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 Discovered dateReporting criterionTitleEvent description
ENS 5703216 March 2024 19:49:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Main Feedwater and Main Steam IsolationsThe following information was provided by the licensee via phone and email: At 1449 CDT, Waterford 3 Steam Electric Station was operating at 100 percent power when a manual reactor trip was initiated due to main feed isolation valve (FW-184B) and main steam isolation valve (MS-124B) going closed unexpectedly. Emergency feedwater (EFW) was automatically actuated. Preliminary evaluation indicates that all plant systems functioned normally after the reactor trip. The unit is currently stable in Mode 3. All control rods fully inserted as expected. This event is being reported as a 4-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the reactor protection system (RPS) when the reactor is critical and as an 8-hour nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as valid actuation of the EFW system. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Decay heat is being removed through the turbine bypass valves and the atmospheric dump valve on loop '2'. There is no primary to secondary system leakage. The cause of the isolations is still being investigated.
ENS 568972 November 2023 01:11:0010 CFR 50.73(a)(1), Submit an LER60 Day Notification for an Invalid Specified System ActuationThe following information was provided by the licensee via email and phone: At 2011 EDT on 11/01/23, with Unit 2 in Mode 3 at 0 percent power, Unit 2 received multiple spurious actuations. These actuations consisted of a partial group 1 and a partial group 5 primary containment isolation and a partial secondary containment isolation. The partial Group 1 isolation resulted in the closure of two main steam isolation valves (MSIVs); all other MSIVs were already closed. The partial group 5 isolation auto closed one of the reactor water cleanup (RWCU) isolation valves. The partial secondary containment isolation resulted in the closure of the inboard refueling floor and reactor building secondary containment isolation valves (SCIVs). Additionally, at 2238 EDT, Unit 2 again received multiple spurious actuations. These actuations consisted of a partial group 5 primary containment isolation and a partial secondary containment isolation. The partial group 5 isolation auto closed one of the RWCU isolation valves The partial secondary containment isolation resulted in the closure of the inboard refueling floor and reactor building SCIVs. And again, at 2354 EDT, Unit 2 received spurious actuations which consisted of a partial secondary containment isolation which resulted in the closure of the inboard refueling floor and reactor building SCIVs. The spurious actuations seen on 11/1/23 are triggered at -35 inches reactor water level (RWL) for group 5 and secondary containment isolations and at -101 inches RWL for group 1 isolations. It was determined that a combination of the RWL fluctuating above and below the wide range instrument reference leg tap, the reactor vessel pressure being lowered, and reactor core isolation cooling introducing colder water conditions near the reference leg tap of the wide range instrument caused the spurious actuations. Using multiple RWL indications for each of the instances mentioned above, the actuations were confirmed to be spurious as RWL was being controlled in a band of +55 inches to +85 inches at the time of the actuations. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an invalid actuation of a partial group 1, a partial group 5, and partial secondary containment logic. The NRC Resident has been notified.
ENS 5675927 September 2023 15:41:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Actuation of Reactor Protection and Containment Isolation Systems

The following information was provided by the licensee via fax: (On 09/27/2023) at 1041 CDT, with the plant at 75 percent power and main turbine control valve testing in progress, a reactor pressure transient resulted in a reactor steam dome high pressure scram and subsequent group 1 primary containment isolation of the main steam lines (MSL). All main steam isolation valves closed as a result of the group 1 isolation signal. Additionally, a group 2 containment isolation signal was received due to reactor pressure vessel (RPV) level less than plus 9 inches during the transient. Operations personnel responded and stabilized the plant. The high-pressure coolant injection (HPCI) system was placed in service to control RPV pressure. HPCI did not inject into the RPV and was not needed to control RPV water level. The cause of the initial pressure transient is under investigation. The NRC Resident Inspector has been notified.

      • UPDATE ON 9/27/2023 AT 2350 EDT FROM NATHAN PIEPER TO LAWRENCE CRISCIONE***

The utility notified the State of Minnesota and Wright and Sherburne counties. Notified R3DO (Orlikowski)

ENS 566106 July 2023 16:32:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionUnanalyzed ConditionThe following information was provided by the licensee via email: On July 6, 2023, at 1232 EDT, while operating in Mode 1 at 100 percent power, the supply check valve from the number 2 steam generator to the turbine driven auxiliary feedwater pump was determined during troubleshooting that it is not able to perform its isolation function. This failure would have resulted in the blowdown of both steam generators during a main steam line break in the number 2 steam generator main steam line upstream of the main steam isolation valves until the operators could isolate the faulted steam generator. Previous evaluation has determined that this condition constituted an unanalyzed condition that could impact containment pressure. There was no radioactive release to the environment. The steam line from the steam generator to the turbine driven auxiliary feedwater pump was isolated by use of a motor operated valve in the discharge line of the number 2 steam generator. There was no impact to Unit 3 which remains at 100 percent power. The NRC Senior Resident Inspector was notified. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B) as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety.
ENS 5653120 May 2023 08:15:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor ScramThe following information was provided by the licensee via phone and email: On 5/20/2023 at 0315 CDT, Browns Ferry Unit 1 was at 80 percent reactor power performing, 'Turbine control valve fast closure turbine trip and RPT (recirculation pump trip) initiate logic testing'. During performance of this test, Unit 1 received a full reactor scram. An investigation is in progress to determine the cause of the scram. All systems responded as expected, and Unit 1 is stable at zero percent power in mode 3. All control rods fully inserted into the core. Main steam isolation valves remained open with main turbine bypass valves controlling pressure. Reactor feedwater pumps remained in service to control reactor water level. Primary containment isolation signals groups 2, 3, 6, and 8 were received with expected system actuations. This event is reportable per 10 CFR 50.72(b)(2)(iv)(B), 'Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation'. The event is also reportable within 8 hours per 10 CFR 50.72(b)(3)(iv)(A), 'Specified System Actuation'. The NRC Resident has been notified.
ENS 564599 April 2023 04:44:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Loss of Reactor Coolant Pumps

The following information was provided by the licensee via email: The following event description is based on information currently available. If through subsequent reviews of this event additional information is identified that is pertinent to this event or alters the information being provided at this time a follow-up notification will be made via the ENS or under the reporting requirements of 10 CFR 50.73. At 2144 MST on April 8, 2023, the Unit 1 reactor automatically tripped due to the loss of reactor coolant pumps stemming from the loss of 13.8 kV power to the pumps. Prior to the reactor trip, the main turbine tripped due to a loss of hydraulic pressure. The main generator output breakers did not automatically open on the turbine trip as expected so the control room operators opened the breakers per procedural guidance. Once the breakers were opened, the two 13.8 kV electrical distribution buses failed to complete a fast bus transfer, which resulted in the loss of power to the reactor coolant pumps, initiating the reactor trip. The control room operators manually actuated a main steam isolation signal per procedure, requiring use of the atmospheric dump valves. Following the reactor trip, all control element assemblies inserted fully into the core. No automatic specified system actuation was required or occurred. No emergency plan classification was required per the Emergency Plan. Safety related buses remained powered from offsite power during the event and the offsite power grid is stable. Unit 1 is stable and in Mode 3. Decay heat is being removed by the atmospheric dump valves and the class 1E powered motor driven auxiliary feedwater pump. The loss of hydraulic pressure, the main generator output breakers failing to automatically open and the fast bus transfer not actuating are being investigated. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B). The NRC Senior Resident Inspector has been informed. Unit 2 is in a refueling outage in Mode 5 and Unit 3 is in Mode 1 at 100 percent power.

  • * * UPDATE ON 4/9/23 AT 0835 EDT FROM TANNER GOODMAN TO ADAM KOZIOL * * *

This update is being made to report the manual actuation of the B-train auxiliary feedwater pump and manual main steam isolation signal (MSIS) actuation affecting multiple main steam isolation valves (MSIVs) following the reactor trip. This event is being reported as a reactor protection system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(2)(iv)(B) and a specified system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Warnick)

  • * * UPDATE ON 5/3/23 AT 1945 EDT FROM LORRAINE WEAVER TO JOHN RUSSELL * * *

This update is intended to clarify the initial description of the event that occurred on 4/8/2023. Prior to the reactor trip, the main turbine tripped due to a loss of hydraulic pressure. The main generator output breakers did not automatically open on the turbine trip. The control room operators manually opened the breakers per procedural guidance. Once the breakers were opened, the two 13.8 kV electrical distribution buses de-energized. A fast bus transfer did not occur per design, which resulted in the loss of power to the reactor coolant pumps, initiating the reactor trip. The control room operators manually actuated a main steam isolation signal per procedure, requiring use of the atmospheric dump valves. The NRC Senior Resident Inspector has been informed of the update. Notified R4DO (Gaddy)

ENS 564556 April 2023 20:46:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionMain Steam Line 'B' Leakage in Excess of Tech Spec LimitsThe following information was provided by the licensee via phone and email: On March 4, 2023, it was determined that the main steam line (MSL) local leak rate test results for MSL 'B' were in exceedance of technical specification (TS) surveillance requirement (SR) 3.6.1.3.10 limits. Additionally, the leakage at the outboard main steam isolation valve (MSIV) 'B', was indeterminate due to a gross packing gland leak. An engineering calculation dated April 6, 2023, showed that this leakage, in conjunction with a design basis loss of coolant accident, would result in the radiological dose exceeding Updated Safety Analysis Report limits to the exclusion area boundary, the low population zone, and the control room. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) as a condition that results in the power plant being in an unanalyzed condition that degrades plant safety. Both inboard and outboard 'B' MSIVs have been reworked and are within the TS SR limits. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5627817 December 2022 05:51:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor ScramThe following information was provided by the licensee via email: On December 16, 2022 at 2351 CST, with the Unit in Mode 1 at 13 percent power, a manual scram was inserted due to lowering Reactor Pressure Vessel (RPV) pressure, which occurred following an unexpected opening of Main Turbine Bypass Valve 1. All control rods fully inserted. Following actuation of the manual scram, RPV pressure lowered, resulting in an automatic Primary Containment lsolation (PCIS) Group 1 isolation (expected response). The main steam isolation valves and steam line drain valves all closed. The Group 1 (isolation) has been reset allowing RPV pressure control with steam line drains to the main condenser. All systems responded as designed. The plant is stable in Mode 3. Investigation of the bypass valve opening is ongoing. This event is reportable under 10 CFR 50.72(b)(2)(iv)(B) RPS Actuation and 50.72(b)(3)(iv)(A) Specified System Actuation. There was no impact on health and safety of the public or plant personnel. The NRC Senior Resident Inspector has been notified.
ENS 5626913 October 2022 22:48:0010 CFR 21.21(d)(3)(i), Failure to Comply or DefectPart 21 - Inadequate Torque ValuesThe following information was provided by the licensee via email: On October 13, 2022, during Refueling Outage 25, 2 bolts and 2 washers were discovered in the strainer basket upstream of the main steam stop valve in the steam line from the 'A' steam generator. It was determined that these bolts and washers were from the main steam isolation valve (MSIV) upstream of the stop valve. One bolt and one washer were also determined to be missing from the MSIV on the line from the 'B' steam generator. The MSIVs are a similar design as the Main Feedwater Isolation Valves (MFIVs). It appears that the torque values for these backseat bolts provided by the vendor weren't sufficient to prevent the bolts from coming loose. Wolf Creek Nuclear Operating Corporation personnel evaluated the condition and determined that the inadequate torque values provided by the vendor could have constituted a substantial safety hazard if left uncorrected. In particular, if bolts had come loose from the MFIVs, they could have traveled downstream to the steam generators and then challenged the integrity of steam generator tubes. The NRC Senior Resident Inspector has been notified. This is a non-emergency notification required by 10 CFR 21.21(d)(3)(i). A written notification will be provided within 30 days.
ENS 5611926 September 2022 07:06:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Reactor Scram

The following information was provided by the licensee via email: At 0001 EDT on September 26, 2022, James A. FitzPatrick (JAF) removed the generator from service as part of a planned shutdown for refueling. At 0306 EDT, with the mode switch in Startup/Hot Standby and inserting rods, JAF experienced a spurious Scram and closure of seven out of eight main steam isolation valves (MSIV's). The reactor protection system (RPS) actuated during the event, resulting in all control rods being fully inserted. The cause of the closure of MSIV's and the Scram is being investigated. This condition is being reported as a four-hour NRC report per 10 CFR 50.72(b)(2)(iv)(B) for RPS actuation, and as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the safety system actuation based on the multiple main steam isolation valves closing on an isolation signal. There was no impact to the health and safety of the public. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 10/4/22 AT 2047 EDT FROM ANDREW WEAVER TO KERBY SCALES * * *

The following update was provided by the licensee via email: This Event Notification is being updated to clarify that the reactor was not critical when this event occurred. Therefore, the reporting requirement is changed from 10 CFR 50.72(b)(2)(iv)(B) to 10 CFR 50.72 (b)(3)(iv)(A) for Reactor Protection System (RPS) actuation along with Main Steam Isolation Valves (MSIV) system actuation. An analysis of reactor criticality was performed for the period of time prior to the RPS actuation event. Operators were inserting control rods per the shutdown Reactivity Management Plan. The Intermediate Radiation Monitoring (IRM) readings preceding the scram signal demonstrate a negative reactivity direction without control rod movement. The analysis concluded that the reactor was subcritical when RPS was actuated. The NRC Resident Inspector has been notified. Notified R1DO (Young).

ENS 5596325 June 2022 01:12:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Main Steam Isolation Valve ClosureThe following information was provided by the licensee via email: At 2012 CDT, Waterford 3 Steam Electric Station, Unit 3 was operating at 100 percent power when an automatic reactor trip occurred due to Main Steam Isolation Valve MS-124B going closed unexpectedly. Subsequently, both main feedwater isolation valves shut. Emergency Feedwater (EFW) was automatically actuated. Preliminary evaluation indicates that all plant systems functioned normally after the reactor trip. The unit is currently stable in Mode 3. All control rods fully inserted as expected and all other plant equipment functioned as expected. This was an uncomplicated scram. This event is being reported as a 4-hour non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) as an actuation of the reactor protection system (RPS) when the reactor is critical and as an 8-hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as valid actuation of the EFW system. The NRC Resident Inspector has been notified.
ENS 5589916 May 2022 19:52:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Scram Due to Electrical TransientsThe following information was provided by the licensee via fax: Unit 2 experienced multiple electrical transients resulting in a Group I Primary Containment Isolation Signal (PCIS) isolation and subsequent unit reactor scram. Low reactor water level during the automatic scram caused PCIS Group II and III isolation signals. Following the PCIS Group I isolation, all main steam lines isolated. All control rods inserted and all systems operated as designed. The following additional information was obtained from the licensee via phone in accordance with Headquarters Operations Officers Report Guidance: Peach Bottom Unit 2 automatically scrammed from 100 percent power due to an electrical transient and subsequent PCIS Group I isolation (Main Steam Isolation Valve closure). Unit 2 lost main feedwater due to the PCIS Group I isolation, however, all other systems responded as expected following the scram. High Pressure Coolant Injection is maintaining pressure control while Condensate Pumps are maintaining inventory. The unit is currently stable and in Mode 3. Peach Bottom Unit 3's Adjustable Speed Drives were impacted by the electrical transients and the unit reduced power to 98 percent power. The NRC Resident Inspector was notified.
ENS 5578512 March 2022 05:50:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentMain Steam Isolation Valve Failed to Shut

The following information was provided by the licensee via email: At 0050 EST on 3/12/22, while shutting down for entry into a scheduled refueling outage, the station discovered that a single Main Steam Isolation Valve (4A MSIV) did not fully close on demand. All other equipment operated as expected. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v). The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 04/26/22 AT 1422 EDT FROM DAVID STOIA TO BRIAN PARKS * * *

The following information was provided by the licensee via email: On 3/12/2022 at 0656 EDT Turkey Point Unit 4 notified the NRC pursuant to 10 CFR 50.72(b)(3)(v)(D) that a single Main Steam Isolation Valve (MSIV) did not fully close when manually demanded from the control room during shutdown of Unit 4 for a refueling outage. Following disassembly and inspection of the MSIV, Florida Power & Light Engineering identified the cause of the deficiency and determined that the valve would have fully seated under its design accident conditions. This notification is a retraction of EN# 55785. The NRC Resident Inspector has been notified of this retraction. Notified R2DO (Miller).

ENS 5558617 November 2021 18:13:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip and Automatic Auxiliary Feedwater ActuationAt 1313 hours on November 17, 2021, with Unit 2 in Mode 1 at 100 percent power, the reactor was manually tripped due to a loss of the 21B Main Feedwater Pump (due to low suction pressure). The Auxiliary Feedwater System automatically started as designed in response to the full power reactor trip. Additionally, the Main Steam Isolation Valves were manually closed to prevent excessive reactor coolant system cooldown. The trip was not complex, with all systems responding normally post-trip. There was no equipment inoperable prior to the event that contributed to the reactor trip or adversely impacted plant response. Operations responded and stabilized the plant. Decay heat is being removed by discharging steam to the atmosphere using the Atmospheric Dump Valves. Beaver Valley Power Station Unit 1 is unaffected and remains at 100 percent power in Mode 1. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, the automatic actuation of the Auxiliary Feedwater System is being reported as an eight-hour, non-emergency Specific System Actuation per 10 CFR 50.72(b)(3)(vi)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident has been notified.
ENS 5557614 November 2021 16:50:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionNON-FUNCTIONAL Steam Supply Check Valve to Turbine Driven Auxiliary Feedwater PumpOn November 14, 2021, at 1150 EST, while operating in Mode 1 at 100 percent power, the supply check valve from the Number 2 steam generator to the turbine driven auxiliary feedwater pump was determined during troubleshooting that it is not able to perform its isolation function. This failure would have resulted in the blowdown of both steam generators during a main steam line break in the Number 2 steam generator main steam line upstream of the main steam isolation valves until the operators could isolate the faulted steam generator. Previous evaluation has determined that this condition constituted an unanalyzed condition that could impact containment pressure. There has been no radioactive release to the environment. The steam lines from the steam generators to the turbine driven auxiliary feedwater pump have been isolated by use of a motor operated valve in the discharge line of the Number 2 steam generator. There has been no impact to Unit 3 which remains at 100 percent power. The NRC Senior Resident has been notified. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B) as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety.
ENS 5557212 November 2021 15:07:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Due to Increasing Steam Generator Water LevelsAt 1007 EST on November 12, 2021, with Unit 2 in Mode 1 at approximately 17 percent power following a refueling outage, the reactor was manually tripped due to increasing steam generator water levels due to an oscillating Main Feedwater Pump Recirculation Valve. Additionally, the Main Steam Isolation Valves were manually closed to prevent excessive reactor coolant system cooldown. Decay heat is being removed by discharging steam to the atmosphere using the Atmospheric Dump Valves. The trip was not complex, with all systems responding normally post-trip. There was no equipment inoperable prior to the event that contributed to the reactor trip or adversely impacted plant response. Operations responded and stabilized the plant. Beaver Valley Power Station Unit 1 is unaffected and remains at 100 percent power in Mode 1. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification, per 10 CFR 50.72(b)(2)(iv)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 555656 November 2021 15:00:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionSteam Supply Check Failure to Turbine Driven Auxillary FeedwaterDuring a Unit 2 refueling outage valve overhaul activity on the steam supply check valve from the number 2 steam generator to the turbine driven auxiliary feedwater pump, 2-MS-4B, the check valve was found with its disc separated from the disc arm. This failure would have resulted in the blowdown of both steam generators during a main steam line break in the steam generator number 2 main steam line upstream of the main steam isolation valves until the operators could isolate the faulted steam generator. On November 6, at approximately 1100 EDT evaluation determined that this condition constituted an unanalyzed condition that could impact containment pressure. There has been no radioactive release to the environment. The valve has been repaired. The check valve in the steam supply from the number 1 steam generator to the turbine driven auxiliary feedwater pump was inspected and found to be satisfactory. There has been no impact to Unit 3 which remains at 100% power. The Senior Resident has been notified. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B) as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety.
ENS 5551411 October 2021 17:21:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Scram After Main Turbine TripAt 1321 EDT on October 11, 2021, Susquehanna Steam Electric Station Unit 2 reactor automatically scrammed due to a trip of the Main Turbine. Unit 2 reactor was being operated at approximately 95 percent RTP (rated thermal power) with no evolutions in progress. The Control Room received indication of a Main Turbine trip with both divisions of RPS (Reactor Protection System) actuated and all control rods inserted. Turbine bypass valves opened automatically to control reactor pressure and subsequently failed open causing the reactor to depressurize. When reactor pressure reached approximately 560 psig, the operations crew manually closed the Main Steam Isolation Valves (MISVs) to stop the depressurization. Reactor water level lowered to -31 inches causing Level 3 (+13 inches) isolations. No (automatic) ECCS (Emergency Core Cooling System) actuations occurred. HPCI (High Pressure Coolant Injection) and RCIC (Reactor Core Isolation Cooling) were manually initiated to control reactor water level. The Operations crew subsequently maintained reactor water level at the normal operating band using RCIC and reactor pressure was controlled with HPCI in pressure control mode and main steam line drains. The Reactor Recirculation Pumps tripped as designed on EOC-RPT (end of cycle recirculation pump trip). The reactor is currently stable in Mode 3. An investigation into the cause of the turbine trip is underway. The NRC Resident Inspector was notified. A voluntary notification to PEMA will be made. This event requires a 4 hour ENS notification in accordance with 10 CFR 50.72(b)(2)(iv)(A), 10 CFR 50.72(b)(2)(iv)(B) and an 8 hour ENS notification in accordance with 10 CFR 50.72(b)(3)(iv)(A).
ENS 5515425 March 2021 14:18:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Due to Lowering Condenser VacuumOn March 25, 2021 at 0901 CDT, River Bend Station Unit 1 (RBS) was operating at 93 (percent) reactor power (limited by 100 (percent) recirculation flow) when condenser vacuum began to lower due to ARC-AOV1A, Steam Jet Air Ejector Suction Valve, going closed. At 0918 CDT, a manual reactor SCRAM was inserted at approximately 80 (percent) reactor power due to condenser vacuum continuing to lower. After the SCRAM, all systems responded as designed and condenser vacuum was restored by starting a mechanical vacuum pump. The cause of the Steam Jet Air Ejector Suction Valve closure is unknown at this time and being investigated. Currently RBS is stable, and pressure is being maintained using Turbine Bypass Valves. The Main Steam Isolation Valves remained opened throughout the event. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical and 10 CFR 50.72 (b)(3)(iv)(A) Specified System Actuation as result of expected post SCRAM level 3 isolations. No radiological releases have occurred due to this event from the unit. NRC Resident Inspector has been notified of this event.
ENS 5499613 November 2020 07:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Scram Due to High Reactor Pressure SignalAt 0245 EST on November 13, 2020, the Limerick Unit 1 reactor automatically scrammed on a valid Reactor High Pressure signal (1096psig). The Reactor High Pressure signal was caused by the closure of the 1B Inboard Main Steam Isolation Valve (MSIV), causing reactor pressure to rise, exceeding the Reactor Protection System (RPS) setpoint of 1096psig. The shutdown was normal and the plant is stable in Hot Shutdown with normal pressure control via the Main Steam Bypass Valves to the Main Condenser and normal level control using the Feedwater System. The closure of the 1B Inboard MSIV appears to have been caused by a loss of Primary Containment Instrument Gas (PCIG) pneumatic supply to the valve. The licensee notified the NRC Resident Inspector, and will be notifying Berks, Chester, and Montgomery Counties, as well as the Pennsylvania Emergency Management Agency.
ENS 548746 March 2020 04:00:0010 CFR 21.21(d)(3)(i), Failure to Comply or DefectPart 21 Report - Failure of Main Steam Isolation Valve Air PacksThe following is a synopsis of information received from the licensee: On March 6, 2020, while at zero percent power and in Cold Shutdown - Mode 4, Nine Mile Point Unit 2 (NMP2) determined through surveillance testing that three Main Steam Isolation Valves (MSIVs) did not meet their Technical Specification closure time. The cause of the MSIV failures has been determined to be delayed Air Pack response. The delay was caused by a buildup of corrosion product and waxy foreign material believed to be dried pipe thread sealant or O-ring assembly lube that accumulated on the internal surfaces of the Air Pack during refurbishment by the vendor Trillium (previously Hiller). The following is action taken or planned to be taken to prevent recurrence: A note will be added to the procurement requirement evaluation form and purchase order for MSIV Air Pack refurbishments to minimize use of O-ring lubricant and thread sealant to limit likelihood of capturing foreign material on Air Pack valve internals. The Energy Industry Identification System (EIIS) component function identifier and system name of each component or system referred to above is: Component - Main Steam Isolation Valves, Air Pack. IEEE 803 Function Identifier - VOP. IEEE805 System Identification - SB. The licensee notified the NRC Resident Inspector. For further information contact: Todd Tierney Plant Manager Nine Mile Point Nuclear Station Exelon Generation Company, LLC Brandon Shultz Site Regulatory Assurance Manager Nine Mile Point Nuclear Station (315) 349-7012 .
ENS 5485525 August 2020 04:05:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationReactor Scram After Loss of Feedwater - Grand GulfOn August 24, 2020 at 2305 CT at Grand Gulf Nuclear Station (GGNS) an Automatic Reactor Scram occurred after a trip of the Reactor Feed Pump B and subsequent lowering of reactor water level to 11.4 inches Narrow Range. The scram occurred with Reactor Power at 14% and the main generator offline. All control rods fully inserted and there were no complications. All systems responded as designed. Main Steam Isolation Valves were manually closed to control reactor cooldown, Currently GGNS reactor pressure is being maintained at 450-600psig. Reactor water level is being maintained with condensate through startup level control. No radiological releases have occurred due to this event from the unit. The NRC Resident has been notified. Decay heat is being removed via the main condenser. Notified R4DO.
ENS 5483918 August 2020 01:13:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Due to Rising Steam Generator LevelOn 08/17/20 at 2113 EDT, with Unit 3 in Mode 1 at approximately 92% (Rated Thermal Power) RTP, the reactor was manually tripped. This was due to a turbine runback caused by CV-3-2011, Low Pressure Feedwater Heater Bypass Control Valve, failing open, followed by rising Steam Generator (S/G) levels. Unit 3 reactor was tripped manually when the 3C S/G Level reached 78% narrow range. Unit 3 Main Steam Isolation Valves were closed manually in accordance with Emergency Operating Procedure (EOP) network due to 38 MSR Main Steam Stop valve position indication lost. All other systems operated normally. Auxiliary Feedwater initiated as designed to provide S/G water level control. EOPs have been exited and General Operating Procedures (GOPs) were entered. Unit 3 is stable in Mode 3 at normal operating temperature and pressure. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. All rods are inserted, decay heat is being removed via S/G through normal secondary systems. The plant is in normal electrical line up. Lightning strike is believed to be the initial cause of the runback.
ENS 548124 August 2020 03:12:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Due to a Loss of Offsite Power

At 2312 EDT, on August 3, 2020, Brunswick Unit 1 declared an Unusual Event due to a loss of offsite power. The unit was at approximately 20 percent power and was not synced to the grid when the unit automatically scrammed. All control rods fully inserted. Emergency Diesel Generators started and began powering the safety buses. Safety systems actuated as expected. The Unit also experienced a loss of Fuel Pool Cooling and Cleanup System, but one pump was returned to service. Unit 2 remains at 100 percent power and is unaffected. The licensee notified State and local governments, as well as the NRC Resident Inspector. Notified DHS SWO, FEMA Operations Center, CISA IOCC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE FROM MARK TURKAL TO DONALD NORWOOD AT 0120 EDT ON 8/4/2020 * * *

At approximately 2302 EDT, a loss of offsite power occurred on Unit 1. This resulted in a Reactor Protection System (RPS) actuation. Per design, emergency diesel generators 1 and 2 properly started and loaded to their respective emergency buses. The Reactor Core Isolation Cooling (RCIC) system was manually started and is being used to control reactor water level. The High Pressure Coolant Injection (HPCI) system was manually started and is being used for pressure control. As previously reported, an Unusual Event was declared at 2312 EDT due to the loss of offsite power. At the time of the event, Unit 1 was in the process of shutting down for maintenance associated with a ground on the main generator. Due to the RPS actuation while critical, this event is being reported as a four-hour, nonemergency notification per 10 CFR 50.72(b)(2)(iv)(B). As a result of the reactor trip, reactor water level reached low level 1 (LL1). The LL1 signal causes a Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sample isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Per design, the loss of offsite power also caused a Group 1 (i.e., main steam isolation valve) isolations. Due to the Emergency Diesel Generator and Primary Containment Isolation System (PCIS) actuations, this event is also being reported as an eight-hour, nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A). Unit 2 was not affected. There was no impact to the health and safety of the public or plant personnel. The safety significance of the event is minimal. All safety related systems operated as designed. Investigation of the cause of the loss of offsite power is in progress. The licensee notified the NRC Resident Inspector. Notified R2DO (Inverso).

  • * * UPDATE ON 8/4/2020 AT 1534 EDT FROM JOSEPH ELKINS TO ANDREW WAUGH * * *

At 1454 EDT on August 4, 2020, the Unusual Event was exited when offsite power was restored to Unit 1. Per design, when the loss of offsite power to Unit 1 occurred, all four emergency diesel generators (EDGs) started and EDGs 1 and 2 properly suppled emergency buses 1 and 2. Since Unit 2 was not affected by the loss of power, EDGs 3 and 4 ran unloaded. With restoration of offsite power to Unit 1, EDG 2 has been secured. EDGs 1, 3, and 4 are being secured as required by plant operating procedure. Notified R2DO (Inverso), NRR EO (Miller), IRD MOC (Grant), DHS SWO, FEMA OC, DHS NICC WO, CISA IOCC (email), DHS SWO (email), FEMA NWC (email), FEMA Ops Center (email), FEMA-NRCC-sasc (email), NRCC THD Desk (email), NuclearSSA (email). ********************************************************************************************************************************

ENS 5479521 July 2020 09:35:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationBiofouling of Intake Structure Leads to Manual Reactor Scram of Unit 1The following was received from TVA - Brown's Ferry at 0858, 21 July 20. On July 21, 2020, at 0435 hours Central Daylight Time, Browns Ferry Unit 1 inserted a manual reactor scram due to degrading main condenser vacuum from marine biofouling at the intake structure. Browns Ferry Unit 2 is in Mode 4 and Browns Ferry Unit 3 is at approximately 76% rated thermal power and stable. Primary Containment Isolation Systems received an actuation signal for groups 2, 3, 6, 8 on reactor water level below +2". All Primary Containment Isolation System groups that received an actuation signal performed as designed. Additionally, all other systems functioned as designed. This event is reportable within 4 hours per 10CFR50.72(b)(2)(iv)(B) - Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation. This event also requires an 8 hour report per 10CFR50.72(b )(3)(iv)(A), Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B), (1) Reactor protection system (RPS) including: reactor scram or reactor trip, except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation and (2) General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs). The NRC Resident Inspector has been notified. The plant is stable in Mode 3 and will remain shutdown until marine growth clogging the intake structure abates.
ENS 5479420 July 2020 18:25:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationBiofouling of Intake Structure Leads to Manual Reactor Scram of Unit 2 and Downpower of Units 1 & 3On July 20, 2020, at 1325 hours Central Daylight Time, Brown's Ferry Unit 2 inserted a manual reactor scram due to degrading main condenser vacuum from marine biofouling at the intake structure. Brown's Ferry Unit 1 performed a down power to 43% and Unit 3 down powered to 76%. Conditions are stable on both Unit 1 and 3 following unit down power. Primary Containment Isolations Systems received an actuation signal for groups 2, 3, 6, and 8 on reactor water level below +2". All Primary Containment Isolations System groups that received an actuation signal performed as designed. Additionally, all other systems functioned as designed. This event is reportable within 4 hours per 10CFR50.72(b)(2)(iv)(B) - Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation. This event also requires an 8 hour report per 10CFR 50.72(b)(3)(iv)(A), "Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B), (1) Reactor protection system (RPS) including: reactor scram or reactor trip, except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation and (2) General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs). The NRC Resident Inspector has been notified. All control rods fully inserted and decay heat is being removed via normal feedwater and condenser.
ENS 5472525 May 2020 09:33:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Scram Due to Main Turbine TripAn (automatic) reactor SCRAM occurred at 0433 CDT, on 05/25/2020, from 66 percent core thermal power. The cause of the SCRAM was due to a Main Turbine Trip. The cause of the Turbine Trip is under investigation. All systems responded as designed. No loss of offsite power or (Emergency Safety Feature) (ESF) power occurred. No (Emergency Core Cooling System) (ECCS) or Emergency Diesel Generator initiations occurred. Main Steam Isolation valves remained open and no radioactive release occurred due to this event. The plant is stable in mode 3. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the Reactor Protection System (RPS), when the reactor is critical. The NRC Resident Inspector has been notified. Decay heat removal is through the Feedwater and Condensate System.
ENS 5470813 May 2020 06:08:0010 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS DischargeAutomatic Reactor TripAt 0208 EDT on 05/13/2020, Sequoyah Unit 1 was at 100% power when an automatic reactor trip signal was received concurrent with a low steam line pressure safety injection signal. The low steam line pressure safety injection signal was actuated from the steam pressure rate of decrease feature. Main steam isolation valves (MSIVs) automatically closed as designed and steam generator pressures stabilized following the isolation. All other safety-related equipment operated as designed, with the exception of 1-FCV-61-122 Glycol inboard containment isolation valve which failed to automatically isolate on a Phase A containment isolation signal. The corresponding outboard containment isolation valve, 1-FCV-61-110, automatically isolated as designed which isolated penetration X-114. Safety injection was terminated at 0221 EDT 5/13/20, and Unit 1 is currently being maintained in Mode 3 at normal operating temperature and pressure with auxiliary feedwater supplying the steam generators and decay heat removal via steam generator atmospheric relief valves. There is no indication of any primary to secondary leakage. The electrical alignment is normal with shutdown power supplied from off-site power. There is no current operational impact to Unit 2. There is no impact on public health or safety. Post safety injection actuation investigation is in progress. The NRC Resident Inspector has been notified.
ENS 5418527 July 2019 23:29:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Scram Due to Main Turbine TripAt 1929 EDT on 7/27/2019, with the Unit in Mode 1 at 98 percent power, the reactor automatically scrammed due to a Main Turbine Trip. The trip was not complex, with all systems responding normally post-trip. Main Steam Isolation Valves (MSIVs) were manually closed to prevent exceeding Reactor Pressure Vessel Cooldown Rate. Rector Core Isolation Cooling (RCIC) was manually initiated to stabilize Reactor Vessel Water Level and Pressure following MSIV closure. The Main Condenser and Feedwater are available. Operations responded and stabilized the plant. Reactor water level is being maintained via RCIC. Decay heat is being removed by discharging steam to the Main Condenser and RCIC. The cause of the Main Turbine Trip is currently under investigation. The site is in a normal electrical lineup. The licensee notified the NRC Resident Inspector.
ENS 5417519 July 2019 13:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Main Steam Isolation Valve Failing ShutAt 0945 (EDT) on July 19, 2019, with Unit 2 in Mode 1 and 100 percent power, the reactor automatically tripped due to Loop 2 'B' Main Steam Isolation Valve failing shut. The Auxiliary Feedwater system (AFW) started automatically as a result of the automatic reactor trip. The trip was not complex, with all systems responding normally. Operations stabilized the plant in Mode 3. Decay heat is being removed through the main steam lines through the steam dumps and into the condenser. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the valid AFW actuation from the reactor trip, this event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A). Unit 1 was not affected. There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspectors have been notified. All control rods fully inserted.
ENS 5410318 April 2019 05:10:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification Due to Invalid Specified System ActuationThis 60-day telephone notification is being made in accordance with the reporting requirements specified by 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to describe an invalid actuation of a general containment isolation signal affecting multiple Main Steam Isolation Valves (MSIVs). On April 18, 2019 at approximately 0110 EDT, during performance of an ASME reactor vessel leak check, all four inboard MSIVs closed as a result of actuation of the Main Steam Line (MSL) high flow instrumentation. The high flow signal was spurious on the 'D' channel with no flow in the MSLs. Since an actual high flow condition did not exist at the time of the actuation, the actuation was considered invalid. The MSIVs functioned as designed on actuation of the MSL high flow instrumentation. All outboard MSIVs were closed at the time of the actuation in accordance with the vessel leak check procedure. The NRC Resident Inspector has been notified.
ENS 5407118 May 2019 03:03:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Scram Due to Degrading Condenser Vacuum

On Friday, May 17, 2019 at 2303 (EDT), with the reactor at 70 (percent) core thermal power, Pilgrim Nuclear Power Station initiated a manual reactor scram due to degrading condenser vacuum as a result of the trip of Seawater Pump B. All control rods inserted as designed. The plant is in hot shutdown. Plant safety systems responded as designed. Pressure is being controlled using the Mechanical Hydraulic Control System and Main Condenser. Reactor water level is being maintained with the feedwater and condensate system. During the manual reactor scram, the plant experienced the following isolation signals as designed:

"Group 2 Isolation: Miscellaneous containment isolation valves
Group 6 Isolation: Reactor Water Clean-up
Reactor Building Isolation Actuation

Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification in accordance with 10 CFR 50.72(b)(2)(iv)(B), 'any event that results in actuation of the reactor protection system (RPS) when the reactor is critical...' This notification is also being made in accordance with 10 CFR 50.72(b)(3)(iv)(A), 'Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) of this section...' (B)(2) 'General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs).' This event has no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The licensee will notify the Massachusetts Emergency Management Agency.

ENS 5396731 March 2019 01:30:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Msiv Failing ClosedAt 2130 (EDT) on March 30, 2019, with Unit 2 in Mode 1 at 30 percent reactor power, the reactor was manually tripped due to a main steam isolation valve failing closed. The trip was not complex, with all systems responding normally. Operations stabilized the plant in Mode 3. Decay heat is being removed through the main steam lines through the steam dumps and into the condenser. The expected actuation of the Auxiliary Feedwater System (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72 (b)(3)(iv)(A). Unit 1 was not affected. There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspectors have been notified.
ENS 5396630 March 2019 21:47:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Scram and Specified System ActuationAt 17:47 Eastern Daylight Time (EDT) on March 30, 2019, with Unit 2 in Mode 1 at approximately 23 percent reactor power and main turbine startup in progress coming out of a refuel outage, a high temperature was sensed at main turbine bearing #9. As a result of and to arrest the high temperature condition, the main control room inserted a manual reactor scram. All control rods inserted as expected during the scram. When the scram was inserted, reactor water level dropped below the Low Level 1 actuation setpoint. Per design, the Low Level 1 signal resulted in Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations. The main control room manually closed all Main Steam Isolation Valves (MSIVs), in anticipation of a low vacuum prior to the Group 1 automatic closure signal being received. High Pressure Coolant Injection (HPCI) was aligned for pressure control and Reactor Coolant Isolation System (RCIC) was aligned for level control. The Reactor Coolant Sample Line Isolation valves closed as expected on low main condenser vacuum. All systems responded as designed. This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) for RPS actuation and 10 CFR 50.72(b)(3)(iv)(A) as an event that results in valid actuations of the Primary Containment Isolation System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. At the time of notification, decay heat was being removed by the condenser through one open MSIV and a feedwater pump running.
ENS 5396228 March 2019 20:54:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Actuation of the Primary Containment Isolation System and the Reactor Protecton SystemAt 1654 EDT on March 28, 2019, with Unit 1 in Mode 3 at 0 percent power, an actuation of the Primary Containment Isolation System occurred, closing the outboard Main Steam Isolation Valves (MSIVs) due to a low condenser vacuum signal. The MSIVs had been manually closed, per procedure, during the shutdown evolution to address drywell leakage. The inboard MSIVs had not been reopened when the isolation occurred. Subsequently, at 1658 EDT a Reactor Protection System (RPS) actuation occurred due to reactor water level dropping below the actuation setpoint. All control rods were inserted at the time of the actuation. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in valid actuations of the Primary Containment Isolation System and the Reactor Protection System. There was no impact on the health and safety of the public or plant personnel. The safety function of both the MSIVs and the RPS had already been completed at the time of the event. The NRC Resident Inspector has been notified.
ENS 5392310 March 2019 04:59:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Scram Resulting in Rps and Eccs ActuationAt 2259 CST on 3/9/2019, Browns Ferry Unit-3 received an automatic SCRAM on Main Generator Breaker Failure and Turbine Load Reject. Unit-3 declared a Notification of Unusual Event SU1 for loss of offsite AC power to Unit-3 specific 4kV Shutdown Boards for greater than 15 minutes. Primary Containment Isolation Systems (PCIS) Groups 1, 2, 3, 6, and 8 isolation signals were received. Upon receipt of these signals, all required components actuated as required. Main steam relief valves lifted on the initial transient. High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) initiated on low reactor water level. HPCI remains in service for reactor level and pressure control. RCIC is not in service at this time, the station is investigating low flow from the pump. All four Unit-3 Diesel Generators started and loaded as expected. Residual Heat Removal System is in service for suppression pool cooling. 4kV Station Unit Boards have been restored from the 161kV system. Actions are in progress to restore 4kV Shutdown Boards to offsite power. This event is reportable within 1 hour in accordance with 10 CFR 50.72(a)(1)(i) for declaration of the Licensees Emergency Plan. Complete as documented on EN 53922. This event requires a 4 hour report per 10 CFR 50.72(b)(2)(iv)(B), 'Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' This event also requires an 8 hour report per 10 CFR 50.72(b)(3)(iv)(A). 'Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B), (1) Reactor protection system (RPS) including: reactor scram or reactor trip, (2) General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs), (4) ECCS (Emergency Core Cooling System) for boiling water reactors (BWRs) including: core spray systems; high-pressure coolant injection system; low pressure injection function of the residual heat removal system, (5) BWR reactor core isolation cooling system; isolation condenser system; and feedwater coolant injection system, and (8) Emergency AC electrical power systems, including: Emergency diesel generators (EDGs).' The NRC resident inspector has been notified. As of the event report, the MSIVs were opened and decay heat was being removed via the bypass valves to the condenser.
ENS 5392210 March 2019 05:12:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationNotice of Unusual Event Due to Loss of Offsite Power

At 0012 EST on 3/10/2019, Browns Ferry Unit-3 declared an Unusual Event due to a spurious trip of the generator breaker, resulting in a loss of AC power to the 4 kV shutdown boards greater than 15 minutes. All diesel generators started and loaded to supply onsite power. The reactor auto-scrammed, with all rods fully inserting. The Main Steam Isolation Valves opened and shutdown cooling was being conducted via the condenser. The licensee will exit the emergency declaration once offsite power is restored. There is no estimated restart date. Browns Ferry Unit 1 remains in Mode-1 (100%), Unit 2 remains in Mode-5 for a refueling outage. The NRC Resident Inspector has been notified. This event is related to EN 53923. Notified DHS SWO, FEMA Operations Center, DHS NICC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE ON 3/10/19 AT 1419 EDT FROM JOHN HOLLIDAY TO BETHANY CECERE * * *

At 1310 CDT, Browns Ferry Unit-3 exited the Unusual Event when 161 kV lines were made available. The licensee is executing procedures for securing the diesel generators while alternate offsite power methods are utilized. Switchyard damage evaluation is in progress. The licensee will notify the NRC Resident Inspector. Notified R2DO (Desai), R2RA (Haney), DNRR (Nieh), NRR EO (Miller), and IRD (Grant). Notified DHS SWO, FEMA Operations Center, DHS NICC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

ENS 538155 January 2019 15:40:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the ReactorEn Revision Imported Date 2/12/2019

EN Revision Text: POTENTIAL LOSS OF MSIV SCRAM FUNCTION DURING MAIN STEAM LINE ISOLATION VALVE TESTING At approximately 1040 EST on January 5, 2019, during evaluation of test results for the 'C' Main Steam Isolation Valve (MSIV), it was determined that closure of three of four Main Steam Lines would not necessarily have resulted in a full scram during testing due to failure of a limit switch (LS-6) associated with MSIV-1C while in the test configuration. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), 'Any event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to: (A) Shut down the reactor and maintain it in a safe shutdown condition.' The system was restored from the testing configuration at 1057 EST and the failed trip channel was placed in the tripped condition at 1326 EST thus restoring the design function. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION AT 1529 EST ON 02/11/19 FROM JOSEPH FRATTASIO TO JEFF HERRERA * * *

The purpose of the notification is to retract ENS Notification 53815 made on 01/05/19 for Pilgrim Nuclear Power Station. The previous notification reported that there was a potential loss of Main Steam Isolation Valve (MSIV) scram function during main steam line isolation valve testing, at the time of discovery, due to failure of a limit switch (LS-6) associated with MSIV-1C while in the test configuration. Subsequent evaluation has demonstrated that the scram function credited in the design basis was not lost. Specifically, after an Engineering Evaluation, it has been determined that the MSIV position RPS logic was not lost for those functions within the design basis and, as such, was capable of performing its intended safety function. The NRC Resident Inspector has been notified. Notified the R1DO (Cahill).

ENS 5377613 October 2018 05:00:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid Specified System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a Primary Containment Isolation System (PCIS) Group 1 for Main Steam Isolation Valves (MSIVs), Group 3 for Reactor Water Cleanup (RWCU), Group 6 for Secondary Containment isolation, Group 7 for Reactor Water Sampling, Diesel Generator, Reactor Core Isolation Cooling (RCIC) System logic, and Residual Heat Removal (RHR) logic. Group 1, Group 6, Diesel Generator actuation, RCIC actuation and RHR actuation are within scope of 10 CFR 50.73(a)(2)(iv). Group 3 and Group 7 are not within scope as they affect only one system. Cooper Nuclear Station (CNS) was shut down in Mode 5 at the time of the event with the reactor cavity flooded. On October 13, 2018, at 0028 Central Daylight Time, CNS received full PCIS Groups 1, 3, and 6, and a half Group 7 on the Division 1 side. The MSIVs and RWCU isolation valves were already closed for maintenance. The Secondary Containment isolated. Control Room Emergency Filter and the Standby Gas Treatment Systems initiated. The inboard Reactor Water Sample valve isolated. Diesel Generator #1 started but was not required to connect to the critical bus. Reactor Core Isolation Cooling System logic actuated with no expected response due to being isolated for shutdown conditions. Division 1 RHR pump logic actuated. Division 1 RHR system was operating in shutdown cooling mode. The actuation caused the Division 1 RHR outboard injection and heat exchanger bypass valves to open. Shutdown cooling was unaffected and remained in service throughout the event. The plant systems responded as expected with no Emergency Core Cooling System injection. At the time of the event, an in-service inspection of welds inside the reactor vessel was taking place using a robot scanner that uses two vortex thrusters to hold the robot to the vessel wall. The robot inadvertently passed over an instrument penetration, drawing suction on the process leg, resulting in low reactor water level indications and the subsequent invalid Level 1 and 2 system actuations. Actual reactor vessel water level remained steady at cavity flooded conditions. The NRC Resident Inspector has been notified of this event.
ENS 5375627 November 2018 06:00:0010 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive MaterialEn Revision Imported Date 12/4/2018

EN Revision Text: INOPERABILITY OF EQUIPMENT FOR CONTROL OF RADIOLOGICAL RELEASE At 2130 CST on 11/27/2018, Division 1 Main Steam Positive Leakage Control System (MS-PLCS) was declared inoperable because of a leaking check valve that caused excessive cycling of the associated air compressor. Division 2 MS-PLCS had been declared inoperable on 11/27/2018 at 1400 CST when a pressure control valve in the system exceeded the maximum allowable stroke time. Because MS-PLCS supplements the isolation function of the main steam isolation valves (MSIVs) by processing fission products that could leak through the closed MSIVs, both divisions of MS-PLCS inoperable at the same time represents a condition that could prevent the fulfillment of a safety function of an SSC (Structures, Systems and Components) that is needed to control the release of radioactive material. The station diesel air compressor is available to supply backup air to the safety relief valves as required by the Technical Requirements Manual." (This is associated with operability of the safety relief valves, due to the inoperable MS-PLCS air compressor.) The unit is in a 7 day shutdown Limiting Condition for Operation (LCO), 1-TS1-18-Div 1 & 2 MSPLCS-685, for the two divisions of MS-PLCS being inoperable. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 12/03/18 AT 1551 EST FROM TIM GATES TO BETHANY CECERE * * *

This event was initially reported under 10 CFR 50.72(b)(3)(v)(C) as a condition that could have prevented the Main Steam Positive Leakage Control System (MS-PLCS) from fulfilling its safety function to control the release of radioactive material. Division I was declared inoperable due to a failed component. Division II was declared inoperable due to a pressure control valve in the system exceeding the maximum allowable time to close by 0.50 seconds. An engineering evaluation has since been performed and concluded that the 2 second maximum allowable time to close was based on the pressure control valve being classified as a rapid closure valve and was established from the original baseline data of 0.50 seconds. This baseline data is an administrative target value per the In-Service Testing Program. There are no technical specification requirements associated with the 2 second closure time. The engineering evaluation also determined that the volume of air supplied through the pressure control valve during the extra 0.50 seconds of valve closure would have an inconsequential effect on the pressure within the volume of leakage barrier between the Main Steam Isolation Valves associated with the MS-PLCS pressure control valve or have any effect on containment over-pressurization. Based on the information provided by the engineering evaluation, the Division II MS-PLCS has been declared operable-degraded non-conforming since time of initial discovery. Consequently, this event is not reportable as a condition that could have prevented the Main Steam Positive Leakage Control System (MS-PLCS) from fulfilling its safety function. The (NRC) Resident Inspector has been notified via e-mail. Notified the R4DO (Gaddy).

ENS 536465 October 2018 05:00:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedEn Revision Imported Date 10/25/2018

EN Revision Text: MAIN STEAM ISOLATION VALVES EXCEEDED PRIMARY CONTAINMENT LOCAL LEAK RATE ACCEPTANCE CRITERIA At 0520 (CDT), on October 05, 2018, it was discovered that a Primary Containment local leak rate test performed on Main Steam Isolation Valves (MSIV) exceeded its acceptance criteria.

During Mode 1, 2, and 3, Surveillance Requirement 3.6.1.3.10 requires MSIV leakage for a single MSIV line to be less than or equal to 106 standard cubic feet per hour (scfh) when tested at 29 psig and Surveillance Requirement 3.6.1.3.12 requires the combined leakage rate for all MSIV leakage paths to be less than or equal to 212 scfh when tested at 29 psig.

As-found for the 'C' MSIV line leakage results were unquantifiable and gave a (minimum) path value greeter than 160 scfh. This leakage rate lead to Surveillance Requirement 3.6.1.3.10 and 3.6.1.3.12 limits to be exceeded. This event is being reported as a condition of the nuclear power plant, including its principal safety barriers, being seriously degraded per 10 CFR 50.72(b)(3)(ii)(A) since the Primary Containment Isolation Valves leakage limits for MSIVs were exceeded. The NRC Resident Inspector has been notified.

  • * * RETRACTION AT 2320 EDT ON 10/24/2018 FROM THOMAS FORLAND TO MARK ABRAMOVITZ * * *

CNS (Cooper Nuclear Station) is retracting the 8-hour non-emergency notification made on October 5, 2018 at 0520 CDT (EN# 53646). Subsequent evaluation concluded that overall as-found 'C' MSIV leakage rate was not at a level that exceeded the surveillance requirement 3.6.1.3.10 and 3.6.1.3.12 limits and thus the Primary Containment Isolation Valve leakage rate limits for the MSIVs were not exceeded. The NRC Senior Resident Inspector has been notified. Notified the R4DO (Drake).

ENS 5361118 September 2018 04:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to a Steam Leak on a High Pressure Feedwater HeaterDue to a steam leak on the reheater line to 36C Feedwater Heater, operators initiated a manual trip of the reactor, verified the reactor trip, and closed all Main Steam Isolation Valves. The plant is currently stable in Mode 3 with the steam leak isolated. The Auxiliary Feedwater System actuated following the trip as expected. This is reportable under 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.72(b)(2)(iv)(B). The unit remains on offsite power in Hot Standby at normal operating temperature and pressure. Decay heat is being removed from the steam generators via the Auxiliary Feedwater System and atmospheric steam dumps. Unit 2 was unaffected and remains at 100 percent power. The licensee notified the NRC Resident Inspector, the State of New York, and the local transmission company.
ENS 5345916 June 2018 05:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip During StartupAt 1121 CDT on June 16, 2018, Arkansas Nuclear One, Unit 1 (ANO-1) performed a manual reactor trip due to a Turbine Bypass valve failing open on reactor startup. At the time, ANO-1 was in Mode 2 at approximately 2 percent power. The failed Turbine Bypass valve resulted in an overcooling event and the Overcooling Emergency Operating Procedure (EOP) was entered. Main Steam Line Isolation (MSLI) automatic actuation occurred on 2 of the 4 channels of Emergency Feedwater Initiation and Control during the overcooling event in the 'B' Steam Generator. The remaining channels of MSLI were manually actuated by the control room staff from the control room. Overcooling was terminated after the closure of the Main Steam Isolation Valve (MSIV) and reactor coolant parameters were stabilized as directed by the Overcooling EOP. Additionally, Gland Sealing Steam was lost to the main turbine due to the closure of the 'B' Steam Generator MSIV and Loss of Condenser Vacuum Abnormal Operating Procedure was entered. This is a 4-hour non-emergency 10 CFR 50.72 (b)(2)(iv)(B) notification due to a Reactor Protection System actuation (scram) and an 8-hour non-emergency 10 CFR 50.72 (b)(3)(iv)(A) notification for safety system actuation." All control rods fully inserted into the core during the trip. Heat removal is via the Atmospheric Dump Control valves to atmosphere. The NRC Resident Inspector has been notified. The licensee also notified the State of Arkansas.
ENS 5329026 March 2018 18:38:00Other Unspec ReqmntTechnical Specifications Required Shutdown Due to Inoperable Main Steam Isolation Valve

On March 25, 2018 at 1833 CDT, while at 100 percent power, Farley Unit 1 (FNP-1) conservatively declared a single Main Steam Isolation Valve (MSIV) inoperable on the 1C Steam Generator line due to indication of Steam Generator pressure rise with a corresponding reduction in flow of that loop. FNP-1 began a reactor shutdown at 0400 CDT on March 26, 2018 to establish plant conditions to support testing the affected main steam line MSIVs while in the required action time of Technical Specification 3.7.2. At 1338 CDT on March 26, 2018, testing confirmed that the single MSIV was inoperable and that valve disassembly will be required. The duration of the valve repair would exceed the required action time of Technical Specification 3.7.2. This report is being made in accordance with 10 CFR 50.72(b)(2)(i), as a plant shutdown required by technical specifications. The licensee has notified the NRC Resident Inspector.

  • * * UPDATE FROM DOUGLAS HOBSON TO KEN MOTT AT 0202 EDT ON 5/16/18 * * *

This EN (event notification) is being updated to clarify the reporting criteria as 'Voluntary'. Farley Technical Specification 3.7.2 allows continuous operation in MODE 2 with an INOPERABLE MSIV as long as the other MSIV in the affected Main Steam Line is closed. The initiation of the shutdown was performed as a prudent action to repair and restore OPERABILITY of the affected MSIV and was not a requirement of the Farley Technical Specifications. The licensee notified the NRC Resident Inspector. The R2DO (Masters) was notified.

ENS 5326918 March 2018 16:58:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram Due to Turbine Control Valve ClosureAt 1158 CDT on March 18, 2018, the Unit 1 reactor automatically scrammed due to a Reactor Protection System (RPS) signal generated from High Reactor Steam Dome Pressure in response to Turbine Control Valve Closure. The reactor had been operating at 100 percent power. Investigation is in progress. All control rods fully inserted into the core. Main Steam Isolation Valves remained open with Main Steam Relief Valves (MSRVs) operating on the initial transient as expected. Main Turbine Bypass Valves are currently controlling reactor pressure. Reactor Feedwater pumps remained in service to control reactor water level. Primary Containment Isolation Signals Groups 2, 3, 6, and 8 containment isolation and initiation signals were received. Upon receipt of these signals all required components actuated as required. All safety system operated as expected. At no time was public health and safety at risk. This event is reportable within 4 hours per 10 CFR 50.72(b)(2)(iv)(B) 'any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' It is also reportable within 8 hours per 10 CFR 50.72(b)(3)(iv)(A) 'any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) of this section, except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation' and requires an LER within 60 days per 10 CFR 50.73(a)(2)(iv)(A). The NRC Resident Inspector has been notified.
ENS 5316210 January 2018 15:28:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram Due to Turbine Control Valve Fast Closure Scram SignalAt 0928 CST on January 10, 2018, the Unit 3 reactor automatically scrammed due to a Reactor Protection System (RPS) signal generated from Turbine Control Valve Emergency Trip System pressure low. The reactor had been operating near 73 percent power for an emergent issue for Turbine Control Valve (TCV) No. 3. With TCV No. 3 out of service and closed, the unit was operating with RPS in a half scram condition. A subsequent failure of the TCV No. 2 sensing line resulted in RPS coincidence logic being met for TCV fast closure SCRAM. The investigation of the TCV No. 2 sensing line failure continues. All control rods fully inserted into the core. Main Steam Isolation Valves remained open with Main Turbine Bypass Valves controlling reactor pressure. Reactor Feedwater pumps remained in service to control reactor water level. Primary Containment Isolation Signals Groups 2, 3, 6, and 8 containment isolation and initiation signals were received. Upon receipt of these signals all required components actuated as required. Neither High Pressure Coolant Injection nor Reactor Core Isolation Cooling initiation signals were received. This event is reportable within 4 hours per 10 CFR 50.72(b)(2)(iv)(B) 'any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical except when the actuation results from and is part of a preplanned sequence during testing or reactor operation.' It is also reportable within 8 hours per 10 CFR 50.72(b)(3)(iv)(A) and requires an LER within 60 days per 10 CFR 50.73(a)(2)(iv)(A). The NRC Resident inspector has been notified.
ENS 531474 January 2018 19:10:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Scram Due to Partial Loss of Offsite Power During Winter StormOn January 4, 2018, at 1410 hours EST, with the reactor at approximately 100 percent power and steady state conditions, the winter storm across the Northeast caused the loss of offsite 345 kV Line 342. Reactor power was reduced to approximately 81 percent and a procedurally required manual reactor scram was initiated. All control rods fully inserted. As a result of the reactor scram, indicated reactor water level decreased, as expected, to less than +12 inches resulting in automatic actuation of the Primary Containment Isolation Systems for Group II - Primary Containment Isolation and Reactor Building Isolation System, and Group VI - Reactor Water Cleanup System. Reactor Water Level was restored to the normal operating band. The Primary Containment Isolation Systems have been reset. The Reactor Protection System signal has been reset. Following the reactor scram, the non-safety related Control Rod Drive Pump "B" tripped on low suction pressure. Control Rod Drive Pump "A" was placed in service. All other systems operated as expected, in accordance with design. This event is reportable per the requirements of Title 10, Code of Federal Regulations (CFR) 50.72 (b)(2)(iv)(B) - "RPS Actuation" and 10 CFR 50.72 (b)(3)(iv)(A) - "Specified System Actuation. This event had no impact on the health and/or safety of the public. The NRC Resident Inspector has been notified. The main steam isolation valves are open with decay heat being removed via steam to the main condenser. Offsite power is still available from 345kV line 355. As a contingency, emergency diesel generators are running and powering safety busses per licensee procedure. The licensee notified the Commonwealth of Massachusetts. The licensee will be notifying the town of Plymouth as part of their local notifications. The licensee will be issuing a press release.
ENS 5306712 November 2017 09:03:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentContainment Spray Pump Control Switches Out of ServiceAt 2119 (CST) on 11/12/2017 a Control Room board walk down discovered that both of the Unit 2 Containment Spray Pump control switches were in pull-out. With the control switches in pull-out, the pumps would not automatically start as required. Unplanned TS (Technical Specifications) 3.0.3 was entered at 2119 as a result of not complying with TS 3.6.5, Containment Spray and Cooling Systems, which requires both trains of Containment Spray to be Operable while in Mode 4. Unit 2 had entered Mode 4 at 0303 on 11/12/2017. TS 3.0.3 was exited at 2127 on 11/12/2017 when both Containment Spray Pump control switches were placed in Automatic restoring Operability. Preliminary investigation determined that while Unit 2 was in Mode 5, Surveillance SP 2099, Main Steam Isolation Valve Logic Test, had taken the Containment Spray Pump control switches to pull-out but did not re-align the control switches to automatic after the test was complete. This 8-hour Non-Emergency report is being made per 10 CFR 50.72(b)(3)(v)(D), Accident Mitigation. The NRC Senior Resident Inspector has been informed.
ENS 529506 September 2017 15:57:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram on Low Reactor Vessel Water LevelOn September 6, 2017 at 1157 (EDT), Nine Mile Point Unit 1 experienced an automatic reactor scram with a Main Steam Isolation Valve (MSIV) and Containment isolation. The scram was due to reactor vessel low water level. The cause of the reactor vessel low water level is under investigation. All control rods fully inserted. Following the scram, pressure was momentarily controlled through the use of the Emergency Condenser (EC) system. At 1205, pressure control was established through the main steam lines to the condenser through the turbine bypass valves. All plant systems responded per design following the scram. The reactor scram is a 4-hour report per 10 CFR 50.72(b)(2)(iv)(B). The following systems automatically actuated after the scram as expected. These system actuations are an 8-hour report per 10 CFR 50.72(b)(3)(iv)(A): 1. The High Pressure Coolant Injection (HPCI) system. HPCI initiated at 1157 and was reset at 1158 when RPV level was restored above the HPCI system low level actuation set point. HPCI is a flow control mode of the normal feedwater systems, and is not an Emergency Core Cooling System. 2. The Core Spray system actuated, but did not discharge to the Reactor Coolant system. The Core Spray system was secured at 1216. 3. Containment and MSIV isolation on reactor vessel low-low water level signal. Nine Mile Point Unit 1 is currently in Hot Shutdown, with reactor vessel water level and pressure maintained within normal bands. Decay heat is being removed via steam to the main condenser using the turbine bypass valves. The offsite grid is stable with no grid restrictions or warnings in effect. The licensee has notified the NRC Resident Inspector. No safety relief valves lifted during the transient. The main steam isolation valves were opened after the isolation signal cleared to facilitate decay heat removal. Offsite power is supplying all plant loads. There was no effect on Unit 2. The licensee notified New York State Department of Environmental Protection and will be issuing a press release.
ENS 5286317 July 2017 21:17:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Declared Due to Loss of Offsite Power

During a rain and lightning storm, plant operators observed arcing from the main transformer bus duct and notified the control room. The decision was made to trip the main generator which resulted in an automatic reactor trip. The plant entered EAL SU.1 as a result of the loss of offsite power for greater than fifteen minutes. Plant safety busses are being supplied by both emergency diesel generators while the licensee inspects the electrical system to determine any damage prior to bringing offsite power back into the facility. Offsite power is available to the facility. No offsite assistance was requested by the licensee. During the trip, all rods inserted into the core. Decay heat is being removed via the atmospheric dump valves with emergency feedwater supplying the steam generators. The main steam isolation valves were manually closed to protect the main condenser. There were no safeties or relief valves that actuated during the plant transient. There is no known primary-to-secondary leakage. Reactor cooling is via natural circulation. All safety equipment is available for the safe shutdown of the plant. The licensee has notified the NRC Resident Inspector, Louisiana Department of Environmental Quality and the local Parish emergency management agencies. Notified DHS SWO, FEMA, DHS NICC, FEMA National Watch Center (email) and Nuclear SSA (email).

  • * * UPDATE ON 7/17/17 AT 2007 EDT FROM MARIA ZAMBER TO DONG PARK * * *

This notification is also made under 10 CFR 50.72(b)(3)(v)(D). This is a non-emergency notification from Waterford 3. On July 17, 2017 at 1606 CDT, the reactor automatically tripped due to a loss of Forced Circulation, which was the result of Loss of Offsite Power (LOOP) to the electrical (safety and non-safety) buses. Both 'A' and 'B' trains of Emergency Diesel Generators (EDGs) started as designed to reenergize the 'A' and 'B' safety buses. The LOOP caused a loss of feedwater pumps, resulting in an automatic actuation of the Emergency Feedwater (EFW) system. Prior to the reactor trip, at 1600 CDT, personnel noticed the isophase bus duct to main transformer 'B' glowing orange due to an unknown reason. Due to this, the main turbine was manually tripped at 1606 CDT. Following the turbine trip, the electrical (safety and non-safety) buses did not transfer to the startup transformers as expected due to an unknown reason. The plant entered the Emergency Operating Procedure for LOOP/Loss of Forced Circulation Recovery. At 1617 CDT, an Unusual Event was declared due to Initiating Condition (IC) SU1 - Loss of all offsite AC power to safety buses (greater than) 15 minutes. All safety systems responded as expected. The plant is currently in mode 3 and stable with the EDGs supplying both safety buses and with EFW feeding and maintaining both steam generators. Offsite power is in the process of being restored. The licensee has notified the NRC Resident Inspector, Louisiana Department of Environmental Quality and the local Parish emergency management agencies.

  • * * UPDATE FROM ADAM TAMPLAIN TO HOWIE CROUCH AT 2203 EDT ON 7/17/17 * * *

The licensee terminated the Notification of Unusual Event at 2056 CDT. The basis for terminating was that offsite power was restored to the safety busses. The licensee has notified Louisiana Department of Environmental Quality, St. John and St. Charles Parishes, Louisiana Homeland Security Emergency Preparedness, and will be notifying the NRC Resident Inspector. Notified IRD (Stapleton), NRR (King), R4DO (Hipschman), DHS SWO, FEMA, DHS NICC, FEMA National Watch Center (email) and Nuclear SSA (email).

  • * * UPDATE FROM SCOTT MEIKLEJOHN TO HOWIE CROUCH AT 1724 EDT ON 7/19/17 * * *

This update is being reported under 10 CFR 50.72(b)(3)(v)(B). During the event discussed in EN# 52863, at 1642 CDT (on July 17, 2017), Condensate Storage Pool (CSP) level lowered to less than 92% resulting in entry to Technical Specification (TS) 3.7.1.3. Level in the CSP was lowered due to feeding from both Steam Generators with EFW. Normal makeup to the CSP was temporarily unavailable due to the LOOP. Filling the CSP commenced at 1815 CDT (on July 17, 2017), and TS 3.7.1.3 was exited on July 18, 2017 at 0039 CDT. The licensee notified the NRC Resident Inspector. Notified R4DO (Hipschman).

  • * * UPDATE FROM SCOTT MEIKLEJOHN TO HOWIE CROUCH AT 1233 EDT ON 9/14/17 * * *

Waterford 3 is retracting a follow up notification made on July 19, 2017 for EN# 52863, concerning the loss of safety function associated with the Condensate Storage Pool (CSP) per 10 CFR 50.72(b)(3)(v)(B). The Condensate Storage Pool was performing its required safety function by providing inventory to the Emergency Feed Water pumps when the required Tech Spec level (T.S. 3.7.1.3) dropped below 92%. The Technical Specification was entered at 1624 (CDT) on July 17, 2017 and exited after filling at 0039 on July 18, 2017. The total allowed outage time allowed by Tech Spec 3.7.1.3 is 10 hours to be in Hot Shutdown if not restored. The Condensate Storage Pool level was restored to greater than 92% prior to exceeding the allowed outage time. Based on level being restored and the Condensate Storage Pool performing its required safety function, 10 CFR 50.72(b)(3)(v)(B) does not apply. Prior to the automatic reactor trip, Condensate Storage Pool level was greater than 92%. The NRC Resident Inspector has been notified of the retraction. Notified R4DO (Groom).