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ENS 5029622 July 2014 17:43:00Diesel Generator for High Pressure Core Spray Declared Inoperable During Surveillance Testing

This report is being made pursuant to 10CFR50.72(b)(3)(v)(D), Event or Condition that could have prevented fulfillment of a Safety Function needed to Mitigate the Consequences of an Accident. During the conduct of the Unit 2 Division 3 High Pressure Core Spray (HPCS) Diesel Generator (DG) surveillance test, one of 2 Cooling Water Outlet Valves failed to automatically open. The Division 3 Diesel is supplied by two redundant trains of cooling water one from each Service Water Divisional Header. Although the redundant cooling water supply was fully available and supplied adequate cooling to the diesel generator, the DG was at reduced margin to have adequate cooling water supply, if required during a loss of offsite power. Due to this loss of margin and inoperable condition, it has been determined that this failure could potentially affect the safety function of this system, and is being reported as an 8 hour ENS notification. The licensee has attributed the failure to high resistance in a relay which is currently being replaced. This places Unit 2 in the Technical Specification Action Statement 3.8.1, which requires restoration of Diesel Generator within 72 hours or commence a Reactor Shutdown. All other ECCS Systems have been verified operable. The licensee informed the NRC Resident Inspector and will inform the State of New York.

  • * * RETRACTION AT 1940 EDT ON 9/2/2014 FROM ANTHONY PETRELLI TO MARK ABRAMOVITZ * * *

This update retracts Event Notification #50296, which reported an event or condition that could have potentially prevented fulfillment of a Safety Function needed to mitigate the consequences of an accident. Upon further review, it was determined that the ability of the HPCS system (single supported train) remained operable and capable of performing its safety function as evaluated by the NMP Unit 2 Safety Function Determination Process (TS 5.5.11). The NRC Resident Inspector has been notified. Notified the R1DO (Ferdas).

ENS 4904315 May 2013 23:34:00Primary Containment Airlock Non-Functional Due to Degraded Seal on Inner Door Concurrent with Personnel Passing Through the Outer Door

At approximately 1934 EDT on May 15, 2013, maintenance personnel entered the primary containment personnel air lock to determine the cause of the inability to attain test pressure during a type B leak rate of the airlock. The inner door seal was found degraded and partially rolled from its required position allowing air from inside the airlock to enter the primary containment. During the limited time the outer airlock door was opened for access into the airlock concurrent with the degraded seal on the inner door, a condition existed that could have prevented the fulfillment of the safety function of the structure to control the release of radioactive material. The inner door seal was subsequently replaced and the leak rate of the personnel air lock completed with satisfactory results. During the seal replacement activity, the outer airlock door remained closed to provide the barrier against the release of radioactive material should it be required. This is a notification per 10 CFR 50.72(b)(3)(v) for a condition that could have prevented the control of the release of radioactive material. It is recognized that this notification (was) not within eight hours of the event. The condition has been entered into the station's corrective action program. The licensee will notify the New York State Public Service Commission and the NRC Resident Inspector.

  • * * RETRACTION ON 6/27/13 AT 1549 EDT FROM KROCK TO HUFFMAN * * *

This notification is being made to retract Event Notification #49043, which reported a condition that could have prevented the control of the release of radioactive material when the primary containment airlock inner door seal was found degraded concurrent with the outer door being open. Further analysis by engineering of the actual conditions which were recorded when the airlock Type B leak rate test was being performed and calibration checks of the leak rate monitor instrumentation used for the test, has determined that the leakage through the degraded inner airlock door seal, when combined with the Appendix J As-Left Minimum Pathway Type B and C leak rates, remains below the Technical Specification Primary Containment As-Left Minimum Pathway Leakage Limit of 0.6 La. Therefore, for the period in which the inner airlock door seal was degraded and the outer airlock door was open, the primary containment function to control the release of radioactive material was maintained and the initial notification per 10 CFR 50.72(b)(3)(v) is being retracted. The licensee has notified the NRC Resident Inspector and the New York State Public Service Commission. R1DO (Ferdas) notified.

ENS 484816 November 2012 05:06:00High Pressure Coolant Injection Actuation Signal

On Tuesday, November 06, 2012, at 00:06 EST, during the application of a tag-out associated with feedwater level control, the 12 feedwater flow control valve (FCV-29-137) unexpectedly partially opened. As a result, reactor vessel water level rose to the high level turbine trip set point causing the main turbine to trip. The turbine trip signal then resulted in the initiation of High Pressure Coolant Injection (HPCI) channels 11 and 12 logic. No actual system component starts or actuations occurred as a result of the logic initiation and no actual HPCI injection occurred due to the system configuration, nor was injection required. Actions were taken to manually isolate the 12 feedwater flow control valve and reactor vessel water level was restored to normal. This meets NRC 8-Hour reporting criteria per 10 CFR 50.72(b)(3)(iv)(A) due to a valid actuation of the High Pressure Coolant Injection System. The licensee has notified the NRC Resident Inspector.

  • * * RETRACTION FROM JERRY HELKER TO CHARLES TEAL ON 12/17/12 AT 1543 EST * * *

This notification is being made to retract Event Notification (EN) #48481, which reported an automatic actuation of the High Pressure Coolant Injection (HPCI) system initiation logic. The HPCI system is automatically initiated based on conditions representing a small break loss of coolant accident (LOCA). The initiation signals are: - Low reactor water level - This is a direct indication of a potential loss of adequate core cooling. - Turbine trip - During a LOCA within the drywell, high drywell pressure due to the line break will cause a reactor scram, which causes a turbine trip, which then by design initiates the HPCI system. The event occurred with the reactor in the cold shutdown condition, with the main turbine and main turbine shaft-driven feedwater pump (#13) out of service. In the cold shutdown condition, the probability of a LOCA is low and the HPCI system is not required by the Technical Specifications to be operable. Neither of the conditions requiring actuation of the safety function of the HPCI system (high drywell pressure or low reactor water level) was present. Although the turbine trip signal was in response to an actual sensed high reactor water level condition, high reactor water level is not a plant condition satisfying the requirement for actuation of the safety function of the HPCI system. With reactor vessel water level high, the safety function of the HPCI system (i.e. to provide adequate core cooling) was already completed. Thus, the HPCI initiation signal was invalid, and the event is not reportable under 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been informed. Notified the R1DO (Hunegs).

  • * * UPDATE FROM JOHN APRIL TO VINCE KLCO ON 4/24/13 AT 0158 EDT * * *

Upon further review, it has been determined the event did constitute a valid actuation of the HPCI system and is reportable per 10CFR50.72(b)(3)(4)(A). The licensee will notify the NRC Resident Inspector. Notified the R1DO (Joustra).

Reactor Vessel Water Level
ENS 4399016 February 2008 00:02:00Potential Inoperability of Emergency Core Cooling Systems Due to an Unalalyzed Condition

This notification is being made in accordance with 10 CFR 50.72(b)(3)(ii) which states in part Any event or condition that results in (A) the condition of the nuclear power plant, including its principle safety barriers, being seriously degraded; or (B) the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety and 10 CFR 50.72(b)(3)(v) which states in part Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (A) Shut down the reactor and maintain it in a safe shutdown condition; (B) Remove residual heat; (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident. This notification describes a licensee identification of a condition where the low pressure emergency core cooling systems (ECCS) may not have been able to perform their safety functions of removing residual heat and significantly degrades plant safety. The condition has been corrected. At 2152 on 15 February 2008, while operating at 100% power, Nine Mile Point Unit 2 completed evaluating a 10 CFR 21 communication from General Electric on ECCS suction strainers, and concluded that the calculation on debris head loss was non conservative. The original design basis net positive suction head calculations assumed a suppression pool water level of 199.5 feet. Based upon the General Electric notification, at this suppression pool water level, the low pressure core spray and all three residual heat removal systems might not have been able to perform their safety functions. Further engineering evaluation determined that if the suppression pool level was (greater than or equal to) 200.3 feet then the suction strainers debris head loss could be met and the low pressure ECCS would be able to perform their safety functions. At 1902 the control room operators took action to raise suppression pool water level while engineering completed their evaluation based on the expectation that suppression pool water would have to be raised. At 1910 on 15 February 2008, suppression pool water level was raised to 200.3 feet, which resulted in the low pressure core spray and residual heat removal systems being able to perform their safety function. The licensee will notify the NRC Resident Inspector.

  • * * RETRACTION ON 4/12/08 AT 1001 EDT FROM PETRELLI TO HUFFMAN * * *

After further review, this event notification report is being retracted based on the following: The notification was initiated due to a 10 CFR 21 communication from General Electric on ECCS suction strainers, indicating that the calculation of suction strainer head loss was non-conservative. As a result, at the assumed suppression pool water level of 199.5 feet, adequate net positive suction head may not be available for the low-pressure ECCS pumps. Suppression pool water level was raised 9.8 inches, to 200.3 feet, which provided assurance that the low pressure ECCS pumps were capable of performing their specified safety functions. Further evaluation by plant staff has determined that there are margins available in the suction strainer head loss calculations and in the design basis ECCS pump net positive suction head calculations that, when combined, exceed the increase in suction strainer debris head loss identified in the General Electric communication. Based on these available margins, there was adequate net positive suction head for the low pressure ECCS pumps at the originally assumed suppression pool water level of 199.5 feet. In addition, the as-found quantity of corrosion products and debris removed from the suppression pool during the current refueling outage was significantly less than the quantity assumed in the design basis suction strainer head loss calculations, indicating that additional analytical margin existed. Thus, the low pressure ECCS pumps were operable and capable of performing their specified safety functions without reliance on the 9.8 inches of water level added to the Suppression pool. Raising the suppression pool water level was a conservative action but was not necessary to maintain operability of the low pressure ECCS pumps. Therefore, this event is not reportable under either 10 CFR 50.72(b)(3)(ii) or 10 CFR 50.72(b)(3)(v). The licensee notified the NRC Resident Inspector. R1DO (Conte) notified.

Safe Shutdown
Unanalyzed Condition
Time of Discovery
ENS 4371011 October 2007 05:00:00Tone Alert Radio System Out of Service for Maintenance

The tone alert radio system for Nine Mile point was taken out of service for planned maintenance. Per Site Emergency Planning procedures this constitutes a partial loss of the Public Prompt Notification System (Loss of Communication) and thus is reportable under 10 CFR 50.72 (3)(b)(xiii). The tone alert radio system is installed in Oswego County residences and businesses who can not hear the siren system when activated. The tone alert radio system notifies Oswego County resident of emergency situations. The tone alert radio system is maintained and operated by the National Weather Service (NWS). NWS estimates that the system will be out of service for approximately 6 hours. The county alert sirens, which also function as part of the public prompt Notification System, are operable. The licensee notified the State and local governments. The licensee will notify the NRC Resident Inspector.

  • * * RETRACTION ON 10/11/07 AT 1510 EDT FROM BRIAN FINCH TO JOHN MACKINNON * * *

The Oswego County Emergency Management Office was notified on 10/11/07 at approximately 1150 by the National Weather Service, NWS (Binghamton, NY) that the Tone Alert System is in service and fully functional. The NWS informed Oswego County that the time the Tone Alert System was out of service from 10/10/07 at 2350 until 10/11/07 at 0013 for a total of 23 minutes. The 23 minutes is less than the one hour criteria for a 10CFR50.72 notification. As such, the initial notification is retracted." R1DO (W. Cook) notified. The NRC Resident Inspector was notified of this retraction by the licensee. State and Local Officials have also been notified of this retraction by the licensee.

ENS 423863 March 2006 23:00:00Reactor Building Ventilation Flowpath Inoperable

This notification is being made in accordance with License Condition 2.F for Nine Mile Point Unit 2 which states in part 'report any violations of the requirements contained in Section 2.C of this license in the following manner: initial notification shall be made within 24 hours to the NRC Operations Center via the Emergency Notification System, with written follow-up within 30 days in accordance with the procedures described in 10 CFR 50.73(b), ( c), and (e).' License Condition 2.C (2) states in part 'Nine Mile Point Nuclear Station, LLC shall operate the facility in accordance with the Technical Specifications.' This notification describes a licensee identified condition where both redundant Standby Gas Treatment (SGT) trains were apparently inoperable in violation of Technical Specifications. The condition has been corrected. At 1800 on 3 March 2006, while operating at 91 % power (coast down to refueling), Nine Mile Point Unit 2 identified a condition in which both trains of SGT were apparently rendered inoperable for intermittent time periods of a few hours in length, starting from 17 February 2006 through about 1900 on 28 February 2006. This was not recognized at the time; as such the requirement to initiate a plant shutdown per LCO 3.0.3 was not performed. The condition was caused by use of a heavy-duty tarp and associated cargo net supporting it from underneath, installed across the Unit 2 Reactor Building Hoist Well. Installation of the tarp and net across the hoist well occurred between the above dates, for time periods of a few hours each, in order to support refueling preparations, thereby avoiding spread of contamination during rigging activities. The blockage of the Reactor Building Hoist Well would have obstructed or significantly degraded the design flow paths of both trains of SGT if called upon to perform their safety functions in a design basis accident. Therefore current information indicates this tarp installation configuration renders the SGT system inoperable. The tarp and net were permanently removed at about 1900 on 28 February 2006 when a supervisor questioned if tarp installation was allowed while the reactor was at power. Although removal of the tarp and net typically required only a few minutes effort by plant workers, its installation and continued blockage of the ventilation flow path would have resulted in declaration of the (SGT) safety systems to be inoperable if not removed. Workers were not sensitive to the safety function of the open ventilation flow path provided by the hoist well, and no programmatic training or administrative requirements were identified which prohibited the configuration at conditions other than cold shutdown. Nine Mile Point is in the process of taking compensatory measures to preclude installation of the tarp when SGT is required to be operable by briefing operations, radiation protection and refuel worker crews on ventilation requirements and sensitivity to safety functions. Operations took physical control (lock and key) of the tarp. Corrective actions to provide administrative controls on the tarp installation are in process. Detailed evaluation of the safety significance of the condition is ongoing. Initial review of plant records indicate that this configuration was also installed intermittently around July 2003. It was recognized as undesirable but was not identified as an operability or reportability issue at the time. Corrective action to prevent its recurrence was not effective. More detailed information on specific dates and durations when this configuration existed will be provided in the 30 day written LER report, after a detailed review.

The instances noted above and any similar conditions identified will be explained in detail in the follow-up LER that will be submitted as required by 10CFR 50.73(a)(2)(i)(B) - 'Any operation or condition which was prohibited by the plants Technical Specifications .'" Unit-1 is not affected since they have a different method to control use of this tarp. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM T. RESTUCCIO TO HUFFMAN AT 2209 ON 3/28/06 * * *

At 1800 on 3 March 2006, while operating at 91% power (coast down to refueling), Nine Mile Point Unit 2 identified a condition in which both trains of the Standby Gas Treatment (SGT) system were apparently inoperable for intermittent time periods of a few hours of length, starting from 17 February 2006 through about 1900 on 28 February 2006. This was not recognized at the time; as such the requirement to initiate a plant shutdown per LCO 3.0.3 was not performed. The condition was caused by use of a heavy-duty tarp and associated cargo net supporting it from underneath, installed across the Unit 2 reactor Building Hoist Well. Installation of the tarp and net across the hoist well occurred between the above dates, for time periods of a few hours each, in order to support refueling preparations, thereby avoiding the spread of contamination during rigging activities. The blockage of the reactor Building Hoist Well would have obstructed or significantly degraded the design flow paths of both trains of SGT if called upon to perform their safety functions in a design basis accident. Review of plant records indicate that this condition was also installed intermittently around July 2003. A subsequent evaluation of the safety significance of this condition has been performed. This evaluation considered actual area of flow path remaining with the tarp in place, as well as bounding outside temperatures during the times the tarp may have been installed. The evaluation has concluded that the secondary containment function, and therefore the SGT system, remained operable and would have performed its intended safety function during a design basis accident during the time periods the tarp may have been installed during the last three years. This evaluation provides the basis for retraction of the ENS report of March 4, 2006. The licensee notified the NRC Resident Inspector. The R1DO(Cook) has been notified.

Coast down
ENS 4158410 April 2005 10:00:00Scram Signal Resulting from Failure of a Supply Valve to the Scram Air Header

Nine Mile Point Unit 1 received a valid RPS SCRAM signal from high water level in the SCRAM Dump Volume (SDV). While restoring the Hydraulic Control Rod Unit (HCU) for control rod 02-35 to service, the internals to the plug valve for the Instrument Air Supply (116 Valve) to the SCRAM Inlet and Outlet valves failed. This failure caused an approximate 1/2" hole in the SCRAM Air Header, which resulted in the SCRAM Air Header pressure lowering rapidly due to the leak. Operators at the HCU recommended isolating the SCRAM Air Header. The Shift Manager was contacted by the job supervisor and received permission to isolate the SCRAM Air Header. SCRAM inlet and outlet valves opened, SDV vents and drains closed due to the loss of SCRAM Air Header pressure. Approximately 3 minutes after SCRAM Air Header depressurization, a full SCRAM signal occurred as expected due to the water level in the SDV. There was no fuel in the Reactor Vessel (RPV). No Control Rod motion occurred due to all Control Rods being inserted or isolated for maintenance. Immediate (8 Hour Non-Emergency) notification of this event being made as a result of the requirements of 10CRF50.72(b)3(iv)(A). The licensee stated that more information on the event can be found in Nine Mile Point Internal document DER - NM-2005-1565. The license will be notifying the NRC Resident Inspector.

  • * * RETRACTION PROVIDED BY LICENSEE (SHEEHAN) TO NRC (HELD) AT 1739 EDT ON 5/19/05 * * *

The scram event that occurred on April 10, 2005 was not initiated from a "valid" scram initiation signal (i.e., none of the instrumentation signals identified in Technical Specification Table 3.6.2a triggered the scram). To the contrary, a valve on a CRD hydraulic control unit (HCU) failed and Operations took action to isolate instrument air from the scram air header. This operator action had the identical effect that a scram signal would have had - the scram air header completely vented through the broken valve and caused the scram inlet and outlet valves on the HCUs to open and the scram discharge volume vents and drains to close. At the time, the reactor was defueled and all control rods were either already inserted or properly removed from service for maintenance, thus, the event did not result in any control rod movement (i.e., the system had been properly removed from service and the safety function had already been performed). Subsequent to the initiating event, as per the design of the CRD and RPS systems, the scram discharge volume filled and a full RPS scram signal was generated. Conclusion: The scram event that occurred on April 10, 2005, resulted from an invalid scram initiation signal. At the time, the reactor was defueled, the CRD system had been properly removed from service and the safety function had been properly performed (no control rods moved). Thus, pursuant to the guidance in NUREG-1022, it is appropriate to conclude that the event is not reportable under 10CFR50.72(b)(2)(iv) or 10CFR50.73(a)(2)(iv). As such, the 8-hour ENS notification that was made at 11:46 on 4/10/05 (reference Event Number #41584) is being retracted The licensee notified the NRC Resident Inspector. R1DO (Bellamy) was contacted.

Scram Discharge Volume