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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5470813 May 2020 06:08:0010 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS DischargeAutomatic Reactor TripAt 0208 EDT on 05/13/2020, Sequoyah Unit 1 was at 100% power when an automatic reactor trip signal was received concurrent with a low steam line pressure safety injection signal. The low steam line pressure safety injection signal was actuated from the steam pressure rate of decrease feature. Main steam isolation valves (MSIVs) automatically closed as designed and steam generator pressures stabilized following the isolation. All other safety-related equipment operated as designed, with the exception of 1-FCV-61-122 Glycol inboard containment isolation valve which failed to automatically isolate on a Phase A containment isolation signal. The corresponding outboard containment isolation valve, 1-FCV-61-110, automatically isolated as designed which isolated penetration X-114. Safety injection was terminated at 0221 EDT 5/13/20, and Unit 1 is currently being maintained in Mode 3 at normal operating temperature and pressure with auxiliary feedwater supplying the steam generators and decay heat removal via steam generator atmospheric relief valves. There is no indication of any primary to secondary leakage. The electrical alignment is normal with shutdown power supplied from off-site power. There is no current operational impact to Unit 2. There is no impact on public health or safety. Post safety injection actuation investigation is in progress. The NRC Resident Inspector has been notified.Steam Generator
Main Steam Isolation Valve
Auxiliary Feedwater
Decay Heat Removal
ENS 517209 February 2016 19:15:0010 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Eccs Discharge to Rcs Via Charging SystemAt 1415 EST on 02/09/2016, Sequoyah Unit 1 was at 0 percent power (mode 3, 526F, 2235 psig) when a low steam line pressure Safety Injection actuated from Loop 2 Steam Generator. Prior to this event, the Loop 2 Main Steam Isolation Valve bypass was opened at 1413 EST for main steam line warm up in preparation for unit startup. Loop 2 Main Steam Isolation Valve bypass closed automatically following low steam line pressure Safety Injection. Following the Safety Injection, all safety-related equipment operated as designed. Current Reactor Coolant System temperature and pressure - Unit 1 is currently being maintained in Mode 3 at approximately 517 F and 2235 psig, with auxiliary feedwater supplying the steam generators and decay heat removal via steam generator atmospheric relief valves. There is no indication of any primary to secondary leakage. The electrical alignment is normal with shutdown power supplied from off-site power. There is no operational impact to Unit 2. The cause of the Safety Injection actuation is under investigation. This event had no impact on the health and/or safety of the public. The NRC Resident Inspector has been notified. Due to RCS pressure, the only system that injected into the RCS was the charging system. The AFW system initiated to feed the steam generators and the Emergency Diesel Generators started but did not load.Steam Generator
Reactor Coolant System
Emergency Diesel Generator
Main Steam Isolation Valve
Auxiliary Feedwater
Decay Heat Removal
Main Steam Line