Semantic search
Entered date | Site | Region | Reactor type | Event description | |
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ENS 56850 | 12 November 2023 22:02:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: On November 12, 2023, at 0300 EST, a Watts Bar contractor was transported offsite for medical treatment due to a work-related injury. Upon arrival at an offsite medical facility, medical personnel determined the injury required the individual to be admitted into the hospital and will be kept overnight. The individual was inside of the Radiological Controlled Area, however was free released with no contamination. The injury and hospitalization were reported to the Occupational Safety and Health Administration (OSHA) under 29 CFR 1904.39(a)(2). The contracting agency informed OSHA at 1319 EST. Watt Bar Operations personnel were officially notified by the contracting agency of the report made to OSHA at 1945 EST. This is a four-hour notification, non-emergency for a notification of other government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). The NRC Resident Inspector has been notified. |
ENS 56845 | 9 November 2023 15:55:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | The following is a summary of information provided by the licensee via email: A controlled substance was found in the protected area. The NRC Resident Inspector has been notified. |
ENS 56809 | 21 October 2023 09:25:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via fax and email: Fire potentially degrading the level of safety of the plant. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: At 0907 EST, the licensee declared a notification of unusual event, under emergency action level HU.4, due to multiple fire alarms and CO2 discharge in the emergency diesel building. When the plant fire brigade entered the building, there was no indication of fire or damage to any plant equipment. The cause of the multiple alarms is under investigation. State and local authorities were notified and no offsite assistance was requested. Both units remain at 100 percent power. The NRC Resident Inspector has been notified. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).
At 1007 EDT, Watts Bar terminated the notification of unusual event. The basis for termination was that no fire or damaged plant equipment was found. The NRC Resident Inspector has been notified. Notified R2DO (Miller), IR-MOC (Crouch), NRR-EO (Felts), DHS-SWO, FEMA Ops Center, CISA Central, FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email).
Watts Bar Nuclear Plant (WBN) is retracting Event Notice 56809, Notice of Unusual Event, based on the following additional information, not available at the time of the initial notification. Specifically, in accordance with the emergency preparedness implementing procedures, WBN reported a condition that was determined to meet emergency action level (EAL) HU4, Initiating criteria number 1, receipt of multiple (more than 1) fire alarms or indicators and the fire was within any Table H2 plant area, which includes the diesel generator building. It was further determined that multiple fire detection zones actuated (spurious and invalid) enabling the discharge of installed fire suppression (CO2) into the space. Upon entry by the site fire brigade, it was determined that no smoke or fire existed and reported to the Shift Manager at 0930 EDT. All fire alarms were reset. Troubleshooting activities are in progress to determine the cause. A fire watch has been established and CO2 has been isolated. The required compensatory measures for the affected areas will remain in place until completion of the investigation, and CO2 suppression is restored to functional. Notified R2DO (Miller), IR-MOC (Crouch), NRR-EO (Felts), DHS-SWO (email), FEMA Ops Center (email), CISA Central (email), FEMA NWC (email), CWMD Watch Desk (email), DHS NRCC THD Desk (email), and DHS Nuclear SSA (email). |
ENS 56660 | 4 August 2023 20:51:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via phone and email: At 1746 EDT on 08/04/2023, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to number 2 steam generator low low level. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed by using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight-hour report under 10 CFR 50.72 (b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the number 2 steam generator low low level is being investigated. |
ENS 56593 | 27 June 2023 19:04:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via phone and email: At 1626 EDT, with Unit 2 in Mode 1 at 100 percent power, the reactor automatically tripped due to a main turbine trip. The (reactor) trip was not complex with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed using the auxiliary feedwater and steam dump systems. Unit 1 is not affected. Due to the reactor protection system actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the auxiliary feedwater system (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72 (b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All control rods are fully inserted. The cause of the turbine trip is being investigated. |
ENS 56592 | 27 June 2023 11:52:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via phone and email: At 0831 (EDT) on June 27, 2023, Sequoyah Nuclear Plant reported an oil discharge into the plant intake located on the Tennessee River to the (Department of Transportation) National Response Center (report number 1371356). The source of oil was from a broken hydraulic hose from equipment in use on the intake. This oil spill is minor and did not exceed any NRC regulations or reporting criteria. This notification is being made solely as a four-hour, non-emergency notification for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56541 | 25 May 2023 17:02:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via phone and email: At 1345 EDT on May 25, 2023, it was determined that a fire barrier for area 737-A1B was not installed, and would render the 2A Emergency Diesel Generator (EDG) not operable in the event of a fire on the Unit 2 side of elevation 737 in the Auxiliary Building. The 2A EDG is the credited power source for fire safe shutdown for a fire located in this area. Without the credited source of power, this places WBN U2 (Watts Bar Nuclear Unit 2) in an unanalyzed condition. A fire watch has been established in the area until the issue is resolved. Therefore, this event is being reported as an eight-hour non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B). The NRC Resident Inspector has been notified. |
ENS 56531 | 20 May 2023 07:45:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via phone and email: On 5/20/2023 at 0315 CDT, Browns Ferry Unit 1 was at 80 percent reactor power performing, 'Turbine control valve fast closure turbine trip and RPT (recirculation pump trip) initiate logic testing'. During performance of this test, Unit 1 received a full reactor scram. An investigation is in progress to determine the cause of the scram. All systems responded as expected, and Unit 1 is stable at zero percent power in mode 3. All control rods fully inserted into the core. Main steam isolation valves remained open with main turbine bypass valves controlling pressure. Reactor feedwater pumps remained in service to control reactor water level. Primary containment isolation signals groups 2, 3, 6, and 8 were received with expected system actuations. This event is reportable per 10 CFR 50.72(b)(2)(iv)(B), 'Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation'. The event is also reportable within 8 hours per 10 CFR 50.72(b)(3)(iv)(A), 'Specified System Actuation'. The NRC Resident has been notified. |
ENS 56505 | 5 May 2023 16:00:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via email: On 05/04/2023 at 2034 CDT, a Browns Ferry Nuclear Plant non-licensed employee supervisor had a confirmed positive drug test identified during random fitness-for-duty medical testing. Employee's unescorted access has been suspended. A review of the employee's work has been completed. The (NRC) Resident Inspector has been notified. |
ENS 56411 | 15 March 2023 04:27:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via email: At 2257 (CDT) on 3/14/2023 during the 2R22 refueling outage on Browns Ferry Nuclear Plant Unit 2, it was determined there was RCS boundary leakage from five of eight sensing lines that pass through containment penetrations X-30 and X-34 that did not meet the requirements of Section XI, of the ASME Boiler and Pressure Vessel Code. The condition will be resolved prior to plant startup. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
The following information was provided by the licensee via email: The purpose of this notification is to retract a previous Event Notification, EN 56411 reported on 3/14/23. Following the initial notification, further analysis of the condition was performed. It was determined that the leaking pipe weld was ASME Section XI Code Class 2 piping which falls under the requirements of ASME Section XI Subsection IWC and not Subsection IWB. Therefore, this condition does not represent a serious degradation of the nuclear power plant, including its principle safety barriers. Based upon the above, the leaks identified on the ASME Section XI Code Class 2 equivalent Main Steam sense lines are not reportable under 10 CFR 50.72(b)(3)(ii). Therefore, the NRC non-emergency 10 CFR 50.72(b)(3)(ii) report was not required and the NRC report 56411 can be retracted and no Licensee Event Report under 10 CFR 50.73(a)(2)(ii) is required to be submitted. Notified R2DO (Miller) |
ENS 56385 | 2 March 2023 17:52:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via email: At 1312 CST on March 2, 2023, Browns Ferry Nuclear Plant Units 1, 2, and 3 initiated voluntary communication to the state of Alabama and local officials as part of the Nuclear Energy Institute (NEI) Groundwater Protection Initiative (GPI), after receiving analysis results for leakage from a demineralized water storage tank that contained activity above the GPI voluntary communication threshold. All these results are significantly less than the limits established by the Nuclear Regulatory Commission (NRC) and Environmental Protection Agency (EPA) for effluents from the station. Further samples obtained of the water prior to entering the Tennessee River were less than detectable. The leakage source has been isolated and additional corrective actions are in progress. This condition did not exceed any NRC regulations or reporting criteria. This notification is being made solely as a four-hour, non-emergency notification for a notification of other government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56371 | 18 February 2023 11:25:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via email: On February 17, 2023 during the planned U2R22 outage on Browns Ferry Nuclear Plant Unit 2, personnel entered the Unit 2 drywell for leak identification. Personnel discovered a cracked weld on the 2A recirculation pump discharge isolation valve drain line. At 0439 CST on February 18, 2023, following engineering evaluation, this drain line was determined to be ASME Code Class 1 piping. This constitutes an 8-hour NRC notification in accordance with 10 CFR 50.72(b)(3)(ii)(A) - Any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. The NRC Resident Inspector has been notified. |
ENS 56322 | 25 January 2023 13:22:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | The following information is a synopsis of information provided by the licensee via fax and phone: On May 23, 2022, Framatome informed Tennessee Valley Authority (TVA) of a deviation of breakers purchased under contract. On January 23, 2023, TVA determined that a defect of the basic component could create a substantial safety hazard. Framatome Inc. identified a deviation in the Siemens medium voltage vacuum circuit breaker where a failure to electrically charge or electrically close could occur. Framatome Inc. identified this as a departure from the technical requirements included in the procurement document. It is noted that the ability to electrically trip the circuit breaker would not be affected by the condition. TVA was notified by Framatome under 10 CFR 21.21(b) to evaluate the application of the breaker for a substantial safety hazard. The TVA evaluation identified these breakers as intended for use in safety related Class 1E applications where a loss of the closure function would impact mitigation of design basis accidents and transients. During the Framatome dedication testing/inspection of Siemens medium voltage vacuum breakers, a hi-pot test failure on one circuit breaker was encountered. Troubleshooting and inspection found damage to charging motor wiring. It was determined that the cause of the damage was due to the manner in which control wiring was routed and connected to the internal bracket in close proximity to a bracket edge. This edge caused damage to wiring after significant number of cycles were applied to the breaker prior to dedication testing. TVA received nine medium voltage vacuum circuit breakers at an offsite warehouse facility. While located at that facility, TVA, with assistance from Framatome, examined the affected breakers for the wire routing condition. The wiring harnesses of certain breakers were corrected. Framatome is to examine medium voltage vacuum circuit breakers that may be purchased under this contract for the wiring condition and correct as necessary before delivery. The NRC Senior Resident Inspector has been notified. This is a non-emergency notification required by 10 CFR 21.21(d)(3)(i).
The following information is a synopsis of information provided by the licensee via phone: The Sequoyah site licensing manager requested via phone call to the HOO that the model number for the basic component with the defect be listed in the Part 21 event narrative in addition to the official Part 21 report. The component discussed is a Siemens 6.9kV, 1200A, 125VDC Vacuum Circuit Breaker, Model No.: 7-HKR-50-1200-130. Notified R2DO (Miller) and the Part 21 Reactors Group (Email). |
ENS 56321 | 24 January 2023 08:43:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via email: At 0121 CST on 01/24/2023, it was discovered that the Unit 1 High Pressure Coolant Injection System (HPCI) was inoperable; therefore, the condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. 1-FCV-073-0006B, HPCI Steam Line Condensate Outboard Drain Valve, failed closed during normal plant configuration. This valve is normally open. The HPCI steam line is not being drained with the valve in the current position. The Unit 1 Nuclear Unit Senior Operator entered Unit 1 Technical Specifications LCO 3.5.1 Condition C with required actions C.1 to immediately verify by administrative means that the Reactor Core Isolation Cooling (RCIC) system is operable and C.2 to restore HPCI to operable status in 14 days. RCIC has been verified operable by administrative means. There was no impact to the safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56274 | 15 December 2022 12:52:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: This 60-day telephone notification is being submitted in accordance with paragraphs 10 CFR 50.73(a)(1) and 50.73(a)(2)(iv)(A) to report an invalid Containment Ventilation Isolation (CVI) actuation at Watts Bar Nuclear Plant (WBN) Unit 1. On November 24, 2022, at 1621 Eastern Standard Time (EST), the Train B CVI actuated due to an invalid high radiation signal from 1-RM-90-131, Containment Purge Air Exhaust Monitor. Upon investigation, the high radiation signal was caused by a failed power supply. Corrective action included replacing the power supply, 1-RM-90-131 ratemeter, and restoring the system to service. Prior to and following the invalid high radiation alarm, all radiation monitors except 1-RM-90-131 were stable at their normal values; therefore, the CVI was invalid. Control room operators performed appropriate checks and confirmed that all required automatic actuations occurred as designed. This event has been entered into the corrective action program as Condition Report 1819098. The NRC Resident Inspector was notified. |
ENS 56257 | 3 December 2022 13:05:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via email: On 12/2/2022 at 2330 (CST) during the planned F311 outage on Browns Ferry Nuclear Plant Unit 3, personnel entered the Unit 3 drywell for leak identification. Personnel discovered a through-wall piping leak on a 0.75 inch test line between the two test line isolation valves. This 0.75 inch test line is located on the residual heat removal (RHR) loop 1 shutdown cooling and RHR return line to the reactor vessel. On 12/3/2022 at 1000 CST, Engineering determined this location is classified as ASME Code Class 1 piping. This constitutes an 8-hour NRC notification in accordance with 10 CFR 50.72(b)(3)(ii)(A) - Any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. The NRC Resident Inspector has been notified. |
ENS 56168 | 18 October 2022 22:08:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via email: On 10/18/2022 at 1440 CDT, Browns Ferry Unit 3 declared both trains of standby liquid control (SLC) inoperable due to acceptance criteria failure of 3-SI-3.1.7.6, 'Standby Liquid Control System ATWS Equivalency Calculation for Newly Established Pump Flow Rate.' The purpose of this surveillance is to ensure the anticipated transient without scram (ATWS) calculation criteria is met after each pump flow test. Chemistry performed the surveillance following pump flow testing and the requirement for equivalency calculation failed low with a result of less than 1.0. CR 1810303 documents this condition in the corrective action program. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v)(A), 10 CFR 50.72(b)(3)(v)(C), and 10 CFR 50.72(b)(3)(v)(D). This condition is also reportable as a 60-day written report in accordance with 10 CFR 50.73(a)(2)(v)(A),10 CFR 50.73(a)(2)(v)(C), and 10 CFR 50.73(a)(2)(v)(D). The NRC Resident Inspector has been notified of this event. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officer's report guidance: The plant entered an 8 hour limiting condition for operation based on the above. The condition was resolved at 2053 CDT when the system was restored to normal operation. |
ENS 55992 | 12 July 2022 17:25:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via fax or email: At 0917 CDT on 7/12/2022, during the performance of U1 (Unit 1) High Pressure Coolant Injection (HPCI) rated flow test, the 1-FCV-73-19 (HPCI governor valve) failed to operate as expected. This condition results in U1 HPCI being inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). The Automatic Depressurization System (ADS) and Reactor Core Isolation Cooling (RCIC) system remain operable. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. U1 entered TS LCO 3.5.1 Condition C, 14-day Shutdown LCO (Limiting Condition for Operation), due to the HPCI inoperability. |
ENS 55867 | 29 April 2022 07:04:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via fax: On 4/28/2022, at 2338 EDT, Sequoyah received an unexpected alarm for seismological recording initiated. At 2341 EDT, unexpected alarm 1/2 Safe Shutdown Earthquake response spectra exceeded was received. The National Earthquake Information Center was contacted to confirm there was no seismic activity, and this was also confirmed on the U.S. Geological Survey website. The alarms were determined to be invalid, and they occurred due to a failure in the seismic monitoring system. This failure results in loss of ability to assess the Emergency Action Level for Initiating Condition HU2 `Seismic event greater than Operating Basis Earthquake (OBE) levels' per procedure EPIP-1, `Emergency Plan Classification Matrix.' If an actual seismic event had occurred, HU2 could not be assessed. However, compensatory measures have been implemented and include assessing OBE criteria based on alternative criteria contained in procedure AOP-N.05, `Earthquake,' which provides conservative guidance when seismic instruments are unavailable. This is an eight-hour, non-emergency notification for an event resulting in a major loss of Emergency Assessment Capability. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii). There is no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified." The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The faulty detector was removed from service, so the remaining detector provides conservative detection as the only source to make-up the logic for a seismological alarm. |
ENS 55866 | 29 April 2022 00:19:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | The following is a summary of information provided by the licensee via telephone: On 04/28/22, at 2355 EDT, with both Sequoyah Unit 1 and 2 in Mode-1, 100 percent, a Notice of Unusual Event was declared due to receiving two seismic alarms and security feeling ground movement. Additionally, security in a tower heard an explosion. Both units remain in Mode-1, 100 percent and they are investigating the validity of the seismic alarms before proceeding with the Abnormal Operating Procedure required shutdown. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee will notify the NRC Resident Inspector. The state of Tennessee and the Tennessee Valley Authority were notified. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS NRCC THD Desk(email), and DHS Nuclear SSA (email).
The following is a summary of information provided by the licensee via telephone: On 4/29/22, at 0406 EDT, Sequoyah Unit 1 and Unit 2 terminated the Notice of Unusual Event. The Civil Engineers determined that the alarms were due to a failed seismic indicator channel. Through interviews, only one security officer felt ground movement for a couple of seconds and heard a faint rumbling sound. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee will notify the NRC Resident Inspector. The state of Tennessee and the Tennessee Valley Authority were notified. Notified R2DO (Miller), NRR EO (Miller), and IR MOC (Gott) via email. Additionally, notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS NRCC THD Desk(email), and DHS Nuclear SSA (email).
The following information was provided by the licensee via email: SQN (Sequoyah Nuclear Plant) is retracting the previous NOUE (Notice of Unusual Event) declaration made on 4/28/22 at 2355 (EDT) based on Emergency Action Level HU2 for a seismic event greater than Operating Basis Earthquake levels. Following the declaration of the NOUE, the station reviewed all available indications and determined that a seismic event had not occurred. The instrumentation failure was documented under Event Notification #55867. Notified R2DO (Miller), and IR MOC (Gott), NRR EO (Miller) via email. |
ENS 55818 | 2 April 2022 15:10:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via fax: At 1345 CDT, Browns Ferry declared a Notification of Unusual Event due to a fire at the 3B Reactor Feedwater Pump within the Turbine Building which was not extinguished within 15 minutes. Subsequently, the fire was extinguished at 1402 CDT. Unit 3 remains in Mode 1 at approximately 9.5 percent rated thermal power (RTP). Unit 1 and 2 remain at 100 percent RTP and unaffected. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The fire began at 1332 CDT. It is believed that the fire was in the oil system of the Feedwater Pump. The fire was extinguished by the on-site fire brigade. No off-site assistance was requested. The Unusual Event was declared under Emergency Action Level HU-4. The licensee notified the NRC Resident Inspector and required State and local government agencies. Unit 3 is currently stable. Notified DHS-SWO, FEMA Ops Center, and CISA Central Watch Officer, and FEMA NWC, DHS NRCC THD Desk, and DHS NuclearSSA via email.
The Notification of Unusual Event was exited at 1544 CDT. Notified R2DO (Miller), IR-MOC (Kennedy), NRR-EO (Felts), DHS-SWO, FEMA Ops Center, and CISA Central Watch Officer. |
ENS 55742 | 16 February 2022 17:01:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via fax or email: At 1128 EST on 2/16/2022, the SQN (Sequoyah Nuclear) Shift Manager was notified that TVA (Tennessee Valley Authority) attempted to notify Tennessee Emergency Management Agency (TEMA) regarding routine siren testing at 0750. TVA was unable to reach TEMA via telephone land line or the Emergency Communication and Notification System (ECNS). TEMA Watch Point staff were located at their back-up facility. TVA subsequently notified TEMA via cell phone that there were communication issues with the primary and backup notification methods. It was determined that the TEMA back-up facility was not able to receive incoming calls. At 0820, TEMA positioned personnel at their primary facility in order to respond to notifications. This restored primary and backup means of notifying the state because the primary facility was not affected by the communication issues. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii) as a Major Loss of Offsite Communications Capability because it affected TVA's ability to notify the State of TN. The licensee has notified the NRC Resident Inspector. |
ENS 55741 | 16 February 2022 16:42:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via fax or email: At 1159 EST, on 2/16/2022, the Watts Bar Nuclear, Shift Manager was notified that Tennessee Valley Authority (TVA) attempted to notify Tennessee Emergency Management Agency (TEMA) regarding routine siren testing at 0750 EST. TVA was unable to reach TEMA via telephone land line or the Emergency Communication and Notification System (ECNS). TEMA Watch Point staff were located at their back-up facility. TVA subsequently notified TEMA via cell phone that there were communication issues with the primary and backup notification methods. It was determined that the TEMA back-up facility was not able to receive incoming calls. At 0820 EST, TEMA positioned personnel at their primary facility in order to respond to notifications. This restored primary and backup means of notifying the state because the primary facility was not affected by the communication issues. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii) as a Major Loss of Offsite Communications Capability because it affected TVA's ability to notify the State of TN. The licensee has notified the NRC Resident Inspector. |
ENS 55706 | 16 January 2022 06:41:00 | Browns Ferry | NRC Region 2 | GE-4 | The following information was provided by the licensee via email: On 1/15/2022 at 2320 (EST) during the planned F108 outage on Browns Ferry Nuclear Plant Unit 1, personnel entered the Unit 1 Drywell for leak identification. Personnel discovered a through-wall piping leak on a 3/4 inch test line upstream of the test valve. This 3/4 inch test line is located on the RHR Shutdown Cooling & RHR Return Line to the reactor vessel and is classified as ASME Code Class 1 Piping. This constitutes an 8-hour NRC notification in accordance with 10 CFR 50.72(b)(3)(ii)(A) - Any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded. The NRC resident has been notified. |
ENS 55660 | 16 December 2021 14:57:00 | Browns Ferry | NRC Region 2 | GE-4 |
This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of the Reactor Protection System (RPS). On October 20, 2021, at approximately 0705 hours Central Daylight Time (CDT), Browns Ferry, Unit 1, 1B RPS bus unexpectedly lost power. The loss of the bus resulted in a half scram, automatic Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolations, and Trains A, B, and C SBGT (Stand-By Gas Treatment) and A CREV (Control Room Emergency Ventilation system) started. All systems responded as expected. At 0720 hours CDT, the bus was placed on the alternate power supply and the half scram and PCIS isolations were reset. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The cause of the RPS bus loss was a trip of the underfrequency relay due to drift of the relay setpoint. The relay was replaced and 1B RPS bus was returned to the normal power supply on October 21, 2021, at 0510 hours CDT. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1729592. The NRC Resident Inspector has been notified of this event. |
ENS 55590 | 18 November 2021 02:21:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | At 2238 Eastern Standard Time (EST), on 11/17/2021, a Watts Bar Nuclear Plant contractor was transported offsite for treatment at an offsite medical facility. The offsite medical facility notified Watts Barr Nuclear Plant at 2310 EST that the individual had been declared deceased. The fatality was not work-related and the individual was inside of the Unit 1 Radiological Controlled Area. The individual was confirmed not to be contaminated. This is a four-hour notification, non-emergency for a notification of other government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The licensee will notify OSHA. |
ENS 55550 | 28 October 2021 14:19:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | At 1340 EDT on October 28, 2021, Watts Bar Nuclear Plant (WBN) Units 1 and 2 initiated voluntary communication to the State of Tennessee and local officials as part of the Nuclear Energy Institute (NEI) Groundwater Protection Initiative (GPI), after receiving analysis results for two on-site monitoring wells that indicated tritium activity above the GPI voluntary communication threshold. The suspected source, a permitted release line, has been isolated, and additional corrective actions are in progress. This condition did not exceed any NRC regulations or reporting criteria. This notification is being made solely as a four-hour, non-emergency notification for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 55421 | 20 August 2021 16:00:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | At 0905 EDT, it was discovered both trains of Auxiliary Building Gas Treatment System (ABGTS) were simultaneously INOPERABLE due to the auxiliary building secondary containment enclosure (ABSCE) being inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. ABSCE and ABGTS were returned to operable.
This is a retraction of the 8-hour Immediate notification (EN55421) made to the NRC by Sequoyah Nuclear Plant on August 20, 2021. Sequoyah is retracting this event notification based on the following: Regulatory Guidance in NUREG-1022, Revision 3, 'Event Reporting Guidelines 10 CFR 50.72 and 50.73', Sections 2.8 'Retraction and Cancellation of Event Reporting', and 4.2.3 'ENS Notification Retraction'. On August 20, 2021 personnel found door A-118 open. This door is part of the ABSCE. During the initial investigation, it was found that other personnel had the door open using Precaution A of 0-TI-SXX-000-016.0 which allows material access through ABSCE doors if the door is closed within three minutes. It was found that A-118 door had been open for greater than three minutes. With this door open the ABSCE was beyond its capability for ABGTS fan to maintain the required pressure during an Aux. Building Isolation. Thus, the site declared the ABSCE and both Trains of ABGTS inoperable per LCO 3.7.12 Conditions A, B and E. With the ABSCE being a single train system, this caused a condition that "could have prevented the fulfillment of the safety function" which requires an Immediate Notification to the NRC within eight hours under 10 CFR 50.72 (b)(3)(v)(C) and 10 CFR 50.72 (b)(3)(v)(D). This Immediate Notification was reported on August 20, 2021 at 1600 EDT. It was later determined that at 'Time of Discovery', although Door A-118 was open, it was not obstructed, the door was open by normal means, was capable of being closed and was now attended. The time requirement per 0-TI-SXX-000-016.0 for closure of an open ABSCE door is within three minutes of notification. Although the individual found holding the door was unaware of the requirement of 0-TI-SXX-000-016.0 to close the door, communications were established and the Main Control Room (MCR), upon discovery of the 'Open Door', could have directed closure starting at the Time of Discovery if required. Since the MCR was aware the door was open, had communications established with personnel at the door, the door was capable of closure and not restricted, the three minute closure requirement of 0-TI-SXX-000-016.0 was met. Subsequently, the door was closed within approximately two minutes of notification to close. The closure of the door with these procedural measures met confirmed the integrity of the ABSCE and therefore Operability of ABGTS. Based on the above critical thinking, entry into LCO 3.7.12 Condition A, B, and E was retracted on August 22, 2021 at 2044 EDT. With the LCO conditions retracted and the above determination that at the Time of Discovery safety function was maintained, the Immediate Notification per 10 CFR 50.72 (b)(3)(v)(C) and 10 CFR 50.72 (b)(3)(v)(D) was not required. The issue of Past Operability remains for instances in time that the door did not have appropriate compensatory measures in place. Any further notification required for this event will be submitted as a Licensee Event Report. Notified R2DO (Miller) |
ENS 55379 | 25 July 2021 16:00:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | At 1238 EDT on July 25, 2021, the Unit 2 Ice Bed became INOPERABLE due to SR (Surveillance Requirement) 3.6.12.1 exceeding its surveillance interval. LCO (Limiting Condition for Operation) 3.6.12 was declared not met as required by SR 3.0.1. SR 3.6.12.1 to verify maximum ice bed temperature is less than or equal to 27 degrees F could not be completed due to a failed temperature recorder. The results of the backup method of temperature verification were verified satisfactory at 1258 EDT and the LCO condition was then exited. The ice bed is a single train system which functions to control radiation release and mitigate the consequences of an accident by scrubbing radioactive iodine and providing a heat sink to limit containment pressure within design limits, therefore the requirements of 10 CFR 50.72 (b) (3) (v) (C) and (D) were met. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 55287 | 1 June 2021 17:46:00 | Browns Ferry | NRC Region 2 | GE-4 | This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of the 2A Reactor Protection System (RPS). On April 1, 2021, at 1302 (CDT), Browns Ferry Unit 2, 2A RPS (Motor Generator) MG set tripped causing a half scram. Unit 2 experienced an unexpected trip of the 2A RPS MG Set that resulted in automatic Primary Containment Isolation System (PCIS) Group 2, 3, 6, and 8 isolations and Trains A, B, and C Standby Gas Treatment (SGT) and Train A Control Room Emergency Ventilation (CREV) starts. At the time of the event, Unit 2 was in a refueling outage and the rods were already fully inserted. All systems responded as expected. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. Based on the troubleshooting conducted, the cause was determined to be a loose wiring connection in the motor circuit. The lugs were replaced with ring lugs. Operations reset the 2A RPS Half Scram and PCIS in accordance with 2-AOI-99-1 on April 1, 2021, at 1324 CDT thus correcting the condition and returning RPS to service. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1683358. The NRC Resident Inspector has been notified of this event. |
ENS 55272 | 24 May 2021 12:01:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | Unit 2 is not impacted and remains stable in Mode 1 at 100 percent power. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and in accordance with 10 CFR 50.72 (b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. No relief valves opened. All Rods fully inserted. Decay heat is being removed by Auxiliary Feedwater via the steam dumps. The plant is in a normal post-trip electrical line-up. |
ENS 55200 | 20 April 2021 15:36:00 | Browns Ferry | NRC Region 2 | GE-4 | A non-licensed, employee supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been terminated. The licensee notified the NRC Resident Inspector. |
ENS 55143 | 17 March 2021 12:59:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | At 1004 EDT on March 17, 2021, with Unit 2 in Mode 1 at 90 percent power, the reactor automatically tripped due to a main turbine trip. The trip was not complex, with all systems responding normally post-trip. Operations responded and stabilized the plant. Decay heat is being removed by the Auxiliary Feedwater and Steam Dump Systems. Unit 1 is not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The expected actuation of the Auxiliary Feedwater System (an engineered safety feature) is being reported as an eight hour report under 10 CFR 50.72 (b)(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. All controls rods fully inserted and the electrical system is in normal shutdown alignment. The cause of the turbine trip is being investigated. |
ENS 55130 | 9 March 2021 11:58:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | This 60-day telephone notification is being submitted in accordance with 10 CFR 50.73(a)(1) and 50.73(a)(2)(iv)(A). The event was an invalid actuation of the Unit 1 Containment Ventilation Isolation (CVI) system. On January 11, 2021 at 1152 Eastern Standard Time (EST) with Unit 1 at 100% power, Train 'A' of the CVI System actuated due to an invalid high radiation signal from 1-RM-90-130, Containment Purge Air Exhaust Monitor. The cause of the signal was determined to be a failed sample pump associated with the radiation monitor. 1-RM-90-130 was in service at the time of the invalid signal. The Train 'A' Containment Ventilation Isolation signal was a full actuation of that train and the system functioned as designed. Prior to and following the invalid high radiation alarms, all radiation monitors except 1-RM-90-130 were stable at their normal values; therefore, the CVI was invalid. Control room operators performed appropriate checks and confirmed that all required automatic actuations occurred as designed. The failed pump was replaced and returned to service. This event was entered into the corrective action program as CR 1663398. The NRC Resident Inspector was notified. |
ENS 55118 | 1 March 2021 16:38:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | At 1511 EST on March 1, 2021, it was discovered that the main control room (MCR) envelope was inoperable due to a MCR door being found ajar; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). The door was closed, restoring the MCR envelope to operable at 1513 EST. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 55083 | 26 January 2021 15:46:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | A licensed operator had a confirmed positive alcohol test during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Resident Inspectors have been notified. |
ENS 54997 | 15 November 2020 06:11:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | At 0144 EST on November 15, 2020, with Unit 1 in Mode 1 at 100 percent power and Unit 2 in Mode 5 at 0 percent power, an actuation of the Emergency Diesel Generator (EDG) system occurred while transferring the 2A-A 6.9 kV Shutdown Board (SDBD) from the maintenance feed to its normal power supply. The reason for the 2A-A 6.9 kV SDBD failing to transfer to the normal power supply is under investigation. The EDGs automatically started as designed when the valid actuation signal was received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the EDGs. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 54994 | 11 November 2020 16:11:00 | Watts Bar | NRC Region 2 | Westinghouse PWR 4-Loop | At 1311 EST on November 11, 2020, it was determined, after evaluation of the Watts Bar Nuclear Plant (WBN) Unit 2 Steam Generator (SG) tube eddy current test data collected during the on-going refueling outage, that the WBN Unit 2 Reactor Coolant System pressure boundary did not meet the performance criteria for SG tube structural integrity. Specifically, SG number 3 failed the condition monitoring assessment for conditional burst probability. WBN has completed tube plugging and additional corrective actions are in progress. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 54983 | 5 November 2020 06:32:00 | Browns Ferry | NRC Region 2 | GE-4 | At 2150 CST on 11/04/2020, it was discovered that Unit 1 High Pressure Coolant Injection System (HPCI) was INOPERABLE; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. During performance of 1-SR-3.5.1.7, HPCI Main and Booster Pump Set Developed Head and Flow Rate Test at Rated Reactor Pressure, Unit 1 HPCI was manually tripped by the control room operator due to local report of excessive shaking of the cooling water supply from the booster pump line. There was no impact to the safety of the public or plant personnel. The NRC Resident Inspector has been notified. CR 1650042 documents this condition in the Corrective Action Program. The Unit is in a 14-day LCO 3.5.1(c). The RCIC System is operable.
ENS Event number 54983, made on 11/05/2020 is being retracted. NRC notification 54983 was made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72 were met when Unit 1 HPCI was manually tripped by the control room operator due to a local report for excessive shaking of the cooling water supply from the booster pump line. A subsequent engineering evaluation concluded on 11/06/2020 there was reasonable assurance of operability with no additional intrusive maintenance performed and that the condition was bounded by a previous evaluation documented in (Condition Report) CR 1347736. As such, the circumstances discussed in the report did not result in any condition that at the time of discovery could have prevented the fulfillment of the safety function of structures of the system that are needed to mitigate the consequences of an accident. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v). TVA's evaluation of this event is documented in the corrective action program. The licensee has notified the NRC Resident Inspector. Notified R2DO (Miller). |
ENS 54977 | 1 November 2020 11:04:00 | Sequoyah | NRC Region 2 | Westinghouse PWR 4-Loop | At 0556 EST on 11/01/2020, Sequoyah received unexpected alarms for seismological recording initiated and (Units) 1/2 Safe Shutdown Earthquake response spectra exceeded. No seismic event was felt on site, the National Earthquake Information Center was contacted to confirm there was no seismic activity, and this was also confirmed on the U.S. Geological Survey website. The alarms were determined to be invalid, and they occurred due to a failure in the seismic monitoring system. This failure results in loss of ability to assess the Emergency Action Level for Initiating Condition HU2 'Seismic event greater than Operating Basis Earthquake (OBE) levels' per procedure EPIP-1. If an actual seismic event occurred, HU2 could not be assessed. However, compensatory measures have been implemented and include assessing OBE criteria based on alternative criteria contained in procedure AOP-N.05 'Earthquake' which provides conservative guidance when seismic instruments are unavailable. This is an eight hour, non-emergency notification for an event resulting in a major loss of Emergency Assessment Capability. This event is reportable in accordance with 10 CFR 50.72(b)(3)(xiii). There is no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 54932 | 5 October 2020 14:25:00 | Browns Ferry | NRC Region 2 | This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On August 6, 2020, at approximately 1749 CDT, Browns Ferry Nuclear Plant (BFN), Unit 2 experienced a loss of Reactor Protection System (RPS) Bus 2A. Primary Containment Isolation System (PCIS) Groups 2, 3, 6, and 8 isolated in response to this event. The PCIS isolations caused the initiation of Standby Gas Treatment (SBGT) trains A, B, and C, and Control Room Emergency Ventilation (CREV) subsystem A. Unit 2 declared RCS leakage detection instrumentation inoperable and entered TS LCO 3.4.5 condition A, B, and D with required action D.1 to enter LCO 3.0.3 immediately. Unit 2 entered TS LCO 3.0.3 with required actions to be in Mode 2 within 10 hours, Mode 3 within 13 hours, and Mode 4 within 37 hours. Upon investigation, it was discovered that an age-related overheating condition resulted in the failure of the 2A RPS Motor Generator (MG) set, causing the feeder beaker from the 2A 480v Remote Motor-Operated Valve distribution board to trip. On August 6, 2020, at approximately 1808 CDT, Operations personnel commenced restoration of Unit 2 to normal after transferring 2A RPS to its alternate power supply. The 2A RPS MG Set drive motor was replaced on August 24, 2020. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel (RV) Low Water Level or Drywell High Pressure. Plant conditions which initiate PCIS Group 3 actuations are RV Low Water Level or Reactor Water Cleanup Area High Temperature. Plant conditions which initiate PCIS Group 6 actuations are RV Low Water Level, High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation. Plant conditions which initiate PCIS Group 8 actuations are Reactor Vessel (RV) Low Water Level or Drywell High Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. All affected safety systems responded as expected. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1628707. The NRC Resident Inspector has been notified of this event. | |
ENS 54931 | 5 October 2020 13:51:00 | Browns Ferry | NRC Region 2 | This 60-day telephone notification is being made under reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of an emergency service water system component that does not normally run and which provides an ultimate heat sink. On August 6, 2020, at approximately 0128 CDT, the A3 Emergency Equipment Cooling Water (EECW) pump received an auto-start signal while performing Post-Maintenance Testing (PMT) on the 3C Core Spray pump. Normally, the involved EECW pump would be started prior to testing to prevent an auto-start; however, in this case the pump was not running prior to the test. When the 3C Core Spray pump breaker was closed while in the test position, an unanticipated actuation of the A3 EECW pump occurred. Work was stopped and the workers reported to the Control Room to evaluate the condition. Based on a review of this event, individuals involved were coached on understanding system response prior to performing work. The A3 EECW pump responded in accordance with the plant design. No other plant equipment was affected during this event. There were no safety consequences or impacts on the health and safety of the public. The event was entered into TVA's corrective action program for evaluation and resolution. Reference corrective action document CR 1628479. The NRC Resident Inspector has been notified of this event. | |
ENS 54918 | 28 September 2020 14:39:00 | Sequoyah | NRC Region 2 | On 9/28/20 at 1143 EDT, a notification to the National Response Center was made after discovery of a visible oil sheen on the waters of the U.S. (Sequoyah's side of the intake forebay skimmer wall at the Essential Raw Cooling Water (ERCW) building). The source was an oil bucket that overflowed with rain at the ERCW pumping station. Efforts are in progress to eliminate all other potential sources of oil at the station that could be released to the environment. Estimate of volume spilled is less than one quart. The following agencies have also been notified: - EPA Region 4 - Tennessee Emergency Management Agency (TEMA) - Tennessee Department of Environment and Conservation (TDEC). Cleanup is in progress. Measures to prevent recurrence are being taken. This is a four-hour notification, non-emergency for a notification of other government agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). The NRC Resident Inspector has been notified. | |
ENS 54870 | 31 August 2020 15:30:00 | Watts Bar | NRC Region 2 | This 60-day telephone notification is being submitted in accordance with paragraphs 10 CFR 50.73(a)(1) and 50.73(a)(2)(iv)(A) to report two invalid Containment Ventilation Isolation (CVI) actuations at Watts Bar Nuclear Plant (WBN) Unit 1. On July 23, 2020, at 0956 Eastern Daylight Time (EDT), the Train A CVI actuated due to an invalid high radiation signal from 1-RM-90-130, Containment Purge Air Exhaust Monitor. Upon investigation, the high radiation signal was caused by a failed power supply. Corrective action included replacing the power supply, 1-RM-90-130 detector, and restoring the system to service. On August 7, 2020, at 2017 EDT, the Train A CVI actuated due to an invalid high radiation signal from 1-RM-90-130, Containment Purge Air Exhaust Monitor. Upon investigation, a small tear was identified in the foil covering the scintillation detector. This defect caused erratic indication and the system actuation. The foil was replaced and the system was restored to service. Prior to and following the invalid high radiation alarms, all radiation monitors except 1-RM-90-130 were stable at their normal values; therefore, the CVI was invalid. Control room operators performed appropriate checks and confirmed that all required automatic actuations occurred as designed. These events were entered into the corrective action program as CR 1625135 and CR 1628904. The NRC Resident Inspector was notified. | |
ENS 54800 | 24 July 2020 09:00:00 | Sequoyah | NRC Region 2 | At 0105 (EDT) on 7/24/20 it was discovered Unit 2 Ice Bed was INOPERABLE. Therefore, since this is a single train system the requirements of 50.72 (b)(3)(v)(C) and (D) have been met. This condition is being reported as an 8-hour non-emergency NRC Notification. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. This condition put the unit in a 48-hour LCO. The old chillers were put into service to bring the temperature of the ICE bed down. At 0833 EDT, the technical specification limit was no longer exceeded and the unit exited the LCO. | |
ENS 54795 | 21 July 2020 08:58:00 | Browns Ferry | NRC Region 2 | The following was received from TVA - Brown's Ferry at 0858, 21 July 20. On July 21, 2020, at 0435 hours Central Daylight Time, Browns Ferry Unit 1 inserted a manual reactor scram due to degrading main condenser vacuum from marine biofouling at the intake structure. Browns Ferry Unit 2 is in Mode 4 and Browns Ferry Unit 3 is at approximately 76% rated thermal power and stable. Primary Containment Isolation Systems received an actuation signal for groups 2, 3, 6, 8 on reactor water level below +2". All Primary Containment Isolation System groups that received an actuation signal performed as designed. Additionally, all other systems functioned as designed. This event is reportable within 4 hours per 10CFR50.72(b)(2)(iv)(B) - Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation. This event also requires an 8 hour report per 10CFR50.72(b )(3)(iv)(A), Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B), (1) Reactor protection system (RPS) including: reactor scram or reactor trip, except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation and (2) General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs). The NRC Resident Inspector has been notified. The plant is stable in Mode 3 and will remain shutdown until marine growth clogging the intake structure abates. | |
ENS 54794 | 20 July 2020 18:11:00 | Browns Ferry | NRC Region 2 | On July 20, 2020, at 1325 hours Central Daylight Time, Brown's Ferry Unit 2 inserted a manual reactor scram due to degrading main condenser vacuum from marine biofouling at the intake structure. Brown's Ferry Unit 1 performed a down power to 43% and Unit 3 down powered to 76%. Conditions are stable on both Unit 1 and 3 following unit down power. Primary Containment Isolations Systems received an actuation signal for groups 2, 3, 6, and 8 on reactor water level below +2". All Primary Containment Isolations System groups that received an actuation signal performed as designed. Additionally, all other systems functioned as designed. This event is reportable within 4 hours per 10CFR50.72(b)(2)(iv)(B) - Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation. This event also requires an 8 hour report per 10CFR 50.72(b)(3)(iv)(A), "Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B), (1) Reactor protection system (RPS) including: reactor scram or reactor trip, except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation and (2) General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs). The NRC Resident Inspector has been notified. All control rods fully inserted and decay heat is being removed via normal feedwater and condenser. | |
ENS 54781 | 15 July 2020 14:58:00 | Watts Bar | NRC Region 2 | At 0835 EDT on July 15, 2020, it was discovered that the main control room (MCR) envelope was inoperable due to a MCR door being found ajar; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). The door was closed, restoring the MCR envelope to operable at 0839 EDT. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. | |
ENS 54753 | 22 June 2020 13:45:00 | Watts Bar | NRC Region 2 | At 1304 EDT on June 22, 2020, Watts Bar Nuclear Plant (WBN) Units 1 and 2 initiated voluntary communication to the State of Tennessee and local officials as part of the Nuclear Energy Institute (NEI) Groundwater Protection Initiative (GPI), after receiving analysis results for one on-site monitoring well that indicated tritium activity above the GPI voluntary communication threshold. WBN identified and corrected the cause. This condition did not exceed any NRC regulations or reporting criteria. This notification is being made solely as a four-hour, non-emergency notification for a Notification of Other Government Agency. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. | |
ENS 54720 | 20 May 2020 12:07:00 | Watts Bar | NRC Region 2 | At 0521 EDT on May 20, 2020, with Unit 2 in Mode 3 at 0 percent power and Unit 1 defueled, an actuation of the Emergency Diesel Generator (EDG) System occurred while transferring the 1B-B 6.9kV Shutdown Board (SDBD) from the maintenance feed to its normal power supply. The reason for the 1B-B 6.9kV SDBD failing to transfer to the normal power supply is under investigation. The EDGs automatically started as designed when a valid actuation signal was received. The event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the EDGs. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |