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 Discovered dateReporting criterionTitleEvent description
ENS 5663725 July 2023 13:24:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Envelope Inoperable

The following information was provided by the licensee via email: At 0924 (EDT) on July 25, 2023, it was discovered that both trains of control room air conditioning system were simultaneously inoperable due to an inoperable control room envelope boundary. The boundary was restored at 0925 (EDT) on July 25, 2023. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. There has been no impact to Unit 3 which remains at 100% power.

  • * * RETRACTION ON 09/26//23 AT 1305 EDT FROM PATRICK SIKORSKY TO JOHN RUSSELL * * *

The licensee determined in a subsequent engineering evaluation of the conditions that existed at the time, that the access hatch being open did not have an adverse impact upon the control room emergency ventilation system and the control room envelopes boundary's ability to perform their safety function including: Radiation dose to the occupants did not exceed the licensing basis, design basis accident calculated value. Protection of control room occupants from hazardous chemicals and smoke. Therefore, this condition is not reportable and NRC Event EN56637 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector. Notified R1DO (Lally)

ENS 5635012 February 2023 13:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Control Room Emergency Ventilation System Inoperable

The following information was provided by the licensee via phone call and email: At 0800 on February 12, 2023, it was discovered that both trains of control room emergency ventilation system were simultaneously inoperable due to a safety injection relief valve discharging to a Unit 1 sump. This leakage in conjunction with design basis loss of coolant accident may result in radiological dose exceeding limits to the exclusion area boundary and to the control room, which is common to both Unit 1 and Unit 2. Therefore, this condition is being reported as an eight-hour, nonemergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D) as an 'Unanalyzed Condition and a Condition that Could Have Prevented Fulfillment of a Safety Function.' There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM ROBERT TAYLOR TO DONALD NORWOOD AT 0530 EDT ON 3/17/2023 * * *

Retraction of EN56350, Control Room Emergency Ventilation System Inoperable: Based on subsequent evaluation, it was determined that the control room emergency ventilation system remained operable due to the maximum measured leak rate being within the bounds of the analysis. The maximum measured leak rate of 32,594 cc/hr from the safety injection system did not challenge the calculated maximum engineered safety features leak rate of 45,600 cc/hr and remained within the current dose analysis limits. As such, this was not an unanalyzed condition and did not prevent the fulfillment of a safety function to mitigate the consequences of an accident. The NRC Resident Inspector has been notified. Notified R1DO (Bickett).

ENS 556276 December 2021 16:25:0010 CFR 50.72(b)(3)(iv)(A), System ActuationValid Safety System Actuation

On December 6, 2021, at 1125 hours Eastern Standard Time (EST), during planned maintenance activities, electrical power was lost to the 4160V emergency bus E-3. The power loss to emergency bus E-3 affected both Unit 1 and 2. Emergency Diesel Generator #3 received an automatic start signal but was under clearance for planned maintenance. Emergency bus E-3 was re-energized at 1315 EST hours via offsite power. The loss of power to E3 resulted in Unit 2 Primary Containment Isolation System (PCIS) Group 2 (i.e., Drywell Equipment and Floor Drain, Residual Heat Removal (RHR) Discharge to Radwaste, and RHR Process Sample), Group 3 (i.e., Reactor Water Cleanup), Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems), and Group 10 (i.e., air isolation to the drywell) isolations. The actuations of PCIVs were completed and the affected equipment responded as designed. Per design, no Unit 1 safety system group isolations or actuations occurred. Other Unit 2 actuations included the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start signal to the Standby Gas Treatment (SGT) System trains A and B and the Control Room Emergency Ventilation System (CREV). Systems functioned as designed. Safety systems functioned as designed following the de-energization of bus E-3. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of PCIS on Unit 2 and an automatic start signal to Emergency Diesel Generator #3. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Except for the Emergency Diesel Generator, which is out of service for planned maintenance, all equipment has been returned to its normal alignment.

  • * * UPDATE FROM JJ STRNAD TO THOMAS KENDZIA AT 2028 EST ON DECEMBER 6, 2021 * * *

The loss of power to E3 resulted in Unit 1 Primary Containment Isolation System (PCIS) Group 6 (i.e., Containment Atmosphere Control/Dilution, Containment Atmosphere Monitoring, and Post Accident Sampling Systems). Other Unit 1 actuations included the Reactor Building Ventilation System isolation (i.e., Secondary Containment isolation), and the automatic start signal to the Standby Gas Treatment (SGT) System trains A and B and the Control Room Emergency Ventilation System (CREV). Systems functioned as designed. Safety systems functioned as designed following the de-energization of bus E-3. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of PCIS on Unit 1. All Unit 1 equipment was returned to its normal alignment. The NRC Resident will be notified. Notified R2DO (Miller).

ENS 552871 April 2021 18:02:0010 CFR 50.73(a)(1), Submit an LER60-Day Telephonic Notification of Invalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of the 2A Reactor Protection System (RPS). On April 1, 2021, at 1302 (CDT), Browns Ferry Unit 2, 2A RPS (Motor Generator) MG set tripped causing a half scram. Unit 2 experienced an unexpected trip of the 2A RPS MG Set that resulted in automatic Primary Containment Isolation System (PCIS) Group 2, 3, 6, and 8 isolations and Trains A, B, and C Standby Gas Treatment (SGT) and Train A Control Room Emergency Ventilation (CREV) starts. At the time of the event, Unit 2 was in a refueling outage and the rods were already fully inserted. All systems responded as expected. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. Based on the troubleshooting conducted, the cause was determined to be a loose wiring connection in the motor circuit. The lugs were replaced with ring lugs. Operations reset the 2A RPS Half Scram and PCIS in accordance with 2-AOI-99-1 on April 1, 2021, at 1324 CDT thus correcting the condition and returning RPS to service. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1683358. The NRC Resident Inspector has been notified of this event.
ENS 549326 August 2020 22:49:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of an Invalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On August 6, 2020, at approximately 1749 CDT, Browns Ferry Nuclear Plant (BFN), Unit 2 experienced a loss of Reactor Protection System (RPS) Bus 2A. Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolated in response to this event. The PCIS isolations caused the initiation of Standby Gas Treatment (SBGT) trains A, B, and C, and Control Room Emergency Ventilation (CREV) subsystem A. Unit 2 declared RCS leakage detection instrumentation inoperable and entered TS LCO 3.4.5 condition A, B, and D with required action D.1 to enter LCO 3.0.3 immediately. Unit 2 entered TS LCO 3.0.3 with required actions to be in Mode 2 within 10 hours, Mode 3 within 13 hours, and Mode 4 within 37 hours. Upon investigation, it was discovered that an age-related overheating condition resulted in the failure of the 2A RPS Motor Generator (MG) set, causing the feeder beaker from the 2A 480v Remote Motor-Operated Valve distribution board to trip. On August 6, 2020, at approximately 1808 CDT, Operations personnel commenced restoration of Unit 2 to normal after transferring 2A RPS to its alternate power supply. The 2A RPS MG Set drive motor was replaced on August 24, 2020. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel (RV) Low Water Level or Drywell High Pressure. Plant conditions which initiate PCIS Group 3 actuations are RV Low Water Level or Reactor Water Cleanup Area High Temperature. Plant conditions which initiate PCIS Group 6 actuations are RV Low Water Level, High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation. Plant conditions which initiate PCIS Group 8 actuations are Reactor Vessel (RV) Low Water Level or Drywell High Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. All affected safety systems responded as expected. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1628707. The NRC Resident Inspector has been notified of this event.
ENS 547385 June 2020 07:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 

EN Revision Imported Date : 10/6/2020 CONTROL ROOM BOUNDARY DOOR FAILURE On June 5, 2020, at 0320 (EDT) a loss of control room envelope (CRE) was declared inoperable due to failure of door 204-36-007. The door was repaired at 0322 (EDT), restoring the CRE to operable. The NRC Resident Inspector, state, and local authorities were notified.

  • * * RETRACTION ON 07/09/2020 AT 1443 EDT FROM GERALD A. BAKER TO OSSY FONT * * *

The purpose of this call is to retract a report made on June 5, 2020, NRC Event Number EN54738. NRC Event Report number EN54738 describes a condition at Millstone Power Station Unit 2 (MPS2) in which a control room envelope boundary door was discovered to not be able to fully close due to the latching mechanism being stuck in the extended position. The condition was reported to the NRC pursuant to 10 CFR 50.72(b)(3)(v)(D) via an 8 hour prompt report as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. Upon further review, MPS2 determined that there was no loss of safety function. An engineering evaluation determined that even with the control room boundary door unable to be fully closed due to the latching mechanism being stuck in, the extended position, control room air in-leakage would not have been sufficient to prevent the control room emergency ventilation system from performing its safety function. Therefore, this condition is not reportable and NRC Event Number EN54738 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector. Notified R1DO (Dimitriadis).

  • * * UPDATE FROM MICHAEL GAGNON TO BRIAN P. SMITH AT 1444 EDT ON 10/01/2020 * * *

The purpose of this call is to provide an update to the retraction for a report made on June 5, 2020, NRC Event Number EN54738. The retraction being updated was made on 7/9/2020 at 1443 hours. NRC Event Report number EN54738 describes a condition at Millstone Power Station Unit 2 (MPS2) in which a control room envelope boundary door was discovered to not be able to fully close due to the latching mechanism being stuck in the extended position. The condition was reported to the NRC pursuant to 10 CFR 50.72(b)(3)(v)(D) via an 8 hour prompt report as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident (the Control Room Envelope). A subsequent engineering evaluation of the conditions that existed at the time, determined that the inability of the control room boundary door to fully close due to the latching mechanism being stuck in the extended position did not have an adverse impact upon the ability of the CRE to perform its safety function. The CRE remained operable throughout this event, and the ventilation system would have performed its safety function. Therefore, this condition is not reportable and NRC Event Number EN54738 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector. Notified R1DO (Lally).

ENS 546979 March 2020 01:21:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On March 8, 2020, at approximately 2021 CDT, Browns Ferry Nuclear Plant Unit 2 experienced an unexpected loss of the 2A Reactor Protection System (RPS). This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and the initiation of Standby Gas Treatment Trains A and B, and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The RPS MG Set trip was believed to have been caused by an intermittent short across a spike suppressor, which led to a loss of generator output signal to a voltage regulator. The affected components have been replaced. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1593265. The NRC Resident Inspector has been notified of this event.
ENS 5466614 April 2020 21:45:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation System InoperableOn April 14, 2020 at 1645 CDT, the Control Room Emergency Ventilation Air Conditioning (CREV AC) system was declared inoperable when the electrical feed breaker to the Refrigeration Compressor Unit (RCU) was found in a tripped condition. As a result, both units entered Technical Specification 3.7.5 Condition A. Investigation is in progress to determine the cause and corrective actions of the RCU feed breaker trip. The CREV AC system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions. This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D) because the CREV system is a single train system, and loss of the CREV AC could impact the plant's ability to mitigate the consequences of an accident.
ENS 5439116 November 2019 04:53:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentTemporary Loss of Control Room Envelope BoundaryAt 2353 EST on November 15, 2019, a Main Control Room (MCR) alarm was received for low control room positive pressure. At 2355 EST, a Control Room Envelope (CRE) door was found ajar and immediately closed. Technical Specification 3.7.10 Control Room Emergency Ventilation System (CREVS) was declared not met for both trains. Watts Bar Unit 1 and Unit 2 entered Condition B. At 2355 EST on November 15, 2019, the alarm cleared, CREVS was declared operable and LCO 3.7.10 Condition B was exited for both units. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. See similar EN #54390. The licensee has taken compensatory measures while investigating the cause.
ENS 5439016 November 2019 03:34:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentTemporary Loss of Control Room Envelope BoundaryAt 2234 Eastern Standard Time (EST) on November 15, 2019, a Main Control Room (MCR) alarm was received for low control room positive pressure. At 2236 EST, a Control Room Envelope (CRE) door was found ajar and immediately closed. Technical Specification 3.7.10 Control Room Emergency Ventilation System (CREVS) was declared not met for both trains. Watts Bar Unit 1 and Unit 2 entered Condition B. At 2236 EST on November 15, 2019, the alarm cleared, CREVS was declared operable and LCO 3.7.10 Condition B was exited for both units. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5435527 October 2019 21:05:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentWater Found in Control Room Emergency Ventilation Air Filtration UnitOn October 27, 2019, at 1605 CDT, the Control Room Emergency Ventilation (CREV) was declared inoperable due to finding water in the system's Air Filtration Unit (AFU) filter enclosure. Technical Specification 3.7.4, Condition A, was entered which requires the CREV system to be restored to an operable status in seven days. No other systems were out of service at the time this was declared inoperable. The CREV system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions. This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D), "Event or Condition That Could Have Prevented Fulfillment of a Safety Function," because the CREV system is a single train system required to mitigate the consequences of an accident. The licensee has notified the NRC Resident Inspector.
ENS 5434129 December 2018 07:20:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On December 29, 2018, at approximately 0220 Central Standard Time (CST), Browns Ferry Nuclear Plant (BFN), Unit 3 experienced an unexpected loss of power to the 3A Reactor Protection System (RPS) Bus due to the trip of the 3A RPS motor generator (MG) set. This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and initiation of Standby Gas Treatment Trains A, B, and C and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected. This event is being reported as a late 60 day non-emergency notification. This missed notification was identified on August 23, 2019. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The cause of the trip of the RPS MG Set was a failure of the motor winding insulation of all three phases. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Reports 1478564 and 1543534. The NRC Resident Inspector has been notified of this event.
ENS 5433220 August 2019 16:33:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid Specified System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On August 20, 2019, at approximately 1133 hours Central Daylight Time (CDT), Browns Ferry Nuclear Plant (BFN), Unit 2 experienced an unexpected loss of the 2A Reactor Protection System (RPS). This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and initiation of Standby Gas Treatment Trains A, B, and C and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The cause of the RPS MG Set trip was dirty potentiometer windings on an Over Voltage Relay. The dirt prevented the potentiometer's wiper from contacting its windings, resulting in erratic setpoint values. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Reports 1542603, 1542608, and 1542569. The NRC Resident Inspector has been notified of this event.
ENS 5430031 July 2019 21:50:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification Due to an Invalid Actuation of a Containment Isolation SignalThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On July 31, 2019, at approximately 1650 hours Central Daylight Time (CDT), Browns Ferry Nuclear Plant (BFN), Unit 1 experienced a Primary Containment Isolation System (PCIS) Group 6 isolation during performance of surveillance procedure 1-SR-3.3.6.2.3(A), Reactor/Refueling Zone Ventilation Radiation Monitor 1-RM-90-140/142 Calibration and Functional Test. The Group 6 isolation caused the initiation of Standby Gas Treatment (SBGT) Trains A, B, and C, and Control Room Emergency Ventilation (CREV) subsystem B. Unit 1 H2O2 Analyzer and Drywell Radiation Monitor CAM, 1-RM-90-256, were declared Inoperable and Technical Specifications (TS) Limiting Condition for Operation (LCO) 3.4.5 Condition B was entered. All affected safety systems responded as expected. Plant conditions which initiate PCIS Group 6 actuations are Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. This condition was the result of two cleared fuses in the alarm logic. The apparent cause is a ground fault on the A6 Open Drain Input/Output Module. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Acton Program as Condition Report 1537358. The NRC Resident Inspector has been notified of this event.
ENS 5402123 April 2019 06:32:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentTemporary Loss of Control Room Envelope BoundaryAt 0232 EDT on April 23, 2019, a Main Control Room (MCR) alarm was received for low control room positive pressure. At 0233 EDT, a Control Room Envelope (CRE) door was found ajar and immediately closed. Technical Specification 3.7.10 Control Room Emergency Ventilation System (CREVS) was declared not met for both trains. Watts Bar Unit 1 entered Condition B. Watts Bar Unit 2 was not performing movement of irradiated fuel assemblies and did not meet the APPLICABILITY for CREVS per LCO 3.7.10. At 0233 EDT on April 23, 2019, the alarm cleared, CREVS was declared operable and LCO 3.7.10 Condition B was exited. The safety function of the CRE boundary is to ensure the in-leakage of unfiltered air into the CRE will not exceed the in-leakage assumed in the licensing basis analysis of Design Basis Accident (DBA) consequences to CRE occupants. From 0232 EDT to 0233 EDT, (Watts Bar Nuclear) WBN was unable to validate that CREVS could fulfill its required Safety Function. This event is being reported pursuant to 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified.
ENS 5401622 April 2019 03:07:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Trip and Specified System Actuation

At 2307 EDT on April 21, 2019, in Mode 1 at approximately 100 percent reactor power, Unit 1 automatically tripped due to a Main Turbine Trip. The Main Turbine Trip was a result of two out of three level instruments sensing a false high reactor water level. All control rods inserted as expected during the scram. Safety Relief Valves G and K lifted per design. The same level instruments that failed also tripped both Reactor Feed Pumps. As a result, reactor water level dropped below the Low Level 1 and 2 actuation setpoints. Per design, the Low Level 1 signal resulted in Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sampling isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations. The Low Level 2 signals resulted in Group 3 (i.e. Reactor Water Cleanup) isolation, a secondary containment isolation signal, and an auto start of Standby Gas Treatment and Control Room Emergency Ventilation. Also, the Low Level 2 resulted in (high pressure coolant injection) HPCI and (reactor core isolation cooling system) RCIC automatically starting and injecting into the vessel. All systems responded as designed. This event is being reported in accordance with 10 CFR 50.72(b)(2)(iv)(B) for RPS actuation and 10 CFR 50.72(b)(3)(iv)(A) as an event that results in valid actuations of the Primary Containment Isolation System. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. Decay heat is currently being removed via the turbine bypass valves. Condensate and feed water are maintaining water level. The reactor is still at saturation temperature and 475 psi, lowering slowly. The reactor is still in a normal electrical lineup. There was no impact to Unit 2 as a result of this event.

  • * * UPDATE ON 04/22/19 AT 0220 EDT FROM ALAN SCHULTZ TO JEFFREY WHITED * * *

The licensee updated the event report to include a 4-Hr Non-Emergency Notification in accordance with 10 CFR 50.72(b)(2)(iv)(A) for Emergency Core Cooling System, HPCI, Discharge to the Reactor Coolant System. Notified R2DO (Dickson), NRR EO (Miller) and IR MOC (Gott).

ENS 5375225 November 2018 01:15:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentEn Revision Imported Date 1/22/2019

EN Revision Text: LOSS OF CONTROL ROOM ENVELOPE DUE TO DOOR FAILURE On 11/24/18 at 2015 EST, a loss of Control Room Envelope (CRE) was declared due to failure of the control room boundary door, 204-36-008. (Abnormal Operating Procedure 8588A Mitigating Actions for Control Boundary Breach was implemented). The door was repaired at 2030 EST, restoring CRE to operable (status). A mechanical failure of the control room door latch prevented the door from closing. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 01/18/19 AT 1457 EST FROM GARY CLOSIUS TO JEFFREY WHITED * * *

The purpose of this call is to retract a report made on November 25, 2018, NRC Event Number EN53752. NRC Event Report number EN53752 describes a condition at Millstone Power Station Unit 2 (MPS2) in which a control room envelope boundary door was discovered to not be able to fully close due to the latching mechanism being stuck in the extended position. The condition was reported to the NRC pursuant to 10 CFR 50.72(b)(3)(v)(D) via an 8-hour prompt report as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. Upon further review, MPS2 determined that there was no loss of safety function. An engineering evaluation determined that even with the control room boundary door unable to be fully closed due to the latching mechanism being stuck in the extended position, control room air in-leakage would not have been sufficient to prevent the control room emergency ventilation system from performing its safety function. Therefore, this condition is not reportable and NRC Event Number EN53752 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector. Notified the R1DO (Carfang).

ENS 5366116 August 2018 05:00:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On August 16, 2018, at approximately 1736 CDT, Browns Ferry Nuclear Plant (BFN), Unit 2 experienced an unexpected loss of the 2B Reactor Protection System (RPS). This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and initiation of Standby Gas Treatment Trains A, B, and C and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected with the exception of the Unit 1 Refuel Zone Supply Fan Outboard Isolation Damper, 1-FCO-64-5, that failed to indicate closed position. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The cause of the RPS MG (Motor Generator) Set trip was a failed (shorted) operating coil associated with the 480 VAC motor starter inside the control box. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Reports 1440047 and 1440050. The NRC Resident Inspector has been notified of this event.
ENS 536579 October 2018 05:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation Ac System InoperableOn October 9, 2018 at 2002 CDT the Control Room Emergency Ventilation Air Condition (CREV AC) system was in the process of being returned to service following maintenance. During the return to service, the end bell on the CREV AC Condenser developed a significant leak requiring isolation. No work was performed on the CREV AC Condenser during the work window. The CREV AC system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions. This notification is being made in accordance with 10CFR50.72(b)(3)(v)(D), "Event or Condition That Could Have Prevented Fulfillment of a Safety Function " because the CREV system is a single train system required to mitigate the consequences of an accident. The NRC Resident Inspector has been notified.
ENS 5359311 September 2018 04:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation System InoperableAt 0113 EDT on September 11, 2018, it was discovered both trains of CREVS (control room emergency ventilation system) were simultaneously inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The door to the main control room habitability zone from the turbine building was left open and unattended for about a minute, breaking the pressure boundary in the room, resulting in an alarm. The door was closed, clearing the alarm and the CREVS was considered operable.
ENS 5329126 March 2018 22:39:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentTemporary Loss of Control Room Envelope BoundaryAt 1839 Eastern Daylight Time (EDT) on March 26, 2018, a Main Control Room (MCR) alarm was received for low control room positive pressure. At 1840 EDT, a Control Room Envelope (CRE) door was found ajar and immediately closed. Technical Specification 3.7.10, Control Room Emergency Ventilation System (CREVS), was declared not met for both trains and Condition B entered. At 1840 EDT on March 26, 2018, the alarm cleared, CREVS was declared operable and LCO (Limiting Condition for Operation) 3.7.10, Condition B was exited. The safety function of the CRE boundary is to ensure the in-leakage of unfiltered air into the CRE will not exceed the in-leakage assumed in the licensing basis analysis of Design Basis Accident (DBA) consequences to CRE occupants. From 1839 EDT to 1840 EDT, WBN (Watts Bar Nuclear) was unable to validate that CREVS could fulfill its required Safety Function. This event is being reported pursuant to 10 CFR 50.72(b)(3)(v)(D). A watch has been posted at the door to prevent recurrence. The NRC Resident Inspector has been notified.
ENS 5328826 March 2018 14:58:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentTemporary Loss of Control Room Envelope BoundaryAt 1058 Eastern Daylight Time (EDT) on March 26, 2018, a Main Control Room (MCR) alarm was received for low control room positive pressure. At 1100 EDT, a Control Room Envelope (CRE) door was found ajar and immediately closed. Technical Specification 3.7.10, Control Room Emergency Ventilation System (CREVS), was declared not met for both trains and Condition B entered. At 1100 EDT on March 26, 2018, the alarm cleared, CREVS was declared operable and LCO (Limiting Condition for Operation) 3.7.10, Condition B was exited. The safety function of the CRE boundary is to ensure the in-leakage of unfiltered air into the CRE will not exceed the in-leakage assumed in the licensing basis analysis of Design Basis Accident (DBA) consequences to CRE occupants. From 1058 EDT to 1100 EDT, WBN (Watts Bar Nuclear) was unable to validate that CREVS could fulfill its required Safety Function. This event is being reported pursuant to 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified.
ENS 5307010 January 2017 09:00:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On September 15, 2017, during a TVA (Tennessee Valley Authority) review of Operations logs, it was determined that a reportable condition occurred in January 2017 but no NRC report had been made. On January 10, 2017, at 0300 Central Standard Time (CST), Browns Ferry Nuclear Plant, Unit 3, received Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolation signals. The Group 2, 3, 6, and 8 isolations caused the initiation of all three trains of the Standby Gas Treatment (SBGT) system and Control Room Emergency Ventilation (CREV) subsystem 'A.' At 0311 CST, Operations personnel discovered that the 3A1 RPS circuit protector had tripped on undervoltage. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywall Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywall Pressure. At the time of the event, these conditions did not exist; therefore the actuation of the PCIS was invalid. All affected equipment responded as designed. This condition was the result of an undervoltage condition on the 3A1 circuit protector. During trouble shooting, the undervoltage setpoints were found to be 116 VAC and 115 VAC, when the normal as left acceptance band is 109.7 VAC to 111.3 VAC. The 3A RPS protective relays had been previously replaced in September 2016. The most likely cause of the undervoltage condition in these relays is infant mortality. The NRC Resident Inspector has been notified of this event.
ENS 530513 November 2017 14:45:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentStation Vent Radiation Monitor Efficiency Factor Non-Conservative

On 11/3/17, with the unit operating in Mode 1 at approximately 100 percent power, an issue was identified with the Station Vent Radiation Monitors. The noble gas channels utilize an efficiency factor for isotope Kr-85 instead of the required Xe-133. For the normal range radiation monitors, the efficiency factor is non-conservative, resulting in both monitors being declared inoperable at 1045 hours EDT. As a result, the Normal Control Room Ventilation System was shut down and isolated, and the Control Room Emergency Ventilation System started in accordance with Technical Specification Required Actions at 1122 hours. The inoperability of both Station Vent Normal Range Radiation Monitors represents a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system needed to mitigate the consequences of an accident. The Station Vent Accident Range Monitors also utilize an efficiency factor for Kr-85 instead of Xe-133, but for the Accident Range Monitors the efficiency factor is conservative. Because alternate means exist to determine release rate, which include use of grab samples and field surveys, this degraded capability does not represent a major loss of emergency assessment capability. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM NICK DOWNING TO DONALD NORWOOD AT 0927 EST ON 12/14/2017 * * *

On 11/3/2017, the efficiency factors for the Station Vent Normal and Accident Range Radiation Monitors were revised to the proper setting for the required isotope, the normal range monitors were declared Operable, and the Control Room Normal Ventilation System was returned to service. An evaluation of the issue with the Station Vent Normal Range Radiation Monitors was performed, which determined the Control Room Ventilation isolation setpoint is well below the point at which the dose to the Control Room Operators would exceed General Design Criteria (GDC) limits following a Design Bases Accident. The error introduced from using an incorrect efficiency value did not challenge the margin to the GDC limits; therefore, the Station Vent Normal Range Monitors remained operable, and this issue did not prevent the monitors from fulfilling their safety function to mitigate the consequences of an accident.

The NRC Resident Inspector has been notified. Notified R3DO (Stone).

ENS 5304430 October 2017 13:42:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentTemporary Loss of Control Room Envelope BoundaryAt 0942 Eastern Daylight Time (EDT) on October 30, 2017, a Main Control Room (MCR) alarm was received for low control room positive pressure. At 0943 EDT, a Control Room Envelope (CRE) door was found ajar and immediately closed. Technical Specification 3.7.10 Control Room Emergency Ventilation System (CREVS) was declared not met for both trains and Condition B entered. At 0945 EDT the alarm cleared, CREVS was declared operable and LCO 3.7.10, Condition B was exited. The safety function of the CRE boundary is to ensure the in-leakage of unfiltered air into the CRE will not exceed the in-leakage assumed in the licensing basis analysis of Design Basis Accident (DBA) consequences to CRE occupants. From 0942 EDT to 0943 EDT WBN (Watts Bar Nuclear) was unable to validate that CREVS could fulfill its required Safety Function. This event is being reported pursuant to 10 CFR 50.72(b)(3)(v)(D). NRC Resident Inspector has been notified.
ENS 5298421 September 2017 22:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation Ac System InoperableOn September 21, 2017 at 1730 (CDT) the Control Room Emergency Ventilation Air Condition (CREV AC) system was declared inoperable due a refrigerant leak from the air conditioning compressor. As a result, Technical Specification 3.7.5 Condition A was entered for Units One and Two. The CREV AC system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions. This notification is being made in accordance with 10CFR50.72(b)(3)(v)(D) because the CREV system is a single train system. The loss of CREV AC could impact the plant's ability to mitigate the consequences of an accident. The NRC Resident Inspector has been notified.
ENS 527885 June 2017 17:52:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Air Conditioning and Emergency Ventilation Systems InoperableAt 1352 hours Eastern Daylight Time (EDT) on June 5, 2017, during control building damper inspection activities, a control building instrument air line was disconnected. This resulted in the inoperability of the three Control Room Air Conditioning subsystems required by Technical Specification (TS) 3.7.4, 'Control Room Air Conditioning (AC) System', and the two Control Room Emergency Ventilation (CREV) subsystems required by TS 3.7.3, 'Control Room Emergency Ventilation (CREV) System. As a result, this condition could have prevented the fulfillment of the safety function for these systems. Control Room AC and CREV system operability was restored at 1407 hours with restoration of control building instrument air. Because Brunswick has a shared control room, this report applies to both Units 1 and 2 and is being made in accordance with 10 CFR 50.72(b)(3)(v)(D), as a condition that at the time of discovery could have prevented fulfillment of the safety function of systems that are needed to mitigate the consequences of an accident. This event did not impact public health and safety. INITIAL SAFETY SIGNIFICANCE EVALUATION: The safety significance of this event is considered minimal. The condition existed for approximately 15 minutes. Plant staff took immediate actions to return the equipment to service. For the brief time the Control Room AC and CREV systems were inoperable, performance of plant personnel and equipment in the Control Room was not adversely affected. The maximum Control Room back panel temperature during this event was approximately 70 degrees F. CORRECTIVE ACTIONS: Control Room AC and CREV system operability was restored at 1407 hours with restoration of control building instrument air. During subsequent investigation of the event, it was determined that at approximately 0930 hours on June 5, 2017, both subsystems of CREV were similarity rendered inoperable due to isolation of control building instrument air. Control Room AC was not affected. Operability of CREV was restored at approximately 1009 hours. This loss of the CREV system was not apparent to Operations personnel at the time of the event. The licensee has notified the NRC Resident Inspector.
ENS 5231524 October 2016 00:08:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation Fan Inoperable Due to Elevated VibrationAt 1908 CDT on 10/23/16, elevated vibration readings were identified on Cooper Nuclear Station (CNS), Control Room Emergency Filter System (CREFS) supply fan A. Vibration readings were evaluated by Engineering and were determined to be indicative of bearing failure on supply fan A. The Control Room declared CREFS inoperable and entered LCO 3.7.4, Condition A, which requires restoration of CREFS to operable status in 7 days. Repair activities have been initiated for this condition. The plant is currently in Mode 5, with refueling activities and OPDRVs (Operation with Potential to Drain Reactor Vessel) in progress. CNS is not currently in the mode of applicability for a USAR defined accident. This condition is being conservatively reported under 10 CFR 50.72(b)(3)(v)(D) as a single train safety system that is required to be OPERABLE during situations under which significant radioactive releases can be postulated. The NRC Resident Inspector has been notified.
ENS 5225319 September 2016 20:50:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation Charcoal Not Meeting Acceptance Criteria

At 1550 (CDT) on September 19, 2016, Dresden received the Methyl Iodide Penetration test results for the Control Room Emergency Ventilation (CREVS) charcoal. The test results did not meet technical specification acceptance criteria. This results in the inoperability of CREVS. CREVS is a single train system and therefore is reportable per 10CFR50.72(b)(3)(v)(D). The Air Filtration Unit (AFU) is required to operate during a design basis accident to maintain Main Control Room habitability. This places unit 2 and unit 3 in a 7 day LCORA (Limiting Condition of Operation Required Action) per Tech Spec 3.7.4 Required Action A.1. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 1635 EDT ON 03/23/17 FROM HENRY WATERS TO S. SANDIN * * *

The licensee is retracting this report based on the following: The purpose of this notification is to retract ENS notification 52253 made on September 19th, 2016, for Dresden Nuclear Power Station. After further evaluation and testing, it has been determined that the Control Room Emergency Ventilation System (CREVS) charcoal would have fulfilled its safety function given the Methyl Iodide Penetration test results. The initial tests were performed with a 2 inch bed depth due to a difference in batches used in each charcoal filter, but testing at a 4 inch bed depth is the correct testing methodology for Dresden's configuration. At a 4 inch bed depth, the test results met the Technical Specification acceptance criteria with significant margin. Therefore, this event does not meet the criteria of 10 CFR 50.72(b)(3)(v)(D) and the ENS report is being retracted. The NRC Resident Inspector has been notified. Notified R3DO (Orlikowski).

ENS 5217211 August 2016 14:15:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Control Room Emergency Ventilation System Declared InoperableAt 1015 (EDT) on August 11, 2016, it was discovered that a Fire Protection damper associated with the Control Room Emergency Ventilation System had closed unexpectedly due to component failure. The closure rendered both trains of the Control Room Emergency Ventilation System (CREVS) inoperable requiring both Unit 1 and 2 to enter Technical Specification Limiting Condition of Operation (LCO) 3.7.10 Condition G. Condition G requires immediate entry into LCO 3.0.3. At 1159 on August 11, 2016, actions were taken to block the deficient damper in the open position restoring both trains of CREVS to a fully operable condition and allowing exit of LCO 3.0.3 and 3.7.10 Condition G. The purpose of CREVS is to provide a protected environment from which occupants can control the (respective) unit following an uncontrolled release of radioactivity, hazardous chemicals, or smoke. In the event of a design basis accident, emergency ventilation components realign to supply filtered air and to pressurize the Control Room Envelop (CRE). While the damper was closed both trains of CREVS were incapable of supplying the Relay Room as well as the Technical Support Center and its associated support spaces. These locations constitute part of the CRE, therefore both trains of CREVS were inoperable. Both trains of CREVS being inoperable affected the habitability of the TSC where the assessment capability of the facility for all emergencies was adversely effected. The NRC Resident Inspector has been notified.
ENS 5212726 July 2016 17:52:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation System InoperableOn July 26, 2016 at 1252 hours (CDT), the Control Room Emergency Ventilation (CREV) system was declared inoperable due to a toxic gas analyzer spurious alarm which resulted in the 'B' Air Filtration Unit (AFU) being inadvertently isolated. In this condition, Control Room Emergency Ventilation (CREV) system cannot be guaranteed to achieve required design flow rate. Tech Spec 3.7.4, Condition A was entered which requires the CREV system to be restored to an operable status in seven (7) days. The CREV system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions as well as protection of the operators from a high dose environment assumed during a design basis accident. This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D), 'Event or Condition That Could Have Prevented Fulfillment of a Safety Function,' because the CREV system is a single train system required to mitigate the consequences of an accident. The NRC Resident Inspector has been notified.
ENS 520519 May 2016 10:26:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of Primary Containment Isolation Valves (Pcivs)This 60-day telephone notification is being made in lieu of a Licensee Event Report (LER) submittal in accordance with 10 CFR 50.73(a)(1) to notify the NRC of an invalid actuation of PCIVs, reportable under 10 CFR 50.73(a)(2)(iv)(A). On May 9, 2016, at 0626 Eastern Daylight Time (EDT), an unexpected trip of the Unit 1 Reactor Protection System (RPS) Bus A occurred, resulting in closure of several PCIVs on loss of power, per design. In addition, the following actuations also occurred per design: - insertion of a half reactor scram signal. - initiation of the standby gas treatment (SBGT) system . - isolation of the secondary containment. - initiation of the control room emergency ventilation (CREV) system smoke and radiation mode. - trip of the operating reactor water cleanup system (RWCU) pump due to closure of its isolation valve. The event resulted from a failed relay coil in the drive motor run logic for the RPS power supply motor-generator (MG) set. The failed relay blew a fuse, which de-energized the RPS drive motor contactor and MG set. This resulted in de-energizing the RPS power supply in the 'A' channel and produced the actuations listed previously, per design. Affected systems and components were restored to their normal configurations by 1000 EDT on May 9, 2016. Since no plant or process conditions existed that required the PCIV isolations (e.g., high drywell pressure or low reactor water level), this event is being reported per 10 CFR 50.73(a)(1) as an invalid actuation. This issue has been entered into the site Corrective Action Program (CR 2027653) for evaluation and implementation of further corrective actions. This event did not result in any adverse impact to the health and safety of the public. The NRC Resident Inspector has been notified.
ENS 517694 March 2016 17:35:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentEmergency Diesel Generator Declared InoperableOn March 3, 2016, during restoration of power to a Unit 1 electrical bus following planned work, an error in the restoration sequence resulted in an invalid auto-start signal to Emergency Diesel Generators (EDGs) 1, 2, 3 and 4. EDG 1 was out-of-service under clearance to support Unit 1 refueling outage modifications and maintenance and, as such, did not start. EDGs 2 and 4 auto-started as designed. However, EDG 3 failed to auto-start. At 1235 EST on March 4, 2016, EDG 3 was declared inoperable when troubleshooting identified a broken fuse block connection in the EDG 3 auto-start circuitry, which would have prevented a Technical Specification (TS) required auto-start of EDG 3. This condition concurrent with EDG 1 out-of-service would have precluded emergency power supply to emergency busses needed to mitigate the consequences of an accident. Technical Specification 3.8.1, Required Action D.3, requires declaring the required features supported by the inoperable EDG 3 inoperable when the redundant required features are inoperable. As a result, both required Conventional Service Water (CSW) pumps were declared inoperable at 1635 EST on March 4, 2016. This also required declaring both Control Building Instrument Air Compressors inoperable. As a result, both Control Room Emergency Ventilation (CREV) subsystems and all three Control Building Air Conditioners were declared inoperable at 1635 EST on March 4, 2016. The above conditions are reportable under 10 CFR 50.72(b)(3)(v)(D), as an event or condition that could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident. This event did not result in any adverse impact to the health and safety of the public. The risk significance of this event is considered to be low. Both EDG 2 and EDG 4 were available and protected, along with the supplemental diesel generator and offsite electrical sources. Except for the periods of time for repair activities and post-repair testing, EDG 3 remained available via manual start. Actions were taken to protect other redundant safety systems and additional defense-in-depth was provided. EDG 3 was restored to Operable status March 4, 2016 at 1834 EST and this has restored the safety functions of the above mentioned systems. The licensee notified the NRC Resident Inspector.
ENS 517125 February 2016 06:09:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentExcessive Control Room In-Leakage Identified

On February 5, 2015 at 0109 EST, the Control Room Emergency Ventilation System (CREVS) was declared inoperable due to a higher than allowed identified in-leakage rate for the Control Room Envelope (CRE) when in the Normal Operating Mode. Unit 1 remains at 100 percent power and Unit 2 remains in Mode 3 for an unrelated planned maintenance outage. Unit 1 and Unit 2 share a common CRE. This in-leakage was detected during additional testing following the event documented in EN #51584. At the time of discovery, there is a reasonable expectation this condition could prevent the fulfillment of the safety function of a system that is required to mitigate the consequences of an accident, thus satisfying the reporting criteria for 10CFR50.72(b)(3)(v)(D). Actions to implement mitigating actions were immediately initiated in accordance with Technical Specification 3.7.10. CREVS has been placed in Recirculation Ventilation Mode, isolating the control room from outside air. The NRC Senior Resident Inspector has been notified of the condition.

  • * * RETRACTION FROM DAVID HELD TO VINCENT KLCO AT 1411 EDT ON 4/4/16 * * *

Following the 8-hour 10 CFR 50.72 notification made on 02/05/2016 (EN 51712) regarding the Control Room Emergency Ventilation System (CREVS) inoperability, further engineering evaluation has determined the identified in-leakage does not result in exceeding the design criteria for dose to the control room personnel. Therefore the degraded Control Room Emergency Ventilation System remained operable with the identified air in-leakage as determined by the Control Room Envelope Habitability Program. As such, the safety function was never lost and the event notification is being retracted as it is not reportable pursuant to 10 CFR 50.72(b)(3)(v)(D). The NRC Resident has been notified. Notified the R1DO (Jackson).

ENS 515897 December 2015 14:25:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation System InoperableOn December 07, 2015, at 0825 hours (CST), the Control Room Emergency Ventilation (CREV) system was declared inoperable due to the Air Handling Unit (AHU) tripping upon attempting to swap from the non-safety related CR HVAC. Swapping was being performed to allow maintenance on the non-safety related system. Technical Specification 3.7.4, Condition A, was entered which requires the CREV system to be restored to an operable status in seven (7) days. Additionally, Technical Specification 3.7.5, Condition A, was entered which requires CREV AC to be restored to an operable status in 30 days. This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D), 'Event or Condition That Could Have Prevented Fulfillment of a Safety Function,' because the CREV system is a single train system required to mitigate the consequences of an accident. The NRC Resident Inspector was notified. The Licensee notified the Illinois Emergency Management Association.
ENS 515844 December 2015 02:07:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentExcessive Control Room In-Leakage Identified

On December 3, 2015 at 2107 (EST), the Control Room Emergency Ventilation System (CREVS) was declared inoperable due to a higher than allowed identified in-leakage rate for the Control Room Envelope (CRE) when in the Normal Operating Mode. Both Unit 1 & Unit 2 remain at 100 percent power and they share a common CRE. At the time of discovery, there is a reasonable expectation this condition could prevent the fulfillment of the safety function of a system that is required to mitigate the consequences of an accident, thus satisfying the reporting criteria for 10CFR50.72(b)(3)(v)(D). Actions to implement mitigating actions were immediately initiated in accordance with Technical Specification 3.7.10. CREVS has been placed in Recirculation Ventilation Mode, isolating the control room from outside air. The NRC Senior Resident Inspector has been notified of the condition.

  • * * RETRACTION ON 1/7/16 AT 1110 EST FROM SHAWN SNOOK TO DONG PARK * * *

Following the 8-hour 10CFR50.72 notification made on 12/4/2015 (EN 51584) regarding the Control Room Emergency Ventilation System (CREVS) inoperability, an engineering evaluation determined inleakage did not exceed limits described in the Beaver Valley licensing basis. Therefore, the degraded Control Room Emergency Ventilation System remained Operable with the identified air inleakage as determined by the Control Room Envelope Habitability Program. As such, the safety function was never lost and the event notification is being retracted as it is not reportable pursuant to 10CFR50.72(b)(3)(v)(D). FENOC is planning to repair the degraded components of the system. The NRC Resident (Inspector) has been notified." Notified R1DO (Dimitriadis).

ENS 5127227 July 2015 22:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Control Room Emergency Ventilation System InoperableOn July 27, 2015, at 1730 hours (CDT), the Control Room Emergency Ventilation (CREV) system was declared inoperable due to the 'B' Air Filtration Unit (AFU) Booster Fan discharge damper stuck open in mid-position. In this condition, the CREV system cannot be guaranteed to achieve required design flow rate. As a result, Technical Specification 3.7.4, Condition A, was entered. The CREV system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions as well as protection of the operators from a high dose environment assumed during a design basis accident. This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D) because the CREV system is a single train system, and loss of the CREV system could impact the plant's ability to mitigate the consequences of an accident as stated in Chapter 6 of the UFSAR (Updated Final Safety Analysis Report). This event is also reportable under 10 CFR 50.72(b)(3)(xiii) since this condition also impacts the control room as an Emergency Response Facility. The NRC Resident Inspector has been notified. Both units are in a seven day technical specification for troubleshooting and repairs. If the control room became uninhabitable, procedure "Complete Loss of Control Room HVAC" would be entered.
ENS 5118728 June 2015 13:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Environmental Boundary Door Found Unlatched

During Security checks of Control Room doors, a boundary door was found not latched. This door is capable of being manually closed and latched. The door was in this condition for 4 hours and 25 minutes. The door is currently closed and latched. This is being reported as it could have prevented the fulfillment of a safety function to mitigate the consequences of an accident per 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified. A condition report has been written and the door is posted to require manual checks to ensure it is latched until the door closing mechanism is repaired.

  • * * RETRACTION FROM THOMAS CLEARY TO VINCE KLCO ON 7/8/2015 AT 1314 EDT * * *

Event Report number 51187 describes a condition at Millstone Power Station Unit 2 (MPS2) in which a control room environmental boundary door was found unlatched. This was reported in accordance with 10CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function to mitigate the consequences of an accident. Upon further review, MPS2 has concluded that there was no loss of safety function, because even with the control room boundary door unlatched, the control room emergency ventilation system would have been able to perform its safety function during accident conditions. The MPS2 control room is pressure neutral and the hydraulic door closure mechanism was verified adequate to ensure the door would close and remain closed during accident conditions (even though it was not latching). Therefore, this condition is not reportable and NRC Event Number 51187 is being retracted. The basis for this conclusion will be provided to the NRC Resident Inspector. Notified the R1DO (Cahill).

ENS 5109327 May 2015 14:52:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Control Room Emergency Ventilation System InoperableOn May 27, 2015, at 0952 CDT, the Control Room Emergency Ventilation (CREV) system was declared inoperable due to opening a ventilation duct hatch to facilitate fire damper inspection without administrative controls. The hatch was opened and upon discovery was immediately shut, re-establishing the boundary of the Control Room Envelope. As a result, Technical Specification 3.7.4, Condition C, was entered and subsequently exited. The CREV system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions as well as protection of the operators from a high dose environment assumed during a design basis accident. This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D) because the CREV system is a single train system, and loss of the CREV system could impact the plant's ability to mitigate the consequences of an accident as stated in Chapter 6 of the UFSAR. This event is also reportable under 10 CFR 50.72(b)(3)(xiii) since this condition also impacts the control room as an Emergency Response Facility. At 0955, Technical Specification 3.7.4, Condition C, for CREV System Inoperable due to inoperable Control Room Envelope was exited. The NRC Resident Inspector has been notified.
ENS 510855 April 2015 09:35:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification for an Invalid Primary Containment Isolation System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of general containment isolation signals affecting containment isolation valves in more than one system. On April 5, 2015 at 0435 CDT, during replacement of a failed fuse (2-FU1-64-16A-K33A), Unit 2 Primary Containment Isolation System (PCIS) logic received the B half of the Unit 2 Group 6 isolation signal. This caused initiation of the B and C Standby Gas Treatment, B Control Room Emergency Ventilation, isolation of the Unit 2 reactor zone and all three refueling zone ventilations. This was not a valid initiation of PCIS. Operations personal responded to the PCIS initiation, ensured that all equipment operated as designed, and returned the affected systems back to service. Plant conditions which initiate PCIS Group 6 actuations are Reactor Vessel Low Water (Level 3), High Drywell Pressure, and Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as PER 1010651. The NRC Resident Inspector was notified of this event.
ENS 5097912 April 2015 22:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentTemporary Loss of Control Room Envelope Boundary

The purpose of this report is to provide a telephone notification under 10 CFR 50.72(b)(3)(v)(D) to notify the NRC of a temporary loss of the Control Room Envelope (CRE) boundary. The safety function of the CRE boundary is to ensure the in-leakage of unfiltered air into the CRE will not exceed the in-leakage assumed in the licensing basis analysis of design basis accident (DBA) consequences to CRE occupants. In addition to an intact CRE boundary maintaining CRE occupant dose from a large radioactive release below the calculated dose in the licensing basis consequence analysis for DBAs, it also ensures the occupants are protected from hazardous chemicals and smoke. The loss of the CRE boundary was due to a failed latching mechanism for a CRE boundary door used for normal passage of personnel into and out of the CRE. The failure of the door to latch as designed is considered a condition that could have prevented the fulfillment of a safety function at the time of discovery, and is therefore reportable as required by paragraph 50.72(b)(3), 'Eight-hour reports.' Procedural controls have restored the safety function of the CRE boundary by mechanically locking the subject door in the closed position through the use of a specifically designed mechanical strong-back until a permanent repair is made. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM MARK HAWES TO JOHN SHOEMAKER AT 1642 EDT ON 6/1/15 * * *

The main control room corridor fire door (76FDR-A-300-10) was found to not be able to latch. The latch was stuck in the latch mechanism because the latch bolt was bent. The latch was replaced on 4/15/2015. The Control Room Emergency Ventilation Air Supply System (CREVAS) provides a protected environment from which occupants can control the plant following an uncontrolled release of radioactivity, hazardous chemicals, or smoke. The Control Room Envelope (CRE) is the physical boundary around the CREVAS environment. The Operability of the CRE boundary depends on its ability to minimize in-leakage of unfiltered air such that after a design bases accident a habitable environment can be maintained for 31 days without exceeding 5 rem whole body dose or its equivalent to any part of the body. The control room is normally pressurized greater than the 0.125 inches water gauge. This causes air to leak out rather than allowing infiltration of air from surrounding areas into the CRE boundary. The pressurized control room pushes this door (76FDR-A-300-10) outward, toward the open direction; however, even though the latch to the door did not work the door was still able to close. The closed door minimized in-leakage and a positive differential pressure was maintained in the control room during this event. These doors are kept closed against the door seals primarily by the closure mechanism. The latch is a secondary means of ensuring that the doors remain closed as well as a means to control personnel access to the control room. The Control Room Envelope (CRE) remained Operable with this deficiency and there was no loss of safety function per 10 CFR 50.72(b)(3)(v)(D). The original notification may be retracted. The licensee has notified the NRC Resident Inspector. Notified the R1DO (Powell).

ENS 509523 April 2015 19:00:0010 CFR 50.72(b)(3)(xiii), Loss of Emergency PreparednessTechnical Support Center Ventilation Nonfunctional During Preplanned Maintenance

On April 3, 2015, at 1500 EDT, the Control Room Emergency Ventilation System on St. Lucie Unit 1 will be declared inoperable due to pre-planned maintenance during the current refueling outage. The Technical Support Center (TSC) ventilation system is part of the Unit 1 Control Room Emergency Ventilation System, therefore, the TSC ventilation system has been rendered non-functional during the course of the work activities. The TSC ventilation is expected to be returned to service in approximately 24 hours. If an emergency is declared requiring TSC activation during this period, the TSC will be staffed and activated using existing emergency planning procedures. Should the TSC become uninhabitable, the TSC staff will relocate to an alternate TSC location in accordance with applicable site procedures. This notification is being made in accordance with 10 CFR 50.72 (b)(3)(xiii) due to the potential loss of an emergency response facility. An update will be provided once the TSC ventilation system has been restored to normal operation. The NRC Resident Inspector has been notified.

  • * * UPDATE PROVIDED BY DAVE FIELDS TO JEFF ROTTON AT 2240 EDT ON 4/03/2015 * * *

The TSC ventilation system has been restored to normal operation as of 2230 EDT on April 3, 2015. The NRC Resident Inspector has been notified. Notified R2DO (Walker).

ENS 5075426 November 2014 20:27:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of a General Containment Isolation Signal Affecting More than One SystemThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On November 26, 2014, at approximately 1427 hours Central Standard Time (CST), the Browns Ferry Nuclear Plant (BFN), 1A Reactor Protection System (RPS) Motor-Generator (MG) Set Power Supply unexpectedly de-energized resulting in a BFN Unit 1 half scram and Primary Containment Isolation System (PCIS) Groups 1, 2, 3, 6, and 8 isolation signals. The PCIS Groups 1, 2, 3, 6, and 8 isolations caused the initiation of all three trains of the Standby Gas Treatment (SBGT) system and Control Room Emergency Ventilation (CREV) subsystem 'A', and isolations of the BFN, Unit 1, Reactor Zone ventilation and BFN, Units 1 and 2, Refuel Zone ventilation (Unit 3 Refuel Zone ventilation was tagged out under 3-TO-2014-0001 at the time of this event). Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, placed the BFN 1A RPS on alternate power, and reset the RPS logic and PCIS isolations. Plant conditions which initiate PCIS Group 1 actuations are Reactor Pressure Vessel (RPV) Low Low Low Water Level (Level 1), Main Steam Line (MSL) High Flow, MSL Area High Temperature, or MSL Low Pressure. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The apparent cause for this condition was an intermittent problem with the BFN 1A RPS MG Set voltage adjust potentiometer. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Problem Evaluation Report 961518. The NRC Resident Inspector has been notified of this event.
ENS 5067815 December 2014 13:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Control Room Emergency Ventilation System InoperableOn December 15, 2014, at 0730 hours (CST) the Control Room Emergency Ventilation (CREV) system was declared inoperable due to a partially stuck open main control room door. The door was unable to be closed to establish the boundary of the control room envelope. As a result, Technical Specification 3.7.4, Condition C, was entered. A repair plan and schedule is being developed. The CREV system maintains a habitable control room environment and ensures the operability of components in the control room emergency zone during accident conditions as well as protection of the operators from a high dose environment assumed during a design basis accident. This notification is being made in accordance with 10 CFR 50.72(b)(3)(v)(D) because the CREV system is a single train system, and loss of the CREV system could impact the plant's ability to mitigate the consequences of an accident as stated in Chapter 6 of the UFSAR. This event is also reportable under 10 CFR 50.72(b)(3)(xiii) since this condition also impacts the control room as an Emergency Response Facility. At 0910 (CST) exited Tech Spec 3.7.4, Condition C, for CREV System Inoperable due to inoperable Control Room Envelope (CRE). The Control Room door is now closed. Completed post maintenance smoke test, satisfactory. The NRC Resident Inspector has been notified.
ENS 506587 October 2014 15:35:0010 CFR 50.73(a)(1), Submit an LERInvalid Specified System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of general containment isolation signals affecting containment isolation valves in more than one system. On October 7, 2014, at 2135 (CDT), while in a refueling outage with the reactor non-critical (Mode 5), work activities were in progress that included replacement of an excess flow check valve and execution of a Technical Specification Surveillance Procedure on the Automatic Depressurization System. Subsequent to valving in a level transmitter (LT), water levels in both the variable and reference legs of the LT were disturbed resulting in a Unit 1 full scram and Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolation signals due to receipt of an invalid low reactor water level signal. The PCIS Groups 2, 3, 6, and 8 isolations caused the initiation of Trains A, B, and C of the Standby Gas Treatment System and Control Room Emergency Ventilation Subsystem 'A'. The Reactor and Refuel Zone ventilation fans tripped and the secondary containment dampers isolated. Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, and placed affected systems back in service. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Problem Evaluation Report 943038. The NRC Resident Inspector has been notified of this event.
ENS 5056527 August 2014 16:09:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation of General Containment Isolation SignalsThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of general containment isolation signals affecting containment isolation valves in more than one system. On August 27, 2014, at 1109 hours Central Daylight Savings Time (CDT), while in a forced unit outage with the reactor noncritical (Mode 3) and with all control rods fully inserted, instrument mechanics were attempting to backfill reactor water level transmitter (LT) 3-53 sensing lines following performance of LT replacement. During this effort, water levels in both the variable and reference legs of the LT were disturbed resulting in a Browns Ferry Nuclear Plant (BFN) Unit 1 full scram and Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolation signals due to receipt of an invalid low reactor water level signal. The PCIS Groups 2, 3, 6, and 8 isolations caused the initiation of Trains B and C of the Standby Gas Treatment (SBGT) System and Control Room Emergency Ventilation (CREV) Subsystem 'A'. The Reactor and Refuel Zone ventilation fans tripped and the secondary containment dampers isolated. Train A of the SBGT System was tagged out of service during the event. Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, and placed affected systems back in service. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Problem Evaluation Report 928777. The NRC Resident Inspector has been notified of this event.
ENS 5045412 September 2014 20:47:00Other Unspec ReqmntStored Fuel May Not Meet Fuel Specifications or Loading Conditions for Hi-Storm 100 Cask SystemArkansas Nuclear One (ANO) identified the potential for stored fuel that does not meet the fuel specifications or loading conditions of the Certificate of Compliance (CoC) for the HI-STORM 100 Cask System. Investigation into the cause of a Control Room Emergency Ventilation System (CREVS) actuation on the morning of 9/12/2014 led to sampling of helium circulating through the Multi-Purpose Canister (MPC-24-060) as part of the Forced Helium Dehydration process in the final stages of cask loading. Sample results indicated the presence of Kr-85. Kr-85 is a fission product that indicates the potential for the fuel that does meet the selection criteria for the HI-STORM 100 Cask System. All fuel assemblies loaded into MPC-24-060 were checked to confirm their intact status (a cask Certificate of Conformance requirement) as part of the selection process. Each assembly's status as intact is based on in-mast sipping and/or ultrasonic testing performed subsequent to their final operating cycle. Results of these sipping and ultrasonic test campaigns are maintained in a comprehensive engineering report used to verify assembly status during cask fuel selection. Per the CoC for the Hi-STORM 100 Cask System, Appendix B, Section 1.0, the definition of 'INTACT FUEL ASSEMBLY' is a fuel assembly without known or suspected cladding defects greater than pinhole leaks or hairline cracks, and which can be handled by normal means. Given the presence of Kr-85 along with the fuels history, it cannot be confirmed that all fuel assemblies meet the definition of 'Intact' and would not meet the CoC Requirements for Fuel to be stored in the HI-STORM 100 SFSC System (Section 2.1.1). The NRC Resident Inspector has been notified.
ENS 504275 September 2014 00:05:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Emergency Ventilation (Crev) System Inoperable

On September 04, 2014, at 1905 hours (CDT), the Control Room Emergency Ventilation (CREV) system was declared inoperable due to the Air Handling Unit (AHU) tripping upon restoration of Control Room Ventilation following testing of Reactor Building Ventilation instrumentation. Troubleshooting is in progress at this time. Technical Specification 3.7.4, Condition A, was entered which requires the CREV system to be restored to an operable status in seven (7) days. Additionally, Technical Specification 3.7.5, Condition A, was entered which requires CREV AC to be restored to an operable status in 30 days. This notification is being made in accordance with 10CFR50.72(b)(3)(v)(D), '(any) event or condition that could have prevented fulfillment of a safety function,' because the CREV system is a single train system required to mitigate the consequences of an accident. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION PROVIDED BY MARK BRIDGES TO JOHN SHOEMAKER AT 1721 EDT ON 10/23/2014 * * *

The purpose of this notification is to retract the ENS notification made on September 4, 2014 (ENS 50427). Upon further investigation it was verified that the function of Control Room Emergency Ventilation System was not affected as discussed in Chapters 6 and 15 of the Updated Final Safety Analysis Report. Therefore, the threshold for reporting the issue as an event or condition that could have prevented the fulfillment of a safety function was not met (NUREG 1022 Revision 3 - Event Report Guidelines Section 3.2.7). The licensee has notified the NRC Resident Inspector and applicable State authorities. Notified R3DO (Pelke)

ENS 5014925 May 2014 13:42:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Ventilation Boundary Door Inoperable

At 0942 on May 25, 2014, the Cook Nuclear Plant (CNP) declared both Control Room Emergency Ventilation trains inoperable in accordance with LCO 3.7.10 due to an inoperable Control Room Envelope when a control room boundary door was identified as not latching correctly during a security door check. The latch would not have been able to maintain the door closed during an event resulting in Control Room Pressurization. At this time, Security established a continuous door post and would have been able to maintain the door closed. At 1602 on May 25, 2014, repairs to the control room boundary door latch were completed restoring the Control Room Envelope to Operable. The licensee has notified the NRC Senior Resident Inspector. This notification should have been made within 8 hours of the event in accordance with 10 CFR 50.72 (b)(3)(v)(D) per guidance in section 3.2.7 of NUREG-1022 - Event or Condition that Could Have Prevented Fulfilment of a Safety Function, but was not recognized at that time.

  • * * RETRACTION FROM PERRY GRAHAM TO JOHN SHOEMAKER AT 1443 EDT ON 6/20/14 * * *

The purpose of this report is to retract EN #50149 (May 25, 2014). On June 19, 2014, Cook Nuclear Plant concluded that the EN could be retracted based on the completion of a Maintenance Rule Evaluation (MRE) performed by Systems Engineering. By design, the Control Room Envelope (CRE) pressure boundary is required to be maintained at a positive pressure during all modes of operation and during any irradiated fuel movement. New information contained in the MRE concluded the CRE function was not lost as the control room boundary door remained closed without manual assistance during normal operations. The amount of make-up air during normal operation is similar to the design flow for accident mode (approx. 800 cfm). It was concluded that the sealing integrity was not lost, thus the CRE function was maintained. The CRE would have remained operable and LCO 3.7.10 would not have been entered for the identified condition. The licensee has notified the NRC Senior Resident Inspector. Notified the R3DO (Valos).

ENS 4994221 January 2014 13:46:0010 CFR 50.73(a)(1), Submit an LER60 Day Optional Telephone Notification of an Invalid Primary Containment Isolation SignalThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On January 21, 2014, at 0746 hours Central Standard Time (CST), during performance of the 3C Emergency Diesel Generator (EDG) post modification test instructions, the EDG was supplying a shutdown board in isochronous mode when the 3B Residual Heat Removal (RHR) pump was started causing the voltage to drop to 2100 volts. At this time, Browns Ferry Nuclear Plant (BFN) Unit 3, received a half scram and Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolation signals as a result of losing the 3B Reactor Protection System (RPS) Motor Generator (MG) set due to a time delay relay failure on under voltage. The PCIS groups 2, 3, 6, and 8 isolations caused the initiation of all three trains of the Standby Gas Treatment (SBGT) system, Control Room Emergency Ventilation (CREV) subsystem 'A', and the Refuel fans tripped and isolated. Operations personnel responded to the PCIS initiation, ensured all equipment operated as designed, and placed affected systems back in service. Plant conditions which initiate PCIS group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The apparent cause for this condition was a failure of a 3B RPS MG set time delay relay due to lack of a preventive maintenance strategy. The vendor manual for the time delay relay did not specify a qualified life. The replacement relay specified a replacement schedule of 10 years. The relay that failed was installed for approximately 13 years. To address this condition, preventive maintenance is being developed for MG set time delay relays. In addition, the only remaining relay, similar to the failed relay, is scheduled be replaced on August 25, 2014, for the 2A RPS MG set. The licensee has notified the NRC Resident Inspector.