Semantic search

Jump to navigation Jump to search
 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5422919 August 2019 13:24:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual HeatAuxiliary Feedwater System InoperableAt 0924 EDT, on August 19, 2019, it was discovered that both trains of the Auxiliary Feedwater System were simultaneously inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(B). The door separating the two steam-driven Auxiliary Feedwater Pump Rooms was inadvertently left open during maintenance activities for more than an hour. The door was immediately closed upon discovery, restoring operability to the Auxiliary Feedwater System. The non-safety grade Motor-Driven Feedwater Pump remained operable during this time; additionally, the beyond-design basis diesel-driven Emergency Feedwater Pump also remained available. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.Feedwater
Auxiliary Feedwater
ENS 5270121 April 2017 06:02:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
High Switchyard Voltage Renders Both Offsite Circuits Inoperable

On 4/21/17, high grid voltage conditions were experienced, resulting in voltages higher than those established for operability of the offsite circuits. Grid voltages have been observed at approximately 355.8 kV on the nominal 345 kV system. As a result, both qualified circuits between the offsite transmission network and the onsite Class 1E AC Electrical Power Distribution System were declared inoperable at 0202 hours (EDT). Main generator voltage control has been lowered to the minimum possible excitation with the unit operating at 100 percent power. The inoperability of both offsite circuits results in a loss of safety function in accordance with NRC reporting guidance. The voltage of the onsite Essential busses remains within acceptable values, and both Emergency Diesel Generators are operable. At 0715 (EDT) on 4/21/17, grid voltage has returned to an acceptable value and the equipment was declared operable. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM ANDREW MILLER TO VINCENT KLCO ON 6/13/17 AT 1128 EDT * * *

Following the reporting of high switchyard voltage on 4/21/17, the licensee-established voltage limits were re-evaluated. The new high voltage limit has been established at 362.94 kV on the nominal 345 kV system, or 105.2 percent of nominal voltage, as compared to the previous maximum grid voltage of 103.3 percent. This new limit is above the 355.8 kV experienced on 4/21/17. Therefore, the equipment remained operable and no loss of safety function existed for the qualified circuits between the offsite transmission network and the onsite Class 1E AC electrical power distribution system, and the notification made per 10 CFR 50.72(b)(3)(v)(A-D) is being retracted.

An evaluation of the past three years of switchyard voltage data was also performed, and it was concluded the AC power system and its connected safety-related equipment remained capable of performing its required safety functions during the three-year evaluation period. The NRC Resident Inspector has been briefed on the evaluation results and informed of this retraction. Notified the R3DO (Stone).

Emergency Diesel Generator
ENS 5224716 September 2016 20:57:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Essential Busses Not Aligned to Power Transformers During Plant Startup

At 1657 Eastern Daylight Time (EDT) the plant entered Mode 4 (from Mode 5), and subsequently, at 1710 EDT, it was discovered that 480V AC essential busses E1 and F1 were being supplied from the shutdown operations transformers. The essential busses E1 and F1 are required to be aligned to the power operations transformers in Mode 4 for operability in accordance with TS 3.8.9. With both E1 and F1 essential busses aligned to the shutdown operations transformers with the plant in Mode 4, both trains of the essential electrical power distribution system were inoperable, resulting in a loss of safety function. At 1733 EDT both E1 and F1 essential busses were aligned to the power operations transformers as required by TS 3.8.9. This issue is being reported as a loss of safety function of the essential electrical busses. The NRC Resident Inspector has been notified of the event.

  • * * RETRACTION AT 1315 EST ON 11/09/2016 FROM ANDY MILLER TO JEFF HERRERA * * *

Engineering reviewed the actual conditions during the approximate 36 minutes the 480V AC essential busses were being supplied from the shutdown operations transformers. Grid voltages were higher than assumed minimum voltages, and electrical loading during Mode 4 conditions were reduced from expected full power operation loading. As a result, Engineering determined that all equipment remained capable of performing its required functions while connected to the shutdown operations transformers. Because the equipment remained capable of satisfying the requirements for Operability, no condition existed that could have prevented the fulfillment of a safety function. Therefore, no loss of safety function existed for the 480V AC essential buses, and the notification made per 10 CFR 50.72(b)(3)(v)(A-D) by the Davis-Besse Nuclear Power Station on 9/16/2016 (EN# 52247) is being retracted. The NRC Resident Inspector has been briefed on the evaluation results and informed of this retraction. Notified the R3DO (Jeffers).

ENS 5118527 June 2015 03:35:0010 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual HeatBoth Aux Feedwater Trains Declared InoperableOn June 26, 2015 at 2335 (EDT), with Auxiliary Feedwater (AFW) train 1 declared inoperable for scheduled surveillance testing, AFW train 2 was declared inoperable as a result of the supply breaker for SW1395, Service Water Loop 2 secondaries isolation valve, being found open, i.e. out of its required position. Limiting Condition for Operation (LCO) 3.7.5 Condition D was entered for two Emergency Feedwater Trains inoperable. AFW Train 1 and the non-safety related motor driven AFW pump were available to provide emergency feedwater if required. The breaker was verified to be functioning as required and then closed, restoring the safety function. All associated LCOs were exited by 0133 (EDT) on June 27, 2015. The licensee notified the NRC Resident Inspector.Feedwater
Service water
Auxiliary Feedwater
05000346/LER-2015-003
ENS 4709626 July 2011 20:00:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Unanalyzed Conditions Involving the Safety Related Direct Current (Dc) SystemInformation was received in regards to an old design issue identified in a Component Design Basis Inspection Unresolved Item. Two issues were identified with the Safety-Related Direct Current (DC) System: 1. The plant's licensing basis states that non-safety-related electrical equipment, whose failure under postulated environmental conditions could prevent satisfactory accomplishment of the specified safety-related electrical equipment required safety functions, is qualified as required. However, the Reactor Coolant Pump (RCP) backup lift oil pump motors and the Containment Emergency Lighting Panel L49E1 are located inside containment and are not environmentally qualified. This could challenge the adequacy of electrical separation between the potentially grounded non-safety related equipment and the safety related batteries. 2. Automatic transfer switches are installed to automatically transfer non-safety related loads such as non-nuclear instrumentation, station annunciators, plant computer, and integrated control system between two non-safety related inverters, which receive power from the safety-related DC power system. If a ground fault existed on one of these switches, the fault could be transferred from one power source to the redundant source, potentially impacting the ability of both safety-related DC power sources to perform their required functions. This type of transfer is not permitted by the plant's licensing basis. The breakers for the 4 RCP backup lift oil pump motors and for the Containment Emergency Lighting were opened. One train of instrumentation power was placed on its alternate power source from the Alternating Current (AC) system, eliminating the potential to impact both trains of the DC power system. This condition is being reported per 10 CFR 50.72(b)(3)(ii)(B) as a condition that results in the plant being in an unanalyzed condition that significantly degrades plant safety, and per 10 CFR 50.72(b)(3)(v)(A-D) as an event or condition that could have prevented fulfillment of a safety function. The licensee has notified state and local authorities and the NRC Resident Inspector.05000346/LER-2011-004
ENS 466533 March 2011 18:53:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
Temporary Loss of Emergency Feedwater TrainsWhile testing fire detection systems, a radio was keyed in the vicinity of the Auxiliary Shutdown Panel. Control Room alarms that occurred at the same time led to a review of plant data. This review revealed two momentary events (approximately 8 and 19 seconds) over an approximate two minute period that caused momentary reductions in the control signals to the Auxiliary Feedwater Pump and Motor-Driven Feedwater Pump discharge control valves. These momentary signal reductions resulted in all trains of Emergency Feedwater being inoperable for approximately two minutes, pending further evaluation. With all trains of Emergency Feedwater inoperable, this event is being reported in accordance with 10 CFR 50.72(b)(3)(v) as a momentary loss of safety function for equipment needed to (A) shut down the reactor and maintain it in a safe shutdown condition and to (B) remove residual heat. Fire detection testing has been completed, and a sign placed on the Auxiliary Shutdown Panel Room door stating that no radio usage is permitted inside the room. All trains of Emergency Feedwater are now operable. The licensee has notified the NRC Resident Inspector.Feedwater
Auxiliary Feedwater
05000346/LER-2011-003