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 Entered dateSiteRegionReactor typeEvent description
ENS 570033 March 2024 15:51:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopThe following information was provided by the licensee via email: At 1142 CST on 3/3/2024, with Unit 2 in Mode 1 at 29 percent power, the reactor automatically tripped due to a turbine trip caused by a loss of suction to the 22 main feedwater pump. All systems responded normally post trip. Decay heat is being removed via the auxiliary feedwater water system. Secondary steam control mechanism is the steam generator PORVs (power operated relief valves). Unit 1 remains at 100 percent power and is unaffected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The resident NRC inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The trip occurred while the licensee was returning to power operations after a refueling outage. During the trip, all rods inserted into the core. The plant is in a normal shutdown electrical lineup with offsite power available. The plant will be maintained at normal operating temperature and pressure. There is no known primary to secondary leakage. The cause of the loss of 22 main feedwater pump suction is under investigation.
ENS 570021 March 2024 17:27:00MonticelloNRC Region 3GE-3The following information was provided by the licensee via email: At 1330 CST, on March 1, 2024, an equipment vendor was coordinating with Wright County performing maintenance on an emergency siren when the county operator mistakenly sent an alarm signal instead of cancel signal, activating all Wright County emergency sirens for approximately 17 seconds. At 1345 CST, the Monticello Nuclear Generating Plant (MNGP) emergency planning coordinator received a notification from the vendor and notified the duty shift manager (of the inadvertent activation). Wright County officials are planning to make a public notification via social media to local residents. No press release by the licensee is planned at this time. This event is reportable per 10 CFR 50.72(b)(2)(xi), 'News Release or Notification of Other Government Agencies.' This is a 4-hour Reporting requirement. The NRC Resident has been notified.
ENS 5699528 February 2024 13:25:00MonticelloNRC Region 3GE-3The following information was provided by the licensee via fax and email: At approximately 0839 (CST) with Unit 1 in Mode 1 at 100 percent power, the reactor automatically scrammed due to the depressurization of the SCRAM air header caused by an invalid signal that (occurred) during system testing. The SCRAM was uncomplicated with all systems responding as expected. The cause and details of the event are under investigation. Containment isolation valves actuated and closed on a valid Group 2 signal. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B), and an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for the Group 2 isolation signal. Operations responded using the emergency operating procedure and stabilized the plant in Mode 3. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. State as well as Wright and Sherburne Counties will be notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The Anticipated Transient Without Scram (ATWS) circuit was being tested when an invalid signal was sent to depressurize the SCRAM air header.
ENS 568271 November 2023 16:52:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopThe following information was provided by the licensee via email: On October 31 at 1856 CDT, Prairie Island Nuclear Generating Plant personnel identified a prohibited item (alcohol) in a kitchen area located within the protected area. An 'Extent of Condition' search was performed of all other protected area kitchen areas, no additional prohibited items were found. The NRC Resident has been notified.
ENS 5680419 October 2023 19:58:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopThe following information was provided by the licensee via phone and email: Reporting due to loss of emergency preparedness capabilities. Seismic monitoring capability is non-functional due to loss of power. These monitors do not have a credited compensatory measure. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The NRC Resident Inspector has been notified. The licensee intends to notify state and local officials.
ENS 5680319 October 2023 15:15:00Prairie IslandNRC Region 3Westinghouse PWR 2-Loop

The following information was provided by the licensee via email: On 10/19/2023, at approximately 1110 (CST), with Unit 1 in mode 1 at 100 percent power, the reactor automatically tripped. All control rods fully inserted into the core following the trip. All safety functions operated as designed. The cause of the trip is being investigated. Operations responded and stabilized the plant. Auxiliary feedwater actuated as expected. Decay heat is being removed by the steam generator through the steam generator power operated relief valve. The trip was complex as non-safety related power was lost to both Unit 1 and Unit 2. Unit 1 is currently in mode 3 and on natural recirculation as both reactor coolant pumps are without power. Unit 2 is currently in a refueling outage with all fuel in the spent fuel pool (SFP). SFP cooling was lost for approximately 70 minutes. No impacts to the SFP temperature were observed. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the actuation of the auxiliary feedwater system following the reactor trip, this event is being reported as a specified system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 10/19/2023 AT 1646 EDT FROM MARTIN CABIRO TO ERNEST WEST * * *

The second paragraph of the original report is amended as follows to correct information regarding the spent fuel pool for Unit 2: Unit 2 is currently in a refueling outage with all fuel in the spent fuel pool (SFP). SFP cooling was maintained at all times with one train of SFP cooling. The second train lost power and was restarted approximately 70 minutes (after power was lost). No impacts to the SFP temperature were observed. Notified R3DO (Orth) and IR MOC (Crouch) and NRR EO (Felts) via email

ENS 5675927 September 2023 15:28:00MonticelloNRC Region 3GE-3

The following information was provided by the licensee via fax: (On 09/27/2023) at 1041 CDT, with the plant at 75 percent power and main turbine control valve testing in progress, a reactor pressure transient resulted in a reactor steam dome high pressure scram and subsequent group 1 primary containment isolation of the main steam lines (MSL). All main steam isolation valves closed as a result of the group 1 isolation signal. Additionally, a group 2 containment isolation signal was received due to reactor pressure vessel (RPV) level less than plus 9 inches during the transient. Operations personnel responded and stabilized the plant. The high-pressure coolant injection (HPCI) system was placed in service to control RPV pressure. HPCI did not inject into the RPV and was not needed to control RPV water level. The cause of the initial pressure transient is under investigation. The NRC Resident Inspector has been notified.

      • UPDATE ON 9/27/2023 AT 2350 EDT FROM NATHAN PIEPER TO LAWRENCE CRISCIONE***

The utility notified the State of Minnesota and Wright and Sherburne counties. Notified R3DO (Orlikowski)

ENS 567071 September 2023 18:05:00MonticelloNRC Region 3GE-3The following information was provided by the licensee via email: On 9/1/23 at 0900 hours, site personnel identified a 1 ounce bottle of vanilla extract in the protected area. Alcohol was identified as an ingredient on the ingredients label. It was determined that the alcohol by volume (ABV) for vanilla extract was 35 percent, above the 0.5 percent ABV considered low alcohol content.
ENS 5658422 June 2023 09:44:00MonticelloNRC Region 3GE-3The following information was provided by the licensee email: This telephone notification is provided in accordance with 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to report an invalid actuation of Division 2 Primary Containment Isolation logic at the Monticello Nuclear Generating Plant (MNGP) that occurred while in a refueling outage. At approximately 0402 Central Daylight Time (CDT) on April 28, 2023 and at approximately 1611 and 2143 CDT on May 4, 2023, momentary losses of 'Y80 Division 2 Uninterruptible 120VAC Class 1E Distribution Panel', which provides power to Division 2 Primary Containment Isolation logic, resulted in a partial Primary Containment Group 2 Isolation (gas systems), initiation of the Standby Gas Treatment system, and the shift of Control Room ventilation to the high radiation mode. The momentary losses of 'Y80' were due to an intermittent, age-related degradation issue with the 'Uninterruptible Power Supply Y81, Division 2 120VAC Class 1E Inverter', which resulted in a temporary loss of output plus a lack of static switch transfer from the inverter supply to the alternate source as designed. The actuations were not initiated in response to actual plant conditions, these were not intentional manual initiations, and there were no parameters satisfying the requirements for initiation. Therefore, these events have been determined to be invalid actuations that were attributed to the same cause. All systems responded as designed to the actuation signal. Operations reset the partial Primary Containment Group 2 Isolation signal, shutdown the Standby Gas Treatment system, and restored Control Room ventilation per the procedure. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5654327 May 2023 20:28:00Prairie IslandNRC Region 3Westinghouse PWR 2-Loop

The following information was provided by the licensee via email: Notification of Unusual Event, HU4.1 declared based on multiple fire alarms in the containment building not verified within 15 minutes. Turbine trip causing reactor trip due to fault on 2GT transformer. At 1845 CDT, verification of no fire in the containment building. Notified DHS Senior Watch Officer, FEMA Operations Center, CISA Central watch officer, DOE Operations Center (email), HHS Operations Center (email), EPA Emergency Operations Center (email), USDA Operations Center (email), FDA EOC (email), FEMA NWC (email) and DHS Nuclear SSA (email), FEMA NRCC (email) and CWMD watch desk (email).

  • * * UPDATE AT 0148 EDT ON 5/28/23 FROM CHRIS BAARTMAN TO BILL GOTT * * *

The following information was provided by the licensee via email: This update is being made to report the actuation of the auxiliary feedwater system following the reactor trip at 1819 CDT. This event is being reported as a specified system actuation in accordance with the reporting criteria of 10 CFR 50.72(b)(3)(iv)(A). This update is also being made for the termination of the notification of unusual event at 2304 CDT on 5/27/2023. The basis for the termination was that there was no indication of a fire. Upon lockout of 2GT transformer, main to reserve power transfer did not occur on 3 of 4 non-safeguards buses. Subsequently, operator action successfully restored power to all non-safeguards buses at 1925 CDT. There was no impact to the health and safety of the public or plant personnel. The NRC resident inspector has been notified of the update. Notified R3DO (Benjam¡n), NRR EO (Walker), IRMOC (Grant), DHS Senior Watch Officer, FEMA Operations Center, CISA Central watch officer, DOE Operations Center (email), HHS Operations Center (email), EPA Emergency Operations Center (email), USDA Operations Center (email), FDA EOC (email), FEMA NWC (email) and DHS Nuclear SSA (email), FEMA NRCC (email) and CWMD watch desk (email).

ENS 5653523 May 2023 22:13:00MonticelloNRC Region 3GE-3The following information was provided by the licensee via phone and fax: On 5/22/23, Xcel Energy performed a notification to the state of Minnesota Duty Officer, in accordance with Minnesota Statute 115.061, regarding 300-600 gallons of pumped ground water that overflowed from a holding tank and returned to the ground area from which it was pumped. The groundwater being pumped is related to recovery activities associated with the event reported on November 22, 2022 (EN 56236). This notification is being made solely as a four-hour, non-emergency report for notification to other government agency. An update is being provided to the Monticello community and published on Xcel Energy's website. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of public or plant personnel. The NRC Resident Inspector has been notified.
ENS 562669 December 2022 00:19:00Prairie IslandNRC Region 3Westinghouse PWR 2-Loop

The following information was provided by the licensee via email: On 12/8/2022, Prairie Island Nuclear Generating Plant initiated a notification to the State of Minnesota due to a HVAC coolant leak reaching waters of the state. The estimated quantity is 5 gallons of NALCO LCS-60. The leak was due to a failed heat exchanger coil and has been isolated. This notification is being made solely as a four-hour, non-emergency notification for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 12/21/2022 AT 1115 EST FROM RAYMOND YORK TO JEFF WHITED * * *

The following information was provided by the licensee via email: At 0019 EST on 12/9/2022, the Prairie Island Nuclear Generating Plant (PINGP) made Event Notification 56266 notifying the NRC of an environmental report to the State of Minnesota due to an estimated 5 gallons of NALCO LCS-60 that leaked from a failed heat exchanger coil and reached the waters of the state. This event notification was made in accordance with 10 CFR 50.72(b)(2)(xi). During further review of NRC reporting guidance, PINGP has concluded that the reported quantity of NALCO LCS-60 that leaked during this event was below the reporting threshold outlined in NUREG 1022, Revision 3. The NRC Resident Inspector has been notified. Notified R3DO (Kozak)

ENS 5623622 November 2022 17:35:00MonticelloNRC Region 3GE-3The following information was provided by the licensee via email: On 11/22/2022, Monticello Nuclear Generating Plant initiated a voluntary communication to the State of Minnesota after receiving analysis results for an on-site monitoring well that indicated tritium activity above the (Offsite Dose Calculation Manual) ODCM and Nuclear Energy Institute (NEI) Groundwater Protection Initiative (GPI) reporting levels. The source of the tritium is under investigation and the station will continue to monitor and sample accordingly. This notification is being made solely as a four-hour, non-emergency report for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5594214 June 2022 15:57:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopThe following information was provided by the licensee via email: A licensed operator supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant is on hold in accordance with the licensee's fitness-for-duty policy. The NRC Senior Resident Inspector has been notified.
ENS 5589613 May 2022 17:47:00MonticelloNRC Region 3GE-3The following information was provided by the licensee via email: On 5/13/22 at 1111 CDT the station entered LCO 3.7.4 Condition B for Control Room Envelope being inoperable. This was due to results from an inspection in the Steam Jet Air Ejector room that identified steam leakage exceeding the leakage rate assumptions made in the Alternate Source Term (AST) dose analysis calculation. Therefore, this is being reported in accordance with 10CFR50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades plant safety and 10CFR50.72(b)(3)(v)(D) for any event or condition that at the time of discovery could have prevented fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. There is no impact to the health and safety of the public. NRC Resident has been notified.
ENS 5570821 January 2022 10:25:00MonticelloNRC Region 3GE-3The following information was provided by the licensee via email: This telephone notification is provided in accordance with 10 CFR 50.73(a)(1) to report an invalid actuation of secondary containment relays in accordance with 10 CFR 50.73(a)(2)(iv)(A). On November 29, 2021, the `B' Fuel Pool radiation monitor spiked high during restoration following the performance of the 0068 procedure `Spent Fuel Pool & Reactor Building Exhaust Plenum Monitor Calibration' due to cable to radiation monitor connector degradation from handling. This resulted in a Partial Primary Containment Group II isolation (gas systems), initiation of Standby Gas Treatment system, and isolation of the Reactor Building Ventilation system. All systems responded as designed to the actuation signal. Operations reset the Partial Primary Containment Group II isolation signal, shutdown Standby Gas Treatment System, and restored Reactor Building Ventilation system per procedures. At the time of the occurrence, the `A' Fuel Pool radiation monitor was reading normal at approximately 1.5 mr/hr. The `B' Fuel Pool radiation monitor spiked above the 50 mr/hr setpoint and continued to read erratically. Work was performed to clean and reconnect the connector and testing per 0068 procedure verified the condition was corrected. The `B' Fuel Pool radiation monitor returned to service. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5552918 October 2021 04:05:00Prairie IslandNRC Region 3Westinghouse PWR 2-Loop

At 1930 CDT on 10/17/2021, it was discovered both of the Unit 2 Emergency Diesel Generators were simultaneously INOPERABLE with a requirement to have one OPERABLE train; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10CFR 50.72(b)(3)(v). Offsite power was OPERABLE during this event. There was no impact on the health and safety of the public or plant personnel. The NRC Senior Resident Inspector has been notified. The cause was corrected and both Emergency Diesel Generators are currently operable.

  • * * RETRACTION ON 12/13/2021 AT 1607 EST FROM CARLOS PARADA TO LLOYD DESOTELL * * *
  • The following information was provided by the licensee via email:

This is a retraction of Event Notification EN55529 in accordance with 10 CFR 50.72(b)(3)(v)(D) made by the Prairie Island Nuclear Generating Plant on October 18, 2021. The original notification stemmed from a loss of power to the non-safety related Unit 2 Emergency Diesel Generator (EDG) starting air compressors. The resulting pressure decay in the EDG starting air receivers led to a decision to declare both EDGs inoperable. A subsequent engineering evaluation has provided reasonable assurance that the Unit 2 EDGs were operable and capable of performing their safety function during the time power was lost. The NRC Resident Inspector has been notified. The HOO notified R3DO (Skokowski).

ENS 555033 October 2021 22:38:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopAt 1525 CDT, 10/3/2021, with Unit 2 in Mode 5 at 0 percent power for a refueling outage, the 22 Turbine-Driven Auxiliary Feedwater (AFW) pump received an actuation signal during preparations for an Integrated Safety Injection test. The reason for the actuation signal is under investigation. The AFW steam admission valve opened and then, due to plant conditions, received a trip signal due to low discharge pressure. The steam supplies to the TD AFW pump were isolated. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. Unit 1 was not affected by this issue. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5537723 July 2021 12:06:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopAt approximately 1040 CDT, July 23, 2021, the Minnesota State Duty Officer was notified by Xcel Energy Environmental Services of a fish kill in the Prairie Island Nuclear Generating Plant discharge canal. The fish kill resulted from a change in temperature due to the loss of power to the plant cooling tower pumps. The cause of the power loss is under investigation. This notification is being made as a four-hour, non-emergency notification in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 552447 May 2021 17:21:00MonticelloNRC Region 3GE-3The following is a summary of information received via email from Monticello Nuclear Generating Plant (MNGP): On March 9, 2021, GE Hitachi (GEH) issued Safety Communication SC 21-02 for PRC 21-02, Transfer of Information, Revision 0, pursuant to 10 CFR 21.21(b). Monticello Nuclear Generating Plant (MNGP) was listed as a potentially affected plant. This is a deviation from the Power Range Nuclear Monitor (PRNM) Licensing Topical Report, NEDC 32410P-A. On May 5, 2021, MNGP completed an evaluation of this deviation and concluded this condition represents a substantial safety hazard in that the condition could result in an Average Power Range Monitoring (APRM) flux reading either below or above the Technical Specification (plus/minus) 2% band. The condition is a defect that is reportable pursuant to 10 CFR 21.21(d)(4). The GEH NUMAC PRNMS was installed in 2009 with System Part No. 299X739NF. Name and Address of the Individual or Individuals Informing the Commission: Thomas A. Conboy, Site Vice President Monticello Nuclear Generating Plant Northern States Power Company - Minnesota 2807 West County Road 75 Monticello, MN 55362 The licensee notified the NRC Resident Inspector.
ENS 549388 October 2020 13:14:00MonticelloNRC Region 3GE-3

At 1125 CDT on 10/8/20 Monticello Nuclear Generating Plant declared a Notification of an Unusual Event (NOUE) due to a Security Condition that did not involve a hostile action, due to a helicopter that hovered over the site for approximately 10 minutes. The unit remained at 100 percent power during the event. The licensee notified the NRC Resident Inspector, the Minnesota State Duty Officer and the Wright County and Sherburne County Sherriff departments of the event. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE ON 10/8/2020 AT 2013 EDT FROM JEFF OLSON TO JEFFREY WHITED * * *

At 1715 CDT Monticello Nuclear Generating Plant terminated the Notice of Unusual Event (HU1.1), upon confirmation through federal law enforcement and conversation with the aircraft owner that the aircraft in question was performing power line inspections for a different utility and was not a threat to the plant. Monticello determined that this condition did not meet the 1-hour reporting requirements of 10 CFR 73.71. Notified R3DO (Orlikowski), NRR EO (Miller), and IRD MOC (Gott). Additionally, notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * RETRACTION ON 10/28/20 AT 1436 EDT FROM JACOB BURSKI TO BETHANY CECERE * * *

Monticello Nuclear Generating Plant (MNGP) is retracting this event notification based on subsequent information received that was not available at the time of the original notification. Following review of the additional information collected by the site through an investigation performed with input from local and federal law enforcement, Xcel Energy determined the helicopter did not constitute a credible threat or compromise site safety or security. There was no impact to public health or safety. The NRC Resident Inspector has been notified. The licensee will notify the State and county. Notified R3DO (Peterson).

ENS 548773 September 2020 15:36:00Prairie IslandNRC Region 3On 9/3/2020, at 1421 (CDT), a notification was made to the National Response Center as a result of a spill of approximately 3 fluid ounces of hydraulic oil into the plant waters of Prairie Island Nuclear Plant intake on 9/2/2020. This notification is being made as a four-hour, non-emergency notification for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact to public health and safety. The NRC resident inspector has been notified.
ENS 5485926 August 2020 18:10:00Prairie IslandNRC Region 3At 1319 CDT, on August 26, 2020, with Unit 1 in Mode 1 at 95.2 percent power in coast down for the 1R32 refueling outage, the reactor automatically tripped due to flux rate. All systems responded normally to these conditions with auxiliary feedwater initiating as expected. Operations stabilized the plant without complication. Decay heat is being removed via a main feedwater pump to the steam generators. Unit 2 is not affected and remains at 100 percent power. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour report per 10 CFR 50.72(b)(3)(iv)(A), specified system actuation. The cause of the scram is under investigation. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5480329 July 2020 04:28:00Prairie IslandNRC Region 3Radiation monitor RE-69, 'Guardhouse Area Radiation Detector' was found failed on operator rounds. RE-69 is a category A1 piece of equipment that provides the sole means of indication for a parameter used to directly assess emergency action level (EAL) RA3.1, 'dose rate greater than 15 mR/hr in either of the following areas: Control Room (R-1), Central Alarm Station (R-69).' A compensatory measure was subsequently established and the ability to assess EAL RA3.1 has been restored. There was no impact on the health and safety of the public or plant personnel. The NRC Senior Resident Inspector has been notified.
ENS 5411111 June 2019 17:55:00MonticelloNRC Region 3At 1132 CDT on 6/11/2019, both manual primary containment isolation valves in a one-inch service air line were found open. This resulted in an open primary containment penetration. Both valves are required to be closed for Primary Containment Isolation Valve Operability. Both valves were closed and independently verified closed at 1149 CDT on 6/11/2019. This is being reported under 10 CFR 50.72(b)(3)(v)(C) and (D), and 10 CFR 50.72(b)(3)(ii)(B). There was no impact to the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The licensee also notified the State of Minnesota State Duty Officer.
ENS 5400015 April 2019 11:36:00MonticelloNRC Region 3At 0511 CDT on 4/15/2019, transport of a potentially radiologically contaminated person from the Monticello Nuclear Plant to a local hospital was performed prior to conducting a radiological survey as a prudent measure to ensure timely medical support. At 0658 CDT a radiological survey determined that the individual and their clothing were not contaminated. This is reportable under 10 CFR 50.72(b)(3)(xii). The NRC Resident Inspector has been notified.
ENS 5399713 April 2019 02:04:00MonticelloNRC Region 3

EN Revision Text: HIGH ENERGY LINE BREAK DOOR FOUND IN INCORRECT POSITION RESULTING IN LPCI AND CORE SPRAY BEING INOPERABLE At approximately 1815 CDT on April 12, 2019, High Energy Line Break (HELB) Door-410A in the Reactor Building was discovered in the closed position. HELB Door-410B was previously closed for maintenance. Either Door-410A or Door-410B must be open to support the current HELB analyses. With both doors closed, this is considered an unanalyzed condition resulting in the loss of a post-HELB safe shutdown path. With Door-410A and Door-410B closed, LPCI (Low Pressure Coolant Injection) and Core Spray injection valves in both divisions are no longer considered available. This condition is being reported under 10 CFR 50.72(b)(3)(ii) as an unanalyzed condition that significantly degrades plant safety and 10 CFR 50.72(b)(3)(v) as an event or condition that could have prevented the fulfillment of a safety function. The condition was resolved at approximately 1845 CDT on April 12, 2019 when Door-410A was blocked open. The health and safety of the public was not affected by this condition. The NRC Resident has been notified.

  • * * RETRACTION FROM JESSE TYGUM TO HOWIE CROUCH AT 1330 EDT ON 5/24/19 * * *

Event Notification (EN) #53997, made on 4/13/2019, is being retracted. An engineering evaluation completed subsequent to this event analyzed the discovered condition with both Door-410A and Door-410B being closed. The engineering evaluation determined that the environmental conditions present with both Door-410A and Door-410B closed would not have impacted the availability of both divisions of the LPCI (Low Pressure Coolant Injection) and Core Spray injection valves nor would it have resulted in the loss of a post-HELB safe shutdown path. Therefore, this condition did not meet the criteria for an 8-hour notification per 10 CFR 50.72(b)(3)(ii) as an unanalyzed condition that significantly degrades plant safety or per 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfillment of a safety function. The NRC Resident Inspector has been notified. The licensee also notified the Minnesota State Duty Officer. Notified R3DO (Cameron).

ENS 5385331 January 2019 10:48:00Prairie IslandNRC Region 3

EN Revision Text: BOTH EMERGENCY DIESEL GENERATORS INOPERABLE DUE TO LOW AIR TEMPERATURE At 0743 (CST) on 1/31/2019, both trains of Unit 2 Diesel Generators were declared INOPERABLE due to outside air temperature exceeding the low temperature design limit for the diesel engines; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v) for an event or condition that could have prevented the fulfillment of a safety function. The Unit 2 Diesel Generators are still able to start if necessary to provide power. Additionally, multiple layers of defense in depth measures are in place to ensure safety. Prairie Island has five sources of offsite power; all of which are currently available. The Unit 1 Diesel Generators are OPERABLE and capable of being cross-connected to Unit 2. Additional equipment capable of responding to beyond design basis events is available on site providing another layer of defense in depth. Both Unit 2 Diesel Generators were returned to an OPERABLE status at 0810 on 1/31/2019 based on outside air temperature rising above the low temperature design limit with forecasted temperatures to remain above the low temperature design limit. There is no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The air temperature limit was -30 degrees Fahrenheit. Unit 1 was not affected. The EDGs were supplied by a different manufacturer with different air temperature limits.

  • * * RETRACTION AT 1340 EDT ON 03/22/2019 FROM BRIAN JOHNSON TO JEFFREY WHITED * * *

Engineering analysis performed subsequent to the event notification has determined that both Unit 2 Diesel Generators would have been able to fulfill their safety function during the period of time when the outside air temperature had exceeded the low temperature design limit. Therefore, EN# 53853 is being retracted. The NRC Resident Inspector has been notified of the event notification retraction. Notified R3DO (McCraw).

ENS 5375728 November 2018 12:30:00Prairie IslandNRC Region 3At 0752 CST, on November 28, 2018, Dakota County inadvertently actuated their sirens while performing a scheduled weekly (Emergency Planning Fixed Siren Test). All seven (7) Dakota County sirens actuated for approximately 9 seconds before Dakota County Dispatch canceled the activation. This 4-hour non-emergency report is being made per 10 CFR 50.72(b)(2)(xi), Offsite Notification (which was made to Dakota County Dispatch). Capability to notify the public was never degraded during this time. All Emergency Notification sirens remain in service. No press release is planned at this time. The licensee has notified the NRC Resident Inspector.
ENS 5370028 October 2018 21:44:00Prairie IslandNRC Region 3

This event is being reported pursuant to 10 CFR 50.72(b)(3)(xiii) for a major loss of emergency assessment capability at the Prairie Island Nuclear Generating Plant. At 1435 CDT on October 28, 2018, troubleshooting of the Seismic Monitoring Panel resulting from the receipt of Control Room annunciator 47023-0603 (Seismic Monitor Panel) determined that the '(Operational Basis Earthquake) OBE Exceedance' alarm on the Seismic Monitoring Panel will not alarm and determined the panel is non-functional. The Seismic Monitoring Panel system functions to provide indication that the OBE threshold has been exceeded following a seismic event and is used in the Prairie Island Nuclear Generating Plant Emergency Plan to perform classification of Initiating Condition 'Seismic event greater than OBE levels' and Emergency Action Level HU2.1. Station personnel are monitoring the seismic recorders for event alarms on a 15 minute frequency due to alarm function failure. The station is developing repair plans for restoration of the alarm function. This event does not adversely affect the safe operation of the plant or health and safety of the public.

The licensee has notified the NRC Resident Inspector.

ENS 5359711 September 2018 18:42:00MonticelloNRC Region 3On 9/10/2018, the 11 Core Spray (CSP) loop was placed in service to support quarterly surveillance testing. With the 11 CSP pump in service it was identified that the check valves isolating the 11 CSP system from the keep fill supply were leaking by. At 1129 CDT on 9/11/2018, it was identified that this leakage may have exceeded the leakage rate assumptions made in the dose analysis calculation for emergency core cooling system (ECCS) leakage outside containment following a loss of coolant accident (LOCA). Therefore, this is being reported in accordance with 10 CFR 50.72(b)(3)(ii)(B) for an unanalyzed condition that significantly degrades plant safety and 10 CFR 50.72(b)(3)(v) for any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident. The potential ECCS leak pathway has been isolated. There is no impact to health and safety of the public. The NRC Resident Inspector has been notified.
ENS 5354610 August 2018 23:13:00Prairie IslandNRC Region 3

On 8/10/2018 at 1445 (CDT) both trains of Cooling Water (Cooling Water Pumps for Emergency Diesel Generators) were declared INOPERABLE and both units entered (Technical Specification) (TS) 3.0.3 due to corroded jacket cooling water plugs for (the) 12 and 22 cooling water pump motors; therefore this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). At 1543 (CDT), 08/10/2018 the 121 Cooling Water pump was aligned to the "A" Cooling Water train and the TS 3.0.3 condition was exited for both units. (After restoring train A cooling water the site entered a seven day limiting condition for operations, TS 3.7.8 for one inoperable cooling water pump.) There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 09/29/2018 AT 2128 EDT FROM BRIAN JOHNSON TO OSSY FONT * * *

Testing and forensic analysis performed subsequent to the notification has determined the as-found condition would not have impacted either diesel-driven pumps' ability to start, run, and meet flow/pressure requirements to perform their required safety function. Therefore, EN# 53546 is being retracted. The NRC Resident Inspector has been notified of the Event Notification retraction. Notified R3DO (Kozak).

ENS 5340817 May 2018 17:33:00Prairie IslandNRC Region 3At 1115 (CDT) on May 17, 2018 with Unit 2 in Mode 1 at 100% power, the station experienced an auto-start of Emergency Diesel Generator, D5. Preliminary information indicates that the Bus 25 Potential Transformer (PT) fuse drawer was inadvertently opened, causing Breaker 25-16 to open and de-energize bus 25. Operators were able to manually close the D5 EDG output breaker to re-energize bus 25. 22 Component Cooling (CC) Pump auto-started on the loss of 21 CC Pump due to low pressure in the CC system as designed. All equipment functioned as designed. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the EDG. There was no impact on the health and safety of the public or plant personnel. The NRC Senior Resident Inspector has been notified.
ENS 5328624 March 2018 01:09:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopThis report is made for a loss of Emergency Assessment Capability associated with Emergency Action Levels for Toxic and Flammable Gas and is reportable under 10 CFR 50.72 (b)(3)(xiii). During an emergency equipment inventory it was identified that methods were not available to detect levels of toxic or flammable gas at the IDLH (Immediately Dangerous to Life and Health) level for a number of substances. The IDLH is used to assess the Alert Emergency Action Level. The ability of the Control Room Staff to detect and respond to the presence of toxic or flammable gas is unaffected. Because there have been no chemical spills or releases that would require sampling to be performed, the health and safety of the public was not affected. The NRC Resident Inspector has been notified. The State of Minnesota will be notified.
ENS 5328523 March 2018 21:07:00MonticelloNRC Region 3GE-3This report is made for a loss of Emergency Assessment Capability associated with Emergency Action Levels for Toxic and Flammable Gas and is reportable under 10 CFR 50.72(b)(3)(xiii). During an emergency equipment inventory, it was identified that methods were not available to detect levels of toxic or flammable gas at the IDLH (Immediately Dangerous to Life and Health) level for a number of substances due to the detector having an unsuitable range. The IDLH is used to assess the Emergency Action Level Alert Range. The ability of the Control Room Staff to detect and respond to the presence of toxic or flammable gas is unaffected. Because there have been no chemical spills or releases that would require sampling to be performed, the health and safety of the public was not affected. The resident NRC Inspector has been notified. The licensee will be notifying the state of Minnesota.
ENS 5313522 December 2017 11:09:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopAt 2050 (CDT) on October 25, 2017, during the Unit 2 refueling outage, with no fuel in the Reactor Vessel, control room operators found that Unit 1 Train B Containment Fan Coil Units (FCUs) had swapped from chilled water to cooling water (CL). Construction Electricians were installing a new relay 2Sl-22X when the plunger on adjacent relay 2Sl-23X was bumped, which caused the swap of the Unit 1 Containment Fan Coil Units (CFCUs) from chilled water to cooling water. Relay 2SI-23X is a slave relay that starts 22 Turbine Driven Auxiliary Feed Water Pump, illuminates blue lights on various control switches, closes MV-32159 Loop A/B CLG WTR HDR XOVR MV B, closes chilled water Isolation Valves to Unit 1 Train B, and closes chilled water Isolation Valves to Unit 2 Train B. This actuation was as expected. CL is a shared system and, upon a Safety Injection (SI) signal on either unit, the CL header splits into two trains and, as a result, the CL supply is isolated to the chillers that supply chilled water to both units' CFCUs. By design, CL is the safety related source of cooling to the CFCUs. 22 Turbine Driven Auxiliary Feed Water Pump did not start as the unit was in 'No Mode' with the control switch for the pump in manual. MV-32159 did automatically close per design. Unit 2 Chilled Water was already isolated due to work in progress with the unit in 'No Mode.' There was no impact on public health and safety. This event is being reported as a 60-day telephone notification in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an invalid actuation of a containment heat removal system (the FCUs were running, but were swapped to their safeguards source due to an invalid actuation of a relay). The licensee notified the NRC Resident Inspector.
ENS 5313422 December 2017 11:09:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopAt 0856 (CDT) on October 23, 2017, during the Unit 2 refueling outage, with no fuel in the Reactor Vessel, an unexpected auto start of the Unit 2 Train B Emergency Diesel Generator (D6) occurred when construction electricians inadvertently bumped the plunger for relay 2Sl-20X while working in the relay rack. Relay 2Sl-20X is a slave relay that actuates a light on the control board, starts D6, and starts 22 Residual Heat Removal (RHR) pump on a Safety Injection signal. In this instance, the RHR pump did not start as its control switch was in pull-out. It is expected that the control board light lit for the brief time the relay plunger was depressed, but this could not be confirmed. The D6 actuation resulted in an unexpected annunciator for D6 EMERGENCY GENERATOR SI SIGNAL EMERGENCY START. Operators responded per the alarm response procedure, performed a walk down of running D6 and then performed a shutdown of D6. D6 started and functioned as expected. There was no impact on public health and safety. This event is being reported as a 60-day telephone notification in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an invalid actuation of an emergency diesel generator. The NRC Resident Inspector has been notified.
ENS 5306713 November 2017 03:57:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopAt 2119 (CST) on 11/12/2017 a Control Room board walk down discovered that both of the Unit 2 Containment Spray Pump control switches were in pull-out. With the control switches in pull-out, the pumps would not automatically start as required. Unplanned TS (Technical Specifications) 3.0.3 was entered at 2119 as a result of not complying with TS 3.6.5, Containment Spray and Cooling Systems, which requires both trains of Containment Spray to be Operable while in Mode 4. Unit 2 had entered Mode 4 at 0303 on 11/12/2017. TS 3.0.3 was exited at 2127 on 11/12/2017 when both Containment Spray Pump control switches were placed in Automatic restoring Operability. Preliminary investigation determined that while Unit 2 was in Mode 5, Surveillance SP 2099, Main Steam Isolation Valve Logic Test, had taken the Containment Spray Pump control switches to pull-out but did not re-align the control switches to automatic after the test was complete. This 8-hour Non-Emergency report is being made per 10 CFR 50.72(b)(3)(v)(D), Accident Mitigation. The NRC Senior Resident Inspector has been informed.
ENS 5301916 October 2017 22:09:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopAt 1425 CDT on 10/16/17, investigation into a boric acid indication was determined to be a through wall leak at the socket weld that joins the 3/4 inch line 2RC-92 to valve 2RC-8-37. Unit 2 is currently in Mode 5 with Reactor Coolant system (RCS) Operational Leakage limits not applicable. The leak is downstream of two first off RCS isolation valves that are normally closed. The leak is not quantifiable as it only consists of a small amount of dry boric acid at the location. This failure constitutes welding or material defects in the primary coolant system that cannot be found acceptable under ASME Section Xl. Therefore, this is a degraded condition reportable under 10 CFR 50.72(b)(3)(ii)(A). At the time of this notification, the Prairie Island Nuclear Generating Plant Unit 2 is in Mode 5 for a planned refueling outage. The identified defect will be repaired prior to entering Mode 4. This condition does not affect the health and safety of the public or station employees. The NRC Resident Inspector has been notified.
ENS 5281420 June 2017 08:18:00MonticelloNRC Region 3GE-3At 2353 CDT on 6/19/2017, while performing the High Pressure Coolant Injection (HPCI) quarterly surveillance following planned maintenance, the HPCI turbine did not start as expected due to the HPCI turbine stop valve failing to open. This issue is being reported under 10 CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function at the time of discovery. Investigation into the failure of the HPCI system to start is in progress. The unit remains at 100% power. The health and safety of the public was not affected. The NRC Resident Inspector has been notified.
ENS 527811 June 2017 23:41:00MonticelloNRC Region 3GE-3Planned maintenance to restore normal power to Plant Computer Systems resulted in an unexpected loss of all Meteorological (MET) Tower Data (at 1645 CDT). As a result, this represents a Loss of Emergency Assessment Capability and is reportable under 10CFR 50.72 (b)(3)(xiii). The isolation was restored and MET Tower Data was restored at 1845. The health and safety of the public was not affected as the plant is operating in a normal condition with no severe weather or storms in the area. Additionally meteorological data was available from the National Weather Service should this data had been necessary. The NRC Resident Inspector has been notified." The licensee will be notifying the State of Minnesota.
ENS 5274911 May 2017 18:11:00MonticelloNRC Region 3GE-3A can of alcohol (16.9 ounce foreign beer) was discovered unopened in an administration building refrigerator. Site security took possession of the can of alcohol. The owner of the can of alcohol is unknown. This licensee is making this 24 hour notification in accordance with 10CFR26.719(b)(1). The licensee notified the NRC Resident Inspector.
ENS 5274210 May 2017 11:46:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopAt approximately 0755 CDT, on May 10, 2017, Pierce County inadvertently actuated their sirens while performing a scheduled weekly cancel test. All fifty two (52) Pierce County sirens actuated county wide for approximately 11 seconds before Pierce County Dispatch canceled the activation. This 4-hour non-emergency report is being made per 10 CFR 50.72(b)(2)(xi), Offsite Notification. Capability to notify the public was never degraded during this time. All Emergency Notification sirens remain in service. No press release is planned at this time. The license has notified the NRC Senior Resident Inspector.
ENS 5271528 April 2017 21:21:00MonticelloNRC Region 3GE-3This report is being made pursuant to 10 CFR 50.72(b)(2)(xi), as an event where notification to other government agencies has been made. On April 28, 2017, notification to the Minnesota State Duty Office was made due to a non-compliance with release of wastewater requirements in the Monticello Nuclear Generating Plant's National Pollutant Discharge Elimination System permit. There were no consequences to the health and safety of the public. The licensee notified the NRC Resident Inspector.
ENS 5268215 April 2017 13:03:00MonticelloNRC Region 3GE-3During shutdown activities with the reactor subcritical, actions were being taken to remove 11 Reactor Feed Pump from service in support of a scheduled refueling outage. Reactor Water Level on Safeguards level instrumentation dropped below +9 inches, which resulted in a valid Reactor Protection System (RPS) Scram signal and Partial Group 2 Primary Containment Isolation System (PCIS) signal. All systems functioned as required. Reactor Water Level on Safeguards instrumentation was restored to greater than +9 inches immediately. RPS and PCIS logic was reset. There was no impact to the health and safety of the public as a result of this event. This actuation of these systems is being reported per 10 CFR 50.72(b)(3)(iv)(A) as an event that resulted in a valid actuation of any of the systems listed in 10 CFR 50.72(b)(3)(iv)(B). The NRC Resident Inspector has been notified.
ENS 5263824 March 2017 17:15:00Prairie IslandNRC Region 3Westinghouse PWR 2-Loop

On February 3, 2017, Prairie Island staff performed maintenance on the transom above Battery Room Door 225. This activity resulted in the transom being unlatched for approximately five minutes. On February 6, 2017, a question from the NRC Resident Inspector resulted in an evaluation of this condition for past operability. On March 20, 2017, the past operability evaluation of Door 225 concluded that, in the event of a postulated HELB (High Energy Line Break), the transom being unlatched during the five minute maintenance period resulted in the inoperability of multiple systems in the Unit 1 and Unit 2 battery, auxiliary feedwater, and Unit 1 safeguards bus rooms that would be required to mitigate the postulated HELB. The loss of safety functions required to mitigate the postulated HELB make the condition reportable under 50.72(b)(3)(ii) for an unanalyzed condition that significantly degrades plant safety. Unlatching the transom above the Battery Room Door creates an opening not accounted for in design bases documents. This occurred due to an improperly prepared work permit. Corrective actions are in place to preclude recurrence. The licensee informed the NRC Resident Inspector.

  • * * RETRACTION FROM MARK LOOSBROCK TO JEFF ROTTON AT 1559 EDT ON 04/10/2017 * * *

Further analysis determined that an unlatched transom would result in a relative humidity of 100 percent in 11 Battery Room for about 10 minutes following a postulated HELB. Since the equipment in the Battery Rooms is not qualified for a harsh environment, the components in 11 Battery Room would have been inoperable. Temperature and relative humidity in the other Battery Rooms, Auxiliary Feedwater Rooms, and the Unit 1 Safeguards Bus Rooms would have remained within the allowable limits. Therefore, for the five minutes the strike was removed from the transom, only equipment in 11 Battery Room and supported A Train components would have been inoperable. This event was not an Unanalyzed Condition that significantly degraded plant safety, under 10 CFR 50.72(b)(3)(ii), as no safety function would have been lost. The licensee notified the NRC Resident Inspector. Notified R3DO (Skokowski).

ENS 524744 January 2017 20:07:00Prairie IslandNRC Region 3Westinghouse PWR 2-LoopA non-licensed employee supervisor had a confirmed positive for a prohibited substance during a random fitness-for-duty test. The individual's unescorted access to the plant has been denied. The licensee notified the NRC Resident Inspector.
ENS 5245421 December 2016 18:00:00MonticelloNRC Region 3GE-3

At 0935 (CST) on 12/21/2016, while performing the High Pressure Coolant Injection (HPCI) Comprehensive Pump and Valve Tests for post-maintenance testing following scheduled maintenance, the HPCI turbine did not start as expected due to the HPCI turbine stop valve failing to open. This issue is being reported under 10CFR50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function at the time of discovery. Investigation into the failure of the HPCI system to start is in progress. The plant remains at 100% power with no challenges to the health and safety of the public. The NRC Resident Inspector has been notified. The plant is in a 14-day action statement under LCO 3.5.1, 'ECCS - Operating' due to the HPCI turbine stop valve failure. The licensee notified the Minnesota State Duty Officer.

  • * * RETRACTION FROM KIM HOFFMAN TO JOHN SHOEMAKER AT 1303 EST ON 1/17/18/17 * * *

On December 21, 2016, the NRC Operations Center was notified of Event Number 52454 that described a failure of the High Pressure Coolant Injection (HPCI) turbine stop valve to open during post maintenance testing prior to being declared operable. The condition was reported in accordance with 10 CFR 50.72 (b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function at the time of discovery. At the time, it was not readily apparent that the failure was due to the maintenance activities. Subsequent return-to-service testing showed the oil system vent and fill had been inadequate following the maintenance. This event occurred as a result of the maintenance process and would not have occurred during normal operation of the system. NUREG-1022, Revision 3 states, 'reports are not required when systems are declared inoperable as part of a planned evolution for maintenance or surveillance testing when done in accordance with an approved procedure and the plant's TS (unless a condition is discovered that would have resulted in the system being declared inoperable).' There was no discovered condition that would have resulted in the safety function of the system being declared inoperable under normal, non-maintenance conditions. Based on the above additional information, Monticello Nuclear Generating Plant is retracting this report. The plant was in a planned evolution and did not discover a condition that could have prevented performing a safety function. The licensee has notified the NRC Resident Inspector. Notified R3DO (McCraw).

ENS 5245121 December 2016 16:38:00MonticelloNRC Region 3GE-3This 60-day telephone notification is being submitted in accordance with 10 CFR 50.73(a)(1) and 10 CFR 50.73(a)(2)(iv)(A) to report an invalid actuation of the 12 Emergency Diesel Generator Emergency Service Water pump (12 ESW pump). At 1745 (CST) on October 24, 2016, an unexpected auto-start of the 12 ESW pump occurred. The 12 Emergency Diesel Generator (12 EDG), was previously properly removed from service and isolated for scheduled maintenance. Upon investigation, is was determined that no valid start signal was present and actuation occurred during relay replacement activities on the 12 EDG in C-92 (12 EDG (G-38) electrical control panel) cabinet when electricians inadvertently bumped a 12 EDG start relay. During this period, the Control Room received annunciators indicating the 12 EDG engine was running/cranking and the 12 ESW pump started. Due to being isolated, the 12 EDG did not actually start. The licensee notified the NRC Resident Inspector.
ENS 5239627 November 2016 21:22:00MonticelloNRC Region 3GE-3At 1447 (CST) on 11/27/2016 while troubleshooting a minor leak on the High Pressure Coolant Injection (HPCI) turbine, it was discovered that the HPCI turbine exhaust drain pot high level bypass switch was not functioning per design to support removal of condensate from the HPCI turbine casing. This resulted in some water accumulation within the HPCI turbine casing. Subsequently, HPCI was declared INOPERABLE and this issue is being reported under 10CFR50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of a safety function at the time of discovery. The plant remains at 100 percent power with no challenges to the health and safety of the public. The NRC Resident Inspector has been notified. Technical Specification limiting condition for operation requires HPCI to be Operable within 14 days. The licensee will be notifying the State of Minnesota regarding the event.