Semantic search

Jump to navigation Jump to search
 Discovered dateReporting criterionTitleEvent description
ENS 568972 November 2023 01:11:0010 CFR 50.73(a)(1), Submit an LER60 Day Notification for an Invalid Specified System ActuationThe following information was provided by the licensee via email and phone: At 2011 EDT on 11/01/23, with Unit 2 in Mode 3 at 0 percent power, Unit 2 received multiple spurious actuations. These actuations consisted of a partial group 1 and a partial group 5 primary containment isolation and a partial secondary containment isolation. The partial Group 1 isolation resulted in the closure of two main steam isolation valves (MSIVs); all other MSIVs were already closed. The partial group 5 isolation auto closed one of the reactor water cleanup (RWCU) isolation valves. The partial secondary containment isolation resulted in the closure of the inboard refueling floor and reactor building secondary containment isolation valves (SCIVs). Additionally, at 2238 EDT, Unit 2 again received multiple spurious actuations. These actuations consisted of a partial group 5 primary containment isolation and a partial secondary containment isolation. The partial group 5 isolation auto closed one of the RWCU isolation valves The partial secondary containment isolation resulted in the closure of the inboard refueling floor and reactor building SCIVs. And again, at 2354 EDT, Unit 2 received spurious actuations which consisted of a partial secondary containment isolation which resulted in the closure of the inboard refueling floor and reactor building SCIVs. The spurious actuations seen on 11/1/23 are triggered at -35 inches reactor water level (RWL) for group 5 and secondary containment isolations and at -101 inches RWL for group 1 isolations. It was determined that a combination of the RWL fluctuating above and below the wide range instrument reference leg tap, the reactor vessel pressure being lowered, and reactor core isolation cooling introducing colder water conditions near the reference leg tap of the wide range instrument caused the spurious actuations. Using multiple RWL indications for each of the instances mentioned above, the actuations were confirmed to be spurious as RWL was being controlled in a band of +55 inches to +85 inches at the time of the actuations. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an invalid actuation of a partial group 1, a partial group 5, and partial secondary containment logic. The NRC Resident has been notified.
ENS 567102 September 2023 10:32:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Scram Due to Feedwater TransientThe following information was provided by the licensee via email: On 9/2/2023 at 0632 EDT, a feedwater transient occurred resulting in an reactor protection system (RPS) automatic reactor scram on low level (Level 3, 159.3 inches). Following the scram, reactor water level dropped below Level 2 (108.8 inches) resulting in a Group 2 recirculation sample system isolation, Group 3 traveling in-core probe (TIP) isolation valve isolation, Group 6 and 7 reactor water cleanup isolation, and Group 9 containment purge isolations. All control rods inserted as expected. High pressure core spray and reactor core isolation cooling initiated and injected as expected. ECCS systems have been secured and normal reactor pressure and level control has been established for hot shutdown. Nine Mile Point Unit 2 is stable and in Mode 3. These 4 hour and 8 hour non-emergency reports are being made in accordance with 10 CFR 50.72(b)(2) (iv)(A), 10 CFR 50.72(b)(2)(iv)(B), and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident was informed. There was no impact on Unit 1.
ENS 5593813 June 2022 16:23:0010 CFR 50.72(b)(3)(iv)(A), System ActuationPartial Loss of Power to RPS During Maintenance

The following information was provided by the licensee via email: During thermography of a reactor protection system (RPS) distribution panel, a circuit breaker (RPS-CB-7B) was inadvertently opened. This resulted in a partial loss of power to RPS Division B, which caused containment isolations to occur in multiple systems (Reactor Water Clean Up, Equipment Drains Radioactive, Floor Drains Radioactive, Reactor Recirculation, and Traversing lncore Probe). Specifically, RWCU-V-1, FDR-V-3, EDR-V-19, RRC-V-19, and TIP-V-15 all closed. All actuations occurred as designed upon the partial loss of RPS power. This event is being reported pursuant to 10 CFR 50.72(b)(3)(iv)(A) due to an unplanned valid actuation of a system pursuant to 10 CFR 50.72(b)(3)(iv)(B)(2). Additionally, this is being reported pursuant to 10 CFR 50.72 (b)(3)(xiii) for a major loss of emergency assessment capability due to the inability to assess primary containment identified and unidentified leakage rates. Emergency assessment capability was restored at 1008 PDT upon system restoration. The NRC resident was notified by the licensee.

  • * * UPDATE FROM SIMEON MORALES TO DONALD NORWOOD AT 1547 EDT ON 6/16/2022 * * *

The following information was received via email: This event is being reported pursuant to 10 CFR 50.72 (b)(3)(xiii) only for a major loss of emergency assessment capability due to the inability to assess primary containment identified and unidentified leakage rates. The containment isolation was not due to actual plant conditions or parameters meeting design criteria for containment isolation. Therefore, this is considered an invalid actuation. Updated ENS Text: During thermography of a reactor protection system (RPS) distribution panel, a circuit breaker (RPS-CB-7B) was inadvertently opened. This resulted in a partial loss of power to RPS Division B, which caused containment isolations to occur in multiple systems (Reactor Water Clean Up, Equipment Drains Radioactive, Floor Drains Radioactive, Reactor Recirculation, and Traversing Incore Probe). Specifically, RWCU-V-1, FDR-V-3, EDR-V-19, RRC-V-19, and TIP-V-15 all closed. All actuations occurred as designed upon the partial loss of RPS power. This is being reported pursuant to 10 CFR 50.72 (b)(3)(xiii) for a major loss of emergency assessment capability due to the inability to assess primary containment identified and unidentified leakage rates. Emergency assessment capability was restored at 1008 PDT upon system restoration. The plant is stable, and all effected systems have been restored. There was no impact to the health and safety of the public or plant personnel. The NRC resident has been notified. Notified R4DO (Azua).

  • * * UPDATE FROM TRACY HOWARD TO ERNEST WEST AT 1853 EDT ON 8/10/2022 * * *

The following information was received via email: At 0923 (PDT) on June 13, 2022, a partial loss of power to the Reactor Protection System (RPS) 'B' occurred due to the inadvertent opening of circuit breaker RPS-CB-7B during thermography of RPS-PP-C72/P001. The partial loss of RPS 'B' resulted in closure of primary containment isolation valves (PCIVs) in multiple systems. No plant parameters existed which would cause the opening of RPS-CB-7B or actuation of the primary containment isolation; therefore, this is considered to be an invalid actuation of a system listed in 10 CFR 50.73(a)(iv)(B). The closure of PCIVs were expected responses to the partial loss of RPS 'B'. Circuit breaker RPS-CB-7B was closed lo restore energy lo RPS 'B' at 1008 (PDT), containment isolation valves were opened, and the affected systems were returned to normal operating conditions for the current configuration per plant procedures. As indicated in 10 CFR 50.73(a)(1), in the case of an invalid actuation reported under 10 CFR 50.73(a)(2)(iv)(A), the licensee may, at its option, provide a telephonic notification lo the NRC Operations Center within 60 days of discovery of the event instead of submitting a written Licensee Event Report. This 60-day telephone notification is being made in accordance with 10 CFR 50.73(a)(1) for invalid actuations reported under 10 CFR 50.73 (a)(2)(iv)(A). This actuation was invalid since it was caused by maintenance activities and not the result of actual plant conditions warranting containment isolation. The following additional information is provided as specified in NUREG-1022: The following inboard containment isolation valves were actuated when personnel inadvertently bumped into RPS-CB-7B during the removal of a panel � RWCU-V-1 Reactor Water Cleanup Suction Inboard Isolation Valve � EDR-V-19 Drywell Equipment Drain Inboard Isolation Valve � FDR-V-3 Drywell Floor Drain Inboard Isolation Valve � RRC-V-19 Reactor Water Sample Inboard Isolation Valve � TIP-V-15 Traversing In-Core Probe Purge Isolation Valve All actuations occurred as designed upon the partial loss of RPS power. There were no actual safety consequences associated with this event since all affected equipment responded as designed. The NRG Residents have been notified. Notified R4DO (O'Keefe).

ENS 558215 April 2022 06:23:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Scram on LOW LevelThe following information was provided by the licensee via telephone and email: On 4/5/2022, at time 0223, during maintenance on Feedwater Level Control Valve 2FWS-LV10B, a Feedwater transient occurred resulting in an RPS Automatic Reactor Scram on Low Level (Level 3, 159.3 inches). Following the scram, reactor water level dropped below Level 2 (108.8 inches) resulting in a Group 2 Recirculation Sample System Isolation, Group 3 TIP ((Traversing Incore Probe)) Isolation Valve Isolation, Group 6 and 7 Reactor Water Cleanup Isolation and Group 9 Containment Purge Isolations. All control rods inserted as expected. High Pressure Core Spray and Reactor Core Isolation Cooling initiated and injected as expected. ECCS Systems have been secured and normal reactor pressure and level control has been established for hot shutdown. Nine Mile Point Unit 2 is stable in Mode 3. These 4 hour and 8-hour non-emergency ENS ((Emergency Notification System)) reports are being made in accordance with 10 CFR 50.72(b)(2)(iv)(A), 10 CFR 50.72(b)(2)(iv)(B), and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident was informed. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: There was no impact on Unit 1.
ENS 5566020 October 2021 13:05:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One System
  • The following information was provided by the licensee via email:

This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of the Reactor Protection System (RPS). On October 20, 2021, at approximately 0705 hours Central Daylight Time (CDT), Browns Ferry, Unit 1, 1B RPS bus unexpectedly lost power. The loss of the bus resulted in a half scram, automatic Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolations, and Trains A, B, and C SBGT (Stand-By Gas Treatment) and A CREV (Control Room Emergency Ventilation system) started. All systems responded as expected. At 0720 hours CDT, the bus was placed on the alternate power supply and the half scram and PCIS isolations were reset. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The cause of the RPS bus loss was a trip of the underfrequency relay due to drift of the relay setpoint. The relay was replaced and 1B RPS bus was returned to the normal power supply on October 21, 2021, at 0510 hours CDT. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1729592. The NRC Resident Inspector has been notified of this event.

ENS 556276 December 2021 16:25:0010 CFR 50.72(b)(3)(iv)(A), System ActuationValid Safety System Actuation

On December 6, 2021, at 1125 hours Eastern Standard Time (EST), during planned maintenance activities, electrical power was lost to the 4160V emergency bus E-3. The power loss to emergency bus E-3 affected both Unit 1 and 2. Emergency Diesel Generator #3 received an automatic start signal but was under clearance for planned maintenance. Emergency bus E-3 was re-energized at 1315 EST hours via offsite power. The loss of power to E3 resulted in Unit 2 Primary Containment Isolation System (PCIS) Group 2 (i.e., Drywell Equipment and Floor Drain, Residual Heat Removal (RHR) Discharge to Radwaste, and RHR Process Sample), Group 3 (i.e., Reactor Water Cleanup), Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems), and Group 10 (i.e., air isolation to the drywell) isolations. The actuations of PCIVs were completed and the affected equipment responded as designed. Per design, no Unit 1 safety system group isolations or actuations occurred. Other Unit 2 actuations included the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start signal to the Standby Gas Treatment (SGT) System trains A and B and the Control Room Emergency Ventilation System (CREV). Systems functioned as designed. Safety systems functioned as designed following the de-energization of bus E-3. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of PCIS on Unit 2 and an automatic start signal to Emergency Diesel Generator #3. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Except for the Emergency Diesel Generator, which is out of service for planned maintenance, all equipment has been returned to its normal alignment.

  • * * UPDATE FROM JJ STRNAD TO THOMAS KENDZIA AT 2028 EST ON DECEMBER 6, 2021 * * *

The loss of power to E3 resulted in Unit 1 Primary Containment Isolation System (PCIS) Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems). Other Unit 1 actuations included the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start signal to the Standby Gas Treatment (SGT) System trains A and B and the Control Room Emergency Ventilation System (CREV). Systems functioned as designed. Safety systems functioned as designed following the de-energization of bus E-3. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of PCIS on Unit 1. All Unit 1 equipment was returned to its normal alignment. The NRC Resident will be notified. Notified R2DO (Miller).

ENS 552871 April 2021 18:02:0010 CFR 50.73(a)(1), Submit an LER60-Day Telephonic Notification of Invalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of the 2A Reactor Protection System (RPS). On April 1, 2021, at 1302 (CDT), Browns Ferry Unit 2, 2A RPS (Motor Generator) MG set tripped causing a half scram. Unit 2 experienced an unexpected trip of the 2A RPS MG Set that resulted in automatic Primary Containment Isolation System (PCIS) Group 2, 3, 6, and 8 isolations and Trains A, B, and C Standby Gas Treatment (SGT) and Train A Control Room Emergency Ventilation (CREV) starts. At the time of the event, Unit 2 was in a refueling outage and the rods were already fully inserted. All systems responded as expected. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. Based on the troubleshooting conducted, the cause was determined to be a loose wiring connection in the motor circuit. The lugs were replaced with ring lugs. Operations reset the 2A RPS Half Scram and PCIS in accordance with 2-AOI-99-1 on April 1, 2021, at 1324 CDT thus correcting the condition and returning RPS to service. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1683358. The NRC Resident Inspector has been notified of this event.
ENS 549326 August 2020 22:49:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of an Invalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On August 6, 2020, at approximately 1749 CDT, Browns Ferry Nuclear Plant (BFN), Unit 2 experienced a loss of Reactor Protection System (RPS) Bus 2A. Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolated in response to this event. The PCIS isolations caused the initiation of Standby Gas Treatment (SBGT) trains A, B, and C, and Control Room Emergency Ventilation (CREV) subsystem A. Unit 2 declared RCS leakage detection instrumentation inoperable and entered TS LCO 3.4.5 condition A, B, and D with required action D.1 to enter LCO 3.0.3 immediately. Unit 2 entered TS LCO 3.0.3 with required actions to be in Mode 2 within 10 hours, Mode 3 within 13 hours, and Mode 4 within 37 hours. Upon investigation, it was discovered that an age-related overheating condition resulted in the failure of the 2A RPS Motor Generator (MG) set, causing the feeder beaker from the 2A 480v Remote Motor-Operated Valve distribution board to trip. On August 6, 2020, at approximately 1808 CDT, Operations personnel commenced restoration of Unit 2 to normal after transferring 2A RPS to its alternate power supply. The 2A RPS MG Set drive motor was replaced on August 24, 2020. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel (RV) Low Water Level or Drywell High Pressure. Plant conditions which initiate PCIS Group 3 actuations are RV Low Water Level or Reactor Water Cleanup Area High Temperature. Plant conditions which initiate PCIS Group 6 actuations are RV Low Water Level, High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation. Plant conditions which initiate PCIS Group 8 actuations are Reactor Vessel (RV) Low Water Level or Drywell High Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. All affected safety systems responded as expected. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1628707. The NRC Resident Inspector has been notified of this event.
ENS 5470916 March 2020 06:02:0010 CFR 50.73(a)(1), Submit an LERInvalid Specified System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On March 16, 2020, at approximately 0102 CDT, Browns Ferry Nuclear Plant (BFN), Unit 3 received motor trip-out alarms and diagnosed Group 2 and 3 Primary Containment Isolation System (PCIS) Isolations, 3C Residual Heat Removal (RHR) Pump tripping and Reactor Water Cleanup (RWCU) system isolating. All affected safety systems responded as expected. BFN, Unit 3, was nearing the end of the U3R19 refueling outage at the time of the event, and was still dependent on the Shutdown Cooling (SDC) system. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. At the time of the event, these conditions did not exist: therefore, the PCIS actuation was invalid. The event was determined to have been caused by clearance restoration activities in an unprotected control panel. A fuse re-installation inadvertently created a fault condition between two different plant 120 VAC power sources when the fuse holder's lower spring clip contacted a different fuse. This was a result of age-related degradation of the fuse holder, its close proximity to other fuses, and the lack of insulating isolation barriers between fuses. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1594925. The NRC Resident Inspector has been notified of this event.
ENS 546979 March 2020 01:21:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On March 8, 2020, at approximately 2021 CDT, Browns Ferry Nuclear Plant Unit 2 experienced an unexpected loss of the 2A Reactor Protection System (RPS). This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and the initiation of Standby Gas Treatment Trains A and B, and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The RPS MG Set trip was believed to have been caused by an intermittent short across a spike suppressor, which led to a loss of generator output signal to a voltage regulator. The affected components have been replaced. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1593265. The NRC Resident Inspector has been notified of this event.
ENS 5434129 December 2018 07:20:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On December 29, 2018, at approximately 0220 Central Standard Time (CST), Browns Ferry Nuclear Plant (BFN), Unit 3 experienced an unexpected loss of power to the 3A Reactor Protection System (RPS) Bus due to the trip of the 3A RPS motor generator (MG) set. This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and initiation of Standby Gas Treatment Trains A, B, and C and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected. This event is being reported as a late 60 day non-emergency notification. This missed notification was identified on August 23, 2019. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The cause of the trip of the RPS MG Set was a failure of the motor winding insulation of all three phases. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Reports 1478564 and 1543534. The NRC Resident Inspector has been notified of this event.
ENS 5433220 August 2019 16:33:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid Specified System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On August 20, 2019, at approximately 1133 hours Central Daylight Time (CDT), Browns Ferry Nuclear Plant (BFN), Unit 2 experienced an unexpected loss of the 2A Reactor Protection System (RPS). This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and initiation of Standby Gas Treatment Trains A, B, and C and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The cause of the RPS MG Set trip was dirty potentiometer windings on an Over Voltage Relay. The dirt prevented the potentiometer's wiper from contacting its windings, resulting in erratic setpoint values. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Reports 1542603, 1542608, and 1542569. The NRC Resident Inspector has been notified of this event.
ENS 5428116 September 2019 13:17:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentAccident MitigationOn 9/16/19 at 0817 CDT, the Division 1 and Division 2 reactor water cleanup (RT) system differential flow instrumentation was declared inoperable due to failing downscale caused by flashing in the sensing lines that occurred during reactor cooldown for refueling outage C1R19. The Division 1 and Division 2 RT differential flow instrumentation were declared inoperable in accordance with Technical Specification 3.3.6.1 Conditions D and E which require restoring at least one division of instruments to operable status within one hour. This condition renders the leakage detection system incapable of performing its safety function, thus it is reportable under 10 CFR 50.72(b)(3)(v)(D). In response to the above, system alignment was changed to increase subcooling to restore indication. Division 1 and 2 Division RT differential flow instrumentation were declared operable at 0852 on 9/16/19. The NRC Resident Inspector has been notified.
ENS 5412130 April 2019 11:50:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification Due to Invalid Actuation of a General Containment Isolation SignalThis 60-day telephone notification is being made in accordance with the reporting requirements specified by 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to describe an invalid actuation of a general containment isolation signal affecting multiple systems. On April 30, 2019, at approximately 0650 CDT, a level 2 containment isolation signal was introduced when a fuse for the Nuclear Steam Supply Shutoff System was removed for a maintenance clearance. The level 2 containment isolation signal caused a trip of the Division I DC bus back-up charger, leaving only the Division I battery to carry the DC bus. At 0707 CDT the bus was de-energized when another unrelated clearance opened the battery supply breaker to the DC bus causing another containment isolation signal. This event did not affect Shutdown Cooling or any other protected Safety Related Equipment. The containment isolation signals caused an isolation of the systems listed below. All components that were not removed from service, gagged in position, already in the expected position due to plant conditions, or de-energized due to plant condition performed as designed. Containment Isolation valves for the following systems isolated as expected: Drywell and Containment Floor Drains, Drywell and Containment Equipment Drains, Condensate Makeup, Fire Protection Water, Service Air, Instrument Air, Reactor Water Cleanup, Spent Fuel Cooling and Cleanup, Reactor Plant Component Cooling Water, Chilled Water, Reactor Recirculation, Main Steam Drains, Reactor Building Ventilation, and Fuel Building Ventilation. The licensee notified the NRC Resident Inspector.
ENS 5401622 April 2019 03:07:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Trip and Specified System Actuation

At 2307 EDT on April 21, 2019, in Mode 1 at approximately 100 percent reactor power, Unit 1 automatically tripped due to a Main Turbine Trip. The Main Turbine Trip was a result of two out of three level instruments sensing a false high reactor water level. All control rods inserted as expected during the scram. Safety Relief Valves G and K lifted per design. The same level instruments that failed also tripped both Reactor Feed Pumps. As a result, reactor water level dropped below the Low Level 1 and 2 actuation setpoints. Per design, the Low Level 1 signal resulted in Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations. The Low Level 2 signals resulted in Group 3 (i.e. Reactor Water Cleanup) isolation, a secondary containment isolation signal, and an auto start of Standby Gas Treatment and Control Room Emergency Ventilation. Also, the Low Level 2 resulted in (high pressure coolant injection) HPCI and (reactor core isolation cooling system) RCIC automatically starting and injecting into the vessel. All systems responded as designed. This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) for RPS actuation and 10 CFR 50.72(b)(3)(iv)(A) as an event that results in valid actuations of the Primary Containment Isolation System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Decay heat is currently being removed via the turbine bypass valves. Condensate and feed water are maintaining water level. The reactor is still at saturation temperature and 475 psi, lowering slowly. The reactor is still in a normal electrical lineup. There was no impact to Unit 2 as a result of this event.

  • * * UPDATE ON 04/22/19 AT 0220 EDT FROM ALAN SCHULTZ TO JEFFREY WHITED * * *

The licensee updated the event report to include a 4-Hr Non-Emergency Notification in accordance with 10 CFR 50.72(b)(2)(iv)(A) for Emergency Core Cooling System, HPCI, Discharge to the Reactor Coolant System. Notified R2DO (Dickson), NRR EO (Miller) and IR MOC (Gott).

ENS 5377613 October 2018 05:00:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid Specified System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a Primary Containment Isolation System (PCIS) Group 1 for Main Steam Isolation Valves (MSIVs), Group 3 for Reactor Water Cleanup (RWCU), Group 6 for Secondary Containment isolation, Group 7 for Reactor Water Sampling, Diesel Generator, Reactor Core Isolation Cooling (RCIC) System logic, and Residual Heat Removal (RHR) logic. Group 1, Group 6, Diesel Generator actuation, RCIC actuation and RHR actuation are within scope of 10 CFR 50.73(a)(2)(iv). Group 3 and Group 7 are not within scope as they affect only one system. Cooper Nuclear Station (CNS) was shut down in Mode 5 at the time of the event with the reactor cavity flooded. On October 13, 2018, at 0028 Central Daylight Time, CNS received full PCIS Groups 1, 3, and 6, and a half Group 7 on the Division 1 side. The MSIVs and RWCU isolation valves were already closed for maintenance. The Secondary Containment isolated. Control Room Emergency Filter and the Standby Gas Treatment Systems initiated. The inboard Reactor Water Sample valve isolated. Diesel Generator #1 started but was not required to connect to the critical bus. Reactor Core Isolation Cooling System logic actuated with no expected response due to being isolated for shutdown conditions. Division 1 RHR pump logic actuated. Division 1 RHR system was operating in shutdown cooling mode. The actuation caused the Division 1 RHR outboard injection and heat exchanger bypass valves to open. Shutdown cooling was unaffected and remained in service throughout the event. The plant systems responded as expected with no Emergency Core Cooling System injection. At the time of the event, an in-service inspection of welds inside the reactor vessel was taking place using a robot scanner that uses two vortex thrusters to hold the robot to the vessel wall. The robot inadvertently passed over an instrument penetration, drawing suction on the process leg, resulting in low reactor water level indications and the subsequent invalid Level 1 and 2 system actuations. Actual reactor vessel water level remained steady at cavity flooded conditions. The NRC Resident Inspector has been notified of this event.
ENS 5366116 August 2018 05:00:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On August 16, 2018, at approximately 1736 CDT, Browns Ferry Nuclear Plant (BFN), Unit 2 experienced an unexpected loss of the 2B Reactor Protection System (RPS). This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and initiation of Standby Gas Treatment Trains A, B, and C and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected with the exception of the Unit 1 Refuel Zone Supply Fan Outboard Isolation Damper, 1-FCO-64-5, that failed to indicate closed position. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The cause of the RPS MG (Motor Generator) Set trip was a failed (shorted) operating coil associated with the 480 VAC motor starter inside the control box. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Reports 1440047 and 1440050. The NRC Resident Inspector has been notified of this event.
ENS 5343531 May 2018 18:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Reactor Water Cleanup System Declared InoperableOn May 31, 2018 at 1420 EDT, the Reactor Water Cleanup (RWCU) System Isolation Differential Flow - High function was declared inoperable as a result of indicating downscale. This condition would have prevented the primary containment isolation valves for the RWCU system from automatically isolating on a high differential flow condition. At 1519 EDT, RWCU was shutdown and the affected penetration flow paths were isolated in accordance with station procedures per Fermi Technical Specifications. The cause of the event is under investigation. There was no radiological release associated with this event. All other RWCU primary containment isolation instrumentation functions remained operable and the associated RWCU system primary containment isolation valves were capable of being remotely closed by the control room operators throughout the event. However, the condition is reportable pursuant to 10 CFR 50.72(b)(3)(v)(C), and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified.
ENS 5342927 May 2018 10:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Reactor Water Cleanup System Declared InoperableOn May 27, 2018 at 0630 EDT, the Reactor Water Cleanup (RWCU) System Isolation Differential Flow - High function was declared inoperable as a result of indicating downscale. This condition would have prevented the primary containment isolation valves for the RWCU system from automatically isolating on a high differential flow instrumentation signal. At 0753, RWCU was shutdown and the affected penetration flow paths were isolated in accordance with station procedures per Fermi Technical Specifications. The cause of the event is under investigation. There was no radiological release associated with this event. All other RWCU primary containment isolation instrumentation functions remained operable and the associated RWCU system primary containment isolation valves were capable of being remotely closed by the control room operators throughout the event. However, the condition is reportable pursuant to 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified.
ENS 5326515 March 2018 19:24:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionFailure to Meet Appendix R RequirementsAt 1524 (EDT) on Thursday, March 15, 2018, Operations was notified of a failure to meet Appendix R requirements for Peach Bottom Atomic Power Station (PBAPS) Unit 2 and Unit 3. Valves associated with the feedwater system for both units were not properly considered as Hi-Lo Pressure interface valves as required by the Appendix R program. This results in the susceptibility to a hot short condition that could open valves, diverting flow from the reactor, damage piping and prevent injection. U3 (Unit 3) Fire Safe Shutdown Credited Reactor Core Isolation Cooling (RCIC) System is affected. U2 (Unit 2) is affected by a potential leak path through the Reactor Water Cleanup system. This event is being reported as an occurrence of an event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety under 10 CFR 50.72(b)(3)(ii). The Station (PBAPS) is performing hourly fire watches for the impacted areas and is also evaluating this condition for corrective action. The licensee notified the NRC Resident Inspector.
ENS 531474 January 2018 19:10:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Scram Due to Partial Loss of Offsite Power During Winter StormOn January 4, 2018, at 1410 hours EST, with the reactor at approximately 100 percent power and steady state conditions, the winter storm across the Northeast caused the loss of offsite 345 kV Line 342. Reactor power was reduced to approximately 81 percent and a procedurally required manual reactor scram was initiated. All control rods fully inserted. As a result of the reactor scram, indicated reactor water level decreased, as expected, to less than +12 inches resulting in automatic actuation of the Primary Containment Isolation Systems for Group II - Primary Containment Isolation and Reactor Building Isolation System, and Group VI - Reactor Water Cleanup System. Reactor Water Level was restored to the normal operating band. The Primary Containment Isolation Systems have been reset. The Reactor Protection System signal has been reset. Following the reactor scram, the non-safety related Control Rod Drive Pump "B" tripped on low suction pressure. Control Rod Drive Pump "A" was placed in service. All other systems operated as expected, in accordance with design. This event is reportable per the requirements of Title 10, Code of Federal Regulations (CFR) 50.72 (b)(2)(iv)(B) - "RPS Actuation" and 10 CFR 50.72 (b)(3)(iv)(A) - "Specified System Actuation. This event had no impact on the health and/or safety of the public. The NRC Resident Inspector has been notified. The main steam isolation valves are open with decay heat being removed via steam to the main condenser. Offsite power is still available from 345kV line 355. As a contingency, emergency diesel generators are running and powering safety busses per licensee procedure. The licensee notified the Commonwealth of Massachusetts. The licensee will be notifying the town of Plymouth as part of their local notifications. The licensee will be issuing a press release.
ENS 5307010 January 2017 09:00:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On September 15, 2017, during a TVA (Tennessee Valley Authority) review of Operations logs, it was determined that a reportable condition occurred in January 2017 but no NRC report had been made. On January 10, 2017, at 0300 Central Standard Time (CST), Browns Ferry Nuclear Plant, Unit 3, received Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolation signals. The Group 2, 3, 6, and 8 isolations caused the initiation of all three trains of the Standby Gas Treatment (SBGT) system and Control Room Emergency Ventilation (CREV) subsystem 'A.' At 0311 CST, Operations personnel discovered that the 3A1 RPS circuit protector had tripped on undervoltage. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywall Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywall Pressure. At the time of the event, these conditions did not exist; therefore the actuation of the PCIS was invalid. All affected equipment responded as designed. This condition was the result of an undervoltage condition on the 3A1 circuit protector. During trouble shooting, the undervoltage setpoints were found to be 116 VAC and 115 VAC, when the normal as left acceptance band is 109.7 VAC to 111.3 VAC. The 3A RPS protective relays had been previously replaced in September 2016. The most likely cause of the undervoltage condition in these relays is infant mortality. The NRC Resident Inspector has been notified of this event.
ENS 5297417 September 2017 13:38:0010 CFR 50.72(b)(3)(iv)(A), System ActuationEmergency Diesel Generator and Primary Containment Isolation System ActuationsOn September 17, 2017, during planned surveillance activities involving Emergency Diesel Generator (EDG) 4, unexpected voltage and frequency indications were noted when EDG 4 was synchronized to Emergency Bus E4. With EDG 4 in manual mode, the Operator responded by lowering load to reopen the EDG 4 output breaker. Opening of the EDG 4 output breaker with the breakers from Balance of Plant (BOP) Bus 2C, which normally feeds the Emergency Bus E4, opened; resulted in de-energizing Emergency Bus E4. The EDG 4 voltage regulator and governor automatically reverted to auto control, and EDG 4 reconnected to Emergency Bus E4. Normal frequency and voltage were restored with EDG 4 in auto control. The momentary power interruption to Emergency Bus E4 resulted in Unit 2 Primary Containment Isolation System (PCIS) Group 2 (i.e., Drywell Equipment and Floor Drain, Residual Heat Removal (RHR) Discharge to Radwaste, and RHR Process Sample), Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems), and Group 10 (i.e., air isolation to the drywell) isolations. The actuations of Primary Containment Isolation Valves (PCIVS) were completed and the affected equipment responded as designed. Per design, no Unit 1 safety system group isolations or actuations occurred. These actuations are being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). Additional Unit 2 actuations included PCIS Group 3 (i.e., Reactor Water Cleanup), Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start of Standby Gas Treatment (SGT) System subsystems A and B. These systems functioned as designed. This event did not impact public health and safety. The NRC Resident Inspector has been notified. The safety significance of this event is minimal. Safety systems functioned as designed following the power perturbation on E4. Plant systems responded as designed. The cause of the event is under investigation.
ENS 5296114 July 2017 18:53:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Containment Isolation ValvesThis report is being made as required by 10 CFR 50.73(a)(2)(iv)(A) to describe an automatic actuation of containment isolation valves in more than one system. Because the actuation was invalid, this 60-day telephone notification is being made instead of a written LER (Licensee Event Report), in accordance with 10 CFR 50.73(a)(1). On 07/14/17, at approximately 1453 hours (EDT), an electrical transient occurred due to an off-site lightning strike that de-energized one of the station's two qualified off-site power sources. This resulted in an automatic fast transfer of four 4 kV electrical buses to the alternate off-site source. The fast transfer occurred as designed without complications. The loss of power had numerous impacts on plant equipment that occurred in accordance with plant design, including a Group 2 primary containment isolation on both units. The Group 2 isolation affected multiple systems, including Reactor Water Cleanup, Instrument Nitrogen, and the Drywell Floor Drain. The fault on the off-site transmission line immediately cleared after the lightning strike and at 1457 hours (EDT) the transmission system operator gave the station permission to reclose the breaker to the off-site source. Following system restorations and equipment walkdowns, plant operators re-established normal connections to the off-site source on 7/14/17 at 2322 hours (EDT) in accordance with station procedures. The containment isolation occurred as a result of the loss of an off-site power source and was not due to actual plant conditions or parameters meeting design criteria for containment isolation. Therefore, this is considered to be an invalid actuation. The NRC Resident Inspector has been informed of this notification.
ENS 527822 June 2017 07:41:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialSecondary Containment Declared InoperableOn 6/2/2017 at 0241 CDT, Clinton Power Station entered Mode 2 with secondary containment boundary doors propped open. Specifically, both doors for Reactor Water Cleanup (RT) 'B' pump room were propped open with welding cables routed through pump room doors to perform welding in the RT pump room. At 0300 CDT, a Senior Reactor Operator identified that the doors were propped open and Secondary Containment was declared inoperable. LCO 3.6.4.1 Required Action A.1 was entered to restore Secondary Containment to Operable in four hours. At 0324 CDT, the cabling for the welding machine was removed and the doors were closed. Investigation determined that authorization had been granted while in mode 4, when secondary containment was not required to be operable. The doors were propped open at the beginning of the shift, prior to the mode change to mode 2 (0241 CDT). This loss of secondary containment is reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented fulfillment of a safety function needed to control the release of radioactive material. The NRC Resident Inspector has been notified.
ENS 520519 May 2016 10:26:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Primary Containment Isolation Valves (Pcivs)This 60-day telephone notification is being made in lieu of a Licensee Event Report (LER) submittal in accordance with 10 CFR 50.73(a)(1) to notify the NRC of an invalid actuation of PCIVs, reportable under 10 CFR 50.73(a)(2)(iv)(A). On May 9, 2016, at 0626 Eastern Daylight Time (EDT), an unexpected trip of the Unit 1 Reactor Protection System (RPS) Bus A occurred, resulting in closure of several PCIVs on loss of power, per design. In addition, the following actuations also occurred per design: - insertion of a half reactor scram signal. - initiation of the standby gas treatment (SBGT) system . - isolation of the secondary containment. - initiation of the control room emergency ventilation (CREV) system smoke and radiation mode. - trip of the operating reactor water cleanup system (RWCU) pump due to closure of its isolation valve. The event resulted from a failed relay coil in the drive motor run logic for the RPS power supply motor-generator (MG) set. The failed relay blew a fuse, which de-energized the RPS drive motor contactor and MG set. This resulted in de-energizing the RPS power supply in the 'A' channel and produced the actuations listed previously, per design. Affected systems and components were restored to their normal configurations by 1000 EDT on May 9, 2016. Since no plant or process conditions existed that required the PCIV isolations (e.g., high drywell pressure or low reactor water level), this event is being reported per 10 CFR 50.73(a)(1) as an invalid actuation. This issue has been entered into the site Corrective Action Program (CR 2027653) for evaluation and implementation of further corrective actions. This event did not result in any adverse impact to the health and safety of the public. The NRC Resident Inspector has been notified.
ENS 5196228 March 2016 17:20:0010 CFR 50.73(a)(1), Submit an LERInvalid Specified System Actuation

This 60-day report, as allowed by 10 CFR 50.73(a)(1), is being made pursuant to 10 CFR 50.73(a)(2)(iv)(A) to describe an unplanned, invalid actuation of containment isolation valves in more than one system. On 3/28/16, at approximately 1320 (EDT), a loss of power occurred on the Unit 2 E124 480 volt load center due to an equipment operator inadvertently opening the main feed breaker during the process of applying a clearance to de-energize the E124-P-A motor control center for planned maintenance. Loss of the E124 load center resulted in Group II and Group III primary containment isolations due to an invalid ESF actuation signal. Systems impacted by the containment isolations included containment instrument nitrogen, containment atmospheric monitoring, reactor water cleanup, and secondary containment. Balance of plant impacts included partial loss of feedwater heating and a reduced condenser vacuum. Reactor power lowered to 86% as a result of the event and further decreased to approximately 80 percent when re-establishing the 3A, 4A and 5A feedwater heaters.

Following direction from the control room, the E124 main feed breaker was promptly re-closed by equipment operators. Affected equipment was restored to its normal or planned configuration and containment isolations were reset at 1406. The containment isolation signal was generated as a result of the loss of power to the E124 load center and was not due to actual plant conditions or parameters meeting design criteria for containment isolation. Therefore, this is considered to be an invalid actuation. The licensee has notified the NRC Resident Inspector.

ENS 5195228 March 2016 05:50:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Inboard Isolation LogicOn Monday, March 28, 2016, Unit 1 was in OPCON 5 (Refueling) conducting a refueling outage. A modification was being installed for an NSSSS (Nuclear Steam Supply Shutoff System) Test Box on Division 1A Group 1 NSSSS logic. At 0150 hours, a logic jumper was removed as directed by the work order and a logic fuse failed. The fuse failure caused an unplanned invalid actuation of the inboard isolation logic. The isolations were reset and the valves were restored to initial conditions at 0246 hours. On Sunday, April 3, 2016, at 0134 hours, one additional logic fuse opening event occurred during the testing which also caused an invalid actuation which was reset at 0405 hours. The fuse openings occurred during jumper manipulations as the modification was tested on the Division 1A and 1D logic during the refuel outage. The investigation determined the fuse openings were due to the testing process. The suspected devices that caused the condition are not permanent plant equipment and there is no degradation of the actual circuit. They were part of a temporary configuration that was installed to support modification installation and acceptance testing. The temporary devices have been removed. The portion of the primary containment isolation system that received an actuation signal functioned successfully. All of the affected open isolation valves automatically closed. The isolation was a partial actuation. This 60-day ENS report is being made per 10CFR 50.73(a)(2)(iv)(A) and 10CFR50.73(a)(1) to report invalid automatic actuations of systems listed in paragraph (a)(2)(iv)(B). The listed system that actuated was general containment isolation signals affecting containment isolation valves in more than one system. Primary containment isolation valves (PCIVs) closed on reactor water cleanup (RWCU), drywell chilled water (DWCW), primary containment instrument gas (PCIG), drywell sumps and the suppression pool cleanup systems. The licensee has notified the NRC Resident Inspector.
ENS 5182729 March 2016 16:23:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Scram Due to Turbine TripA Reactor Scram occurred at 1123 CDT on 03/29/2016 from 35% CTP (core thermal power). The cause of the Scram appears to be a Turbine Generator trip. The station's procedures, '05-S-01-EP-2 RPV (Reactor Pressure Vessel) Control, 05-1-02-I-1 Reactor Scram ONEP (Off Normal Event Procedure) and 05-1-02-l-2 Turbine Generator Trip ONEP,' were entered to mitigate the transient with all systems responding as designed. No loss of offsite or ESF (engineered safety feature) power occurred. No ECCS (emergency core cooling systems) initiation signals were reached and no ESF or Diesel Generator initiations occurred. All control rods fully inserted. MSIVs (main steam isolation valves) remained open, no SRVs (safety relief valves) lifted, and no containment isolation signals were generated. Currently, reactor water level is being maintained by the Condensate and Feedwater System in normal band and reactor pressure and temperature are being maintained by the Reactor Water Cleanup System. The main condenser is available. There are no challenges to Primary or Secondary Containment at this time. The licensee has notified the NRC Resident Inspector.
ENS 5165916 January 2016 02:38:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialMomentary Loss of Secondary ContainmentOn January 15, 2016 at 2038 CST, an alarm was received indicating Secondary Containment Differential Pressure rose unexpectedly above the Technical Specification Surveillance Requirement, SR 3.6.4.1.1, limit of 0.10 inch of vacuum water gauge. This loss of differential pressure occurred when Operations had entered the 2A Reactor Water Cleanup Pump room. The pump room door was closed and Secondary Containment Differential Pressure returned to Technical Specification limits in approximately 4 minutes. The Standby Gas Treatment System remained in standby and fully operable. This condition represents a failure to meet Surveillance Requirement 3.6.4.1.1. As a result, entry into Technical Specification 3.6.4.1, Condition A, was made momentarily due to secondary containment being inoperable. Given the temporary loss of secondary containment, this event is reportable under 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of a safety function. The NRC Senior Resident Inspector has been notified." The licensee also notified the State of Illinois Emergency Management Agency.
ENS 5150510 September 2015 01:03:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe invalid actuation containment isolation signals affecting containment isolation valves in more than one system. On September 9, 2015 at 2103 hours Eastern Daylight Time (EDT), Unit 1 experienced a loss of electrical power to motor control center 1CB when the substation E6 feeder breaker tripped. The loss of power resulted in closure of primary containment isolation valves (PCIVs) in Unit 1 Primary Containment Isolation System (PCIS) Group 2 (i.e. Drywell Equipment and Floor Drains, Residual Heat Removal (RHR) Discharge to Radwaste, RHR Process Sample, and Traversing lncore Probe), Group 3 (i.e., Reactor Water Cleanup), and Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems). It has been determined that affected PCIVs appropriately closed. However, the limit switch within the motor operator of the inboard RWCU PCIV (i.e. 1-G31-F001) malfunctioned; resulting in an inaccurate remote position indication. Testing has confirmed that 1-G31-F001 properly closed and can perform its intended safety function. These PCIV isolations were the result of a substation E6 feeder breaker trip to motor control center 1CB and not in response to actual plant conditions (i.e., to mitigate the consequences of an event) and, therefore, were invalid. This event did not result in any adverse impact to the health and safety of the public. The NRC Resident Inspector was notified.
ENS 5148023 August 2015 16:42:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid Primary Containment Isolation SignalOn 8/23/2015 at 1242 (EDT), with the reactor at 100% power, an invalid RPS MG (Reactor Protection System Motor-Generator) set 'A' trip resulting in a loss of RPS bus 'A'; this occurred during testing of the RPS instrument channels. All equipment operated as designed as a result of the loss of power to the 'A' RPS bus. The invalid trip was determined to be a result of the overvoltage relay being set too low. The above event meets the reporting criteria of 10CFR50.73(a)(2)(iv)(A) since the loss of RPS bus resulted in primary containment isolation signals affecting containment valves in more than one system. The following systems isolated as a result of the loss of 'A' RPS bus: Reactor Water Cleanup, Reactor Building ventilation, 'A' Containment Atmosphere Dilution, Torus Vent and Purge, Drywell Equipment and Floor Drain Sumps, 'A' Drywell Containment Atmospheric Monitors, Recirculation System Sample Line, Main Steam Line Drains and Residual Heat Removal drain valve to radwaste. 'A' Standby Gas Treatment System started as designed. This notification is being made in accordance with 10CFR50.73(a)(2)(iv)(A) to provide information pertaining to an invalid 'A' Reactor Protection System actuation. Completed actions were the replacement of overvoltage relay and voltage setpoint change, completed on 9/11/2015. In accordance with 10CFR50.73(a)(i) a telephone notification is being made instead of submitting a written Licensee Event Report.
ENS 5112824 May 2015 23:30:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification for an Invalid Actuation of Containment Isolation ValvesThe following was received via phone call and email: This 60-day report, as allowed by 10CFR 50.73(a)(1), is being made pursuant to 10CFR 50.73(a)(2)(iv)(A) to describe an unplanned, invalid actuation of containment isolation valves. At 1930 EDT on May 24, 2015, a loss of power to Reactor Protection System (RPS) Train B occurred. Initial investigation found the RPS Motor Generator (MG) Set B not running, with its Motor Off light illuminated caused by both Normal EPA breakers and MG Set B output breaker being tripped. Visual inspection at the distribution cabinet was inconclusive at the time and revealed no abnormalities and no abnormal odors in the area. Further investigation of the RPS MG Set B verified normal voltages on all fuse clips, and all power and control power fuses were operational. As a result of the loss of RPS B, the following containment isolation valves closures occurred: Reactor Water Cleanup (RWCU) Outboard Isolation valves, Torus Water Management System (TWMS) Outboard Isolation valves, Division 2 Drywell Pneumatics Inboard and Outboard Isolation valves, Primary Containment Radiation Monitoring System Inboard and Outboard Isolation valves, Reactor Recirculation Pump Seal Purge Flow Outboard Isolation valves, and Drywell Floor and Equipment Drain Sump Inboard Isolation Valves. The Resident Inspector has been notified.
ENS 511122 June 2015 02:11:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor Scram Due to Low Reactor Water Level

At 2111 (CDT) River Bend Nuclear Station sustained an Automatic Reactor Scram due to low Reactor Water Level (Level 3). The plant is currently stable, with level being maintained in a normal band of 10 - 51 inches with Condensate and Feedwater. Reactor Pressure is in the prescribed band of 500-1090 psig. The plant is in Mode 3, Hot Shutdown, and will remain in Mode 3 until investigation of the scram is complete. The transient began with a trip of Reactor Feed Pump 'A', followed by a Reactor Scram and a trip of Reactor Feed Pump 'C'. Reactor water level was recovered with Reactor Feed Pump 'B' to a normal post scram level band. There was a problem noted with the Reactor Feedwater Master Level Controller; this was mitigated by the Operator placing the controller to manual. There was no subsequent Level transient. Reactor Pressure was stabilized in normal pressure band with Turbine bypass valves. During the transient, a Reactor Recirculating Flow Control Valve Runback was not received as expected. Reactor Recirculating Pump 'A' responded as expected to transient (switching to low pump speed), Reactor Recirculating Pump 'B' tripped during transient. A Level 3 isolation signal was received, all expected isolations occurred. The cause of the transient is currently under investigation. The reactor is stable in Mode 3 with decay heat being removed via turbine bypass valves, and a normal electrical line up. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM JACK MCCOY TO HOWIE CROUCH AT 0712 EDT ON 6/2/15 * * *

At 2231 on 6/1/15, Reactor Water Cleanup System isolated on High Reactor Water Cleanup System Heat Exchanger room temperature due to loss of Turbine Building chill water during the initial transient. All Reactor Water Cleanup System Valves isolated as expected. Reactor Water Cleanup was the only system affected by this isolation signal. The licensee has notified the NRC Resident Inspector. Notified R4DO (Whitten).

ENS 5100324 February 2015 22:02:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephone Notification of Invalid System Actuation Due to Motor Generator Output Breaker TripOn February 24, 2015, at approximately 1702 CDT, while the plant was in cold shutdown, power was lost on the Division 1 reactor protection system (RPS) bus. This event resulted in the automatic closure of the Division 1 primary containment isolation valves in the residual heat removal (RHR) and reactor water cleanup systems. Additionally, the primary containment atmospheric monitoring system automatically actuated, and ventilation systems in the fuel building, auxiliary building, and control building shifted to emergency mode. The closure of the isolation valves in the residual heat removal system caused an automatic trip of the 'A' RHR pump, which had been in the shutdown cooling alignment. The equipment response to the isolation signal was as expected. This event is being reported in accordance with 10 CFR 50.73(a)(1) as an invalid actuation of the Division 1 primary containment isolation system. The isolation was promptly diagnosed as having resulted from a trip of the output breaker of the RPS motor generator (MG) set 'A,' and not from a valid signal. Operators implemented the appropriate response procedures to align power to the bus via the alternate source, and began restoring the affected systems. The 'A' RHR pump was re-started within twelve minutes, during which time coolant temperature increased approximately seven degrees to a maximum of approximately 100F. Other affected systems were restored over the next few hours. The causal analysis concluded that the MG set output breaker tripped due to an overly conservative setpoint on the overvoltage trip relay. The low trip setpoint was a latent condition that had existed since the output voltage was raised in 1988 at the recommendation of the vendor, but at which time the trip setpoint was not changed. To correct this condition, the MG overvoltage trip setpoint was raised to restore adequate operating margin to the normal MG output voltage. At the time of the event, the plant was in MODE 5 with the reactor cavity flooded to greater than 23 feet above the vessel flange. The shutdown cooling system was promptly restored to service. This event was of minimal safety significance to the health and safety of employees and the public. The licensee has notified the NRC Resident Inspector.
ENS 507947 February 2015 05:55:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialLeakage Detection System InoperableOn 2/6/15 at 2300 (CST) the Division 1 Reactor Water Cleanup (RT) system differential flow instrument was declared inoperable due to erratic indication. The Division 1 RT differential flow instrument was declared inoperable in accordance with Technical Specification 3.3.6.1 Action D.1. At time 2355 Division 2 RT differential flow instrument failed downscale and was declared inoperable in accordance with Technical Specification 3.3.6.1 Action D.1 and also Technical Specification 3.3.6.1 Action E.1 (entered due to Division 1 RT differential flow already inoperable). Since this condition renders the Leakage Detection System incapable of performing its safety function, it is reportable under 10CFR50.72(b)(3)(v)(C). Division 1 RT differential flow was declared Operable at time 0036 on 2/7/15. Division 2 RT differential flow was restored to Operable at time 0225 on 2/07/2015. The NRC Resident (Inspector) has been notified.
ENS 507746 December 2014 16:12:0010 CFR 50.73(a)(1), Submit an LER60 Day Optional Report - Half Scram and a Division 2 Primary Containment Isolation SignalOn December 6, 2014, at approximately 1012 CST, while the plant was operating at 100 percent power, the Division 2 reactor protection system (RPS) bus de-energized unexpectedly. This resulted in a half-scram and a Division 2 primary containment isolation signal. Operators executed the appropriate abnormal operating procedures to begin an orderly restoration of the affected systems. Atmospheric pressure in the primary containment momentarily reached the high-pressure alarm setpoint, necessitating entry into the emergency operating procedure for that condition. Automatic isolation valves in the following systems closed as designed: - reactor plant component cooling water - drywell unit cooler water supply - reactor building floor and equipment drains - reactor building HVAC chilled water supply - containment airlock seal air supply - reactor recirculation system flow control valve hydraulics - main steam line drains - reactor water cleanup - auxiliary building and annulus HVAC systems These engineered safety systems actuated as designed: - standby gas control filter trains - fuel building filter trains - control building filter trains The event occurred approximately 25 hours after the Division 2 RPS motor-generator (MG) was aligned to the bus following replacement of the voltage regulator. Following the event, the MG set was found running with its output breaker tripped. A failure analysis determined that the spike suppressor and the field flash card were potential sources of the MG breaker trip. The spike suppressor was replaced. Inspection of the field flash card found a strand of wire from one of the attached leads nearly touching a trace on the circuit board. Testing determined that the wire strand was the most likely cause for the breaker trip. With no spare card readily available, the wire strand was removed and the field flash card was re-installed. Other cards were inspected, and no similar conditions were found. The MG set was load tested for 30 hours, and was placed in service on December 17(, 2014). Additionally, it is suspected that there is an intermittent failure occurring in the field flash card. A design change will be developed to correct that condition. The licensee has notified the NRC Resident Inspector.
ENS 5075426 November 2014 20:27:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On November 26, 2014, at approximately 1427 hours Central Standard Time (CST), the Browns Ferry Nuclear Plant (BFN), 1A Reactor Protection System (RPS) Motor-Generator (MG) Set Power Supply unexpectedly de-energized resulting in a BFN Unit 1 half scram and Primary Containment Isolation System (PCIS) Groups 1, 2, 3, 6, and 8 isolation signals. The PCIS Groups 1, 2, 3, 6, and 8 isolations caused the initiation of all three trains of the Standby Gas Treatment (SBGT) system and Control Room Emergency Ventilation (CREV) subsystem 'A', and isolations of the BFN, Unit 1, Reactor Zone ventilation and BFN, Units 1 and 2, Refuel Zone ventilation (Unit 3 Refuel Zone ventilation was tagged out under 3-TO-2014-0001 at the time of this event). Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, placed the BFN 1A RPS on alternate power, and reset the RPS logic and PCIS isolations. Plant conditions which initiate PCIS Group 1 actuations are Reactor Pressure Vessel (RPV) Low Low Low Water Level (Level 1), Main Steam Line (MSL) High Flow, MSL Area High Temperature, or MSL Low Pressure. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The apparent cause for this condition was an intermittent problem with the BFN 1A RPS MG Set voltage adjust potentiometer. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Problem Evaluation Report 961518. The NRC Resident Inspector has been notified of this event.
ENS 506587 October 2014 15:35:0010 CFR 50.73(a)(1), Submit an LERInvalid Specified System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of general containment isolation signals affecting containment isolation valves in more than one system. On October 7, 2014, at 2135 (CDT), while in a refueling outage with the reactor non-critical (Mode 5), work activities were in progress that included replacement of an excess flow check valve and execution of a Technical Specification Surveillance Procedure on the Automatic Depressurization System. Subsequent to valving in a level transmitter (LT), water levels in both the variable and reference legs of the LT were disturbed resulting in a Unit 1 full scram and Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolation signals due to receipt of an invalid low reactor water level signal. The PCIS Groups 2, 3, 6, and 8 isolations caused the initiation of Trains A, B, and C of the Standby Gas Treatment System and Control Room Emergency Ventilation Subsystem 'A'. The Reactor and Refuel Zone ventilation fans tripped and the secondary containment dampers isolated. Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, and placed affected systems back in service. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Problem Evaluation Report 943038. The NRC Resident Inspector has been notified of this event.
ENS 5056527 August 2014 16:09:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of General Containment Isolation SignalsThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of general containment isolation signals affecting containment isolation valves in more than one system. On August 27, 2014, at 1109 hours Central Daylight Savings Time (CDT), while in a forced unit outage with the reactor noncritical (Mode 3) and with all control rods fully inserted, instrument mechanics were attempting to backfill reactor water level transmitter (LT) 3-53 sensing lines following performance of LT replacement. During this effort, water levels in both the variable and reference legs of the LT were disturbed resulting in a Browns Ferry Nuclear Plant (BFN) Unit 1 full scram and Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolation signals due to receipt of an invalid low reactor water level signal. The PCIS Groups 2, 3, 6, and 8 isolations caused the initiation of Trains B and C of the Standby Gas Treatment (SBGT) System and Control Room Emergency Ventilation (CREV) Subsystem 'A'. The Reactor and Refuel Zone ventilation fans tripped and the secondary containment dampers isolated. Train A of the SBGT System was tagged out of service during the event. Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, and placed affected systems back in service. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Problem Evaluation Report 928777. The NRC Resident Inspector has been notified of this event.
ENS 5045026 July 2014 17:13:0010 CFR 50.73(a)(1), Submit an LERElectrical Transient Causes an Invalid System Actuation

At 1313 (EDT) on 7/26/14, the plant experienced an electrical transient on bus EK-1-B1 (safety-related 120 volt AC distribution panel) that resulted in partial Balance of Plant Division 2 isolation signals and alarms received in the Control Room. The following component actuations occurred: valve 1P50F140 closed, resulting in a trip of Containment Vessel Chilled Water C; valve 1G41F140 closed, isolating the Fuel Pool Cooling and Clean-up return from the containment building upper pools; valve 1B33F019 closed, isolating Reactor Water sampling; valve 1D17F071B closed, isolating the Drywell Atmosphere Radiation Monitor; valve 1D17F081B closed, isolating the Containment Atmosphere Radiation Monitor; valves 1G61-F030, 1G61-F150, 1G61-F075, and 1G61-F165 closed, isolating the Containment and Drywell Floor and Equipment drain sumps; valve 1G50-F272 closed isolating the Reactor Water Cleanup Backwash Receiving Tank: 1M25F020B, Control Room HVAC Inboard supply damper, closed and Division 2 indicated an auto initiation (M25-S12, Auto Initiate Active amber light was on). This event is considered an invalid system actuation reportable under 10 CFR 50.73(a)(2)(iv)(A).

The isolation was not initiated in response to actual plant conditions or parameters, and was not a manual initiation. Therefore, this notification is provided via a 60 day optional phone call in accordance with 10 CFR 50.73(a)(1) instead of submitting a written Licensee Event Report. The event meets reporting criteria specified in 10 CFR 50.73(a)(2)(iv)(B)(2) as a general containment isolation valve signal affecting containment isolation valves in more than one system. All affected systems functioned as expected in response to the electrical transient on bus EK-1-B1 that resulted in the partial Balance of Plant Division 2 isolation signals. The valves were reopened in accordance with plant procedures. The failure mechanism that caused the electrical transient was a failed capacitor in regulating transformer EFB1B2. The capacitor was replaced and tested with satisfactory results. The NRC Resident Inspector has been notified.

ENS 503465 August 2014 22:34:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram

This notification is being provided pursuant with SAF 1.6 10CFR50.72(b)(2)(iv)(B) and SAF 1.7 10CFR50.72(b)(3)(iv)(A). At 1734 CDT on August 5, 2014, LaSalle Unit 2 automatically scrammed due to an RPS actuation. The MSIVs isolated on a Group 1 signal, the cause is under investigation. The reactor water cleanup system isolated during the transient. The plant is stable with Reactor Pressure Control being maintained by the Reactor Core Isolation Cooling System and SRVs and level being controlled by the Low Pressure Core Spray System. The plant is planned to remain in hot shutdown pending investigation of the trip." The Unit 2 electric plant is in a normal shutdown lineup. All control rods inserted fully on the scram. Unit 1 was not affected by the Unit 2 transient. The licensee notified the NRC Resident Inspector.

  • * * UPDATE PROVIDED BY MICHAEL FITZPATRICK TO JEFF ROTTON AT 1650 EDT ON 8/6/2014 * * *

The initial notification to the NRC stated that the reactor water cleanup system had isolated during the transient. The actual status is being corrected to state that the reactor water cleanup pump tripped during the transient. The licensee has notified the NRC Resident Inspector. Notified R3DO (Stone).

ENS 4994221 January 2014 13:46:0010 CFR 50.73(a)(1), Submit an LER60 Day Optional Telephone Notification of an Invalid Primary Containment Isolation SignalThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On January 21, 2014, at 0746 hours Central Standard Time (CST), during performance of the 3C Emergency Diesel Generator (EDG) post modification test instructions, the EDG was supplying a shutdown board in isochronous mode when the 3B Residual Heat Removal (RHR) pump was started causing the voltage to drop to 2100 volts. At this time, Browns Ferry Nuclear Plant (BFN) Unit 3, received a half scram and Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolation signals as a result of losing the 3B Reactor Protection System (RPS) Motor Generator (MG) set due to a time delay relay failure on under voltage. The PCIS groups 2, 3, 6, and 8 isolations caused the initiation of all three trains of the Standby Gas Treatment (SBGT) system, Control Room Emergency Ventilation (CREV) subsystem 'A', and the Refuel fans tripped and isolated. Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, and placed affected systems back in service. Plant conditions which initiate PCIS group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The apparent cause for this condition was a failure of a 3B RPS MG set time delay relay due to lack of a preventive maintenance strategy. The vendor manual for the time delay relay did not specify a qualified life. The replacement relay specified a replacement schedule of 10 years. The relay that failed was installed for approximately 13 years. To address this condition, preventive maintenance is being developed for MG set time delay relays. In addition, the only remaining relay, similar to the failed relay, is scheduled be replaced on August 25, 2014, for the 2A RPS MG set. The licensee has notified the NRC Resident Inspector.
ENS 4980011 December 2013 13:18:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Primary Containment Isolation System (Pcis) Valves During I&C MaintenanceThis 60-day report, as allowed by 10 CFR 50.73(a)(1 ), is being made per 10 CFR 50.73(a)(2)(iv)(A) to describe an unplanned, invalid closure of Unit 2 Primary Containment Isolation System (PCIS) valves. On December 11, 2013, at 0818 EST, an instrument technician was adjusting the output voltage of the 'A' 120-volt Reactor Protection System (RPS) motor-generator (MG) set, which is the normal power supply for the 'A' RPS bus. As the adjustment potentiometer was being moved, output voltage momentarily dropped below the setpoint of an Electrical Protection Assembly (EPA) on the 'A' RPS bus. The EPA tripped and removed power from the 'A' RPS bus. Removing power from the RPS bus resulted in PCIS valves receiving a close signal. Affected valves or systems were a Reactor Water Sample valve, Main Steam Line Drain valves, Containment Atmospheric Control System valves, Drywell Equipment Drain and Floor Drain valves, and a Reactor Water Cleanup System valve. Other systems affected were Standby Gas Treatment, Control Room Emergency Ventilation, and Radiation Monitoring on Main Steam Lines, Main Stack, Reactor Building Vent, and Main Condenser. All actuations that resulted from the loss of power to RPS Bus 'A' were completed as expected. This event resulted from the attempt to adjust the voltage control potentiometer on the RPS MG set. When a technician attempted to adjust the potentiometer, the movement caused the RPS MG set to momentarily and unexpectedly experience a low voltage on the output, tripping the output breakers. Power was restored to the affected RPS bus by 0858 EST on December 11, 2013, and all affected systems were subsequently returned to service. Since no actual plant or process conditions existed which would have caused the various actuations described above, this event is being reported per 10 CFR 50.73(a)(1) as an invalid actuation. This issue has been entered into the site Corrective Action Program (CR 651284) for evaluation and implementation of further corrective actions. The NRC Resident Inspector has been informed of this notification.
ENS 4946023 August 2013 14:54:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification for an Invalid Primary Containment Isolation Valve Actuation

At 0754 on 8/23/13, a loss of power to the Reactor Protection System (RPS) 'B' occurred due to the unexpected opening of the circuit breaker (RPS-CB-MG2) for the RPS 'B' motor generator due to a failure of the voltage regulator circuit card. The loss of RPS 'B' resulted in a half scram signal, closure of Primary Containment Isolation Valves (PCIVs) from multiple systems and loss of power to main steam line radiation monitors (MS-RIS-610B & MS-RIS-610D). No plant parameters or maintenance activities existed which would cause the opening of RPS-CB-MG2 or actuation of the primary containment isolation; therefore, this is considered to be an invalid actuation of a system listed in 10CFR50.73(a)(2)(iv). The half scram signal, closure of Primary Containment Isolation Valves (PCIVs) from multiple systems, and loss of power to main steam line radiation monitors were an expected response to the loss of RPS 'B'. RPS 'B' was repowered from an alternate power supply. The half scram signal was reset, the containment isolation valves were opened and the affected systems were returned to normal operation. The voltage regulator circuit card was replaced and RPS 'B' was returned to its normal power supply. As indicated in 10CFR50.73(a)(1), in the case of an invalid actuation reported under 10CFR50.73(a)(2)(iv)(A), the licensee may, at its option, provide a telephonic notification to the NRC Operations Center within 60 days of discovery of the event instead of submitting a written LER. This 60-day telephone notification is being made to meet the reporting requirements instead of submitting an LER since the actuation was invalid. The following additional information is provided as specified in NUREG-1022: The specific train(s) and system(s) that were actuated: PCIVs in multiple systems

    EDR-V-19 Drywell Equipment Drain Inboard Isolation Valve
    EDR-V-20 Drywell Equipment Drain Outboard Isolation Valve
    FDR-V-3 Drywell Floor Drain Inboard Isolation Valve
    FDR-V-4 Drywell Floor Drain Outboard Isolation Valve
    RWCU-V-1 Reactor Water Cleanup Suction Inboard Isolation Valve
    RWCU-V-4 Reactor Water Cleanup Suction Outboard Isolation Valve
    RRC-V-19 Reactor Water Sample Inboard Isolation Valve
    RRC-V-20 Reactor Water Sample Outboard Isolation Valve
    TIP-V-15 Traversing In-Core Probe Purge Isolation Valve
    CRD-V-11 Control Rod Drive Scram Discharge Volume Drain Valve

Whether each train actuation was complete or partial:

    All PCIVs actuations for a loss of RPS 'B' were complete.
    The reactor half scram for a loss of RPS 'B' was a partial activation.

Whether or not the system started and functioned successfully:

    All PCIVs functioned successfully.

The licensee notified the NRC Resident Inspector.

ENS 4929622 August 2013 11:55:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Reactor Protection Actuation (Scram)On Thursday, August 22, 2013 at 0755 hours (EDT), with the reactor critical at approximately 98% core thermal power, and the mode switch in RUN, a manual reactor scram was inserted due to lowering reactor water level. The cause of the lowering reactor water level was due to the trip of all three Feedwater Pumps. The cause of the Feedwater Pump trip event is currently under investigation. Following the reactor scram, all control rods were verified to be fully inserted. All 4kV busses transferred to the Startup Transformer as designed. Following the scram the reactor water level lowered to +12 inches initiating the Primary Containment Isolation System (Group II, Reactor Building Isolation System (RBIS); and Group VI - Reactor Water Cleanup System) automatically as per design. Reactor water level lowered to -46 inches initiating Primary Containment Isolation System Group I - Main Steam Isolation Valves (MSIVs); Emergency Core Cooling Systems (ECCS) actuated which included automatic start and injection of the High Pressure Coolant Injection (HPCI) System and the Reactor Core Isolation Cooling (RCIC) System and an automatic start of the Emergency Diesel Generators as designed. Reactor water level was promptly restored to normal level. Currently a cooldown is in progress with reactor pressure is being maintained by the HPCI System operating in the pressure control mode and reactor water level is being maintained by the RCIC System. Reactor Water Clean-up System and normal reactor building ventilation have been restored. Off-site power is being supplied to the station by the Start-up Transformer (normal power supply for shutdown operations). This event had no impact on the health and/or safety of the public. The USNRC Senior Resident Inspector has been notified. This 4-hour notification is being made in accordance with 10 CFR 50.72 (b)(2)(iv)(A) and (B). The plant is transferring from decay heat removal to the torus to decay heat removal to the main condenser. Reactor pressure is 371 psig. Initial indications are that a main feedwater power supply breaker tripped.
ENS 4912015 June 2013 19:22:0010 CFR 50.72(b)(3)(iv)(A), System ActuationDivision 1 and 2 Emergency Diesel Generators Power Buses After Momentary Offsite Power LossColumbia Generating Station is shutdown for a refueling outage and is currently in Mode 4. At 1222 PDT June 15, 2013, the 115 kV offsite power to the backup transformer relayed off and then came back on. Both Division 1 and Division 2 4.16 kV critical switchgear buses were powered from the backup transformer at the time of the loss of backup power. Upon detection of under voltage conditions, Emergency Diesel Generators 1 and 2 started and powered the Division 1 and Division 2 4.16 kV critical switchgear buses after approximately 5 seconds. The temporary loss of power to the Division 1 and Division 2 4.16 kV critical switchgear buses also resulted in the closure of containment isolation valves in the Reactor Water Cleanup System, Equipment Drain System and the Floor Drain System. Shutdown cooling had previously been secured in preparation of performing the reactor pressure vessel hydro test. Investigation into the cause of the temporary loss of the 115 kV offsite power is on-going. The Division 1 and Division 2 4.16 kV critical switchgear buses are currently being powered from the 230 kV offsite power through the startup transformer. There were no radiological releases as a result of this event." The licensee notified the NRC Resident Inspector.
ENS 490779 April 2013 10:06:0010 CFR 50.73(a)(1), Submit an LER60 Day Report of an Invalid Primary Containment System Isolation SignalThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On April 9, 2013, at 0506 hours Central Daylight Time (CDT), during placement of clearance 2-TO-2013-0003, section 2-099-0001, Browns Ferry Nuclear Plant (BFN), Unit 2, received Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolation signals. The PCIS Groups 2, 3, 6, and 8 isolations caused the initiation of all three trains of the Standby Gas Treatment (SBGT) system and Control Room Emergency Ventilation (CREV) subsystem 'A', and isolations of the BFN, Unit 2, Reactor Zone ventilation and BFN, Units 1, 2, and 3, Refuel Zone ventilation. Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, and stopped the clearance placement. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The apparent cause for this condition was the outage tagging personnel did not prepare clearance 2-TO-2013-0003 section 2-099-0001 as a stand alone clearance, detail the effect on PCIS initiation on cover placement instructions, place clearance 2-TO-2013-0003 in the right sequence, and perform a thorough review of clearance 2-TO-2013-0003 section 2-099-0001 to identify the missing detail related to PCIS initiation. Personnel performance issues are being addressed in accordance with the Tennessee Valley Authority policies and processes. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Problem Evaluation Report 711266. The NRC Resident Inspector has been notified of this event.
ENS 4892315 April 2013 02:17:0010 CFR 50.72(b)(3)(iv)(A), System ActuationSpecified System Actuations While Shutting DownOn Sunday, April 14, 2013 at 2217 hours, with the Pilgrim Nuclear Power Station (PNPS) Reactor Mode Select Switch (RMSS) in Start-up, the turbine generator previously removed from service, and the reactor sub-critical on Intermediate Range Monitors Range 2 and lowering, a manual reactor scram was inserted due to reactor pressure lowering beyond established control bands. At the time of the manual reactor scram PNPS was conducting a planned reactor shutdown to commence refueling outage (RFO) -19. All control rods fully inserted and Primary Containment Isolation System Group II (Reactor Building) and Group VI (Reactor Water Cleanup System) actuations occurred as designed due to the expected reactor water level shrink associated with the scram signal. All plant systems responded as designed. Off-site power was unaffected and was supplied by the start-up transformer (normal power supply for refuel and reactor shutdown operations). The Main Steam Isolation Valves (MSIV) were manually closed to terminate the reactor pressure reduction and the High Pressure Coolant Injection (HPCI) system was manually started in the reactor pressure control mode. The Reactor Protection System (RPS) was reset as were the reactor building and reactor water clean-up system isolation signals. Currently, the plant cooldown is continuing with the HPCI system in pressure control and reactor water level being maintained within normal bands with the condensate and feedwater system. The cause of the lowering reactor pressure has not been determined and remains under review. This event had no impact on the health and/or safety of the public. This 8-hour notification is being made in accordance with 10 CFR 50.72 (b)(3)(iv)(A). The NRC Senior Resident Inspector has been notified. The licensee will also be notifying state authorities.
ENS 488096 March 2013 10:01:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual HeatMomentary Loss of Shutdown Cooling

At 0401 CST on 3/6/2013, while in RHR-High (Residual Heat Removal-High) water level the plant experienced a momentary Loss of Shutdown Cooling which resulted in a loss of safety function for Residual Heat Capability. Division 2 RHR shutdown cooling was restored within approximately 90 seconds without issue. No changes were experienced in refuel volume temperature or level during the loss of RHR shutdown cooling. This occurred shortly after a flow adjustment on the system was made utilizing the outboard valve. The inboard valve was reopened and an investigation is in progress. At the time of the valve closure, decay heat removal continued from Reactor Water Cleanup in heat reject mode and fuel pool cooling (with the fuel pool gates removed) is in service. Division 1 RHR (Shutdown Cooling) was available (not Operable) at the time of the loss. It is not currently understood why the injection valve closed. All systems functioned as required except for the spurious closing of MO-2015 (the Div 2 RHR inboard injection valve). The following make-up sources are available: Divisions 1 and 2 RHR, Divisions 1 and 2 Core Spray, CRD (Control Rod Drive), CST (Condensate Storage Tank) via a Core Spray with pressurizing station bypassed. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION AT 1419 EDT ON 4/11/2013 FROM RYAN RICHARDS TO MARK ABRAMOVITZ * * *

On March 6, 2013 (Notification No. 48809) NSPM (Northern States Power Monticello) reported in accordance with 10 CFR 50.72 (b)(3)(v)(B), a momentary closure of valve MO-2015 in the operating Residual Heat Removal (RHR) subsystem as an event or condition that at the time of discovery could have prevented the fulfillment of a safety function. Following the event, the RHR SDC (shut down cooling) subsystem was removed from operation for equipment forensics and troubleshooting. Results validated that valve MO-2015 was operable and no issues were identified with the associated electrical circuitry, or the RHR SDC subsystem. The decay heat removal requirements of LCO 3.9.7, RHR - High Water Level, were met and there was not a loss of safety function. Therefore, NSPM retracts the March 6, 2013 notification for this event. The licensee notified the NRC Resident Inspector, state and local authorities, and may make a press release. Notified the R3DO (Passehl).