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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5654430 May 2023 08:46:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Reactor TripThe following information was provided by the licensee via email: At 0446 EDT on 5/30/2023, with Millstone Power Station Unit 3 operating at approximately 100 percent reactor power, an automatic reactor trip occurred due to a turbine trip caused by electrical protection. The reactor trip was uncomplicated and decay heat is being removed via steam dumps to the condenser. All systems responded as expected to the trip. Auxiliary feedwater actuated automatically as expected following the trip due to low-low levels in the steam generators. There was no risk to the public. There was no impact to Millstone Unit 2. This event is being reported as a four hour report under 10CFR50.72(b)(2)(iv)(B) as a condition that resulted in actuation of the reactor protection system while the reactor was critical, and as an eight hour report under 10CFR50.72(b)(3)(iv)(A) and 10CFR50.72(b)(3)(iv)(B) for actuation of the auxiliary feedwater system. The NRC Resident Inspector has been notified.Steam Generator
Reactor Protection System
Auxiliary Feedwater
ENS 5466313 April 2020 19:50:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Trip Due to Low Condenser VacuumAt 1550 EDT on 4/13/2020, with Millstone Power Station Unit 3 operating at approximately 82 percent reactor power, an automatic reactor trip occurred following a turbine trip due to low condenser vacuum caused by the trip of multiple circulating water pumps. Due to the loss of the circulating water pumps, decay heat removal was established by the steam generator atmospheric dump valves. All other systems responded as expected to the trip. Auxiliary feedwater actuated automatically as expected following the trip due to low-low levels in the steam generators. There was no risk to the public. There was no impact to Millstone Unit 2. The Senior Resident Inspector has been informed. This event is being reported as a four hour report under 10 CFR 50.72(b)(2)(iv)(B) as a condition that resulted in actuation of the reactor protection system while the reactor was critical, and as an eight hour report under 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.72(b)(3)(iv)(B) for actuation of the auxiliary feedwater system. The licensee also notified the state of Connecticut, the Connecticut Department of Energy and Environmental Protection, and the city of Waterford.Steam Generator
Reactor Protection System
Auxiliary Feedwater
Decay Heat Removal
ENS 546311 April 2020 20:25:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Trip Due to Circuit FaultOn April 1, 2020, at 1625 EDT, Milllstone Unit 3 was in Mode 1, at 100 percent power, when an automatic reactor trip occurred following a main generator trip. The cause was due to a circuit fault between the main generator breaker and the offsite switchyard. The reactor trip was not complicated and the reactor remains stable in Mode 3. One of the two offsite electrical sources remain inoperable with an investigation of the circuit fault underway. Decay heat removal is maintained by the main condenser. There was no effect on Unit 2. The NRC Resident Inspector was notified. The licensee notified State and local government agencies.Decay Heat Removal
Main Condenser
ENS 5445727 December 2019 12:04:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Trip Due to Feedwater Pump Trip

This is a synopsis of initial information received via phone: On December 27, 2019, at 0705 EST, while Unit 2 was at 100 percent (Mode 1), the 'A' Main Feedwater Pump tripped due to an unknown cause. The reactor was manually tripped and is currently at zero (0) percent power (Mode 3). Decay heat is being removed via Auxiliary Feedwater. The 'B' Feedwater pump is operable. There was no impact on Unit 3. The licensee notified the NRC Resident Inspector. Additionally, Connecticut Department of Environmental Protection, Waterford Dispatch, and East Lyme Emergency Management Division will be notified.

  • * * UPDATE ON 12/27/2019 AT 1330 EST FROM JASON PARIS TO CATY NOLAN * * *

This is an update to NRC Event Number 54457. At 0704 EST, on 12/27/2019, with Millstone Unit 2 operating at 100 percent power, operators inserted a manual reactor trip. The trip was initiated due to a trip of the 'A' Main Feedwater Pump. The Auxiliary Feedwater System (AFW) automatically actuated as required. All control and shutdown rods fully inserted. All safety systems responded as designed. No primary or secondary safety valves actuated during or after the transient. Unit 2 is currently stable at normal operating pressure and temperature in Mode 3, Hot Standby. Reactor Coolant System (RCS) temperature is being maintained by the steam dump system with all Reactor Coolant Pumps (RCPs) in service. Main Feedwater has been secured, and Auxiliary Feedwater is in service. The electrical system is in normal alignment. There was no impact on Unit 3. There was no impact to the health and safety of the public or plant personnel. Due to Reactor Protection System (RPS) actuation while critical, this event was reported as a four hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B); and an eight hour non-emergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of the AFW system. The licensee will notify the NRC Resident Inspector of the update. Notified R1DO (Cherubini).

Reactor Coolant System
Feedwater
Reactor Protection System
Auxiliary Feedwater
ENS 5216911 August 2016 13:59:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Due to Loss of Two Circulating Water PumpsReactor operators manually tripped the reactor due to the loss of two out of four circulating water pumps which caused a drop in condenser vacuum. The trip was uncomplicated. The reactor is shutdown and stable with decay heat removal via steam dumps to the condenser. The cause of the circulating water pump trips is currently unknown, but initial indications are that the pumps tripped due to a lightning strike that caused an electrical perturbation. The reactor will remain shutdown while the licensee investigates the cause. Unit 3 was not affected. The licensee notified the NRC Resident Inspector and the State and Local governments.Decay Heat Removal
ENS 5192915 May 2016 10:38:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Due to Main Generator Hydrogen Leak in Turbine Building

At 0638 EDT on 5/15/2016, an Unusual Event (EAL GU.2) was declared on Millstone Unit 3 due to a Main Generator hydrogen gas leak into the Turbine Building. At 0645 EDT, operators manually tripped the reactor. All rods inserted. All systems functioned as expected following the reactor trip. Operators are currently venting the remaining hydrogen from the generator through the normal vent path. There is no safety related equipment out-of-service. The plant is in a normal post-trip electrical line-up. All Emergency Diesel Generators are available. The licensee notified the State of Connecticut and the NRC Resident Inspector. Notified DHS SWO, FEMA Ops Center, and DHS NICC Watch Officer. Notified via E-mail FEMA National Watch Center and NuclearSSA.

  • * * UPDATE FROM MIKE CICCONE TO HOWIE CROUCH AT 1044 EDT ON 5/15/16 * * *

At 0949 EDT, the licensee terminated the Unusual Event. At 0645 EDT on 5/15/16, a manual reactor trip was initiated at Millstone Unit 3 due to a hydrogen leak from the main generator. As expected, Auxiliary Feedwater System (AFW) initiated on the reactor trip. The trip was uncomplicated and the plant is currently in Mode 3 with a normal electric lineup and decay heat is being removed via steam dumps to the condenser. The cause of the hydrogen leakage is under investigation. This is reportable under 10 CFR 50.72(b)(2)(iv)(B) - RPS actuation while critical, and 10 CFR 50.72 (b)(3)(iv)(A) - valid specified system actuation. The licensee has notified Waterford Township, the State of Connecticut and the NRC Resident Inspector. Notified R1DO (Burritt), NRR ET (McDermott), NRR EO (Morris), IRD (Grant), DHS SWO, FEMA Ops Center, DHS NICC, FEMA National Watch Center (email) and NuclearSSA (email).

Emergency Diesel Generator
Auxiliary Feedwater
ENS 5168225 January 2016 06:47:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Reactor Coolant Pump TripAt 0147 EST on 1/25/16, the 'B' Reactor Coolant Pump (RCP) tripped offline. This caused a reactor trip on low coolant flow. As expected, the Aux Feedwater System (AFW) initiated on the reactor trip. The trip was uncomplicated and the plant is currently shutdown in Mode 3 with a normal electrical lineup and decay heat is being removed via steam dumps to the condenser. The cause of the 'B' RCP trip is under investigation. A containment entry is planned for dayshift on 1/25/16 to inspect and troubleshoot the 'B' RCP. The Licensee has notified the NRC Resident Inspector.Feedwater05000423/LER-2016-001
ENS 515218 November 2015 07:30:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Due to Reactor Coolant Pump Oil LeakDuring power ascension following refueling outage, a decreasing oil level in the 'C' Reactor Coolant Pump was noted. When the oil level reached 69 percent, with the reactor at approximately 56 percent rated thermal power, per plant procedure, a rapid downpower was initiated which brought the plant to approximately 15 percent power and a manual reactor trip was initiated at that point. The reactor trip was uncomplicated and all plant equipment responded as expected. The licensee notified the NRC Resident Inspector.
ENS 5014225 May 2014 11:02:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness
Unusual Event Due to Loss of Offsite Power

At 0702 EDT on 5/25/14, Millstone Units 2 and 3 experienced a loss of offsite power and subsequent trip of both units. An Unusual Event was declared by Millstone Units 2 and 3 at 0715 EDT. Power is currently being supplied to all emergency busses by the emergency diesel generators. Offsite power is not available. At this time, it appears that the loss of offsite power is due to a localized issue in the Millstone switchyard. The surrounding areas were not affected. A decision was made to take the NRC to monitoring mode at 0749 EDT with Region 1 in the lead. Notified DHS SWO, FEMA Ops Center, NICC Watch Officer, DOE Ops Center, USDA Ops Center, HHS Ops Center, and Nuclear SSA via email.

  • * * UPDATE FROM MICHAEL CICCONE TO CHARLES TEAL AT 1330 EDT ON 5/25/14 * * *

All EDGs have been secured and offsite power has been restored. The licensee is reporting the loss of two stack radiation monitors - 8168 and 8169. This is reportable under 10CFR50.72(b)(3)(xiii). Notified R1DO (Gray), R1DRA (Lew), NRR EO (Kokajko), IRD MOC (Grant).

  • * * UPDATE FROM MICHAEL CICCONE TO DANIEL MILLS AT 1548 EDT * * *

At 1414 EDT the licensee terminated the Unusual Event. Notified R1DO (Gray), R1DRA (Lew), NRR EO (Kokajko), IRD MOC (Grant), DHS SWO, FEMA Ops Center, NICC Watch Officer, DOE Ops Center, USDA Ops Center, HHS Ops Center, and Nuclear SSA via email.

Emergency Diesel Generator05000336/LER-2014-006
ENS 5014125 May 2014 11:02:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unusual Event Due to Loss of Offsite Power

At 0702 EDT on 5/25/14, Millstone Units 2 and 3 experienced a loss of offsite power and subsequent trip of both units. An Unusual Event was declared by Millstone Units 2 and 3 at 0715 EDT. Power is currently being supplied to all emergency busses by the emergency diesel generators. Offsite power is not available. At this time, it appears that the loss of offsite power is due to a localized issue in the Millstone switchyard. The surrounding areas were not affected. A decision was made to take the NRC to monitoring mode at 0749 EDT with Region 1 in the lead. Notified DHS SWO, FEMA Ops Center, NICC Watch Officer, DOE Ops Center, USDA Ops Center, HHS Ops Center, and Nuclear SSA via email.

  • * * UPDATE FROM MICHAEL CICCONE TO DANIEL MILLS AT 1330 EDT * * *

The loss of offsite power was due to one main line coming into the plant shorting to ground. Emergency plan procedures have been implemented, natural circulation has been established, and the plant is stable. Offsite electrical power has been restored to both Unit 2 and Unit 3. Emergency diesel generators have been secured, and plant equipment has been restored to a normal line up. Extended loss of instrument air following the loss of offsite power complicated the recovery actions. The normal reactor coolant system letdown flow path was not able to be established. This resulted in the rupture of the pressurizer relief tank rupture disk inside containment. The relief valve on the volume control tank lifted when restoring normal letdown. This caused the primary drains transfer tank to overflow into the auxiliary building. This overflow path has been isolated. Supplementary leakage collection system radiation monitor HVR-RE19B, and auxiliary building normal ventilation radiation monitor HVR-RE10B, are indicating normal levels. Notified R1DO (Gray), R1DRA (Lew), NRR EO (Kokajko), IRD MOC (Grant).

  • * * UPDATE FROM MICHAEL CICCONE TO DANIEL MILLS AT 1548 EDT * * *

At 1414 EDT the licensee terminated the Unusual Event. Notified R1DO (Gray), R1DRA (Lew), NRR EO (Kokajko), IRD MOC (Grant), DHS SWO, FEMA Ops Center, NICC Watch Officer, DOE Ops Center, USDA Ops Center, HHS Ops Center, and Nuclear SSA via email.

Reactor Coolant System
Emergency Diesel Generator
05000336/LER-2014-006
ENS 495259 November 2013 20:13:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Loss of Condenser VacuumMillstone Unit 2 automatically tripped following a turbine trip due to a loss of condenser vacuum. The loss of vacuum was caused by the trip of the "C" circ water pump with the "D" circ water pump out of service. The licensee is still investigating the trip of the "C" circ water pump. The MSIVs are open with steam generators discharging steam to the main condenser. Auxiliary feedwater automatically started as expected following the reactor trip. All rods fully inserted and there were no complications following the reactor trip. All systems functioned as required and the unit is stable in Mode 3. There was no impact on Unit 3. The licensee has notified state and local authorities and the NRC Resident Inspector.Steam Generator
Auxiliary Feedwater
Main Condenser
ENS 4926010 August 2013 01:19:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip on Low Steam Generator Water LevelThe loss of a non-vital 480v bus resulted in a feedwater transient that caused steam generator water level to lower below the automatic reactor trip setpoint. The reactor trip and plant response was uncomplicated with all rods being inserted into the core. The auxiliary feedwater system automatically actuated and is currently being to used to feed the steam generators. Decay heat is being removed via the steam dumps to the condenser. No relief valves or safeties lifted during the transient. The plant is currently stable in Mode 3 at normal operating pressure and temperature and is in its normal shutdown electrical lineup. There was no impact on Unit 2 which is currently operating at 100% power. The licensee has notified state and local authorities and the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
ENS 5200013 June 2013 00:13:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Technical Specification Required Shutdown and Reactor Trip

At 2013 EDT on 6/12/16, Millstone Unit 3 commenced a Technical Specification (TS) required shutdown due to excessive Reactor Coolant System leakage from the "A" Reactor Coolant Pump (RCP) third stage seal. The leakage from the third stage seal was approximately two gpm which is greater than the Technical Specification (TS) limit of less than one gpm. During the shutdown, oscillations developed in the Main Feedwater which required the operator to initiate a manual reactor trip. Unit 3 is currently stable in Mode 3. Decay heat is being released via the Steam Dumps to the Main Condenser. Normal offsite power is available and the unit is in a normal shutdown electrical line-up. The cause of the Main Feedwater oscillations is being investigated. The licensee notified the NRC Resident Inspector. The licensee notified State and local government agencies.

  • * * UPDATE FROM WALTER ORF TO DONALD NORWOOD AT 0129 EDT ON 6/13/2016 * * *

The following clarifies Feedwater isolation vs. Feedwater oscillation: At 2337 EDT on 6/12/16, a manual reactor trip was initiated on Unit 3 following feedwater isolation. As expected, Aux Feedwater system (AFW) initiated on the reactor trip. The trip was uncomplicated and the plant is currently in Mode 3 with a normal electric line-up and decay heat is being removed via steam dumps to the condenser. This is reportable under 10 CFR 50.72(b)(2)(iv)(B) - RPS Actuation - Critical and 10 CFR 50.72(b)(3)(iv)(A) - Valid Specific System Actuation." The Feedwater isolation occurred due to high Steam Generator water level. The licensee notified the NRC Resident Inspector. Notified R1DO (Arner).

Steam Generator
Reactor Coolant System
Feedwater
Main Condenser
ENS 4746120 November 2011 22:58:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Loss of Condenser Vacuum During StartupMillstone Unit 3 was manually tripped at low power during startup following the loss of condenser vacuum. The loss of vacuum was caused by the loss of the auxiliary steam boiler. The auxiliary steam boiler supplies gland seal steam to the turbine at low power and without the gland seal steam, the licensee could not maintain a condenser vacuum. All rods fully inserted and there were no complications during the trip. All systems functioned as required and the unit is stable in Mode 3. There was no impact on Unit 2. The licensee has notified state and local authorities and the NRC Resident Inspector.
ENS 4697120 June 2011 15:52:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Unit 2 Reactor Trip Following the Loss of the "B" Main Feedwater (Mfw) PumpAt 1152 EDT on 6/20/11 while operating at 60% power, the "B" MFW Pump tripped for reasons unknown. There was no maintenance or I&C work on-going at the time involving this pump. Operators initiated a manual reactor trip, however, (they) are not certain whether the automatic reactor trip setpoint of 49.5% Steam Generator Water Level Narrow Range (SGWL NR) was reached first. SGWL decreased to the Auxiliary Feedwater (AFW) setpoint of 26.8% NR causing the initiation of both motor-driven AFW Pumps. All Control Rods fully inserted. Unit 2 is currently stable in Mode 3, Hot Standby, removing decay heat via the Main Steam line to the Condenser. Operators secured AFW and will initiate feed to the Steam Generators using the "A" MFW Pump. Unit 2 is in a normal post-trip electrical lineup with all sources of offsite power available. The licensee has the cause of the "B" MFW Pump trip under investigation. The licensee informed both state/local (Waterford Dispatch) and the NRC Resident InspectorSteam Generator
Feedwater
Auxiliary Feedwater
Main Steam Line
Control Rod
ENS 4644128 November 2010 20:15:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip After Turbine Trip Due to Loss of Condenser VacuumLoss of two circulating water pumps in one condenser caused a high main condenser backpressure. The high main condenser back pressure caused an automatic main turbine and reactor trip while critical >15%. Low steam generator water level following the trip caused an automatic Auxiliary Feedwater actuation. The low water level condition has cleared. Normal post-trip response has been verified and the plant is stable. The licensee removed one circulating water pump from service in preparation of performing scheduled maintenance when the other circulator unexpectedly tripped. The cause of the pump trip is under investigation. During the trip, all rods inserted into the core. There were no primary safety valves that lifted during the transient but main steam safeties "chattered" during the transient and have fully reseated. There is no known primary to secondary leakage. The electrical grid is stable and supplying plant loads in a normal shutdown electrical lineup. The reactor is stable at normal operating pressure and temperature with decay heat being removed via the steam dumps to condenser. The licensee has notified the State of Connecticut Department of Environmental Protection, the town of Waterford, CT, and the NRC Resident Inspector.Steam Generator
Auxiliary Feedwater
Main Turbine
Main Condenser
Main Steam
ENS 4594522 May 2010 20:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Loss of Steam Generator Water Level ControlThe licensee experienced a feedwater transient which initiated the event. All safety systems are available. All control rods fully inserted. The electrical lineup is normal. The decay heat path is through the condenser steam dumps. No relief valves or safety valves lifted during the transient. Primary plant temperature is 533 degrees Fahrenheit and primary plant pressure is 2256 psia. The licensee is investigating the cause of the feed transient. The licensee notified the NRC Resident Inspector, the Waterford Dispatch, and the State Department of Environmental Protection. Earlier, the licensee was experiencing oscillations in the feedwater regulating valve (FRV) for the #2 steam generator when the valve was in automatic control. Troubleshooting planning was underway but no troubleshooting activities were in progress at the time of the trip. When the operator placed the #2 steam generator FRV in manual control, the steam generator water level began to increase and could not be recovered. The operator then manually tripped the reactor prior to reaching the high steam generator level trip setpoint. An Auxiliary Feed Water system actuation did occur during the transient. The trip and plant response was considered uncomplicated.Steam Generator
Feedwater
Auxiliary Feedwater
Control Rod
05000336/LER-2010-002
ENS 4593117 May 2010 14:17:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Low Steam Generator Water LevelSystem Affected: RPS actuation and reactor trip. Actuation Initiation Signals: AFW auto initiation. Cause: Low level 'C' steam generator. Effect of event on Plant: Reactor and turbine trip. Actions taken or Planned: Standard post trip actions. Additional information: Plant stabilized at NOP/NOT. The licensee experienced a feedwater transient which initiated the event. All safety systems are available. All control rods fully inserted. The electrical lineup is normal. The decay heat path is through the condenser steam dumps. There were no relief valve or safety valve lifted during the transient. Primary plant temperature is 555 degrees Fahrenheit, and primary plant pressure is 2250 psig. The licensee is investigating the cause of the feed transient. The licensee notified the NRC Resident Inspector, the Waterford Dispatch, and the State Department of Environmental Protection,Steam Generator
Feedwater
Control Rod
ENS 4572926 February 2010 16:25:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Loss of Two Circulating Water PumpsThe "C" Circulating Water Pump tripped on high delta pressure across the screens. Another Circulating Water Pump was out of service for maintenance. This condition required a shutdown, therefore the reactor was manually tripped. This caused the steam generator level to reach the low level setpoint. There was a loss of Main Feedwater Pumps when breaking condenser vacuum. Auxiliary Feedwater Pumps started automatically upon low level in the steam generators. The letdown system was isolated post trip and the charging and letdown systems are restored to normal lineup. The plant is in Mode 3. All rods fully inserted. Decay heat is being removed via atmospheric dump valves. There are no known primary to secondary leaks in the steam generator tubes. The electrical lineup is normal with offsite power. The licensee has notified the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
ENS 4558320 December 2009 03:53:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Caused by a Turbine/Generator Electrical FaultAn automatic reactor trip occurred due to a turbine trip caused by a generator electrical fault trip. The cause of the electrical fault is under investigation. All rods fully inserted into the reactor. The auxiliary feedwater pump started and is maintaining steam generator level. The reactor is NOP and NOT. The post trip electrical line-up is being back-fed from off-site power through the RSST transformer. All other post trip actions are standard and all systems are operating as expected. There was no affect on Unit-2. The licensee will contact the NRC Resident Inspector.Steam Generator
Auxiliary Feedwater
ENS 451833 July 2009 17:05:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationReactor Trip Resulting from Turbine TripA reactor trip occurred at 1305 EDT and a Connecticut "echo" event was declared at 1315 EDT. The load dispatcher reported a loss of a 115 kV line at the time of the trip which may have caused and/or contributed to the turbine trip. The turbine trip may have resulted from a loss of B12 MCC (motor control center) which carries stator cooling pumps or a momentary interruption to non-vital instrument panels VR11 and VR21. The following events occurred: 1) loss of non-vital power may have caused the turbine trip, 2) RPS (Reactor Protective System) actuation from turbine trip, 3) system operator reported brief loss of 115 kV line immediately prior to trip, 4) Primary PORV (Pilot Operated Relief Valve on the pressurizer) lifted (at its setpoint of 2397psia), 5) Steam generators reached a high level, and 6) Main feed pump manually tripped due to high steam generator level and manually started AFW pumps (Auxiliary Feedwater Pumps). Note: The 'C' charging pump was inoperable at the time of the event. All control rods fully inserted on the trip. The plant is in its normal shutdown electrical lineup. Decay heat is being dumped to the main condenser and steam generator level is being maintained with the AFW pumps. There was no effect on Unit-3. The licensee notified the NRC Resident Inspector.Steam Generator
Feedwater
Main Condenser
Control Rod
ENS 4456412 October 2008 02:36:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Turbine Trip/ Automatic Reactor Trip on Low Steam Generator Level

At 2236 on 10/11/08 while reducing power for a planned refueling outage, "C" Steam Generator water level decreased and the turbine tripped. The reactor tripped on the turbine trip. Auxiliary feedwater initiated as expected and decay heat is being removed via the condenser steam dumps. All control rods fully inserted. No significant safety equipment is out of service and all safety buses are being supplied by offsite power. Emergency Diesel generators are available if needed. No PORVs or primary/secondary relief valves lifted. The licensee is evaluating cause of steam generator level excursion. Unit 2 is unaffected.

The licensee notified the NRC Resident Inspector.
Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
Control Rod
ENS 4432628 June 2008 15:46:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip Due to Loss of Both Feedwater PumpsAt 1146, the reactor was manually tripped due to a feedwater transient that was caused by a loss of both feedwater pumps. The exact cause of the loss of both feedwater pumps is still being investigated. Prior to the reactor trip, the licensee was performing main turbine stop valve testing and during that testing received an isolation of extraction steam. On the manual reactor trip, all control rods fully inserted. No RCS PORVs or reactor safety valves lifted. The steam generator atmospheric dump valves did lift and reseat. Decay heat is being removed to the condenser via the turbine dump valves. Auxiliary Feedwater (AFW) initiated and fed the steam generators after the loss of both main feedwater (MFW) pumps. MFW was restored and is controlling steam generator levels. AFW has been secured. The electric plant is in a normal shutdown lineup and the EDGs are available. There was no effect on Unit 3. The licensee has notified the NRC Resident Inspector, Connecticut Department of Environmental Protection, and all local emergency response organizations.Steam Generator
Feedwater
Auxiliary Feedwater
Main Turbine
Control Rod
ENS 4423824 May 2008 13:54:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
Loss of Offsite Power

The licensee entered an Unusual Event after an automatic reactor trip due to a loss of offsite power per EAL Designation PU-1. Currently the plant is stable in Mode 3 with power being supplied to the "A" & "B" Emergency Diesel Generators (EDG) running supplying power to the safety buses. Decay heat is being removed by the motor driven Auxiliary Feedwater Pump supplying water to the steam generators exhausting to atmosphere via atmospheric relief valves. There are no primary to secondary tube leaks. NRC Resident Inspector has been notified.

  • * * UPDATE FROM SKIP JORDAN TO JOHN KNOKE AT1252 EDT ON 05/25/08 * * *

At 1252 EDT the licensee terminated from their Unusual Event. After the loss of offsite power due to a failure of the Reserve Station Service Transformer (RSST) the licensee began to troubleshoot the problem as well as beginning to restore offsite power. At 1106 on 5/24/08 a cross-tie from Unit 3 was connected to Unit 2 and "A" EDG was secured. At 0950 on 5/25/08 the RSST was powered up and the non-vital busses were energized. At 1136 the "B" and "D" Reactor Coolant Pumps were started. At 1230 the vital bus was energized and the "A" EDG was secured. The licensee notified the NRC Resident Inspector. Notifications to: R1 (Marc Dupas, David Lew), R1DO (Mel Gray), NRR EO (Fred Brown), IRD MOC (William Gott), DHS (Fred Hill), FEMA (Dan Sullivan), USDA (Amanda Jimenez,), HHS (Mason Pyle), DOE (Julia Muse). The NRC Resident Inspector was notified.

Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
ENS 4423422 May 2008 18:20:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationReactor Trip Due to Lightning Strike

Lightning struck the main transformer for Millstone Unit 2 and caused actuation of the reactor protection system. The reactor had an uncomplicated trip. Reactor shutdown and all control rods fully inserted. No primary or secondary relief valves lifted. Plant is stable in Hot Standby at NOP and NOT. Level is being maintained with normal feedwater and AFW is available if required. Decay heat is being removed via steam bypass valves. The licensee notified the NRC Resident Inspector.

  • * * UPDATE PROVIDED AT 2127 EDT ON 05/23/08 FROM MARK STROLLO TO JEFF ROTTON * * *

The purpose of this update is to clarify the stated cause of the reactor trip and plant response. The original title was 'Reactor Trip Due to lightning Strike on Main Transformer'. Although there was a lightning storm in the vicinity of Millstone 2 at the time of the reactor trip, the cause of the reactor trip may be related to a grid disturbance caused by a lightning strike on a transmission line off site. This cause remains under investigation. (Initial) event report states that no primary or secondary relief valves lifted. A steam generator safety relief valve (secondary) lifted for about 34 seconds. The NRC Sr. Resident Inspector has been notified. Notified R1DO (Gray).

Steam Generator
Feedwater
Reactor Protection System
Main Transformer
Safety Relief Valve
Control Rod
ENS 4272525 July 2006 13:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationReactor Trip Breakers Opened During Maintenance on Steam Generator Wide Level Channels

The licensee was performing maintenance on "D" Steam Generator Low Level bistables when 4 (four) out of 8 (eight) trip control breakers opened possibly due to a 24 V DC power supply transient to 2 (two) of 4 (four) logic matrix relays. The reactor trip logic was verified to be functional and capable of processing valid reactor trip signals. The actuation was invalid as no plant transient occurred and no process variable was exceeded which would otherwise have required a reactor trip. The licensee notified the State and the NRC Resident Inspector.

  • * * RETRACTION ON 08/14/06 AT 0947 ET BY M. EWER TO MACKINNON * * *

Upon further review, the initial notification of this event is determined to have been conservative. A review of NUREG 1022, Rev. 2, 'Event Reporting Guidelines, 10 CFR 50.72 and 50.73,' as well as the supporting comments in the notice of final rulemaking for changes to 10 CFR Parts 50 and 72 contained in the Federal Register on October 25, 2000, indicates that these documents stress the need for reporting of system actuations. As stated in NUREG 1022, 'actuation of multichannel actuation systems is defined as actuation of enough channels to complete the minimum actuation logic. Therefore, single channel actuation logic,' Per the final rulemaking, 'the principal reason for reporting an actuation of one of these systems is that it is indicative of an unplanned plant transient that the NRC needs to evaluate to determine if action is necessary to address a safety problem.' In the event described in CR-06-06880, a portion of the RPS actuation sufficiently to cause four of the eight TCBs to open (i.e, a half trip), but not enough channels actuated to complete the minimum actuation logic for RPS (i.e, insufficient channels to fulfill the safety function of the RPS to deenergized the control rod drive mechanisms to shutdown the reactor). There was no unplanned plant transient as a result of the half trip. Determination Based on the above assessment, this condition in NOT reportable per 10 CFR 50.73(a)(2)(iv)(A) as an actuation of any of the systems listed in paragraph 10 CFR 50.73(a)(2)(iv)(B). Accordingly, the report of a 4 hour non-emergency event under 10 CFR 50.72(b)(2)(iv)(b) for a half RPS trip actuation should be withdrawn. R1DO (Lorson) notified. The NRC Resident Inspector will be notified by the licensee of this retraction.

Steam Generator
Control Rod
ENS 4236723 February 2006 15:22:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Loss of Main FeedwaterLoss of main feedwater occurred due to an instrument air line failure during a maintenance activity. The reactor was manually tripped and all control rods inserted fully. Auxiliary feedwater received an auto start signal and is providing feedwater to the steam generators. No safety relief valves or PORVs lifted. Decay heat removal is via the turbine bypass valves to the condenser. The plant is in a normal shutdown plant electrical lineup and there was no effect to Unit 3. The licensee notified the State of Connecticut and the city of Waterford. A media press release will be made at a later time. The licensee notified the NRC Resident Inspector.Steam Generator
Feedwater
Auxiliary Feedwater
Decay Heat Removal
Control Rod
ENS 421801 December 2005 19:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip Due to Low Steam Generator LevelWhile reducing power in order to enter containment, and following a manual main turbine trip due to high vibration, an automatic reactor trip on low steam generator level was received as a result of the turbine trip transient. Containment was being entered to investigate the source of an RCS identified leakage, which was less than the Technical Specification limit. In conjunction with the reactor trip, an automatic actuation of the Auxiliary Feedwater System was received as expected. All control rods fully inserted on the automatic trip. The current decay heat removal path is via the steam dumps to the main condenser. No primary or secondary relief valves lifted during the transient. There are no known primary to secondary leaks. All safety related buses are powered from offsite power. With the exception of one diesel out of service for planned maintenance, all emergency diesel generators are available and in standby. Unit 2 was not affected. The licensee notified State and local agencies and the NRC Resident Inspector.Steam Generator
Emergency Diesel Generator
Auxiliary Feedwater
Decay Heat Removal
Main Condenser
Control Rod
ENS 4202429 September 2005 17:10:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip Due to Loss of Circulating Water PumpsThe licensee reported that high wind and wave action at the site has resulted in sea weed and related debris buildup at the Unit 3 intake structure. The traveling screens were unable to keep pace with the debris buildup and two out of six circulating water pumps tripped on high differential pressure across the traveling screens. Based on procedural requirements, the licensee is required to manually trip the plant due to the loss of the two circ water pumps. The reactor trip was characterized as uncomplicated with all systems functioning as required. All rods fully inserted. No primary or secondary relief valves lifted. Auxiliary feedwater automatically started as expected and is supplying cooling water to the steam generators. Decay heat is being discharged to the condenser via the turbine bypass valves. The plant is stable in hot standby at no-load temperature and pressure. The plant trip had no impact on Unit 2. The debris buildup on the Unit 2 intake is being monitored but is less of a problem due to the orientation of the Unit 2 intake structure. The NRC Resident Inspector has been notified by the licensee. The licensee has also notified State and local authorities and has made a press release.Steam Generator
Auxiliary Feedwater
ENS 4160717 April 2005 12:42:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(a)(1)(i), Emergency Class Declaration
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Alert Declared Due to Unit 3 Main Steam Relief Valves Not Reseating After Actuation

At 09:23 the licensee indicated that several Main Steam Relief Valves lifted and stayed open. A high pressure flow signal from the secondary Steam Generator caused initiation of Unit 3 Safety Injection, which in turn caused the Reactor to trip. All rods fully inserted as required. Activation of the Safety Injection subsequently caused the Pressurizer level to go solid. About 30 minutes into the event the primary Reactor Coolant and Main Steam Systems stabilized, including the Pressurizer level and pressure. During the initial briefing, about 09:35, the licensee reported that all secondary Safety Relief Valves have reseated. Decay heat is being directed to the Atmospheric Dumps due to the Main Condenser not being available. The licensee is attempting to establish ERDS. Initial assessment of this incident is believed not to be security related, however, follow-up is being conducted to verify same. At 09:48, NRC management made a decision to enter into Monitoring Mode. At about 11:15 the licensee indicated that a valve in the Charging System indicated some leakage, therefore it was isolated. Licensee stated that no radiological releases and no S/G tube leakage was indicated. Licensee notified State and local emergency response agencies. They will notify the NRC Resident Inspector. Notified DHS (Doyle), FEMA (Biscue), DOE (Smith), USDA (Magners), and HHS (Hogan).

  • * * UPDATE FROM D. DODSON TO W. GOTT 1328 EDT 04/17/05 * * *

At approximately 0830 on April 17, 2005 Millstone Unit 3 experienced an automatic reactor trip from full power. The Reactor is in a stable shutdown condition and is proceeding to Mode 5 cold shutdown. No release of radioactivity other than those minor releases associated with normal plant operation has occurred. There were no personnel injuries associated with the event. In addition to the Reactor Trip, half-train Safety Injection (SI) and half-train Main Steam Isolation (MSI) actuations occurred. Control room personnel were successful at manually initiating full SI and MSI. SI has since been terminated and RCS pressure control has been restored. Multiple steam line safety valves (MSSV) lifted with at least one MSSV indicating a failure to reclose. As a result, an ALERT was declared at approximately 0853 due to the failure of at least one MSSV failing to reclose. All MSSVs are currently closed. Auxiliary Feedwater (AFW) actuated automatically as expected, however, the turbine driven auxiliary feedwater pump (TDAFWP) tripped on start-up and was subsequently reset locally. Both motor driven auxiliary feedwater pumps (MDAFWPs) operated as expected to maintain steam generator water levels. Due to the additional inventory injected to the Reactor Coolant System (RCS) as a result of the SI actuation, the pressurizer filled and a primary system safety valve (PSSV) actuated at a lower than expected pressure. All PSSVs are currently closed, however, there is indication of leakage past either a PSSV or Pilot Operated Relief Valve (PORV). Upon alignment of the Charging system to Refueling Water Storage Tank recirculation flow path, 2 valves had indication of packing leakage. Those packing leaks have been terminated. The cause of the event is under investigation. The licensee has issued a press release. The licensee will notify the NRC Resident Inspector. Notified R1 DO (J. White) and IRD Manager (T. McGinty)

  • * * UPDATE FROM D. DODSON TO W. GOTT AT 1915 ON 04/17/05 * * *

The previously reported time of the Alert declaration should be corrected to read 08:42. Millstone Unit 3 entered Mode 4 (Hot Shutdown) at approximately 19:03 on April 17, 2005. The event at Millstone Unit 3 was terminated at 19:05. The cause of the event is under investigation. A recovery plan is being formulated. Internal NRC notifications, DHS (Frost), NRC/EPA (Threatt), FEMA (Erwin), DOE (Morone), USDA (Smeltzer), HHS (Desi) The licensee will notify the NRC Resident Inspector. At 23:45 the Agency exited Monitoring Mode and entered into Normal Mode.

Steam Generator
Reactor Coolant System
Auxiliary Feedwater
Safety Relief Valve
Main Condenser
Main Steam
ENS 4059116 March 2004 01:20:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Trip at Millstone 2 Due to Spurious Loss of One Main Feed PumpThe licensee reported that an automatic reactor trip occurred on 3/15/04 at 2020 EST due to the spurious trip of one main feed pump which caused a low steam generator water level trip signal. The plant has two main feed pumps. Operators reset the tripped main feed pump but steam generator levels didn't recover in time. The lowest level observed was in the "B" steam generator at 15% level as compared to the normal level of 65%. The trip setpoint is at 50% level. All control rods properly inserted into the core. The auxiliary feed water system automatically initiated as designed and expected. The plant remains stable in mode 3 while the licensee commenced the post trip review to determine the cause of the main feed pump trip. Decay heat removal was established using the AFW system to feed steam generators and bleed steam to the main condenser through the condenser dump valves. The licensee notified the NRC Resident Inspector.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Main Condenser
Control Rod
05000336/LER-2004-002
ENS 405706 March 2004 05:50:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip at Millstone 2 Due to Spurious Trip of the "B" Feed PumpThe licensee reported that the "B" Steam Generator Feed Pump tripped unexpectedly and would not reset causing lowering steam generator water levels. Operators manually tripped the reactor and all control rods properly inserted. The auxiliary feed water (AFW) system automatically initiated to restore steam generator water levels. The lowest steam generator water level observed during the event was 55% level as opposed to the normal level of 70%. No primary relief valves lifted. Operators established decay heat removal capability using AFW system and the atmospheric steam dump valves. The licensee initiated a post trip review to determine the cause of the feed pump trip. The NRC Resident inspector has been notified by the licensee.Steam Generator
Auxiliary Feedwater
Decay Heat Removal
Control Rod
05000336/LER-2004-001
ENS 4036129 November 2003 03:05:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationManual Reactor Trip from 11% Power Due to Turbine VibrationAt 2205 EST on 11/28/03 while at 11% power, Millstone Unit 2 performed a required manual reactor trip when main turbine vibration reached a turbine trip set point of 12 MILS. The turbine vibration did not reduce when the turbine was tripped which required breaking condenser vacuum and ultimately a manual reactor trip. The main turbine vibrations were anticipated during power ascension due to a newly installed low pressure "Mono-Block" rotor. All control rods fully inserted during the reactor trip and no ECCS injection occurred or primary relief valves lifted. The licensee informed the NRC Resident Inspector.Main Turbine
Control Rod
ENS 4035827 November 2003 11:29:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationPlant Had a Manual Reactor Trip from 23% Power Due to Turbine Vibration

While rolling the turbine when at 20% power they experienced an over speed turbine trip. During a second attempt when at 23% power, the turbine had high vibration so they manually tripped the reactor. Cause for the vibration is being investigated since a new rotor had just been installed in the turbine. All rods fully inserted during the reactor trip and no ECCS injection occurred or primary relief valves lifted. The licensee notified the NRC Resident, the State of Connecticut and Local agencies

  • * * UPDATE AT 1423 EST ON 11/28/03 FROM FRANKS TO GOTT * * *

The following clarifying information was provided by the licensee. While at 23% power of a scheduled power ascension following a refueling outage, Millstone Unit 2 performed a required manual reactor trip when main turbine vibration reached a trip set point of 12 MILS. The main turbine vibrations were anticipated during the power ascension due to a newly installed low pressure "Mono-Block" rotor. All control rods fully inserted during the reactor trip and no ECCS injection occurred or primary relief valves lifted. The overspeed trip discussed in the original report was a test conducted prior to placing the main turbine on the grid. Notified R1DO (Dimitriadis). The licensee will notify the NRC Residence Inspector.

Main Turbine
Control Rod