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ENS 569411 February 2024 18:17:00Offsite Notification - Workplace Injury

The following information was provided by the licensee via email: On February 1, 2024, a contract worker was transported offsite for medical treatment due to a work-related injury that required the individual to be admitted to the hospital. The individual was free-released from the site prior to transport. The injury and hospitalization were reported by the contract worker's employer to OSHA per 29 CFR 1904.39(a)(2). Based upon that notification to another government agency, Tennessee Valley Authority is reporting this per 10 CFR 50.72(b)(2)(xi). The NRC Senior Resident Inspector has been notified of this event.

  • * * RETRACTION ON 2/29/24 AT 12:29 EST FROM MATTHEW SLOUKA TO KAREN COTTON * * *

The following information was provided by the licensee via email: The purpose of this notification is to retract a previous Event Notification, EN 56941, reported on 02/01/2024. On 02/01/2024, at 15:32 EST, Browns Ferry Nuclear Plant (BFN) made an Event Notification 56941 notifying the NRC of a notification to another government agency. During further review of NRC reporting guidance, BFN has concluded that the contract worker's employer report to OSHA was below the reporting threshold outlined in NUREG 1022, Revision 3. The NRC Resident Inspector has been notified.

ENS 5641115 March 2023 03:57:00Reactor Coolant System (RCS) Boundary Degraded Condition

The following information was provided by the licensee via email: At 2257 (CDT) on 3/14/2023 during the 2R22 refueling outage on Browns Ferry Nuclear Plant Unit 2, it was determined there was RCS boundary leakage from five of eight sensing lines that pass through containment penetrations X-30 and X-34 that did not meet the requirements of Section XI, of the ASME Boiler and Pressure Vessel Code. The condition will be resolved prior to plant startup. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 03/28/2023 AT 1059 EST FROM CASEY CARTWRIGHT TO THOMAS HERRITY * * *

The following information was provided by the licensee via email: The purpose of this notification is to retract a previous Event Notification, EN 56411 reported on 3/14/23. Following the initial notification, further analysis of the condition was performed. It was determined that the leaking pipe weld was ASME Section XI Code Class 2 piping which falls under the requirements of ASME Section XI Subsection IWC and not Subsection IWB. Therefore, this condition does not represent a serious degradation of the nuclear power plant, including its principle safety barriers. Based upon the above, the leaks identified on the ASME Section XI Code Class 2 equivalent Main Steam sense lines are not reportable under 10 CFR 50.72(b)(3)(ii). Therefore, the NRC non-emergency 10 CFR 50.72(b)(3)(ii) report was not required and the NRC report 56411 can be retracted and no Licensee Event Report under 10 CFR 50.73(a)(2)(ii) is required to be submitted. Notified R2DO (Miller)

ENS 549835 November 2020 03:50:00High Pressure Coolant Injection Inoperable

At 2150 CST on 11/04/2020, it was discovered that Unit 1 High Pressure Coolant Injection System (HPCI) was INOPERABLE; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. During performance of 1-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated Reactor Pressure, Unit 1 HPCI was manually tripped by the control room operator due to local report of excessive shaking of the cooling water supply from the booster pump line. There was no impact to the safety of the public or plant personnel. The NRC Resident Inspector has been notified. CR 1650042 documents this condition in the Corrective Action Program. The Unit is in a 14-day LCO 3.5.1(c). The RCIC System is operable.

  • * * RETRACTION FROM MARK ACKER TO HOWIE CROUCH AT 1607 EST ON 12/29/2020 * * *

ENS Event number 54983, made on 11/05/2020 is being retracted. NRC notification 54983 was made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72 were met when Unit 1 HPCI was manually tripped by the control room operator due to a local report for excessive shaking of the cooling water supply from the booster pump line. A subsequent engineering evaluation concluded on 11/06/2020 there was reasonable assurance of operability with no additional intrusive maintenance performed and that the condition was bounded by a previous evaluation documented in (Condition Report) CR 1347736. As such, the circumstances discussed in the report did not result in any condition that at the time of discovery could have prevented the fulfillment of the safety function of structures of the system that are needed to mitigate the consequences of an accident. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v). TVA's evaluation of this event is documented in the corrective action program. The licensee has notified the NRC Resident Inspector. Notified R2DO (Miller).

Time of Discovery
ENS 5394217 March 2019 12:35:00En Revision Imported Date 4/24/2019

EN Revision Text: HIGH PRESSURE COOLANT INJECTION SYSTEM DECLARED INOPERABLE At 0735 CDT on March 17, 2019, the High Pressure Coolant Injection (HPCI) system was isolated due to a water-side leak from the HPCI Gland Seal Condenser. Unit 3 declared the HPCI system Inoperable and entered Technical Specification LCO 3.5.1 Condition C with required actions to verify the Reactor Core Isolation Cooling system is Operable, and to restore the HPCI system to Operable status within 14 days. All other Unit 3 Emergency Core Cooling Systems (ECCS) remain Operable. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(V)(D), 'Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.' This is also reportable as a 60-day written report in accordance with 10 CFR 50.73(a)(2)(V)(D). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified of this event.

  • * * RETRACTION FROM WESLEY CONKLE TO HOWIE CROUCH ON 4/23/19 AT 1549 EDT * * *

ENS Event Number 53942, made on March 17, 2019, is being retracted. NRC Notification 53942 was made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72 (b)(3)(v)(D) were met when the licensee discovered an event, that at the time of discovery, could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. At 0735 CDT, on March 17, 2019, during the performance of a routine surveillance, a momentary pressure transient of 844 psig from the Feedwater system was introduced into the High Pressure Coolant Injection (HPCI) system discharge and suction piping that ruptured the seal on the gland seal condenser and flooded the U3 HPCI Room. Unit 3 HPCI was declared inoperable due to isolation of the waterside of the HPCl system. On April 11, 2019, a Past Operability Evaluation was completed which determined that the HPCI System remained operable. The evaluation of the potential pressure transient and room flooding concluded that the HPCI System could have performed its specified safety function of vessel injection throughout the time that the gland seal was ruptured. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(D). TVA's evaluation of this event is documented in the Corrective Action Program in Condition Report 149973. The licensee has notified the NRC Resident Inspector. Notified R2DO (Ehrhardt).

Time of Discovery
Past operability
ENS 5375021 November 2018 06:00:00En Revision Imported Date 12/31/2018

EN Revision Text: HPCI UNEXPECTEDLY TRANSFERRED TO ALTERNATE SUCTION SOURCE DURING TESTING At 2125 (CST) on 11/21/2018, it was discovered that U1 High Pressure Coolant Injection System (HPCI) was inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. During performance of a routine surveillance, HPCI automatically transferred from its normal suction source to the alternate suction source. The control room operator then manually tripped the HPCI turbine. HPCI was already inoperable in accordance with Technical Specifications (TS) Limiting Condition for Operability (LCO) 3.5.1, ECCS Operating, Condition C during performance of the surveillance. However, this condition was not expected nor induced by the testing. There was no impact to the safety of the public or plant personnel. The NRC Resident Inspector has been notified. CR 1469109 documents this condition in the Corrective Action Program.

  • * * RETRACTION ON 12/28/18 AT 1300 EST FROM MARK MOEBES TO JEFFREY WHITED * * *

ENS Event Number 53750, made on November 22, 2018, is being retracted. NRC notification 53750 was made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72(b)(3)(v)(D) were met when the licensee discovered an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. During performance of a routine surveillance, the High Pressure Coolant Injection (HPCI) System automatically transferred from its normal suction source to the alternate suction source. As a result, Unit 1 HPCI was declared inoperable. On December 20, 2018, a Past Operability Evaluation was completed which determined that the HPCI System remained operable. The evaluation determined that the HPCI System could have performed its specified safety function of vessel injection throughout the time that the suction path was aligned to the torus. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(D). TVA's evaluation of this event is documented in the Corrective Action Program in Condition Report 1469109. The licensee has notified the NRC Resident Inspector. Notified R2DO (Desai).

Time of Discovery
Past operability
ENS 5367821 October 2018 05:00:00Technical Specification Shut Down Due to Chemistry Limit Exceeded

At 0200 Central Daylight Time on 10/21/2018, Browns Ferry Nuclear Plant Unit 3 commenced a reactor shutdown as required by the Technical Requirements Manual Limiting Condition for Operation 3.4.1 Coolant Chemistry Condition D due to conductivity greater than 10 micro mho/cm at 25 degrees Celsius. The required action for this condition is to immediately initiate an orderly shutdown and be in Mode 4 as rapidly as cooldown rate permits. This event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Senior Resident Inspector has been notified.

  • * * RETRACTION AT 1719 EST ON 12/13/2018 FROM NEEL SHUKLA TO MARK ABRAMOVITZ * * *

ENS Event Number 53678, made on 10/21/18, is being retracted. NRC notification 53678 was made to ensure that the four-hour non-emergency reporting requirements of 10 CFR 50.72 were met when the licensee discovered a condition requiring shut down of a reactor. 10 CFR 50.72 requires a report in accordance with 50.72(b)(2)(i) for any Technical Specifications (TS) required reactor shutdown. NUREG-1022 only specifies TS applicability and makes no mention of a Technical Requirements Manual (TRM) required shutdown. Because the shutdown comes from the TRM and not the TS as discussed in 10 CFR 50.72 and NUREG-1022, an EN was not required. TVA's evaluation of this event notification is documented in the corrective action program. The licensee notified the NRC Resident Inspector. Notified the R2DO (Ehrhardt).

ENS 5326716 March 2018 05:00:00Unanalyzed Condition Affecting Residual Heat Removal System

At 1604 (CDT) on March 16, 2018, Browns Ferry Nuclear Plant (BFN) Engineering reported an unanalyzed condition affecting the Residual Heat Removal (RHR) heat exchangers in a postulated fire event. It was discovered that the Residual Heat Removal Service Water (RHRSW) heat exchanger piping associated (with) the credited heat exchangers in the NFPA 805 Nuclear Safety Capability Analysis (NSCA) could experience water hammer damage. Fire damage to the cables for the RHRSW outlet motor operated valves could cause the valves to spuriously open and drain the RHRSW piping. Subsequent starting of the RHRSW pumps on the affected header could cause water hammer loads and damage the piping. Review of NFPA 805 analyses show the cables associated with this condition are routed in Fire Areas 01-03, 02-03, 02-04, 03-03, 16 and 23. There are 11 cases where the deterministically credited heat exchanger could be affected. Compensatory fire watch measures have been established. This event requires an 8 hour report in accordance with 10CFR50.72(b)(3)(ii)(B), 'Any event or condition that results in: (B) The nuclear power plant being in an unanalyzed condition that significantly degrades plant safety. CR 1139620 documents this condition in the Corrective Action Program. The NRC Resident Inspector has been notified.

  • * * RETRACTION AT 2215 EST ON 11/29/2018 FROM NEEL SHUKLA TO MARK ABRAMOVITZ * * *

NRC notification 53267 was made to ensure that the eight-hour non-emergency reporting requirements of 10 CFR 50.72 were met when the licensee discovered an unanalyzed condition with the potential to significantly degrade plant safety. On August 22, 2018, an independent analysis was completed which determined that the RHRSW system would remain functional during the postulated scenario. Based on this analysis, a revised functional evaluation was performed by BFN which determined that the condition did not constitute an unanalyzed condition that significantly degraded plant safety. For credited RHR heat exchangers for fire events in Fire Areas 01-03, 02-03, 02-04, 03-03, 16, and 23, the RHRSW piping will remain intact and the valves will operate manually after a water hammer event. This condition did not significantly degrade plant safety and is therefore not reportable under 10 CFR 50.72(a)(2)(ii)(B). On November 16, 2018, TVA canceled the 60 day report which had been submitted for this condition. TVA's evaluation of this event notification is documented in the corrective action program. The licensee has notified the NRC Resident Inspector. Notified the R2DO (Shaeffer).

Unanalyzed Condition
Fire Watch
ENS 5115312 June 2015 15:30:00High Pressure Coolant Injection Declared Inoperable

On June 12, 2015 at 1030 CDT, the Browns Ferry Nuclear Plant Unit 3 High Pressure Coolant Injection (HPCI) system was declared inoperable due to the time to drain the Turbine Exhaust Drain Pot after running the system for periodic testing. The concern is that the turbine may be partially flooded after shutting down and a subsequent restart could cause a water hammer event, possibly damaging the system. This issue was previously analyzed by Engineering as acceptable, but the time to drain the pot after the latest test indicates more water in the exhaust than the maximum amount used in the analysis. Technical Specification 3.5.1, ECCS Operating, Condition C, was entered as a result of the inoperable HPCI system. This constitutes an unplanned HPCI system inoperability and requires an 8-hour NRC notification in accordance with 10 CFR 50.72(b)(3)(v)(D) due to the failure of a single train system affecting accident mitigation, and a 60 day written report in accordance with 10 CFR 50.73(a)(2)(v) The NRC Resident Inspector has been notified. The Technical Specification Action statement allows 14 days to restore the HPCI system to operable status.

  • * * RETRACTION FROM MATTHEW SLOUKA TO DANIEL MILLS AT 1623 EDT ON 9/10/15 * * *

Browns Ferry Nuclear Plant is retracting the 8-hour NRC notification (EN# 51153) made on June 12, 2015 at 1030 CDT. The notification on June 12, 2015, reported a condition where the HPCI system was declared inoperable due to the time to drain the Turbine Exhaust Drain Pot after running the system for periodic testing. The concern was that the turbine may be partially flooded which could cause water hammer and damage the HPCI system. Subsequent evaluation concluded that the HPCI system under the identified flooded turbine conditions will not produce a transient that exceeds design values, therefore, HPCI system operability was maintained and no reportable condition existed during this time. The NRC Resident Inspector has been notified of this retraction. Notified R2DO (Shaeffer).

ENS 4588830 April 2010 21:48:00Light Socket Short Causes Isolation Systems to Actuate

At 1648 CDT, while the Control Bay AUO (Auxiliary Unit Operator) was attempting to change a light bulb for 1-IL-99-1AA, 1A (Reactor Protection System) RPS (Motor Generator) MG Set available light, the light socket shorted causing the loss of 1A RPS. The loss of 1A RPS resulted in Groups 2, 3, 6, and 8 primary containment isolations and initiated Standby Gas Treatment and Control Room Emergency Ventilation. All systems responded as designed. The Control Room operators entered the appropriate abnormal operating instruction, 1-AOI-99-1, to restore the affected systems. Operations entered TS LCO 3.3.1.1 conditions A.1 (place channel in Trip in 12 hours) and C.1 (restore RPS trip capability in 1 hr). At 1734 CDT, Operations exited TS LCO 3.3.1.1 upon restoration of 1A RPS per 1-AOI-99-1. This event is reportable within 8 hours per 10CFR 50.72(b)(3)(iv)(A) 'Any event or condition that results in a valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B) (b. General Containment Isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs)), except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' This event also requires an LER within 60 days per 10CFR 50.73(a)(2)(iv)(A). The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM RAY SWAFFORD TO DONG PARK AT 1522 EDT ON 6/29/10 * * *

Retraction of an 8 hour non-emergency notification for invalid Primary Containment Isolation System (PCIS) actuation from a loss of power to the Reactor Protection System (RPS) 1A. Browns Ferry Nuclear Plant (BFN) is retracting the 10 CFR 50.72(b)(3)(iv)(A) eight-hour non-emergency report made on April 30, 2010, at 2131 hours Central Daylight Time. BFN's initial report was categorized as a valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B). The loss of power to RPS 1A resulted in PCIS Groups 2, 3, 6, and 8 primary containment isolations and initiation of Standby Gas Treatment and Control Room Emergency Ventilation. However, plant conditions which require PCIS actuations and system initiations (e.g., low reactor water level, high drywell pressure, abnormal area radiation level, high area temperature) did not exist, therefore, the actuation was invalid. As a consequence, TVA has concluded that this event does not meet the reporting requirements of 10 CFR 50.72. The event is reportable under 10 CFR 50.73(a)(2)(iv)(A). A 60-day phone call will be made in accordance with 10 CFR 50.73(a)(1). (See EN #46054) TVA's evaluation of this event is documented in the Corrective Action Program (PER 227662). TVA has notified the NRC Resident Inspector. Notified R2DO (Desai).

ENS 4522724 July 2009 19:15:00Hpci Inoperable Due to Oil Leak in Mechanical Trip Hold Valve

During performance of surveillance 1-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated Reactor Pressure, the HPCI Turbine Stop Valve Mechanical Trip Hold Valve, 1-PCV-73-18C, developed an oil leak of approximately 0.25 gpm. HPCI was INOPERABLE at the time of discovery due to performance of SR and continued to be INOPERABLE due to the oil leak that developed. This event is reportable within 8 hours in accordance with 10CFR 50.72(b)(3)(v) as an event or condition that at the time of discovery could have prevented the fulfillment of a safety function. It also requires a 60 day written report in accordance with 10CFR 50.73(a)(2)(vii). The licensee notified the NRC Resident Inspector.

  • * * RETRACTION ON 9/22/2009 AT 1700 EDT FROM RAYMOND SWAFFORD TO DONG PARK * * *

On July 24, 2009, the High Pressure Coolant Injection (HPCI) Stop Valve Mechanical Trip Hold Valve (PCV-073-0018C) developed a ruptured diaphragm resulting an approximate 0.25 to 0.5 gallon per minute oil leak during scheduled performance of Surveillance Instruction, HPCI Main and Booster Pump Set Developed Head and Flow Rate at Rated Reactor Pressure. At the time BFN (Browns Ferry Nuclear) made (event) notification 45227, there were concerns regarding the ability of HPCI to fulfill its safety function, hence, BFN made an eight hour notification in accordance with 10CFR50.72(b)(3)(v)(B) and 10CFR50.72(b)(3)(v)(D). An evaluation performed in response to this notification concluded that the HPCI System was capable of performing its intended safety function with the oil leak. TVA Engineering evaluated the rate of oil loss considering a worse case failure of PCV-073-0018C diaphragm and determined that the turbine oil system capacity is such that the oil loss thru the failed diaphragm would not impact HPCI operation during its mission time for the Design Basis accidents and transients for which HPCI is credited. The circumstances discussed in the notification did not result in any condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or system that are needed to remove residual heat and mitigate the consequences of an accident. Therefore, this event is not reportable under 10CFR50.72(b)(3)(v)(B) and 10CFR50.72(b)(3)(v)(D). TVA documented the evaluation of this event notification in its corrective action program (PER 177206). The licensee has notified the NRC Resident Inspector. Notified R2DO (Rudisail).

Time of Discovery
Mission time
ENS 442521 June 2008 16:48:00Lube Oil Moisture Content Greater than Acceptable Limit

A sample was taken of the lubrication/control oil from the Unit 1 High Pressure Coolant Injection (HPCI) System for moisture content analysis. The results of this analysis concluded that the moisture content in the oil exceeded acceptable levels. As a result of this condition the Browns Ferry Nuclear Unit 1 HPCI system was declared inoperable at 11:48 on 6/1/08. This event is reportable within 8 hours in accordance with 10 CFR 50.72 (b)(3)(v) as event or condition that at the time of discovery could have prevented the fulfillment of a safety function. It also requires a 60 day written report in accordance with 10 CFR 50.73 (a)(2)(vii). Unit 1 remains at 100% power. Unit 1 has entered Technical Specification LCO 3.5.1 and is performing the required actions. Troubleshooting of the moisture intrusion condition is in progress, and a corrective action plan is being developed. The NRC Resident inspector has been notified.

  • * * RETRACTION AT 1239 EDT ON 7/17/08 FROM BAKER TO HUFFMAN * * *

ENS Event Number 44252, made on June 1, 2008, is being retracted. NRC Notification 44252 was conservatively made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72 were met when an oil sample indicated the Unit 1 High Pressure Coolant Injection (HPCI) System turbine oil system contained excessive amounts of water. An evaluation performed in response to this report concluded that the Unit 1 HPCI System was capable of performing its intended safety function with the turbine oil system containing more water than recommended in the TVA Lubrication Oil Analysis and Monitoring Program. TVA found through an engineering evaluation that the amount of water contained in the turbine oil system would not impact the HPCI operation during its mission time for the Design Basis Loss-of-Coolant Accident. As such, the circumstances discussed in the report did not result in any condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat, or mitigate the consequences of an accident. Thus, there was no impact on nuclear safety. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(B) or 10 CFR 50.72(b)(3)(v)(D). TVA's evaluation of this issue is documented in the corrective action program (PER 145517). The licensee has notified the NRC Resident Inspector. R2DO (Haag) notified.

Time of Discovery
Mission time
ENS 441864 May 2008 20:30:00Hpci Declared Inoperable

During the required quarterly oil sample taken following scheduled flow rate surveillance, the Unit 2 HPCI oil system was found to contain excessive amounts of water. HPCI declared inoperable. This event is reportable under 10CFR50.72(b)(3)(v)(B), 'Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat.' Unit 2 remains at 100% power 14 day TS LCO 3.5.1 has been entered and troubleshooting is in progress. NRC Resident has been notified.

  • * * RETRACTION PROVIDED AT 1648 ON 06/30/08 FROM MICHAEL HUNTER TO JEFF ROTTON * * *

ENS Event Number 44186, made on May 4, 2008, is being retracted." NRC Notification 44186 was conservatively made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72 were met when a required quarterly oil sample taken following a flow rate surveillance on the Unit 2 High Pressure Coolant Injection (HPCI) System indicated that the turbine oil system contained excessive amounts of water. An evaluation performed in response to this report concluded that the HPCI System was capable of performing its intended safety function even though the turbine oil system contained more water than recommended in the TVA Lubrication Oil Analysis and Monitoring Program. TVA found through visual inspection and engineering evaluation that the amount of water contained in the turbine oil system would not impact the HPCI operation during its' mission time for the Design Basis Loss-of-Coolant Accident. As such, the circumstances discussed in the report did not result in any condition that at the time of discovery could have prevented the fulfillment of the safety function of structures of system that are needed to remove residual heat. Thus, there was no impact on nuclear safety. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(B). TVA's evaluation of this event notification is documented in the corrective action program. The licensee has notified the NRC Resident Inspector. The licensee has changed the oil and continues to monitor the oil reservoir monthly until the problem causing the excessive water (Turbine Admission valve) is corrected . Notified R2DO (O'Donohue)

Time of Discovery
Mission time
ENS 4394029 January 2008 00:43:00High Pressure Core Injection (Hpci) Inoperable

On 1/28/08 at 1843 CST, Browns Ferry Unit 1 was performing 1-SR-3.3.5.1.3(D) HPCI System Condensate Header Low Level Switch Calibration and Functional Test when 1-LS-73-56A failed to actuate. Per TS 3.3.5.1, 1-LS-73-56A is inoperable. 1-SR-3.3.5.1.3(D) defeats the logic relay normally actuated by 73-56A & B. This causes HPCI to be inoperable per TS 3.3.5.1.D if the relay is defeated for greater than 1 hour. Failure of the 73-56A switch prevented restoration of the relay within the 1 hour time frame. This event is reportable under 10CFR 50.72(b)(3)(v)(B) 'any event or condition that at the time of discovery could have prevented the fulfillment of the Safety Function of structures or systems that are needed to: Remove Residual Heat' and 10CFR 50.72(b)(3)(v)(D) 'any event or condition that at the time of discovery could have prevented the fulfillment of the Safety Function of structures or systems that are needed to: mitigate the consequences of an accident.' This event also requires a 60 day written report in accordance with 10CFR 50.73(a)(2)(v)(B) and 10CFR 50.73(a)(2)(v)(D). The defeated relay was restored to normal and the HPCI system returned to operable status at 2330 CST on 1/28/08. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION AT 1359 EDT ON 3/17/08 FROM RASMUSSEN TO HUFFMAN * * *

On January 28, 2008, Browns Ferry Unit 1 entered an LCO to perform a planned maintenance activity, High Pressure Coolant Injection System Condensate Header Low Level Switch Calibration and Functional Test, 1-SR-3.5.5.1.3(D). During the calibration of 1-LS-073-0056A and 1-LS-073- 0056B, 1-LS-073-0056A was found inoperable. The removal of both level switches from service (and as a result the HPCI transfer on low condensate header level function) was a planned maintenance activity, performed in accordance with an approved procedure and in accordance with the plants TSs. During this time no condition was discovered that could have prevented HPCI from performing its intended function because 1-LS-073-056B was considered OPERABLE. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(B) or 10 CFR 50.72(b)(3)(v)(D). The licensee notified the NRC Resident Inspector. R2DO(Lesser) notified.

Time of Discovery
ENS 4380928 November 2007 08:30:00Hpci Inoperable Due to Level Switch Failure

On 11/28/2007 at 0230 CST, Browns Ferry Unit 1 received a 'HPCI PUMP SUCT HDR LEVEL LOW' alarm and HPCI automatically transferred its suction from the Condensate Storage Tank (CST) to the Suppression Pool. With the HPCI suction not aligned to its normal source, the HPCI system was declared inoperable. At 0710 CST, trouble shooting identified a level switch malfunction. This switch was removed from service allowing HPCl to be returned to the normal Standby Readiness configuration. The System was declared Operable at 0710 when the system was aligned back to normal suction source. This event is reportable under 10CFR 50.72(b)(3)(v)(B) 'any event or condition that at the time of discovery could have prevented the fulfillment of the Safety Function of structures or systems that are needed to: Remove Residual Heat' and 10CFR 50.72(b)(3)(v)(D) 'any event or condition that at the time of discovery could have prevented the fulfillment of the Safety Function of structures or systems that are needed to: mitigate the consequences of an accident.' This event also requires a 60 day written report in accordance with 10CFR 50.73(a)(2)(v)(B) and 10CFR 50.73(a)(2)(v)(D). The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM TODD BOHANAN TO HOWIE CROUCH AT 1311 HRS. EST ON 01/25/08 * * *

ENS Event Number 43809, made on 11/28/2007, is being retracted. NRC Notification 43809 was conservatively made to ensure that the eight-hour non-emergency reporting requirements of 10 CFR 50.72 were met pending the evaluation of an atypical system alignment with the High Pressure Coolant Injection (HPCI) (system). An evaluation has been performed in response to this event. The evaluation concluded that the HPCI system was capable of performing its intended safety function in this atypical configuration. As such, the circumstances discussed in the report did not result in any condition that could have prevented the fulfillment of the safety function of structures or systems needed to mitigate the consequences of an accident. Thus there would have no impact on nuclear safety. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(B) or 10 CFR 50.72(b)(3)(v)(D). TVA's evaluation of this event is documented in the corrective action program. The licensee has notified the NRC Resident Inspector. Notified R2DO (Desai).

Time of Discovery
ENS 4339228 May 2007 06:00:00Hpci Pump Inoperable Due to Differential Pressure Setting Not within Specification

On 5/28/07 at 0100 CDT, Browns Ferry Unit 1 was performing 1-SR-3.5.1.7 (Comp) HPCI Comprehensive pump test when it was determined that HPCI pump set differential pressure was not within specifications and therefore would not support a declaration of operability for HPCI. The event is reportable under 10CFR 50.72(b)(3)(v)(B) - 'any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat' and 10CFR 50.72(b)(3)(v)(D) - 'any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident'. This event also requires a 60 day written report in accordance with 10CFR 50.72(b)(3)(v)(B) and 10CFR50.73(a)(2)(v)(D). Initial investigation reveals a potential problem with the test equipment. The licensee notified the NRC Resident Inspector.

  • * * RETRACTION FROM M. RASMUSSEN TO W. HUFFMAN AT 1810 EDT ON 6/29/07 * * *

This report is being retracted. Engineering has re-evaluated the test results and determined that HPCI System pump met its design basis requirements during testing activities. As such, the circumstance discussed in this event report did not result in any condition that could have prevented the fulfillment of the safety function of structures or systems needed to mitigate the consequences of an accident. Therefore, this event is not reportable under 10CFR50.72(b)(3)(v)(B) or 10CFR50.72(b)(3)(v)(D). The licensee notified the NRC Resident Inspector. R2DO (Ayres) notified.

Time of Discovery