Semantic search

Jump to navigation Jump to search
 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5616314 October 2022 14:07:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection InoperableThe following information was provided by the licensee via email: Unit 1 High Pressure Coolant Injection (HPCI) was declared inoperable due to an inadvertent division 2 isolation signal and subsequent valve closure. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system that is needed to mitigate the consequences of an accident. The NRC Resident will be notified.High Pressure Coolant Injection
ENS 5548423 September 2021 18:43:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System Declared InoperableDuring planned testing of the Unit 1 HPCI (high pressure coolant injection) system, flow controller oscillations occurred which prevented successful completion of the surveillance test. Operators secured Unit 1 HPCI and declared the system inoperable. HPCI inoperable placed the licensee in a 14-day limiting condition for operation that was extended to 30 days after their risk-informed completion time evaluation was done. The licensee has notified the NRC Resident Inspector.High Pressure Coolant Injection
ENS 5500016 November 2020 10:15:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection InoperableDuring normal plant start up on Limerick Unit 1, reactor pressure was raised above 200 psig prior to unisolating the Unit 1 high pressure coolant injection system (HPCI) which remained inoperable. Per TS 3.5.1, HPCI is required to be operable in Mode 2 above 200 psig. HPCI has since been restored to operable. The NRC Resident Inspector has been notified.High Pressure Coolant Injection
ENS 5334117 April 2018 14:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System Declared InoperableUnit 1 HPCI (High Pressure Coolant Injection) was declared inoperable due to a Main Pump seal leak that was identified during surveillance testing. Unit 1 HPCI was declared inoperable at 1030 EDT. HPCI was secured and was manually re-aligned to an available status. At the time of this notification, repairs have been completed and the licensee is making preparations to re-perform the surveillance. The licensee has notified the NRC Resident Inspector.High Pressure Coolant Injection
ENS 531088 December 2017 18:10:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Inoperable Due to a Leaking Check ValveU/2 HPCI (Unit 2/High Pressure Coolant Injection) was declared inoperable due to leak by of the pump discharge check valve after pump shutdown from flow testing. This resulted in cycling of the minimum flow valve. The discharge valve was closed to prevent the continued cycling of the minimum flow valve. This condition was identified during normal surveillance testing. The licensee notified the NRC Resident Inspector.High Pressure Coolant Injection
ENS 5287427 July 2017 17:15:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Injection System Declared Inoperable(Unit 2) HPCI was declared inoperable due to improper valve alignment stemming from an incorrect sequence directed from a work order. (Unit 2) HPCI was inoperable for 20 minutes and was manually re-aligned to an operable status. The licensee notified the NRC Resident Inspector.
ENS 513683 September 2015 23:01:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection (Hpci) Declared InoperableAt 1901 EDT on 9/3/2015, the Unit 2 HPCI system inboard steam supply valve isolated due to a high steam flow instrument failure. The inboard steam supply valve closed and isolated as expected. There were no indications of a steam leak. Drywell parameters and affected Reactor Enclosure rooms and piping areas were inspected with no indications of a steam leak. In addition, the steam leak detection system did not indicate any rising temperatures for any of the affected areas. The issue has caused Unit 2 HPCI to be declared inoperable and unavailable. Unit 2 has entered into a 14 day (Technical Specification) Limited Condition of Operation per T.S. 3.5.1. The licensee notified the NRC Resident Inspector.High Pressure Coolant Injection
ENS 492395 August 2013 18:56:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentBoth Offsite Power Sources Inoperable During Undervoltage TestingBoth Limerick 4 KV offsite sources were inoperable and Technical Specification 3.0.3 was entered for Unit 2 from 1456 to 1512 (EDT) during D23 4KV Undervoltage testing. During the undervoltage test, the affected diesel and one offsite source (101 Bus) are inoperable. During the test, the alternate offsite source (201 Bus) UV relay was tested and found to be inoperable, resulting in the need to declare the second offsite source (201 Bus) inoperable. When notified of the failure, action was taken to restore the 101 Bus offsite source to operable and exit the 3.0.3 condition (at) (1512 EDT). The 201 Bus Relay was successfully calibrated and tested to subsequently restore the 201 Bus to operability (at) (1543 EDT). Testing of the 201 bus UV relay is directed per procedure while the 101 bus is powered from the diesel generator. The licensee notified the NRC Resident Inspector.05000352/LER-2013-002
ENS 4883720 March 2013 18:47:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection (Hpci) Turbine Oil Leak

After securing the Unit 1 HPCI turbine from service following a planned pump, valve, and flow surveillance test an oil leak of approximately 1 pint per minute developed. The oil leak was stopped by securing the auxiliary oil pump for the HPCI system. There was no loss of oil pressure while the HPCI turbine was operating. This issue has caused the Unit 1 HPCI system to be declared inoperable and unavailable. Per LGS (Limerick Generating Station) Unit 1 Technical Specifications section 3.5.1, the HPCI system must be restored to operable status within 14 days. The cause of the oil leak is being investigated." The licensee notified the NRC Resident Inspector.

  • * * UPDATE FROM DANIEL WILLIAMSON TO DONALD NORWOOD AT 1510 EDT ON MARCH 21, 2013 * * *

UNIT 1 HPCI has been restored to operable status following repairs and post-maintenance testing at 1300 EDT on March 21, 2013. The licensee changed the reporting requirement from 10CFR50.72(b)(3)(ii)(A) to 10CFR50.72(b)(3)(v((D). The licensee will notify the NRC Resident Inspector. Notified R1DO (Trapp).

High Pressure Coolant Injection05000352/LER-2013-001
ENS 4697923 June 2011 15:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System Declared InoperableDuring performance of scheduled surveillance testing, the Unit 1 High Pressure Coolant Injection (HPCI) turbine control valve did not fully close when the system was secured. The HPCI system was removed from service and the control valve was inspected. The inspection identified a broken steam supply valve internal to the control valve. This condition would have prevented HPCI from fulfilling its safety function and is being reported for the inability of a single train system to mitigate the consequences of an accident.High Pressure Coolant Injection
ENS 4647412 December 2010 16:28:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System UnavailableDuring quarterly operability verification of the HPCI Turbine Overspeed Trip Assembly, the Trip/Reset knob was manually lifted and released to time the automatic reset function. Upon release of the knob, the Trip Assembly failed to automatically reset (the HPCI Turbine Stop and Control Valves remained closed). Adjustment of the Trip/Reset needle valve was unsuccessful. The HPCI Turbine Stop and Control Valves remain in the tripped condition, rendering HPCI unavailable. Engineering and Maintenance have been dispatched to troubleshoot and repair the Overspeed Trip Assembly and restore HPCI to operable status. All other required systems are available, operable, and protected. The licensee is in the 14 day LCO 3.5.1. The licensee has notified the NRC Resident Inspector.High Pressure Coolant Injection05000352/LER-2010-002
ENS 446232 November 2008 20:50:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHpci System Declared Inoperable Due to Controller FailureThe Unit 1 MCR (Main Control Room) HPCI (High Pressure Coolant Injection) flow indicator was observed oscillating just above zero gpm with periodic spikes to approximately 50% of scale (3000 gpm) with a concurrent drop in flow controller output signal while in standby. There were no activities in progress on or near the HPCI system when the oscillation and instrument spikes occurred. Walkdown of the instrument rack and HPCI room equipment found no abnormalities. The HPCI system was declared inoperable at 1550 hours 11/2/2008 (14 day Shutdown LCO). Troubleshooting is in progress to determine the cause of the flow oscillations. The HPCI system is considered available as there are no indications of controller failure that would impact operation in manual flow control mode. Unit 1 RCIC, and all other ECCS systems remain OPERABLE. The licensee will inform the NRC Resident Inspector.
ENS 4364517 September 2007 05:49:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHpci Unable to Perform It'S Safety Related FunctionDuring performance of the quarterly HPCI valve stroke test the HV-055-2F093, HPCI Vacuum Breaker Outboard PCIV, failed to close. The PCIV was declared inoperable. The valve was subsequently closed and de-energized to meet Technical Specification requirements. The valve did close from the handswitch on the subsequent attempt, investigation into the cause is in progress. The closure of this valve at 0149 on 9/17/07 prevents Unit 2 HPCI from performing it's safety related function. Unit 2 RCIC and all other Unit 2 ECCS systems remain operable. The licensee notified the NRC Resident Inspector.
ENS 4343621 June 2007 07:15:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHpci Inoperable Due to Quarterly Valve Stroke Test Failure

During performance of the quarterly HPCI valve stroke test the HV-55-2F006, HPCI pump discharge isolation valve to Core Spray failed to open within the maximum allowed time. The HV-55-2F006 valve is a motor operated valve and the maximum allowed opening time is 17.25 seconds. The valve was given an open signal via the hand switch as required by the test but did not initially respond. Several minutes later the valve went full open. HPCI was declared inoperable at 0315 on 6/21/2007. Cause for valve stroke time failure is not known at this time. As a result, the licensee is in a 14 day shutdown LCO. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM ARNOSKY TO HUFFMAN AT 0807 EDT ON 8/01/07 * * *

This is a retraction of the event notification made on 6/21/07 at 04:05 hours EDT. This event (#43436) was initially reported as a condition that at the time of discovery could have prevented the fulfillment of the High Pressure Coolant Injection (HPCI) system safety function under the requirement of 10CFR50.72(b)(3)(v)(D). The Unit 2 HPCI system was declared inoperable due to failure of the HPCI pump discharge isolation valve to Core Spray to open within the maximum allowed time during surveillance testing. The valve was required to open within 17.25 seconds but opened several minutes after the open signal was initiated. The open contactor was replaced and the valve was successfully tested. The affected valve was declared operable on 6/22/07 at 04:07 hours. The HPCI system was restored to operable on 6/23/07 at 04:07 hours following completion of maintenance and testing activities. An evaluation determined that HPCI was capable of injecting sufficient flow to complete its safety function through the unaffected operable injection flow path to the feedwater header. The achievable flow rate would have exceeded the leakage from a one-inch liquid line break. Also, HPCI operation remained capable of being terminated by operator action during an ATWS event. Therefore, HPCI remained capable of fulfilling its safety function while the injection flow path to Core Spray was unavailable. A condition did not exist at the time of discovery that could have prevented the fulfillment of the HPCI safety function. The licensee notified the NRC Resident Inspector. R1DO (White) notified.

Feedwater
High Pressure Coolant Injection
Core Spray
ENS 4290715 October 2006 12:46:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHpci InoperableDuring routine testing of the Unit 2 High Pressure Coolant Injection (HPCI) Turbine Hydraulic Control System, the HPCI Turbine Control Valve failed to Open as expected. The Unit 2 HPC1 system was declared Inoperable per T/S 3.5.1 (14 day LCO). This report made pursuant to 10CFR 50.72 (b)(3)(v)(D) for the inability of single train system to mitigate the consequences of an accident. All other ECCS systems are operable. The licensee notified the NRC Resident Inspector.High Pressure Coolant Injection05000353/LER-2006-001
ENS 428837 October 2006 10:57:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHpci Declared Inoperable

A division 2 Primary Containment Isolation Instrument System component inoperable required the manual isolation of High Pressure Coolant Injection (HPCI) outboard Primary Containment Isolation valves (PCIV). This isolation was required by T/S action 3.3.2.b.1. This report made pursuant to 10CFR 50,72 (b)(3)(v)(D) for the inability of single train system to mitigate the consequences of an accident. At approximately midnight on 10/7/06, Control Room Operators received a Div 2 Steam Leak Detection Trouble Alarm. Troubleshooting identified the failure as associated with the GE NUMAC drawer where temperature inputs are processed. The applicable 14-day T/S LCO Action Statement requires completion of repairs within 6 hours or isolation of HPCI 1 hour later. HPCI was isolated at 0657 EDT. There was no I&C work in progress at the time of the failure. Repair parts are available and onsite. The licensee informed the NRC Resident Inspector.

  • * * RETRACTION RECEIVED FROM EDWARD DENNIN TO JOE O'HARA AT 1500 ON 12/04/06 * * *

This is a retraction of the event notification made on 10/07/06 at 11:05 hours. This event (#42883) was initially reported as a safety system functional failure under the requirement of 10CFR50.72(b)(3)(v)(D). Unit 2 High Pressure Coolant Injection (HPCI) system was declared inoperable due to a manual closure of the HPCI steam line outboard primary containment isolation valve (PCIV). The PCIV was closed to support the maintenance on an inoperable steam leak detection (SLD) channel and to satisfy the Technical Specification (TS) 3.3.2 Isolation Actuation Instrumentation action statement. The event was initiated at 00:06 hours by a trouble alarm due to a 'self test fault' condition on the Division 2 SLD instrument channel. Troubleshooting determined that the instrument channel was inoperable. TS 3.3.2 Action 'b.1' requires the channel to be restored to operable status within 6 hours. Since this action could not be completed Table 3.3.2-1 Action 23 was applicable. Action 23 required the affected system isolation valves to be closed within one hour and the system (HPCI) to be declared inoperable. This action was completed at 06:57 hours. Two modules were replaced in the SLD instrument chassis. The instrument channel was tested satisfactorily and returned to service, Unit 2 HPCI was restored to operable status at 23:48 hours. The system was removed from service as part of a planned evolution to conduct maintenance in accordance with an approved procedure and the plant's Technical Specifications. The system was secured for the purpose of conducting maintenance on an inoperable SLD instrument channel and completing the TS action. The failed instrument did not adversely affect the HPCI system's capability of performing its safety function. HPCI remained capable of automatic initiation until the PCIV was manually closed to support maintenance by completing the TS actions. A condition did not exist at the time of discovery that could have prevented the fulfillment of the HPCI safety function. The licensee notified the NRC Resident Inspector. Notified R1DO(Sykes).

High Pressure Coolant Injection
Primary containment
ENS 4154028 March 2005 22:38:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Temporarily InoperableThe following information was obtained from the licensee via facsimile (licensee text in quotes): Unit 2 High Pressure Coolant Injection (HPCI) (was) declared inoperable due to a loose control power fuse clip associated with the HPCI Pump Suction from Suppression Pool Valve HV-055-212041. The loose clip resulted in loss of control power to this DC motor operated valve and therefore rendered the HPCI system inoperable. The fuse clip has been replaced and the HPCI system returned to an operable status. This report is being made pursuant to 10CFR 50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system that is needed to mitigate the consequences of an accident. The licensee will notify the NRC Resident Inspector.High Pressure Coolant Injection
ENS 4060019 March 2004 19:08:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHpci System Declared Inoperable at Limerick 1 Due to a Broken Hand Switch

On 3/19/04 at 14:08 PM EST, the Unit-1. HPCI system was declared inoperable due to a hand-switch failure, which prevented main control room operation of the HV-055-1F0O1 HPCI steam admission valve. The system had just successfully completed its functional surveillance test and the switch broke resulting in the operators using an, alternate means to shutdown the HPCI system. The steam admission valve is not a PCIV. The valve was open all the time; the system was shutdown using an alternate procedure. The system is now blocked for hand-switch replacement. This report is being made pursuant to 10CFR50.72(b)(3)(v) for failure of a single train accident mitigation system. The NRC Resident inspector was notified. Operators entered the unit into a 14 day LCO for declaring HPCI system inoperable.

          • RETRACTED ON 4/14/04 AT 12:56 FROM GAMBLE TO LAURA*****

This is a retraction of the event notification made on 3/19/04 at 21:00 hours. This event (#40600) was initially reported as a safety system functional failure under the requirement of 10CFR50.72(b)(3)(v)(D). Unit 1 High Pressure Coolant Injection (HPCI) system was declared inoperable due to a handswitch failure that prevented operation of the HV-055-1F001 HPCI steam admission valve from the main control room. The handswitch failed while attempting to close the steam admission valve during system shutdown at the conclusion of surveillance testing. The operator then closed the outboard steam line isolation valve to complete the system shutdown. HPCI is automatically initiated by low reactor level or high drywell pressure signals. Manual HPCI initiation for inventory makeup is performed by depressing the initiation pushbutton. Both automatic initiation and manual initiation using the pushbutton open the steam admission valve. The failed handswitch did not adversely affect the initiation of the HPCI system in the inventory makeup mode. The manual startup of the system in the test mode of operation is unavailable when the handswitch is failed. The test mode can be used to remove decay heat following an isolation of the main steam lines but it is not a credited safety function. The steam admission valve handswitch would not be used to shutdown the system when an automatic initiation signal is present; the outboard steam line isolation valve would be closed to secure the system. This is the method that was used to secure the system during the surveillance test. The handswitch is mainly used to startup and secure the system during surveillance testing. The system was removed from service as part of a planned evolution to conduct surveillance testing in accordance with an approved procedure and the plant's Technical Specifications. The system was secured for the purpose of concluding the surveillance test and replacing the handswitch. The failed handswitch did not adversely affect the systems capability of performing its safety function. A condition did not exist at the time of discovery that could have prevented the fulfillment of the HPCI safety function. Notified R1DO (B. MCDERMOTT).

High Pressure Coolant Injection
Main Steam Line