFR Part 21 evaluation. The vendor (Engine Systems Inc. (ESI)) was contacted and the purchaser (Fermi) assumed responsibility for performing the Part 21 evaluation for the supplied mechanism. This Part 21 evaluation is being tracked by Fermi CARD 23-20075. It has been determined the direct cause of the event was due to the Dynalco speed switch model SST-2400A-1, supplied by ESI, not functioning over its published voltage and frequency ranges. Corrective actions were taken to develop a design change to correct MDCT fan speed control system returning the MDCT fans, ultimate heat sink, and the service water subsystems to service on March 24, 2023. The root cause evaluation is ongoing, and written follow-up will be provided in 30 days by providing a supplement to the original LER by June 24, 2023. No new commitments are being made in this submittal.
ENS 5648726 April 2023 06:15:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification - Spilled Sodium HypochloriteThe following information was provided by the licensee via email: On 4/25/2023 at approximately 2315 (MST) it was reported that there was possible sodium hypochlorite actively leaking near the 'A' essential spray pond (ESP). Upon investigation, it was determined that the 'low flow' line of sodium hypochlorite supply to the 'A' spray pond had developed a leak. Sodium hypochlorite had pooled at the leak location and subsequently run down the ESP apron, into the road, and into the storm drain located in the protected area fence. An estimate of approximately 300 gallons of spilled sodium hypochlorite was determined based on the time frame that the sodium hypochlorite was scheduled to start injecting into the 'A' spray pond and the time the leak was isolated. The leak was isolated on 4/25/2023 at approximately 2330. The leak was contained in the storm drain with the storm gates closed, therefore nothing was released offsite. The cleanup effort in progress includes diluting the sodium hypochlorite with domestic service water, collecting it into the storm drain, pumping it to a tank truck, and transporting it to the Palo Verde Water Resources Facility for neutralization. Condition Report 23-04519 was generated to document the leak. The Palo Verde Senior Environmental Scientist was notified and subsequently informed the Environmental Protection Agency (EPA) National Response Center (NRC#1365638) on 4/26/23 at 0005 in accordance with the 91DP-0EN03 Environmental Spill Response (local procedure). The NRC Senior Resident Inspector was also notified. No personnel were injured and no equipment was damaged as a result of the spill. The Palo Verde Fire Department was notified and the area was barricaded off to prevent personnel from entering the area during the cleanup effort.
ENS 5646416 February 2023 12:05:00Other Unspec Reqmnt
10 CFR 50.73(a)(1), Submit an LER
60 Day Notification for an Invalid Actuation of the Emergency Service Water SystemThe following information was provided by the licensee via email: This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid specific system actuation of the Emergency Service Water (ESW) System. On 2/16/2023, while performing a calibration planned maintenance (PM) for a jacket water pressure indicator during a D13 diesel generator system outage window, the 'C' ESW pump unexpectedly auto-started. Subsequent investigation identified that the affected jacket water pressure indicator shares a common sensing line with a jacket water pressure switch that provides a back-up to the engine speed switch for the engine running signal. At the time the jacket water pressure indicator calibration PM was being performed, the power circuits for D13 diesel generator instrumentation were energized. Pressurization of the energized jacket water pressure switch during the pressure indicator calibration activity resulted in initiation of a false engine running signal to the `C' ESW pump start logic. This event is considered an invalid system actuation because the 'C' ESW pump started in response to a false signal that the D13 EDG was running when the D13 EDG did not start. The actuation was not initiated in response to actual plant conditions or parameters and was not a manual initiation. The ESW system functioned as expected in response to the actuation. The affected ESW pump was shut down in accordance with plant procedures. There was no impact on the health and safety of the public or plant personnel. The licensee notified the NRC Resident Inspector.
ENS 562832 November 2022 23:29:0010 CFR 50.73(a)(1), Submit an LER60-DAY Telephonic Notification - Invalid Specific System ActuationThe following information was provided by the licensee via email: This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to describe an invalid specific system actuation of the Emergency Service Water System (ESW). On 11/2/2022, during normal reactor operations, multiple main control room alarms were received for D12 Emergency Diesel Generator (EDG) running and Unit 1 Division 2 Safeguard Battery Ground. The D12 EDG did not start; however, the 'B' ESW Pump auto started. Subsequent troubleshooting determined that the cause of the D12 EDG running alarms and the inadvertent auto start of the 'B' ESW Pump was a malfunction on the D12 EDG speed switch. This event is considered an invalid system actuation because the 'B' ESW Pump started in response to a false signal that the D12 EDG was running when D12 EDG did not start. This was a complete actuation of the ESW System and the system functioned as expected in response to the actuation. The affected ESW Pump was shut down in accordance with plant procedures and the degraded D12 EDG speed switch was replaced. There was no impact on the health and safety of the public or plant personnel. The licensee notified the NRC Resident Inspector.
ENS 5624128 November 2022 09:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System Inoperable

The following information was provided by the licensee via email: At 0400 EST on November 28, 2022, during the performance of Division 2 Residual Heat Removal (RHR) cooling tower fan operability and RHR Service Water valve lineup verification, it was reported that the Mechanical Draft Cooling Tower (MDCT) Fan 'B' was making a loud metallic noise. The cause of the metallic noise is unknown at this time. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The EECW system cools various safety related components including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on inoperable cooling water to the HPCI room cooler, per LCO 3.0.6. Investigation into the Division 2 MDCT Fan 'B' abnormal noise is in progress. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM JEFF MYERS TO LLOYD DESOTELL AT 1615 EST ON 12/09/2022 * * *

The following information was provided by the licensee via email: The purpose of this notification is to retract a previous Event Notification 56241 reported on 11/28/2022. On 11/28/22, an event notification to the NRC was made when mechanical draft cooling tower (MDCT) Fan B was declared inoperable and issued Limited Condition of Operation (LCO) 2022-0428 for Division 2 MDCT Fan B abnormal noise. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS) (Technical Specification (TS) 3.7.2). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system (TS 3.7.2), which cools various safety related components, including the High-Pressure Coolant Injection (HPCI) system room cooler (TS LCO 3.0.6). Subsequent inspection and evaluation determined that the brake noise is expected while fans are running at low speeds. This is supported by plant technical procedure, 24.205.10 `Div. 2 RHR Cooling Tower Fan Operability and RHRSW Valve Line-up Verification' (line item 2.2 in Precautions and Limitations) which states `Chatter from the brakes of the MDCT Fans is expected and no cause for discontinuing the test.' The equipment vendor stated that brake chatter is possible and common given that the internal components are free to move along the splined connections. Internal Operating Experience from experienced station operators and maintenance technicians confirmed that the condition is normal and expected. Both Division 2 MDCTs exhibited the same behavior at low speed and passed surveillance testing satisfactorily. No other concerns were noted during fan operation. Therefore, HPCI remained operable and there was no loss of safety function. The event did not involve a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). EN 56241 is retracted and no Licensee Event Report under 10 CFR 50.73(a)(2)(v)(D) is required to be submitted. The NRC Resident Inspector has been notified. Notified R3DO (Stoedter).

ENS 5611619 September 2022 06:32:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentSafety System InoperabilityThe following information was provided by the licensee via email: At 0132 CDT on September 19, 2022, River Bend Station (RBS) was operating at 100% power when the high pressure core spray (HPCS) system was declared inoperable in accordance with technical specification 3.8.9, condition E (declare HPCS and standby service water system pump 2C inoperable immediately) due to a E22-S003, HPCS transformer feeder malfunction. The HPCS is a single train system at RBS, therefore this event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfilment of a safety function. The reactor core isolation cooling system has been verified to be operable. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: RBS has entered a 14-day limiting condition for operation due to the loss of HPCS and they have upgraded their on-line plant risk model to "yellow".
ENS 5597330 June 2022 19:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Scram Due to Loss of TransformerThe following information was provided by the licensee via phone and email: At 1445 (CDT) on June 30, 2022, with Grand Gulf Nuclear Station in Mode 1 and at 100 percent power, the reactor was manually scrammed due to the loss of balance of plant (BOP) transformer 23. All control rods fully inserted into the core and all systems responded appropriately. Reactor level is being maintained with condensate and feedwater. Reactor pressure is being maintained with turbine bypass valves. The cause of the loss of BOP transformer 23 is under investigation at this time. Standby Service Water 'A' and 'B' were manually initiated to supply cooling to Control Room A/C, ESF switchgear room coolers, and plant auxiliary loads. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) as an event or condition that resulted in actuation of the Reactor Protection System and 10 CFR 50.72(b)(3)(iv)(A) due to the actuation of Standby Service Water. The NRC Senior Resident Inspector was notified.
ENS 559722 May 2022 04:05:00Other Unspec Reqmnt
10 CFR 50.73(a)(1), Submit an LER
Invalid Specified System ActuationThe following information was provided by the licensee via phone and email: This non-emergency notification is being made pursuant to the provisions of 10 CFR 50.73(a)(1) to report the occurrence of an invalid automatic actuation satisfying the reporting criterion of 10 CFR 50.73(a)(2)(iv)(A), specifically for the actuation of one train of the Essential Service Water (ESW) system that occurred on May 1, 2022. On May 1, 2022, with the plant shut down and the core offloaded, control room personnel were performing a fast power transfer from Engineered Safety Feature (ESF) transformer XNB02 to ESF transformer XNB01. In anticipation of this activity, the `B' load shedder and emergency load sequencer (LSELS) had been removed from service. Also, at the time, a portion of the `A' ESW train was isolated to support performance of a local leak rate test (LLRT) of a containment isolation valve in the affected portion of `A' ESW train piping. Service Water was supplying cooling water flow to `A' train loads (in lieu of ESW cooling water). When the power transfer was performed, an unexpected automatic start of the `A' ESW pump, along with some associated, automatic valve repositioning, occurred. The actuation occurred due to inadvertent satisfaction of automatic start logic for the ESW pump. The logic is intended to detect loss of ESW flow when the opposite train LSELS isolates Service Water during an undervoltage condition on a safety bus. The flow transmitter involved in the actuation is situated in a portion of the ESW piping that was isolated for the LLRT. The low-flow signal from the transmitter was consequently not reflective of low cooling water flow to plant loads in light of the fact that cooling water flow was being supplied to plant loads and the transmitter was locally isolated. In regard to the ESW train actuation, therefore, although the undervoltage signal was considered a valid signal due to the voltage drop caused by the fast transfer activity, the low-flow signal from the noted transmitter was considered to be invalid. For this invalid actuation, it was concluded that the actuation was not part of a pre-planned sequence, that the affected system was not properly removed from service during the occurrence, and that the safety function had not already been performed relative to the occurrence. (The) NRC Resident Inspector has been notified and an email of this report has been sent to hoo.hoc@nrc.gov.
ENS 558597 March 2022 04:40:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation 60-DAY Telephone NotificationThe following information was provided by the licensee via fax or email: This 60-day telephone notification is being made in lieu of an LER submittal per 10 CFR 50.73(a)(1). This notification is made pursuant to the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) for invalid actuations of systems listed in 10 CFR 50.73(a)(2)(iv)(B). At approximately 0040 Eastern Standard Time (EST) on March 7, 2022, Unit 1 received inadvertent High-Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) initiation signals. Subsequently, at approximately 0148 EST on March 7, 2022, Unit 1 received inadvertent Low-Pressure Coolant Injection (LPCI) and Core Spray initiation signals. In addition, all four Emergency Diesel Generators auto started, Group 10 (Instrument Air) Primary Containment Isolation System actuations occurred, and the Residual Heat Removal (RHR) Service Water Booster pumps tripped resulting in a brief interruption (approximately 9 minutes) to the Shutdown Cooling (SDC) heatsink. Jumpers, installed per planned refueling outage activities, prevented discharge of Emergency Core Cooling Systems into the reactor. HPCI, RCIC, and RHR Loop `A' were removed from service and under clearance. RHR SDC remained operable via RHR Loop `B' and forced circulation was maintained in the reactor. At the time of these events, Unit 1 was shutdown for refueling and the `A' and `C' reactor water level transmitters had been isolated in preparation for planned replacement. Leak-by of the instrument isolation valves occurred on both transmitters. Leak-by on the `C' instrument occurred at a faster rate with the `A' instrument providing the confirmatory signals resulting in Low Level 2 (LL2) and Low Level 3 (LL3) indication at approximately 0040 EST and 0148 EST, respectively. All actuations occurred as designed for LL2 and LL3 signals. During these events, reactor water level remained stable at the Reactor Vessel Head Flange and the `B' and `D' reactor water level transmitters remained off-scale-high, as expected under these conditions. Therefore, the actuations were not initiated in response to actual plant conditions, it was not an intentional manual initiation, and there were no parameters satisfying the requirements for initiation of the system (i.e., there was no low reactor water level condition). Considering the above, these actuations were invalid. There was no impact on the health and safety of the public or plant personnel.
ENS 556821 January 2022 17:10:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray System Declared Inoperable

The Licensee provided the following information via fax: During performance of a surveillance of the High Pressure Core Spray (HPCS) service water system on January 1, 2022, the HPCS system was declared inoperable for performance of the surveillance. During the surveillance, pump discharge pressure and flow were above the action range curve specified in the surveillance. For the given flow rate, pump discharge pressure was too high. This condition prevents declaring the HPCS service water system and HPCS system operable. The HPCS service water and HPCS systems remain inoperable. The station entered Technical Specification (TS) 3.7.2.A and TS 3.5.1.B at 0910 (PST) on January 1, 2022. In accordance with TS 3.5.1.B, the Reactor Core Isolation Cooling (RCIC) system was verified to be operable. TS 3.5.1 Action B provides a 14-day completion time to restore HPCS to an operable status. All other Emergency Core Cooling systems (ECCS) are operable. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function credited for mitigating the consequences of an accident per 10 CFR 50.72(b)(3)(v)(D). The HPCS system is a single train system at Columbia. The NRC resident has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee is investigating the cause of the high pump discharge pressure and verifying instrumentation accuracy.

  • * * RETRACTION ON 1/6/22 AT 1715 EST FROM CHASE WILLIAMS TO TOM KENDZIA * * *

This Notification is to retract EN 55682, Unplanned High Pressure Core Spray (HPCS) Inoperability. On 1/1/2022 at (1735 EST), Columbia Generating Station notified the NRC under 10 CPR 50.72(b)(3)(v)(D) of the inoperability of a single train of safety system (HPCS) for performance of the surveillance. During the surveillance pump discharge pressure and flow were above the action range curve specified in the surveillance. Engineering performed an analysis of this event and concluded the HPCS was operable during the event and would have performed its required safety function. The results of initial IST testing of HPCS-P-2 via OSP-SW/IST-Q703 on 01/01/22 resulted in measured parameters falling outside of the acceptable range specified for this pump. Systematic error was suspected as the cause of the failure and the test was reperformed following taking actions to eliminate the suspected systematic errors. The second performance of the test on 01/01/22 resulted in acceptable pump performance. Evidence exists that the initial performance of the test failed due to imprecise averaging techniques due to difficulties in averaging continuously changing values on the test instrument. The second performance of OSP-SW/IST-Q703 should be considered a successful test and the test of record as the systematic error was eliminated and measured parameters are considered valid. The NRC Resident Inspector has been notified. The HOO notified R4DO (Rolando-Otero).

ENS 5542522 August 2021 15:30:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notification of Potential Oil DischargeOn August 22, 2021, Columbia Generating Station determined that no more than approximately eight (8) gallons of silicone oil was inadvertently released into a plant service water system due to a failed heat exchanger on a plant installed air compressor. The plant service water system returns water to a water basin that contains at a minimum 300,000 gallons of water. The water basin is connected to the Columbia River via a blowdown line. Although not confirmed, it is suspected that an unknown quantity of silicone oil may have been released to the Columbia River. A visual inspection of the basin did not identify any oil sheen or film, and there are no additional actions needed to mitigate this issue. It does not appear the oil release poses a threat to human health or the environment, however because there could have been a discharge of an unknown quantity of silicone oil into the Columbia River this matter is immediately reportable under RCW 90.56.280 to the US Coast Guard National Response Center and Washington State Department of Ecology. This condition is being reported pursuant to 10 CFR 50.72(b)(2)(xi) for news release or notification of other government agencies concerning an event related to the health and safety of the public or protection of the environment. Notifications to off-site agencies were performed at 1825 PDT on 8/23/2021. The NRC resident has been informed.
ENS 550791 December 2020 14:46:0010 CFR 50.73(a)(1), Submit an LER60-DAY Optional Telephonic Notification of an Invalid Specified System ActuationThis 60-day optional telephone notification is being made in lieu of an LER submittal, as allowed by 10 CFR 50.73(a)(1). This notification is made pursuant to the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) for an invalid actuation of one of the systems listed in 10 CFR 50.73(a)(2)(iv)(B). At 0946 hrs on December 1, 2020, with unit 2 in Mode 5 at 0% power, an invalid actuation of the Emergency Diesel Generators (EDG) 'A' and 'B', 'A' Residual Heat Removal (RHR) Pump, 'A' Service Water Booster Pump (SWBP), and Auxiliary Feed Water (AFW) Pumps 'A' and 'B' occurred. The actuation was caused by a Safety Injection (SI) signal while installing simulations to support Reactor Safeguards testing. The SI signal occurred when two out of three logic was met for Low Pressurizer Pressure, which was caused by a high resistance connection to a test point from a loose test lead. All aligned equipment, 'A' and 'B' EDGs, 'A' RHR Pump, 'A' SWBP and 'A' and 'B' AFW Pumps, responded properly to the auto-start signal and the actuation was complete. The actuation was not initiated in response to actual plant conditions, it was not an intentional manual initiation, and there were no parameters satisfying the requirements for initiation of the system. Therefore, this event has been determined to be an invalid actuation. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector was notified.
ENS 549316 August 2020 06:28:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of an Invalid Specified System ActuationThis 60-day telephone notification is being made under reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of an emergency service water system component that does not normally run and which provides an ultimate heat sink. On August 6, 2020, at approximately 0128 CDT, the A3 Emergency Equipment Cooling Water (EECW) pump received an auto-start signal while performing Post-Maintenance Testing (PMT) on the 3C Core Spray pump. Normally, the involved EECW pump would be started prior to testing to prevent an auto-start; however, in this case the pump was not running prior to the test. When the 3C Core Spray pump breaker was closed while in the test position, an unanticipated actuation of the A3 EECW pump occurred. Work was stopped and the workers reported to the Control Room to evaluate the condition. Based on a review of this event, individuals involved were coached on understanding system response prior to performing work. The A3 EECW pump responded in accordance with the plant design. No other plant equipment was affected during this event. There were no safety consequences or impacts on the health and safety of the public. The event was entered into TVA's corrective action program for evaluation and resolution. Reference corrective action document CR 1628479. The NRC Resident Inspector has been notified of this event.
ENS 548804 September 2020 01:48:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray InoperableRiver Bend Station experienced an inadvertent initiation and injection of High Pressure Core Spray (HPCS) at 2048 (CDT) on 9/3/2020 while operating at 92% power. Initial investigation indicates a power supply failure in the Division III trip units which feeds HPCS and Division III Diesel Initiation signals. The Control Room Operator responded to the event by taking manual control of Feedwater Level Control to maintain Reactor Water Level nominal values. The HPCS injection valve was open for approximately 25 seconds before operators manually closed the valve. The manual closure of the injection isolation valve caused the system to be incapable of responding to an automatic actuation signal. The manual override of the injection isolation valve was reset approximately 52 minutes after the event. The HPCS system has remained inoperable. The event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as a condition that caused loss of function of the HPCS System. No radiological releases have occurred due to this event. The Senior NRC Resident Inspector has been notified. These conditions put the unit in a 14-day LCO (3.5.1) for HPCS Inoperability and a 30-day LCO (3.7.1) for one Standby Service Water Pump Inoperable (2C).
ENS 548164 August 2020 21:45:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor

EN Revision Imported Date : 8/20/2020 BOTH SERVICE WATER HEADERS DECLARED INOPERABLE On 8/4/20, at 1745 EDT, Millstone Unit 2 entered technical specification (TS) 3.0.3 due to both service water headers being declared inoperable because strainer differential pressures (D/Ps) were greater than 9 psid. The high service water strainer D/P was the result of heavy debris impingement caused by tropical storm Isaias. To reduce heat loads and service water flow, Unit 2 reduced power to 75 percent. One service water header was restored to operable at 1816 EDT, at which time TS 3.0.3 was exited. At 1843 EDT both service water headers were declared operable. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 8/19/2020 AT 1141 EDT FROM ERIC DONCH TO KIRBY SCALES * * *

The purpose of this call is to retract a report made on August 4, 2020, NRC Event Number EN 54816 describes a condition at Millstone Power Station Unit 2 (MPS2) in which both trains of service headers were declared inoperable due to service water strainer differential pressures greater than 9 psid. The condition was reported to the NRC pursuant to 10 CFR 50.72(b)(3)(v)(A), (B) and (D) via an 8 hour prompt report as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to shutdown the reactor and maintain it in a safe shutdown condition, remove residual heat and mitigate the consequences of an accident. Upon further review, MPS2 determined that there was no loss of safety function. An engineering evaluation supports the conclusion that a strainer differential pressure of 16 psid would not challenge the system flow distribution during worst case conditions. The evaluation also demonstrates that flowrates on both headers were observed to be unaffected during the timeframe of the high strainer differential pressure conditions. Therefore, both service water headers would have provided the required flows to perform their safety function. Therefore, this condition is not reportable and NRC Event Number EN 54816 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector. Notified R1DO (Greives).

ENS 5470114 March 2020 19:44:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Spray Pond Pump System - 60 Day ReportsThe following event descriptions are based on information currently available. If through subsequent reviews of these events additional information is identified that is pertinent to the events or alters the information being provided at this time a follow-up notification will be made via the ENS or under the reporting requirements of 10 CFR 50.73. This telephone notification is being made pursuant to the reporting requirements of 10 CFR 50.73(a)(2)(iv)(A) and 50.73(a)(1) to describe invalid actuations of both trains of the Palo Verde Nuclear Generating Station (PVNGS) Unit 3 essential spray pond (SP) system, which serves as an emergency service water system that does not normally run and serves as an ultimate heat sink as described in 10 CFR 50.73(a)(2)(iv)(B)(9). This notification covers two similar, but separate invalid actuations occurring in Unit 3 on March 14, 2020 at 12:44 (MST) and again on April 25, 2020 at 12:10 (MST). On each day, an invalid actuation of the Unit 3 train "B" Fuel Building Essential Ventilation Actuation Signal (FBEVAS) occurred during performance of the Balance of Plant Engineered Safety Features Actuation System weekly auto test. The auto/manual pushbutton was depressed to initiate the test and the sequencer immediately tripped FBEVAS train "B" with subsequent cross trip of FBEVAS train "A". These actuations resulted in complete and successful actuations of both trains of essential spray pond pumps. The events were entered into the PVNGS corrective action program and a station evaluation is in progress. There was no adverse impact to public health and safety nor to plant employees. The NRC resident inspectors have been informed.
ENS 5443711 December 2019 18:56:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionPotential Tornado Missile VulnerabilitiesOn December 11, 2019, at 1356 EST, it was concluded that certain safety-related equipment is vulnerable to design basis tornado missiles which could render the equipment inoperable and not able to perform its design function. This applies to the following Technical Specification equipment: 1. Component cooling water piping for the 'A' spent fuel cooling water system heat exchanger. This heat exchanger is vulnerable to a horizontal missile traveling through the roll-up door, which would challenge operability of the Technical Specification required component cooling system equipment. 2. All three (3) emergency service water pumps and their diesel fuel oil supply tank. The emergency service water pumps and diesel fuel oil tank are vulnerable to a horizontal missile penetrating the missile screens. 3. Certain component cooling water system pump discharge piping is vulnerable from a vertical missile penetrating the auxiliary building roof. 4. The Unit 1 auxiliary feedwater (AFW) system pumps and the pump suction and discharge piping are vulnerable to a missile traveling through the screens on the sides and roof of the main steam valve house. This vulnerability also exists for the Unit 2 AFW. This condition puts Unit 1 and 2 into Technical Specification 3.01 which requires the units to be in hot shutdown within 6 hours and in cold shutdown within the following 30 hours. The NRC Resident Inspector has been notified.
ENS 543716 November 2019 00:11:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentTwo Diesel Generators Concurrently Inoperable

On November 5, 2019 at 1811 CST, station service water A and the Division 1 diesel generator (DG) were declared inoperable based on the results of an engineering evaluation of a Class 3 piping leak. This was determined to be a potential inability to fulfill a safety function due to concurrent inoperability of two emergency diesel generators. Division 3 DG was inoperable due to planned maintenance on November 4, 2019 at 0000 CST. This event is being reported an 8-hour non-emergency notification per 10 CFR 50.72 (b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function (Accident Mitigation). Division 3 DG and high pressure core spray have been restored, and the fulfillment of the accident mitigation safety function has been restored. The NRC Senior Resident Inspector has been notified.

  • * * RETRACTION ON 11/11/19 AT 1739 EST FROM GABRIEL HARGROVE TO BETHANY CECERE * * *

This was initially reported under 10 CFR 50.72(b)(3)(v)(D). However, subsequent engineering evaluation determined that the condition did not affect safety system operability. The evaluation determined that the leakage was within allowable limits and piping structural integrity was not challenged at this time nor in the past three years. The Division 1 DG and SSW A were at the time of discovery OPERABLE and EN54371 is being retracted. The licensee will notify the NRC Resident Inspector. Notified R4DO (Drake).

ENS 5429325 September 2019 16:03:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Declared Inoperable

At 1203 EDT, on September 25, 2019, during a Division 2 Emergency Equipment Service Water (EESW) pump and valve surveillance test, the Division 2 Emergency Equipment Cooling Water (EECW) Temperature Control Valve was found to be approximately 80 percent open rather than in its required full open position during fail safe testing. The Division 2 EESW system is required to support operability of the Division 2 EECW system. The Division 2 EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. An investigation is underway into the cause of the failure. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The NRC Senior Resident Inspector has been notified. The licensee is in 72-hour shutdown action statement.

  • * * RETRACTION ON 11/21/19 AT 1547 EST FROM PAUL ANGOVE TO BRIAN LIN * * *

Subsequent engineering evaluation has determined that the EECW TCV was capable of passing sufficient flow to perform its design basis functions, including supporting the HPCI room cooler, while approximately 80% open. Therefore, HPCI remained operable and there was no loss of safety function. The event did not involve a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). EN 54293 is retracted and no Licensee Event Report under 10 CFR 50.73(a)(2)(v)(D) is required to be submitted. The NRC Resident Inspector has been notified. Notified R3DO (Cameron).

ENS 541973 August 2019 07:26:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
En Revision Imported Date 8/7/2019

EN Revision Text: AUTOMATIC REACTOR SCRAM ON LOW REACTOR WATER LEVEL At 0226 (CDT), an automatic scram on low reactor water level occurred due to a trip of the 'B' Reactor Feed pump. All control rods fully inserted. Reactor water level 2 was reached and the High Pressure Core Spray system, Reactor Core Isolation Cooling system, Division 3 diesel generator, Standby Gas Treatment Systems 'A' and 'B' and all shutdown safety related service water pumps started as expected. Reactor Core Isolation Cooling and High Pressure Core Spray injected as expected. All level 2 containment isolation signals occurred as expected and all level 2 containment valves closed as expected. Reactor water level is currently being controlled in band by condensate. Reactor pressure is being maintained by main turbine Bypass Valves. This event is being reported under 10 CFR 50.72(b)(2)(iv)(A), for ECCS discharge to RCS; 10 CFR 50.72(b)(2)(iv)(B), for RPS actuation, and 10 CFR 50.72(b)(3)(iv)(A), for specified system actuation. The NRC Senior Resident Inspector has been notified. No safety relief valves lifted during the transient. The plant is in a normal shutdown electrical lineup with all safety equipment available. The licensee notified the Illinois Emergency Management Agency per their communications protocol.

  • * * UPDATE FROM DAVID LIVINGSTON TO HOWIE CROUCH AT 0321 EDT ON 8/4/19 * * *

Following automatic initiation of the High Pressure Core Spray (HPCS) System as described above, the HPCS System was manually secured following station procedures after verification that additional RPV (reactor pressure vessel) injection was no longer required. Securing HPCS injection in this manner prevents automatic restart of the system in the event of a subsequent low RPV level condition, rendering it inoperable. As the HPCS system is considered a single train safety system, this meets the reportability requirements of 10 CFR 50.72(b)(3)(v)(D). This reportable condition was identified following review of post-scram actions. The HPCS system has been restored to a Standby lineup. The licensee will be notifying the NRC Resident Inspector. Notified R3DO (Pelke).

  • * * UPDATE FROM JAMES FORMAN TO KERBY SCALES AT 1545 EDT ON 8/6/19 * * *

Following the scram, the Primary Containment to Secondary Containment and the Drywell to Primary Containment differential pressure limits were exceeded. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.4, Primary Containment Pressure, and 3.6.5.4, Drywell Pressure, Actions A.1, B.1, and B.2 were entered. Primary Containment to Secondary Containment differential pressure and Drywell to Primary Containment differential pressure were restored to within the LCO limits at 1505 on 8/3/19 and the associated TS Actions were exited. This event is reportable under 10 CFR 50.72(b)(3)(ii)(B) as an unanalyzed condition that could have prevented the fulfillment of the primary containment function due to being outside the initial conditions to ensure that drywell and containment pressures remain within design values during a loss of coolant accident. This event is also reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of the drywell and primary containment functions to control the release of radioactive material for the same reason. The licensee notified the NRC Resident Inspector. Notified R3DO (Pelke).

ENS 5417621 July 2019 12:26:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due Non-Essential Service Water System Degraded ConditionOn July 19, 2019, DC Cook Unit 2 started experiencing degraded performance on the Unit 2 Non-Essential Service Water System (NESW) which affected one (1) NESW pump. On July 21, 2019, a second NESW pump on Unit 2 experienced degradation. On July 21, 2019, DC Cook Unit 2 elected to do a rapid downpower over approximately 40 minutes and perform a Manual Reactor Trip from 17 percent (rated thermal power) to repair the condition before any threshold was exceeded. The manual reactor trip was completed at 0826 EDT on July 21, 2019. This notification is being made in accordance with 10 CFR 50.72(b)(2)(iv)(B), Reactor Protection System (RPS) actuation as a four (4) hour report, and under 10 CFR 50.72(b)(3)(iv)(A), Reactor Protection System (RPS), as an eight (8) hour report. The DC Cook NRC Resident Inspector has been notified. Unit 2 is being supplied by offsite power. All control rods fully inserted. Aux Feedwater pumps were started as required and are operating properly. Decay heat is being removed via the Steam Generator Power Operated Relief Valves following breaking Main Condenser Vacuum for expedited cooldown of the Main Turbine. Preliminary evaluation indicates all plant systems functioned normally following the reactor trip. DC Cook Unit 2 remains stable in Mode 3. No radioactive release is in progress as a result of this event. Unit 1 was not affected.
ENS 5416315 July 2019 17:35:0010 CFR 50.72(b)(2)(xi), Notification to Government Agency or News ReleaseOffsite Notiification Due to Oil LeakAt 1335 EDT on 7/15/2019, during dredging activities in Fermi 2's General Service Water (GSW) intake canal, a hydraulic line on the dredging machine became disconnected and approximately one quart of hydraulic oil spilled into Lake Erie. The oil leak to navigable waters has been stopped. The oil was contained within a boom, cleanup activities commenced immediately, and cleanup was completed at 1500 EDT. The cause of the oil leak is under investigation. Environmental spill reports were made to local, state, and federal government agencies. This is considered a news release or notification to other government agencies, therefore this event is reportable under 10 CFR 50.72(b)(2)(xi). The NRC Resident Inspector has been notified. The State agencies notified were Michigan Department of Environmental Protection and the Michigan Pollution Emergency Alerting System. The licensee also notified the National Response Center.
ENS 5408524 May 2019 11:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentLow Pressure Core Spray InoperableAt 0730 (EDT) on May 24, 2019, it was discovered that the Low-Pressure Core Spray System was inoperable. At Perry, the Low-Pressure Core Spray system is considered a single train system in Modes 1, 2, and 3; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). Inoperability of the Low-Pressure Core Spray system was caused by Emergency Service Water Pump A inoperability. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5406212 May 2019 15:39:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Reactor Scram Due to Partial Loss of Service Water

At 1039 CDT the reactor was manually (scrammed) due to a partial loss of plant service water. The loss of plant service water was caused by a loss of (balance of plant) BOP transformer 23. Reactor power was reduced in an attempt to restore pressure to plant service water. Reactor level is being maintained with condensate and feedwater. Reactor pressure is being maintained with bypass control valves. Standby Service Water A and B were manually initiated to supply cooling to Control Room A/C and (Engineered Safety Feature) ESF switchgear room coolers. The cause is under investigation. The NRC Resident Inspector has been notified. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B) as any event or condition that results in actuation of the Reactor Protection System (RPS), when the reactor is critical and also reported under 10 CFR 50.72(b)(3)(iv)(A), as any event or condition that results in actuation of RPS and Standby Service Water. The plant is currently in a normal electrical lineup.

  • * * UPDATE ON 5/12/19 AT 1846 EDT FROM GERRY ELLIS TO JEFFREY WHITED * * *

This is an update to the original notification. The Drywell and Containment exceeded the technical specification (TS) temperature limits of 135 degrees F (TS Limiting Condition of Operation (LCO) 3.6.5.5) and 95 degrees F (TS LCO 3.6.1.5), respectively. An 8-hour notification is being added for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to control the release of radioactive material per 10 CFR 50.72(b)(3)(v)(C). Notified R4DO (Alexander).

ENS 5400517 April 2019 06:37:0010 CFR 50.72(b)(3)(iv)(A), System ActuationUndervoltage to a Safety Related Bus Resulting in Valid System ActuationAt approximately 0137 CDT, with the Plant (Callaway) in No Mode (Defueled) the "B" Switchyard Bus cleared resulting in a loss of normal power to "A" Train Safety Related Transformer XNB01. This resulted in an under voltage condition on Safety Related Bus NB01. The "A" Emergency Diesel started per design and re-energized Bus NB01. This actuated the shutdown sequencer which first sheds loads including the "A" Spent Fuel Pool Cooling Pump and started "A" Essential Service Water Pump, "A" Component Cooling Water Pump, "A" Control Room A/C and other design loads. No complications were identified. The "A" Switchyard Bus remained energized at all times. The "A" Spent Fuel Pool Cooling Pump was restarted per off normal procedure response at 0149 CDT. Spent Fuel Pool water temperature started at 102 F and rose to 103 F prior to restart. There was no movement of irradiated fuel in progress in the Fuel Building during this time. The plant remains stable in No Mode (Defueled). At the time of the loss of "B" Switchyard Bus, the plant was closing Generator Output breaker MDV53 to establish a backfeed alignment. Further investigation is in progress. This event is reportable per 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident has been notified.
ENS 539736 November 2018 05:00:0010 CFR 21.21(d)(3)(i), Failure to Comply or DefectPart 21 Report - Residual Heat Removal System Motor Operated Globe Valve Experienced Stem FailuresThe following was received via e-mail: This notification is being submitted pursuant to the guidelines of 10 CFR Part 21 to report that a 24in Class 150 Globe valve for RHRSW HX (Residual Heat Removal Service Water Heat Exchanger) Isolation MOV (motor operated valves), E1150F068B at Detroit Edison - Fermi 2, experienced two stem failures. The site notified WVC USA (Weir Valves and Controls, USA) on November 6 of this issue involving two stems. WVC USA had supplied these stems on orders 20000262-10 and 20012001-10, Detroit Edison PO's (part orders) 4700505700 and 4701149217. A new stem failed after approximately 1 month in service in valve F068B. A replacement stem was installed and failed soon after being placed in service. This second stem failure had previously been in service for approximately three years while installed in sister valve F068A. Both stem breakages occurred at the transition area of the stem backseat and were visually identical. See pictures of failure in Attachment A. In the as found condition, the disc to stem connection appears to have lacked design clearances. The cause of this clearance issue was cleaning of the disc surface where the disc nut is tack welded. The material supplied is A276 410 heat treated and tempered to obtain (269-311 BHN). This material was approved by Powell as an acceptable alternate to the original material A182 F6 (269-311 BHN). During original Part 21 evaluation, testing of the stem material revealed low impact values and reflected effects of temper embrittlement. Other possible contributors to the failure were transition region at stem backseat and the valve service conditions where vibration due to throttling has been experienced. It was determined that although temper embrittlement and other factors may have contributed to the failures, that the lack of design clearance led to the failure of the stems and was not reportable by WVC USA. However, after discussions with Detroit Edison, WVC USA was requested to evaluate the failure considering the effects of temper embrittlement that might lead to future failures. WVC USA engineering is unable to determine the effects of temper embrittlement for the A276 410 material. Powell engineering was also consulted and there are no known methods to evaluate the potential for failure on the stem in this condition. As noted in NRC Information Notice No. 85-59, tempering in the 700 degrees F to 1050 degrees F range is not recommended because it results in low and erratic impact properties and poor resistance to corrosion and stress corrosion for 410 stainless steel. The stem failures in this case reflected these low and erratic impact properties based on material testing that was performed by DTE (Detroit Edison) Fermi and WVC USA. The A276 410 materials supplied in this event were tempered at 1025 degrees F and 1050 degrees F. The best solution is to eliminate the potential for temper embrittlement by using a higher required tempering temperature. The recommendation is to use A276 410 tempered at a minimum of 1100 degrees F. This is also in alignment with Code Case N-62-7. We are in the process of updating our item records to reflect this minimum tempering requirement and expect this action to be completed within one month. WVC USA is notifying the following sites of this potential issue so that they can evaluate the impact on the safe operation of the plant. 74347-10 Entergy PO 10118969 Site Grand Gulf Item Number P 26126666ASSEMAO_QLA Stem & Disc Assy 14" Qy (1) Shipped 7/28/06 0020005433-10 Georgia Power Company PO SNG10081312 REV. 2 Site Hatch Item Number P0000419C Stem/Disc Assy 24-300 Globe Valve Qty (1) Shipped 10/29/15 0020006979-10 Detroit Edison Company PO 4700846295 Site Fermi 2 Item Number P0000455C Stem Bin Gate Valve Qty (1) Shipped 6/29/15 0020011676-10 Detroit Edison Company PO 4701123403 Site Fermi 2 Item Number P0000455C Stem Bin Gate Valve Qty (1) Shipped 2/14/18 0020013251-10 Detroit Edison Company PO 4701230062 Site Fermi 2 Item Number P0000283 Stem Globe 24in 150# Qty (1) Shipped 9/19/18 0020013586-10 Detroit Edison Company PO 4701259926 C0#6 Site Fermi 2 Item Number P0000283 Stem Globe 24in 150# Qty (1) Shipped 11/13/18 Stem supplied under order 0020013251-10 is currently installed in F068A and order 0020013586-10 was delivered but not installed. F068B valve has been restored by Detroit Edison with a stem which has acceptable properties for the service. The above Part 21 notification affects Grand Gulf, Fermi 2, and Hatch. Point of Contact: Allen Fisher Director of Engineering 978-825-8451 allen.fisher@mail.weir
ENS 537779 October 2018 05:00:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid Specified System ActuationThis 60-day telephone notification is being made in accordance with 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to provide information pertaining to an invalid Engineered Safety Feature actuation signal. On October 9, 2018, Arkansas Nuclear One, Unit 2 was in refueling Mode 6, when a vital inverter failed while aligned from its alternate power source causing a loss of one of four vital instrument buses. The loss of the instrument bus resulted in one of the four engineered safety feature protection channels to enter a tripped state. Because one of the other four channels was already in a tripped state in support of a channel power supply replacement activity, two out of four protection channels were now in the tripped state resulting in a Safety Injection Actuation Signal, Containment Spray Actuation Signal, Containment Cooling Actuation Signal, Recirculation Actuation Signal, Emergency Feed Actuation Signal, and Containment Isolation Actuation Signal. In general, only one train of equipment is protected and assumed to be available during Mode 6 operations. Due to the defense-in-depth plant configuration in Mode 6, which is intended to avoid inadvertent start of emergency systems, the resulting actuations caused no adverse impact to Shutdown Cooling or Spent Fuel Pool cooling operations. At least one train of the following systems was aligned for automatic actuation: Service Water Emergency Diesel Generator Containment Penetration Room Exhaust Fan Other non-essential components which are shed or realigned upon safeguards actuation The few systems and components that were aligned for automatic operation responded as designed, including containment isolation valves and valves associated with the above systems (if aligned for automatic operation). The Service Water system was already in operation and, therefore, no Service Water pumps actuated. All systems and components which were capable of automatic operation performed as designed. The Emergency Diesel Generator started but did not synchronize to the bus. No safety injection occurred to the core. This actuation was caused by equipment failure and was not an actual signal resulting from parameter inputs. The affected actuation signals do not perform a safety function in Mode 6 and are not required to be available or operable. Therefore, this actuation is considered invalid. This event was entered into ANO's corrective action program for resolution. This event did not result in any adverse impact to the health and safety of the public. In accordance with 10 CFR 50.73(a)(i) a telephone notification is being made in lieu of submitting a written Licensee Event Report. The licensee has notified the NRC Resident Inspector.
ENS 5369928 October 2018 04:00:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Non Essential Service Water InoperableDuring the performance of Service Water Essential header swap, SWN-6 (Supply to Turbine Building Oil Coolers) valve stem became disconnected from its gear box at 85% open and could not be operated. Therefore, the non-essential service water system was inoperable. LCO 3.0.3 was entered at 0930 (EDT) with required actions to be in Mode 3 in 7 hours, Mode 4 in 13 hours and Mode 5 in 37 hours. Repair efforts were successful at shutting SWN-6, and LCO 3.0.3 was exited at 1305 (EDT) before adding any negative reactivity in support of shutdown. ('TS Required S/D' box not checked.) This condition constituted a loss of safety function which requires an 8 hour report (in accordance with) IAW 50.72(b)(3)(v)(B): Without the ability to close SWN-6, the non-seismic portion of the conventional Service Water System could not be isolated as required in the event of either a seismic event or as required in the EOPs. The nonessential service water system is required to support the recirculation phase post (Design Basis Accident) DBA for accident mitigation. The licensee notified the NRC Resident Inspector and the State of New York.
ENS 534853 July 2018 05:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionEn Revision Imported Date 8/1/2018

EN Revision Text: DISCOVERY OF AN UNANALYZED CONDITION THAT SIGNIFICANTLY DEGRADES PLANT SAFETY On July 3, 2018, while performing a review of Emergency Operating Procedures, a concern was identified regarding the potential for excessive loss of ultimate heat sink inventory (UHS) through the auxiliary feedwater (AFW) system mini-flow recirculation pathway. This condition would have the potential to prevent the ultimate heat sink from providing an adequate inventory of water for a 30-day mission time.

The normal water supply for the Callaway AFW system is the condensate storage tank (CST). The CST is a non-safety grade component. The safety-grade supply for AFW is the essential service water (ESW) system. The ESW system is supplied by the UHS. The UHS thermal performance analysis accounts for a loss of UHS inventory to the AFW system up until the point of the accident sequence that the AFW pumps would be secured. The analysis did not include an allowance for loss of UHS inventory through the AFW mini-flow recirculation pathway following the AFW pumps being secured. The EOP guidance that secures the AFW pumps does not isolate the mini-flow recirculation pathway.

Initial estimates indicate that loss of UHS inventory through the mini-flow recirculation pathway, if not isolated, would preclude the UHS from completing its 30-day mission time. This potential for depletion of the UHS placed the plant in an unanalyzed condition that significantly degraded safety.

Callaway has issued interim guidance to the on-shift personnel regarding this concern to ensure that the ultimate heat sink water level is maintained at a level that will be adequate to mitigate the potential loss of inventory.

This condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades safety. The NRC Resident Inspectors have been notified of this condition.

  • * * RETRACTION ON 07/31/2018 AT 1430 EDT FROM LEE YOUNG TO ANDREW WAUGH * * *

Event Notification (EN) 53485, made on July 3, 2018, is being retracted because re-evaluation performed subsequent to the notification has demonstrated, based on actual plant equipment and environmental conditions, that the unanalyzed inventory losses previously reported by EN 53485 would not have depleted the UHS inventory to an unacceptable level during its 30-day mission time. The re-evaluation has led to the conclusion that the previously unanalyzed losses of UHS inventory would not have prevented the UHS from performing its specified safety functions and meeting its 30-day mission time requirements. With the UHS capable of performing its specified safety functions and meeting its 30-day mission time requirements, the systems supported by the UHS would have remained capable of performing their specified safety functions. Based on these considerations, it has been determined that the condition reported in EN 53485 did not result in the plant being in an unanalyzed condition that significantly degraded safety. Consequently, the condition did not meet the criteria for an 8-hour notification per 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades safety. The NRC Resident Inspector has been notified of the Event Notification retraction. Notified R4DO (Gaddy).

ENS 534381 June 2018 04:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Tornado Missile Vulnerabilities

During the period of evaluation of tornado missile vulnerabilities and the potential impacts to technical specification (TS) plant equipment, it was determined that the power cables to a safety related motor control center (MCC) in the service water (SW) intake structure are not adequately protected from tornado generated missiles. During walk downs, it was identified that the installed SW pipe tunnel barrier is not adequate. A tornado could generate missiles capable of striking the power cables and rendering a SW MCC inoperable. These conditions are reportable per 10 CFR 50.72(b)(3)(ii)(B) and per 10 CFR 50.72(b)(3)(v)(D). This condition is being addressed in accordance with NRC enforcement guidance provided in Enforcement Guidance Memorandum (EGM) 15-002, 'Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance,' Revision 1, and DSS-ISG-2016-01, 'Clarification of Licensee Actions in Receipt of Enforcement Discretion per Enforcement Guidance Memorandum EGM 15-002, Enforcement Discretion for Tornado- Generated Missile Protection Noncompliance,' Revision 1. Compensatory measures have been implemented in accordance with these documents. The NRC Resident Inspector has been notified. The licensee will be notifying the Lower Alloways Creek Township.

  • * * UPDATE ON 6/18/2018 AT 1604 EDT FROM JUSTIN HARGRAVE TO RICHARD SMITH * * *

During subsequent walk downs, PSEG (Public Service Enterprise Group) identified that both the Unit 1 and Unit 2 turbine driven auxiliary feedwater pumps are also not adequately protected from tornado generated missiles. The steam exhaust pipe could be potentially impacted and cause crimping that could reduce steam exhaust flow and pump capacity. EN 53438 is updated to include both Salem units and these additional components. This condition is being addressed in accordance with NRC enforcement guidance provided in enforcement Guidance Memorandum (EGM) 15-002, 'Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance,' Revision 1, and DSS-ISG-2016-01, 'Clarification of Licensee Actions in Receipt of Enforcement Discretion per Enforcement Guidance Memorandum EGM 15-002, Enforcement Discretion for Tornado-Generated Missile Protection Noncompliance,' Revision 1. Compensatory measures have been implemented in accordance with these documents." The NRC Resident Inspector has been notified. The licensee will be notifying the Lower Alloways Creek Township. Notified R1DO (Burritt).

ENS 5339912 May 2018 04:27:0010 CFR 50.72(b)(3)(iv)(A), System ActuationInadvertent Actuation of the Emergency Diesel GeneratorOn 5/11/2018, at 2327 hours CDT, with the plant in Mode 5, Grand Gulf Nuclear Station was making preparations for surveillance test 06-OP-1P75-R-0003, Standby Diesel Generator 1 Functional Test. The Grand Gulf Nuclear Station experienced an auto-start of the Division 1 (Emergency) Diesel Generator (EDG) when the 15AA Bus Potential Transformer (PT) fuse drawer was racked out instead of the line PT fuse drawer for Bus 15AA feeder breaker 152-1514. This resulted in the 15AA Incoming Feeder Breaker 152-1511 from Engineered Safety Features Transformer 12 opening, de-energizing the 15AA Bus. The Division 1 EDG started and energized Bus 15AA. The Division 1 LSS SYSTEM FAIL annunciator was received and Standby Service Water A failed to start due to the 15AA Bus PT fuse drawer being racked out. Standby Gas Treatment Train B was manually initiated per the Loss Of AC Power Off Normal Emergency Procedure. Station equipment operated as expected based on the PT fuse drawer that was racked out. The Division 1 EDG was manually tripped from the Control Room because cooling from the Standby Service Water A was not available. RHR (residual heat removal) B was in Shutdown Cooling (mode) and was verified not affected The licensee has notified the NRC Resident Inspector.
ENS 533938 May 2018 06:39:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedContainment Leak Rate Greater than Tech SpecOn May 8, 2018 at 0139 Central Daylight Time, Farley Nuclear Plant Unit 1 declared containment inoperable due to total containment leak rate greater than technical specifications. The 1B containment cooler had seat leakage of approximately 30 gallons per minute from a service water drain valve. Though the containment cooler service water supply is not tested per the Appendix J program, a loss of the containment barrier is possible under accident conditions. The service water flow path to the 1B containment cooler has been isolated to exit the condition. The licensee will notify the NRC resident inspector.
ENS 533803 May 2018 17:20:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessLoss of Emergency Assessment CapabilityDuring planned maintenance on Unit 2 Radiation Monitor 2-RE-4270 (Service Water Train B to Discharge Canal Rad Monitor), at 1220 CDT, several other Unit 2 Radiation Monitors that are used for Emergency Action Level evaluation became nonfunctional for about 1 hour. With these radiation monitors non-functional, all of the Emergency Action Levels associated with these monitors could neither be evaluated nor monitored. This unplanned condition is reportable as a loss of assessment capability per 10 CFR 50.72(b)(3)(xiii). A PC11 computer reboot restored the affected radiation monitors to a functional status. The NRC Resident Inspector has been notified.
ENS 5322320 February 2018 18:25:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
All Three Auxiliary Feedwater Pumps Inoperable Due to Helb Door Being Open

At 1225 CST, all three Auxiliary Feedwater (AFW) pumps were declared inoperable at the Callaway Plant upon discovery that a door (DSK13311) credited for protection of equipment from the effects of a high-energy line break (HELB) hazard had come partially open due to vibration harmonics from the running turbine-driven Auxiliary Feedwater pump (TDAFP). Immediate investigation identified that play in the mechanism that holds the door closed had rendered it susceptible to movement from the vibration harmonics. The affected HELB door specifically protects safety-related instruments that provide a swap-over signal upon detection of a low suction pressure condition for the AFW pumps and thereby automatically effect a suction transfer for the AFW pumps from the condensate storage tank (normal/standby source) to the Essential Service Water (ESW) system (credited safety-related source). All of the AFW pump suction transfer instrument channels were declared inoperable. Per Technical Specifications (TS) 3.3.2, 'Engineered Safety Feature Actuation System (ESFAS) Instrumentation,' the applicable Condition(s) and Required Action(s) for inoperable AFW pump suction transfer instrumentation only addresses a single channel being inoperable. Thus, the condition of having all three instrument channels inoperable required entry into TS Limiting Condition for Operation (LCO) 3.0.3. At the same time, however, with the automatic suction transfer capability rendered inoperable, all three AFW pumps, i.e., the TDAFP and the 'A' and 'B' motor-driven AFW pumps, were declared inoperable. Although LCO 3.0.3 was applicable, entry into the Required Actions of LCO 3.0.3 was suspended per the Note attached to Required Action E.1 of TS 3.7.5, 'Auxiliary Feedwater (AFW) System,' which states, 'LCO 3.0.3 and all other LCO Required Actions requiring MODE changes are suspended until one AFW train is restored to OPERABLE status.' At 1336 CST, Operations took actions to prevent the TDAFP from running, so the remaining (AFW Pumps) could be returned to Operable status. Operations then declared the affected instrumentation and the 'A' and 'B' motor-driven AFW pumps Operable. This allowed LCO 3.0.3 and Conditions A, B, D, and E under TS 3.7.5 to be exited. With only the TDAFP inoperable, TS 3.7.5 Condition C and its Required Actions remain in effect. Due to the degraded HELB door rendering all three AFW pumps inoperable, the unidentified condition is being reported as an unanalyzed condition that significantly degraded plant safety (per 10 CFR 50.72(b)(3)(ii)(B)) as well as a condition that could have prevented the fulfillment of the safety functions of structures or systems that are needed to shut down the reactor and maintain it in a safe shutdown condition, remove residual heat, and mitigate the consequences of an accident (per 10 CFR 50.72(b)(3)(v)(A), (B), and (D), respectively). The NRC Senior Resident Inspector has been notified.

  • * * RETRACTION ON 4/4/2018 at 1109 EDT FROM JONATHAN LAUF TO DAVID AIRD * * *

Event Notification (EN) # 53223, made on 2/20/2018, is being retracted because new information has been obtained that negates the original basis for reporting the unanalyzed condition. Specifically, an evaluation of the HELB that is postulated to occur in the TDAFP room has determined that without crediting door DSK13311 for protection, the affected safety-related instruments would not be exposed to environmental conditions beyond their analyzed capability. This resulted in a conclusion that the unanalyzed condition of door DSK13311 being open did not prevent the affected safety-related instruments or their supported AFW pumps from performing their required safety functions to shut down the reactor and maintain it in a safe shutdown condition, remove residual heat, and/or mitigate the consequences of an accident, nor did it significantly degrade plant safety. Consequently, the condition did not meet the criteria for an 8-hour notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(A), (B), or (D). The licensee notified the NRC Resident Inspector. Notified R4DO (Drake).

ENS 531056 December 2017 02:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessUnplanned Loss of Multiple Radiation Monitors During MaintenanceAt 2000 (CST), Comanche Peak experienced a failure of SCADA B of the PC11 Radiation Monitor System. This failure caused a loss of Unit 1 Main Steam Line 1-01 and 1-03 Radiation Monitors (1-RE-2325 and 1-RE-2327) and Train A and Train B Station Service Water Radiation Monitors (1-RE-4269 and 1-RE-4270). With the Main Steam Line Radiation Monitors nonfunctional, all of the emergency action levels for a steam generator tube rupture in steam generators 1-01 and 1-03 could neither be evaluated nor monitored. With the Station Service Water Radiation Monitors non-functional, all of the emergency action levels for a radioactive release through station service water could neither be evaluated nor monitored. This unplanned condition is reportable as a loss of assessment capability per 10 CFR 50.72(b)(3)(xiii). Comanche Peak Nuclear Power Plant (CPNPP) has assurance of steam generator integrity, reactor coolant system integrity, and fuel cladding integrity and there is a negligible safety significance to condition from a public health and safety perspective. Additionally, compensatory measures are in place to assure adequate monitoring capability is available to implement the CPNPP emergency plan in the unlikely event of challenges to the steam generator, reactor coolant system, or the fuel cladding. Until these radiation monitors were restored, Operations implemented compensatory measures to monitor the Condenser Off Gas Radiation Monitor for early signs of a steam generator tube leak/rupture and Radiation Technicians were briefed on taking local readings with a Geiger-Mueller tube on the Main Steam Lines. Chemistry Technicians were performing hourly samples of Station Service Water and reporting results to the Control Room. Corrective actions were pursued to restore the non-functional radiation monitors back to service. Those actions are complete and all radiation monitors have been restored to service. The NRC Resident Inspector has been notified. PC11 is a computer common to both Units. The failure happened during radiation monitor maintenance to a single monitor, which unexpectedly affected multiple monitors.
ENS 530836 October 2017 14:10:0010 CFR 50.73(a)(1), Submit an LERInvalid Specified System ActuationOn October 6, 2017 at 0910 CDT hours, with Unit 1 in Mode 1 (Power Operation), the 1A Diesel Generator Cooling Water Pump (DGCWP) automatically started. The cause was the misoperation of the 1B/C RHR (Residual Heat Removal) Room Cooler Fan (1VY03C) control switch, which was placed in the start position instead of the intended pull-to-lock position. The start of the 1VY03C fan resulted in the automatic actuation of the 1A DGCWP. This system actuation is reportable in accordance with 10CFR50.73(a)(2)(iv)(A). The invalid actuation was not part of a pre-planned sequence during testing or reactor operation. The 1A DGCWP, an emergency service water system that does not normally run and that serves as an ultimate heat sink, responded satisfactorily. This call is being made in accordance with 10CFR50.73(a)(1), which states that in the case of an invalid actuation reported under 10CFR50.73(a)(2)(iv), other than an actuation of the reactor protection system when the reactor is critical, the licensee may provide a telephone notification to the NRC Operations Center within 60 days after discovery of the event instead of submitting a written Licensee Event Report. The licensee notified the NRC Resident Inspector.
ENS 528884 August 2017 19:11:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Inoperable Due to Opening in Service Water Piping

On August 4, 2017, at 1511 EDT, Unit 1 Secondary Containment was declared inoperable due to a small (i.e., approximately 0.75 inch diameter) hole in Service Water system piping which was found during ultrasonic testing activities. The affected portion of piping penetrates Secondary Containment and flow in the piping creates a vacuum condition; thus bypassing Secondary Containment. The identified hole is being evaluated with respect to its impact on operability of the Service Water system. This condition is being reported in accordance with 10 CFR 50.72(b)(3)(v)(C), as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. This event did not result in any adverse impact to the health and safety of the public. Initial Safety Significance Evaluation: The initial safety significance of this event is minimal. At the time of discovery, Unit 1 was at 100% steady state conditions. Reactor Building Ventilation was in service in a normal alignment. No abnormal radioactivity conditions existed within Secondary Containment. Corrective Actions: Temporary repair of the affected Unit 1 Service Water piping has been completed. This repair was evaluated by Engineering and it has been determined that the repair meets the requirements to maintain Secondary Containment operable. Unit 1 Secondary Containment operability was restored at 1704 EDT on August 4, 2017. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM MIKE BRADEN TO RICHARD SMITH AT 1447 EDT ON 9/27/17 * * *

Based upon further evaluation, Duke Energy is retracting Event Notification 52888. The safety objective of Secondary Containment is to limit the release of radioactivity to the environment after an accident so that the resulting exposures are kept to a practical minimum and are within regulatory limits. A bounding engineering evaluation was performed which demonstrates that potential releases from Secondary Containment could not have resulted in offsite or control room doses exceeding regulatory limits. Furthermore, the condition did not impact Technical Specification operability of Secondary Containment in that the ability of Secondary Containment to maintain the required vacuum was not impacted. Therefore, this condition does not represent an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material and is not reportable in accordance with 10 CFR 50.72(b)(3)(v)(C), and the event notification is being retracted. The NRC Senior Resident was notified of this retraction. Notified R2DO (A. Masters).

ENS 5281216 June 2017 20:35:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Loss of Safety Function Due to Keowee Dam Units Being Declared InoperableKeowee Hydro Units (KHU) 1 and 2 were both declared inoperable at 1635 (EDT) on 6-16-17 due to discovery of breaker 1GSC-1 (KHU-1) in the intermediate position, and breaker 2GSC-1 (KHU-2) in the open position. Keowee Hydro Units are required to be operable per TS (Technical Specification) 3.8.1 (AC Sources - Operating), TS 3.8.2 (AC Sources - Shutdown), and TS 3.7.10 (Protected Service Water, applies only to KHU aligned to the Overhead Power Path). All Tech Spec required conditions were entered, and all required actions completed. Both Standby Buses were energized from a Lee Combustion Turbine via an isolated power path at 1715 (EDT) on 6-16-17 in accordance with TS 3.8.1 Condition (I), Required Action (I.1). It has been determined by station personnel that a loss of safety function did occur between 1635 (EDT) (when the Keowee Hydro Units were declared inoperable) and 1715 (EDT) (when the Standby Buses were energized from a Lee Combustion Turbine via an isolated power path). Investigation has determined the cause of breakers 1GSC-1 and 2GSC-1 being out of their required closed position to be inadvertent bumping while performing station work activities. Breakers 1GSC-1 and 2GSC-1 have been reclosed, and both Keowee Hydro Units have been declared operable as of 2351 (EDT) on 6-16-17. The licensee notified the NRC Resident Inspector.
ENS 5280615 June 2017 14:58:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray Declared InoperableAt 0958 hours (CDT), during planned surveillance testing of the Division 3 Shutdown Service Water (SX) subsystem, the Division 3 SX pump tripped for unknown reasons. The Division 3 SX subsystem was declared inoperable and in accordance with Technical Specification 3.7.2, Action A.1, the High Pressure Core Spray (HPCS) system was declared inoperable. Since the HPCS system is a single train safety system, this event is reportable under 10CFR50.72(b)(3)(v)(D). An investigation is underway to determine the cause of the SX pump trip. The NRC Resident has been notified.
ENS 5264729 March 2017 19:08:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Discovery of Non-Conforming Conditions During Tornado Hazards AnalysisDuring an evaluation of protection for Technical Specification (TS) equipment from the damaging effects of tornados, Palisades Nuclear Plant personnel identified conditions in the plant design such that specific TS equipment is considered not adequately protected from tornado missiles. Specifically, vulnerabilities were identified in the following systems and components: Service Water System - Service water pump discharge header and service water pump cable trays. Fuel Oil Transfer System - Fuel oil transfer piping and transfer pump cable trays. Emergency Diesel Generators - Vent lines on the fuel oil day tanks. Control Room Heating, Ventilation, and Cooling System - Both the normal and emergency intake ducts. Steam Driven Auxiliary Feedwater Pump - Feedwater pump relief valves. Component Cooling Water System - Component cooling water surge tank. The identified vulnerabilities are being addressed in accordance with Enforcement Guidance Memorandum (EGM), 15-002, and Interim Staff Guidance, DSS-ISG-2016-01. Initial compensatory measures are in place. The licensee notified the NRC Resident Inspector.
ENS 5264531 January 2017 19:25:0010 CFR 50.73(a)(1), Submit an LER60-Day Report Due to Invalid Eccs Actuation Signal

The following report is made pursuant to 10 CFR 50.73(a)(2)(iv)(A) due to an unintended initiation signal that occurred on January 31, 2017 with James A. FitzPatrick Nuclear Power Plant (JAF) in Mode 5 at zero (0) percent power. On January 31, 2017 at 1425 (EST) the control room received multiple annunciations associated with the following Systems / Trains: Primary Containment Isolation System (PCIS) / Trains A and B Residual Heat Removal System (RHR) / Trains A and B Core Spray (CS) / Trains A and B Reactor Core Isolation Cooling (RCIC) All four (4) Emergency Diesel Generators (EDG) auto-started with their associated Emergency Service Water pumps operating. RHR and CS both received initiation signals but were defeated per procedure. The HPCI (High Pressure Coolant Injection) auxiliary oil pump was taken to Pull-to-Lock per procedure, and the RCIC steam isolation valve cycled until the breaker was opened to close the valve. An evaluation concluded that the (Emergency Core Cooling System - ECCS) initiation signals were caused by the opening of a portable job box that was stored near sensitive equipment. Upon opening the job box, the lid bumped a reference leg resulting in the initiation signals. All initiation signals were reset and systems restored to normal shutdown lineups. The licensee notified the NRC Resident Inspector.

  • * * UPDATE ON 3/30/17 AT 0840 EDT FROM DUSTIN SCURLOCK TO DONG PARK * * *

To the original report, the licensee added, "This condition recurred at 1624 (EDT on 1/31/17). The licensee notified the NRC Resident Inspector. Notified R1DO (Cook).

ENS 5245521 December 2016 18:50:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed Condition Due to Valve FailureDuring review of the Limerick future modification list, a concern was raised with a proposed modification for HV-011-015A, ESW (Emergency Service Water) 'A' Discharge to 'B' RHR Service Water Return, which failed to fully close during routine testing. As a result of the failure to close, a clearance was applied and a 10CFR50.59 screening was performed to close and de-energize HV-011-015A and open and de-energize valve HV-011-011A, ESW 'A' Discharge to 'A' RHR (Residual Heat Removal) Service Water Return. This clearance isolated one of the two ESW return flow paths so that only one flow path is available to return cooling water flow to the spray pond. The 10CFR50.59 screening did not address that fire areas 12 (Unit 1 4kV D13 switch gear room) and 18 (Unit 2 4kV D23 switch gear room) are not in compliance with the existing fire safe shutdown (FSSD) analysis. The FSSD analysis credits both flow paths so that Emergency Service Water can be returned to the spray pond. With only one of the two return flow paths available, a single spurious fire induced valve operation can result in deadheading an ESW pump and starving an operating emergency diesel generator of cooling water. Running the emergency diesel generator with a loss of cooling water will initiate a diesel protective trip on high temperature. Compensatory measures are in place for the specific fire areas listed above. The licensee has notified the NRC Resident Inspector.
ENS 5245124 October 2016 23:45:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid Specified System ActuationThis 60-day telephone notification is being submitted in accordance with 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to report an invalid actuation of the 12 Emergency Diesel Generator Emergency Service Water pump (12 ESW pump). At 1745 (CST) on October 24, 2016, an unexpected auto-start of the 12 ESW pump occurred. The 12 Emergency Diesel Generator (12 EDG), was previously properly removed from service and isolated for scheduled maintenance. Upon investigation, is was determined that no valid start signal was present and actuation occurred during relay replacement activities on the 12 EDG in C-92 (12 EDG (G-38) electrical control panel) cabinet when electricians inadvertently bumped a 12 EDG start relay. During this period, the Control Room received annunciators indicating the 12 EDG engine was running/cranking and the 12 ESW pump started. Due to being isolated, the 12 EDG did not actually start. The licensee notified the NRC Resident Inspector.
ENS 524147 December 2016 19:43:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Discovery of Non-Conforming Conditions During Tornado Hazards AnalysisDuring the evaluation of tornado missile vulnerabilities and the potential impacts to Technical Specification (TS) plant equipment, it was concluded that the following SSCs (systems, structures, and components) were vulnerable to tornado generated missiles. The Service Water Intake Structure (SWIS) intake and exhaust ventilation hoods, located on the roof of the SWIS, are not adequately protected from missiles generated by a tornado. Should a tornado-generated missile strike the SWIS intake and exhaust ventilation hoods, the hoods could crimp thus reducing air flow and challenging the performance of their heating and cooling safety functions. If the intake hoods were damaged or removed due to a missile strike, entry of rainwater could occur due to severe weather high wind velocity, and could affect safety related electrical equipment in the rooms directly below the hoods. These potential conditions could render Service Water trains inoperable on either or both units. This condition is reportable per 10 CFR 50.72(b)(3)(ii)(B) for any event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety, and per 10 CFR 50.72(b)(3)(v)(D) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. This condition is being addressed in accordance with EGM-15-002 and DSS-ISG-2016-01 (enforcement discretion and interim guidance documents). Required actions have been taken. Corrective actions will be documented in a follow up licensee event report. The NRC Resident Inspector will be notified. The licensee is evaluating the operability of the service water system. Should one train be declared inoperable, the licensee would be in a 72 hr. LCO action statement. If both trains are inoperable, then the licensee would enter T.S. 3.0.3.