Semantic search
Entered date | Site | Region | Reactor type | Event description | |
---|---|---|---|---|---|
ENS 56875 | 29 November 2023 17:02:00 | Indian Point | NRC Region 1 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: This notification is being made per 10 CFR 50.72(b)(2)(xi), as a result of notifications made to State and local government agencies for the discovery of an oil sheen in the discharge canal outside Unit 3. The New York State Department of Environmental Conservation and Westchester County Department of Health were notified. No sheen was observed in the river or at the southern end of the discharge canal near the outfall gates. Clean up efforts are underway. The licensee will notify the NRC Project Manager. |
ENS 56856 | 16 November 2023 05:15:00 | Calvert Cliffs | NRC Region 1 | CE | The following information was provided by the licensee via email: At 0227 EST on 11/16/23, Calvert Cliffs Unit 2 experienced an automatic trip from the reactor protection system (RPS) based on reactor trip bus undervoltage (UV). At that time, a loss of U-4000-22 (13 kV to 4 kV transformer) caused a loss of 22, 23, and 24 4 kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV. The loss of 22 and 23 4 kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4 kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser. RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4 hour report ESFAS (engineering safety features actuation system) actuation (2B DG start on UV) is reportable under 10 CFR 50.72(b)(3)(iv)(A) - 8 hour report AFW operation is reportable under 10 CFR 50.73(a)(2)(iv)(A) - 60 day report The NRC Senior Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All rods fully inserted. There was no impact on Unit 1 operations. Unit 2 is stable in mode 3.
ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8 hour report Notified R1DO (Defrancisco). |
ENS 56846 | 10 November 2023 03:14:00 | Susquehanna | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: At 0118 EST, with Unit 1 in Mode 1 at 100 percent power, the reactor was manually scrammed due to degrading main condenser vacuum. The scram was not complex, with all systems responding normally post-scram. The main turbine bypass valves opened automatically to maintain reactor pressure. Operations responded and stabilized the plant. Reactor water level is being maintained via feedwater pumps. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 2 is not impacted. Due to Reactor Protection System actuation while critical, this event is being reported as a four-hour and eight-hour non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). Unit 1 reactor is currently stable in mode 3. An investigation is in progress into the cause of the degrading condenser vacuum. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56841 | 8 November 2023 13:27:00 | Calvert Cliffs | NRC Region 1 | CE | The following information was provided by the licensee via phone and email: At 0645 EST, on November 8, 2023, with Unit 2 in Mode 3 at zero percent power, a manual actuation of the auxiliary feedwater system (AFW) occurred during a planned plant cooldown. The reason for the AFW manual-start was a trip of the 22 steam generator feed pump due to a high casing level. The 23 AFW motor driven pump was manually started in accordance with implementation of AOP-3G, Malfunction of Main Feedwater System to restore steam generator levels. There was no impact to Unit 1. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: No other systems were affected. No other compensatory or mitigation strategies implemented. Plant cooldown was the only significant evolution in progress. No impact to other technical specifications or limiting conditions for operation. All systems functioned as required. The electric plant is being supplied by offsite power with all diesel generators available. No significant increase in plant risk. There was nothing unusual or not understood. |
ENS 56839 | 7 November 2023 18:42:00 | Calvert Cliffs | NRC Region 1 | CE | The following information was provided by the licensee via email: At 1617 on 11/7/2023, Calvert Cliffs Unit 2 experienced an automatic trip from a Reactor Protection System (RPS) based on reactor trip bus under voltage (UV). At that time a loss of U-4000-22 caused a loss of 22, 23, and 24 4kV busses. This resulted in a loss of both motor generator (MG) sets causing the reactor trip bus UV condition. The loss of 22 and 23 4kV non-safety related busses resulted in a loss of main feedwater. Auxiliary feedwater (AFW) was manually initiated and is feeding both steam generators. The 2B diesel generator (DG) started and restored the 24 4kV safety related bus. Heat removal is via the normal turbine bypass valves to the main condenser. RPS actuation is reportable under 10 CFR 50.72(b)(2)(iv)(B) - 4-hour report. ESFAS actuation (2B DG start on UV) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8-hour report. ESFAS actuation (AFW manual initiation) is reportable under 10CFR50.72(b)(3)(iv)(A) - 8-hour report. Site Senior NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: Unit 1 was unaffected. Estimation of duration of shutdown is 24 hours. |
ENS 56838 | 7 November 2023 18:18:00 | Seabrook | NRC Region 1 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: On November 07, 2023 at 1200 EST, it was discovered that all pumps in the Auxiliary Feedwater system were inoperable due to the loss of control power to the 'B' train Emergency Feedwater (EFW) flow control valve which supplies the 'D' steam generator. The redundant 'A' train EFW control valve for the 'D' steam generator remains functional, as well as the capability of the Auxiliary Feedwater system to supply all steam generators. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(v)(B). The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The 'A' and 'B' EFW Flow Control Valves are arranged in a series configuration for each Steam Generator. Failure of any of the 8 EFW Flow Control Valves to meet its Surveillance Requirements will render all EFW Pumps inoperable per tech specs. |
ENS 56822 | 30 October 2023 17:06:00 | FitzPatrick | NRC Region 1 | GE-4 | The following information was provided by the licensee via phone call and email: A non-licensed supervisory employee had a confirmed positive test during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Resident Inspector has been notified. |
ENS 56815 | 25 October 2023 15:09:00 | Pilgrim | NRC Region 1 | GE-3 | The following information was provided by the licensee via phone and email: This is a non-emergency 30-day notification for missing licensed material. This event is reportable in accordance with 10 CFR 20.2201(a)(1)(ii). On September 25, 2023, while performing the required semi-annual source leak check and inventory, radiation protection personnel could not locate seven sealed radioactive sources. Five of the sources exceed the reporting threshold of ten times the activity listed in 10 CFR 20 Appendix C. Of the five sources, four were Ni-63 sources previously utilized in security bomb detection equipment with a current source radioactivity of between 7.1 and 8.7 mCi. The fifth sealed source exceeding the reporting threshold is an Am-241 former lab calibration standard with a source radioactivity of 0.97 microcuries. These sources were last accounted for on July 6, 2022. Pilgrim's accountability process does not require leak checks or physical inventory of sources that are out of service. A search was conducted for the missing sources; however, they could not be located. These sealed sources are classified as Category 5 radioactive sources in accordance with the International Atomic Energy Agency (IAEA) Safety Guide No. RS-G-1.9. Sources that are less than Category 3 (Cat 4 and 5 sources) are very unlikely to cause permanent injury to individuals. Based on the activity of Ni-63 and Am-241 present in the sources, this 30-day phone notification to NRC is provided pursuant to 10CFR20.2201(a)(1)(ii). The required written report pursuant to 10CFR20.2201(b)(1) will be provided to NRC within 30 days. The Resident Inspector has been notified. The licensee will notify State and local authorities. THIS MATERIAL EVENT CONTAINS A 'Less than Cat 3' LEVEL OF RADIOACTIVE MATERIAL Sources that are "Less than IAEA Category 3 sources," are either sources that are very unlikely to cause permanent injury to individuals or contain a very small amount of radioactive material that would not cause any permanent injury. Some of these sources, such as moisture density gauges or thickness gauges that are Category 4, the amount of unshielded radioactive material, if not safely managed or securely protected, could possibly - although it is unlikely - temporarily injure someone who handled it or were otherwise in contact with it, or who were close to it for a period of many weeks. For additional information go to http://www-pub.iaea.org/MTCD/publications/PDF/Pub1227_web.pdf |
ENS 56810 | 22 October 2023 01:43:00 | Nine Mile Point | NRC Region 1 | GE-2 | The following information was provided by the licensee via phone and email: On October 21, 2023, at 2048 EDT, reactor recirculation pump (RRP) 12 tripped. The cause for the trip is under investigation. Following the RRP trip, the average power range monitors (APRMs) flow bias trips were inoperable due to reverse flow through RRP 12. The APRMs were restored to operable on October 21, 2023, at 2058 EDT, when the RRP 12 discharge blocking valve was closed. This 8-hour non-emergency report is being made based upon requirements of 10CFR50.72(b)(3)(v)(A) which states: "Licensee shall notify the NRC of any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (A) Shut down the reactor and maintain it in a safe shutdown condition." The NRC Resident Inspector has been notified. |
ENS 56790 | 12 October 2023 23:31:00 | Ginna | NRC Region 1 | Westinghouse PWR 2-Loop | The following information was provided by the licensee via email: On 10/12/23 at 2127 EDT, with the Unit 1 in Mode 1 at 100% Power, operators identified degrading condenser vacuum and manually tripped the reactor. All control rods inserted as expected. The trip was not complex, and all systems responded normally post-trip. The cause of the degraded condenser vacuum was an unexpected closure of the condenser air ejector regulator. The cause of the air ejector regulator going closed is not fully understood and is being investigated. Following the SCRAM, Operators responded and stabilized the plant. Decay heat is being removed by the Main Steam System through the Atmospheric Relief Valves (ARVs) and Auxiliary Feed Water (AFW) systems. Due to the Reactor Protection System (RPS) actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for a valid specified system actuation. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56753 | 21 September 2023 10:31:00 | Peach Bottom | NRC Region 1 | GE-4 | The following information was provided by the licensee via phone and email: A licensed operator had a confirmed positive test for alcohol during another entity's pre-access fitness-for-duty screening for unescorted access authorization. The individual's unescorted access at Peach Bottom Atomic Power Station has been denied. The NRC Resident Inspector has been notified. |
ENS 56731 | 9 September 2023 15:35:00 | Ginna | NRC Region 1 | Westinghouse PWR 2-Loop | The following information was provided by the licensee via email: On 9/9/23 at 1143 EDT, with the Unit 1 in Mode 1 at 100 percent power, all 4 turbine control valves closed resulting in a reactor protection system (RPS) automatic reactor trip on over temperature differential temperature. All control rods inserted as expected. The trip was not complex and all systems responded normally post-trip. The cause of the control valve closure has not been determined. Following the SCRAM, operators responded and stabilized the plant. Decay heat is being removed by the main steam system through the atmospheric relief valves and auxiliary feed water systems. Due to the RPS actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B) and an eight-hour non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A) for a valid specified system actuation. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56710 | 2 September 2023 09:46:00 | Nine Mile Point | NRC Region 1 | GE-5 | The following information was provided by the licensee via email: On 9/2/2023 at 0632 EDT, a feedwater transient occurred resulting in an reactor protection system (RPS) automatic reactor scram on low level (Level 3, 159.3 inches). Following the scram, reactor water level dropped below Level 2 (108.8 inches) resulting in a Group 2 recirculation sample system isolation, Group 3 traveling in-core probe (TIP) isolation valve isolation, Group 6 and 7 reactor water cleanup isolation, and Group 9 containment purge isolations. All control rods inserted as expected. High pressure core spray and reactor core isolation cooling initiated and injected as expected. ECCS systems have been secured and normal reactor pressure and level control has been established for hot shutdown. Nine Mile Point Unit 2 is stable and in Mode 3. These 4 hour and 8 hour non-emergency reports are being made in accordance with 10 CFR 50.72(b)(2) (iv)(A), 10 CFR 50.72(b)(2)(iv)(B), and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident was informed. There was no impact on Unit 1. |
ENS 56667 | 8 August 2023 17:03:00 | FitzPatrick | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: A licensed (non-active) individual failed to comply with fitness for duty testing policies. The individual's unescorted access was terminated. |
ENS 56652 | 3 August 2023 16:58:00 | Nine Mile Point | NRC Region 1 | GE-2 | The following information was provided by the licensee via email: A licensed employee had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Senior Resident Inspector was notified. |
ENS 56645 | 30 July 2023 18:20:00 | Seabrook | NRC Region 1 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: On July 30, 2023 at 1526 EDT, with unit 1 in mode 1 at 100 percent power, the reactor was manually tripped due to low main turbine electro-hydraulic control oil level. The trip was uncomplicated with all systems responding normally post-trip. Operations stabilized the plant in mode 3. Decay heat removal is being accomplished using the steam dumps in steam pressure mode to the main condenser. Emergency Feedwater actuated due to low-low steam generator level as expected. This event is being reported pursuant to 10 CFR 50.72(b)(2)(iv)(B) and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. |
ENS 56637 | 25 July 2023 16:06:00 | Millstone | NRC Region 1 | CE | The following information was provided by the licensee via email: At 0924 (EDT) on July 25, 2023, it was discovered that both trains of control room air conditioning system were simultaneously inoperable due to an inoperable control room envelope boundary. The boundary was restored at 0925 (EDT) on July 25, 2023. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. There has been no impact to Unit 3 which remains at 100% power.
The licensee determined in a subsequent engineering evaluation of the conditions that existed at the time, that the access hatch being open did not have an adverse impact upon the control room emergency ventilation system and the control room envelopes boundary's ability to perform their safety function including: Radiation dose to the occupants did not exceed the licensing basis, design basis accident calculated value. Protection of control room occupants from hazardous chemicals and smoke. Therefore, this condition is not reportable and NRC Event EN56637 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector. Notified R1DO (Lally) |
ENS 56620 | 12 July 2023 12:49:00 | Millstone | NRC Region 1 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: At 0449 (EDT) on 7/12/2023, Millstone Unit 3 declared the 'B' train of the emergency core cooling system (ECCS) inoperable due to a degraded damper associated with the ventilation support system for the 'B' charging pump. At the time of this event, the 'A' train of service water was already inoperable due to planned maintenance on a breaker that would have prevented an 'A' service water valve powered from this breaker from closing on a safety signal. This configuration resulted in the possibility that the 'A' train of ECCS would not have been available to fulfill its design function under all postulated accident conditions. This event is being reported under 10 CFR 50.72(b)(3)(v)(B), '(any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to: (B) remove residual heat).' Subsequently, the 'A' train of service water was restored to operable at 0548 on 7/12/2023. Repairs and investigation continue on the 'B' train ECCS damper. The NRC resident has been notified. This event did not impact Millstone Unit 2. There was no impact to the public.
The following information was provided by the licensee via email: The condition was reported to the NRC pursuant to 10 CFR 50.72(b)(3)(v)(B), via an 8-hour report as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat. A subsequent engineering review of the conditions that existed at the time determined that, based on area temperature response, any impact on ventilation flows into and out of the `B' charging pump cubicle did not generate an observable change in the temperature trend. Based on this, it is concluded with reasonable assurance that the functional requirement of the support system was maintained and the `B' charging pump would have continued to perform its safety function until the `A' train of service water was restored to operable and as a result safety function was not lost. Therefore, this condition is not reportable and NRC Event Number 56620 is being retracted. The basis for this conclusion has been provided to the NRC Resident Inspector." Notified R1DO (Bicket). |
ENS 56610 | 6 July 2023 16:48:00 | Millstone | NRC Region 1 | CE | The following information was provided by the licensee via email: On July 6, 2023, at 1232 EDT, while operating in Mode 1 at 100 percent power, the supply check valve from the number 2 steam generator to the turbine driven auxiliary feedwater pump was determined during troubleshooting that it is not able to perform its isolation function. This failure would have resulted in the blowdown of both steam generators during a main steam line break in the number 2 steam generator main steam line upstream of the main steam isolation valves until the operators could isolate the faulted steam generator. Previous evaluation has determined that this condition constituted an unanalyzed condition that could impact containment pressure. There was no radioactive release to the environment. The steam line from the steam generator to the turbine driven auxiliary feedwater pump was isolated by use of a motor operated valve in the discharge line of the number 2 steam generator. There was no impact to Unit 3 which remains at 100 percent power. The NRC Senior Resident Inspector was notified. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(ii)(B) as a condition that resulted in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety. |
ENS 56569 | 11 June 2023 09:02:00 | Beaver Valley | NRC Region 1 | Westinghouse PWR 3-Loop | The following information was provided by the licensee via email: At 0130 EDT on June 11, 2023, it was discovered that the Beaver Valley Power Station, Unit No. 2 auxiliary building door A-35-5A, credited for tornado missile protection of the primary component cooling water system, was open and unlatched. Upon discovery, the door was shut and latched. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(B). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56565 | 8 June 2023 09:37:00 | Seabrook | NRC Region 1 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: On 05/06/2023, at 1552 (EDT) with Seabrook Unit 1 in Mode 3 at zero percent power, while performing digital rod position indication system surveillance testing, shutdown bank 'E' stopped withdrawing. In response, the reactor trip breakers were manually opened, initiating a valid actuation of the reactor protection system (RPS). Subsequently, at 2253 while continuing to perform digital rod position indication system surveillance testing, shutdown bank 'C 'stopped inserting. Reactor trip breakers were manually opened, initiating a valid actuation of the RPS. The RPS responded as designed during both events, and both actuations are being reported pursuant to 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. |
ENS 56564 | 8 June 2023 09:37:00 | Seabrook | NRC Region 1 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: On April 12, 2023, with Seabrook Station Unit 1 in Mode 6 at zero percent power, a valid actuation of the 'B' emergency diesel generator (EDG) emergency power sequencer occurred due to a loss of power to the 'B' train emergency bus. The 'B' EDG was removed from service for scheduled maintenance during this time. This event is being reported pursuant to 10 CFR 50.72(b)(3)(iv)(A) for a valid actuation of the 'B' EDG emergency power sequencer. The NRC Resident Inspector has been notified. |
ENS 56560 | 6 June 2023 13:19:00 | Three Mile Island | NRC Region 1 | B&W-L-LP | The following information was provided by the licensee via email: At 0937 EDT on June 6, 2023, it was discovered that a site employee suffered a non-work-related fatality. The individual was found non-responsive outside the Radiological Controlled Area. This is a four-hour, non-emergency notification for which a notification to other government agencies has been made. This event is reportable in accordance with 10 CFR 50.72(b)(2)(xi). The NRC Region I inspector has been notified. |
ENS 56559 | 5 June 2023 21:58:00 | Ginna | NRC Region 1 | Westinghouse PWR 2-Loop | The following information was provided by the licensee via email: At 1823 EDT, the shift manager was notified that one siren, part of the public notification system (siren number 10), spuriously activated for approximately one minute. Monroe County agencies were notified regarding the actuation. The cause of the actuation is being investigated and the ability for the siren to actuate has been removed until the cause is determined. There is no impact to the emergency planning zone. This event is a four-hour, non-emergency report for notification to other government agencies in accordance with 10 CFR 50.72(b)(2)(xi). |
ENS 56556 | 5 June 2023 17:26:00 | Seabrook | NRC Region 1 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: On June 2, 2023, a blind specimen provided to a laboratory did not analyze as expected. The specimen reported a false negative for amphetamines and a false positive for opiates. This event is being reported pursuant to 10 CFR 26.719(c)(2) and 10 CFR 26.719(c)(3). The NRC Resident Inspector has been notified.
Follow-up investigation by an independent Health and Human Services laboratory confirmed that the blind specimen in question was analyzed correctly. The error is thought to have occurred during the preparation of the blind specimen, prior to delivery to the site. The NRC Resident Inspector has been notified." Notified R1DO (Eve) and FFD Group (email) |
ENS 56544 | 30 May 2023 08:34:00 | Millstone | NRC Region 1 | Westinghouse PWR 4-Loop | The following information was provided by the licensee via email: At 0446 EDT on 5/30/2023, with Millstone Power Station Unit 3 operating at approximately 100 percent reactor power, an automatic reactor trip occurred due to a turbine trip caused by electrical protection. The reactor trip was uncomplicated and decay heat is being removed via steam dumps to the condenser. All systems responded as expected to the trip. Auxiliary feedwater actuated automatically as expected following the trip due to low-low levels in the steam generators. There was no risk to the public. There was no impact to Millstone Unit 2. This event is being reported as a four hour report under 10CFR50.72(b)(2)(iv)(B) as a condition that resulted in actuation of the reactor protection system while the reactor was critical, and as an eight hour report under 10CFR50.72(b)(3)(iv)(A) and 10CFR50.72(b)(3)(iv)(B) for actuation of the auxiliary feedwater system. The NRC Resident Inspector has been notified. |
ENS 56532 | 22 May 2023 16:24:00 | Susquehanna | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: A non-licensed contract supervisor had a confirmed positive for alcohol during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Resident Inspector has been notified. |
ENS 56527 | 19 May 2023 12:33:00 | Beaver Valley | NRC Region 1 | Westinghouse PWR 3-Loop | The following information was provided by the licensee via email: At 0852 (EDT) on May 19, 2023, with Unit 2 in Mode 3 at zero percent power, an actuation of the auxiliary feedwater system (AFW) occurred. The reason for the AFW auto-start was a failed start attempt of the 'B' main feedwater pump. The 'A' and 'B' motor driven auxiliary feedwater (MDAFW) pumps automatically started as designed when the 'Loss of Both Main Feedwater Pumps' signal was received. This event is being reported in accordance with 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the AFW system. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56519 | 16 May 2023 08:09:00 | Beaver Valley | NRC Region 1 | Westinghouse PWR 3-Loop | The following information was provided by the licensee via phone: A licensed operator failed a test specified by the FFD testing program. The individual's site access has been terminated. The NRC Resident Inspector has been notified. |
ENS 56513 | 9 May 2023 17:41:00 | Peach Bottom | NRC Region 1 | GE-4 | The following information was provided by the licensee via phone and email: At 1455 (EST) on Tuesday May 9, 2023, Peach Bottom Atomic Power Station (PBAPS) technical support center (TSC) ventilation system lost power. Power loss was caused by a tree down on the 361 transmission line. Power was not able to be restored within an hour. At 1639 (EST), power was restored to TSC ventilation, and capability was restored. This report is being submitted pursuant to 10 CFR 50.72(b)(3)(xiii) as a major loss of emergency preparedness capabilities due to a reduction in the effectiveness of the onsite TSC. NRC Resident has been notified. |
ENS 56503 | 4 May 2023 12:25:00 | Indian Point | NRC Region 1 | Westinghouse PWR 4-Loop | The following summary was provided by the licensee via phone: On May 4, 2023 at 1145 EDT, the licensee found contact dose rates of 215 and 555 millirem-per-hour at 2 separate spots on the top of an exclusive use package during receipt survey. These dose rates are above the 200 millirem-per-hour allowable. No loose surface contamination was identified. The package contains tools from Holtec and was intact on delivery. The package has subsequently been secured in a locked radiation storage building. No overexposure or unauthorized exposure resulted to plant personnel. The licensee suspects shielding, internal to the package, may have shifted and the licensee will investigate further. Dose rates at one foot from the package were recorded at 65 millirem per hour. |
ENS 56502 | 4 May 2023 10:27:00 | Limerick | NRC Region 1 | GE-4 | The following information was provided by the licensee via phone and email: A non-licensed, non-supervisor contractor was found to be in possession of alcohol in the protected area. The individual's site access has been terminated. The NRC Senior Resident Inspector has been notified. |
ENS 56495 | 30 April 2023 02:30:00 | Hope Creek | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: At 0200 EDT on 04/30/23, a Technical Specification required shutdown was initiated at Hope Creek Unit 1. Technical Specification Action 3.6.1.1 Primary Containment Integrity was entered on 04/30/23 at 0100 with a required action to restore primary containment integrity within 1 hour. This required action was not completed within the allowed outage time; therefore, a Technical Specification required shutdown was initiated, and this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(i). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56494 | 30 April 2023 02:30:00 | Hope Creek | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: At 0100 EDT on 04/30/23, it was determined that the primary containment integrity did not meet (Technical Specification) TS 4.6.1.1.d requirement, suppression chamber in compliance with TS 3.6.2.1 due to the inability to establish test conditions for the bypass leakage test in accordance with TS 4.6.2.1.f. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D) & 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. |
ENS 56485 | 22 April 2023 21:35:00 | Beaver Valley | NRC Region 1 | Westinghouse PWR 3-Loop | The following information was provided by the licensee via email: At 1942 EDT on April 22, 2023, during the Beaver Valley Power Station, Unit No. 2 refueling outage, while performing examinations of the 66 reactor vessel head penetrations, it was determined that one penetration could not be dispositioned as acceptable per ASME Code Section XI. The reactor vessel vent line penetration will require repair prior to returning the vessel head to service. The indication was not through-wall as there was no evidence of leakage based on inspections performed on the top of the reactor vessel head. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified |
ENS 56468 | 13 April 2023 22:48:00 | Maine Yankee | NRC Region 1 | CE | The following information was provided by the licensee via phone and email: At 1905 (EDT), a security force member discovered what appeared to be a sewage leak along the gravel roadway northwest of the gatehouse entrance. The affected area was approximately 12' X 15'. The water was slowly bubbling up from the ground about 20' along one of our access roads. Large absorbent spill containment barriers were placed at the scene to minimize the incident. Water usage was stopped within our facility, and sewer pumps isolated. The Maine State Department of Environmental Protection (DEP) was notified of the incident (DEP spill # 23-0004705). The area was inspected at approximately 2130 (EDT), and water discharge was no longer observed. Maine Yankee site management is currently in the process of contacting contractors to resolve the issue. The site is safe and secure. The concrete cask heat removal system is operable, and the temperature monitoring system is functional. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee notified Region 1 personnel. |
ENS 56464 | 11 April 2023 11:05:00 | Limerick | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid specific system actuation of the Emergency Service Water (ESW) System. On 2/16/2023, while performing a calibration planned maintenance (PM) for a jacket water pressure indicator during a D13 diesel generator system outage window, the 'C' ESW pump unexpectedly auto-started. Subsequent investigation identified that the affected jacket water pressure indicator shares a common sensing line with a jacket water pressure switch that provides a back-up to the engine speed switch for the engine running signal. At the time the jacket water pressure indicator calibration PM was being performed, the power circuits for D13 diesel generator instrumentation were energized. Pressurization of the energized jacket water pressure switch during the pressure indicator calibration activity resulted in initiation of a false engine running signal to the `C' ESW pump start logic. This event is considered an invalid system actuation because the 'C' ESW pump started in response to a false signal that the D13 EDG was running when the D13 EDG did not start. The actuation was not initiated in response to actual plant conditions or parameters and was not a manual initiation. The ESW system functioned as expected in response to the actuation. The affected ESW pump was shut down in accordance with plant procedures. There was no impact on the health and safety of the public or plant personnel. The licensee notified the NRC Resident Inspector. |
ENS 56458 | 8 April 2023 00:59:00 | Susquehanna | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: At 2052 EDT on April 7, 2023, during routine system preventative maintenance functional testing, the Unit 1 HPCI turbine stop valve, FV-15612, remained in the intermediate position. This failure resulted in the Unit 1 HPCI system being inoperable. This is being reported as a loss of an entire safety function condition in accordance with 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The Unit 1 HPCI inoperability places Unit 1 in a 14-day Technical Specification (TS) Limiting Condition for Operation (LCO). |
ENS 56452 | 4 April 2023 19:55:00 | Susquehanna | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: At 1915 EDT, Susquehanna Nuclear Control Room was notified of a reportable oil release from a spare transformer outside of its secondary containment of an unknown quantity. Oil staining was observed on the ground outside of the designed containment vault stored on the grounds of Susquehanna Nuclear. The quantity and duration of the oil leak is unknown and thus poses a potential pollution risk to groundwater. Spill response measures are in-progress and as of 1500 on 4/4/2023 a field walkdown reported no visible oil outside of the containment vault. The spill event is reportable under Pennsylvania Department of Environmental Protection (PADEP) Clean Streams Law (PACSL) per PA Code 91.33 and 25 PA code 92a.41. This notification is being written to notify the US Nuclear Regulatory Commission within 4 hours of determination of a required report to another government agency per 10 CFR 50.72(b)(2)(xi). The NRC Resident Inspector has been notified. |
ENS 56435 | 28 March 2023 08:59:00 | Beaver Valley | NRC Region 1 | Westinghouse PWR 3-Loop | A non-licensed supervisor had a confirmed positive for a controlled substance during a random fitness-for-duty test. The employee's access to the plant has been terminated. The NRC Resident Inspector has been notified. |
ENS 56434 | 26 March 2023 19:41:00 | Susquehanna | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: On 03/26/2023 at 1603 EDT, while performing Appendix J local leak rate testing, it was determined that the Secondary Containment Bypass Leakage (SCBL) limit had been exceeded for Unit 2. During performance of the leak rate test, SE-259-027 for X-9B penetration, it was determined that the combined SCBL limit of 15 standard cubic feet per hour for the as-found minimum pathway was exceeded, as specified in Technical Specification, Surveillance Requirement 3.6.1.3.11. This event is being reported pursuant to 10CFR50.72(b)(3)(ii). The Resident Inspector has been notified. |
ENS 56430 | 23 March 2023 20:40:00 | Susquehanna | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: At 1736 EDT on March 23, 2023, during overcurrent testing of the '2B' (Emergency Safeguards System) ESS Bus, the work group was re-installing tested relays and inadvertently caused a '2B' ESS Bus lockout. This resulted in the '2B' ESS Bus deenergizing and a valid start signal provided to the 'B' Emergency Diesel Generator (EDG). The 'B' EDG started and functioned as designed. This is being reported as an unplanned actuation of systems that mitigate the consequences of significant events in accordance with 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident Inspector has been notified. |
ENS 56421 | 18 March 2023 19:07:00 | Nine Mile Point | NRC Region 1 | GE-2 | The following information was provided by the licensee via email: On 3/18/2023 at 1410 EDT, with Nine Mile Point Nuclear Station Unit 1 in a planned refueling outage, the main control room was notified of the results of an automated examination of a dissimilar metal weld on reactor penetration N2E. The results indicate a defect present which cannot be found acceptable under ASME Section XI, IWB-3600. This 8-hour non-emergency report is being made based upon requirements of 10CFR50.72(b)(3)(ii)(A) which states, `The licensee shall notify the NRC ... of the occurrence of ... any event or condition that results in: (A) The condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.' The NRC Senior Resident was informed. A repair plan is being developed. |
ENS 56410 | 14 March 2023 22:50:00 | Yankee Rowe | NRC Region 1 | The following information was provided by the licensee via fax: On March 14, 2023, at 2000 EDT, in accordance with 10 CRFR 50.72(b)(3)(xiii). Yankee Nuclear Power Station Independent Spent Fuel Storage Installation (ISFSI) determined that the impacts of a severe winter storm have resulted in a major loss in off site response capability. Since approximately 0200, very heavy snow has fallen and greater than two feet has accumulated on site. All security related equipment has remained functional, and there have been no impacts to methods of offsite communications or emergency assessment capability. The concrete cask heat removal systems have remained operable in accordance with the NAC International multi-purpose container system (NAC-MPC) technical specifications. From approximately 0550 until 1840, offsite power was lost, and the site was powered by the security diesel generator. Periodically throughout the day, the Security Shift Supervisor was in contact with State and local police to ensure response capability. At the 2000 hours update, the law enforcement agencies reported that there were recent reports of trees and power lines being downed by the weight of the snowfall causing road closures and significantly impacting routes and response times to the site. The site remains fully staffed.
On March 14, 2023, at 2000 EDT, in accordance with 10 CFR 50.72(b)(3)(xiii), Yankee Nuclear Power Station Independent Spent Fuel Storage Installation determined that the impacts of a severe winter storm resulted in a major loss in offsite response capability. Downed trees and power lines in conjunction with up to thirty-six (36) inches of snow prevented vehicle passage on normal response routes. On March 15, 2023, at approximately 1700 EDT, these roadways were passable, and employees and emergency vehicles regained normal access to the site. However, the Town of Rowe, Massachusetts police chief informed the site that the town remained in an emergency status and the roadways may need to be intermittently closed in order for utility workers to restore power lines and continue to clear tree limbs. On March 16, 2023, 1815 EDT, the Town of Rowe, Massachusetts police chief secured from the emergency. Therefore, this update is to inform the NRC that the Yankee Nuclear Power Station Independent Spent Fuel Storage Installation has similarly returned to baseline operations. NRC Region I management has been updated throughout the progression of the storm and recovery. A press release is not anticipated. Notified R1DO (Bickett) | |
ENS 56409 | 14 March 2023 15:52:00 | Susquehanna | NRC Region 1 | GE-4 | The following information was provided by the licensee via email: At 1000 EDT on March 14, 2023, during valve diagnostic testing, the high pressure core injection (HPCI) lube oil cooling water supply isolation valve did not stroke open. This failure resulted in the Unit 2 HPCI system being inoperable. This is being reported as a loss of an entire safety function condition in accordance with 10CFR50.72(b)(3)(v)(D). The licensee notified the NRC Resident Inspector.
The following information was provided by the licensee via email: The purpose of this notification is to retract event notification (EN) 56409 reported on 03/14/2023. On March 09, 2023, Susquehanna Unit 2 entered a routine high pressure core injection (HPCI) maintenance outage. In support of this system outage, Technical Specification (TS) 3.5.1, Condition D was entered for an inoperable HPCI system. On March 14 as reported in EN 56409, the HPCI lube oil cooling water supply isolation valve did not electrically stroke open following engagement of manual clutch lever. Specifically, to support the maintenance evolution, electricians declutched the valve actuator to move it from the motor/electric operational mode to the manual operational mode as part of planned valve diagnostic data collection. In this testing configuration (i.e., manual operational mode), an attempt to electrically stroke the valve was made, resulting in the valve failure to stroke. Prior to this maintenance evolution, the HPCI lube oil cooling water supply isolation valve was found in the expected full-closed position with the motor/electric operational mode enabled, meaning prior to the HPCI maintenance outage, the affected valve was operating as designed and capable of performing all design functions. The described condition was therefore determined to be the result of the maintenance activity. NUREG-1022, Section 3.2.7, states: 'reports are not required when systems are declared inoperable as part of a planned evolution for maintenance or surveillance testing when done in accordance with an approved procedure and the plant's TS (unless a condition is discovered that would have resulted in the system being declared inoperable).' Following completion of investigation and repair, Susquehanna determined that, per NUREG-1022, Section 3.2.7, the event was not reportable. HPCI was declared inoperable as part of a maintenance evolution which was done in accordance with an approved procedure and the TS. The described condition was not a pre-existing condition that would have resulted in the system being declared inoperable prior to the planned maintenance activity. Notified R1DO (Schroeder) |
ENS 56386 | 3 March 2023 09:48:00 | Calvert Cliffs | NRC Region 1 | CE | The following information was provided by the licensee via phone and email: A non-licensed supervisor tested positive in accordance with the FFD (fitness-for-duty) testing program. The individual's authorization for site access has been terminated. The NRC Senior Resident Inspector has been notified. |
ENS 56373 | 19 February 2023 08:56:00 | FitzPatrick | NRC Region 1 | GE-4 | The following information was provided by the licensee via fax or email: At 0105 EST on February 19, 2023, with the James A. FitzPatrick Nuclear Power Plant (JAF) at 100 percent power, a valid high main steam line radiation signal was received. An actuation of a fire protection foam system caused migration of high conductivity water into a low conductivity sump. Organic compounds were introduced into the primary coolant and resulted in a temporary increase in nitrogen-16 which was detected by main steam line radiation monitors and actuated primary containment isolation signals in more than one system. The reactor water recirculation sample system isolated. The signal also went to the normally isolated main steam line drain system and condenser air removal system. The event is reportable in accordance with 10 CFR 50.72(b)(3)(iv)(A). The elevated radiation condition no longer exists. Health and safety of the public was not impacted by this event. The NRC Resident Inspector was notified. |
ENS 56350 | 12 February 2023 14:41:00 | Beaver Valley | NRC Region 1 | Westinghouse PWR 3-Loop | The following information was provided by the licensee via phone call and email: At 0800 on February 12, 2023, it was discovered that both trains of control room emergency ventilation system were simultaneously inoperable due to a safety injection relief valve discharging to a Unit 1 sump. This leakage in conjunction with design basis loss of coolant accident may result in radiological dose exceeding limits to the exclusion area boundary and to the control room, which is common to both Unit 1 and Unit 2. Therefore, this condition is being reported as an eight-hour, nonemergency notification per 10 CFR 50.72(b)(3)(ii)(B) and 10 CFR 50.72(b)(3)(v)(D) as an 'Unanalyzed Condition and a Condition that Could Have Prevented Fulfillment of a Safety Function.' There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
Retraction of EN56350, Control Room Emergency Ventilation System Inoperable: Based on subsequent evaluation, it was determined that the control room emergency ventilation system remained operable due to the maximum measured leak rate being within the bounds of the analysis. The maximum measured leak rate of 32,594 cc/hr from the safety injection system did not challenge the calculated maximum engineered safety features leak rate of 45,600 cc/hr and remained within the current dose analysis limits. As such, this was not an unanalyzed condition and did not prevent the fulfillment of a safety function to mitigate the consequences of an accident. The NRC Resident Inspector has been notified. Notified R1DO (Bickett). |
ENS 56347 | 9 February 2023 15:40:00 | Calvert Cliffs | NRC Region 1 | CE | The following information was provided by the licensee via email: This 60-day optional telephone notification is being made in lieu of an LER (Licensee Event Report) submittal as allowed by 10 CFR 50.73(a)(1). This notification is made pursuant to the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) for an invalid actuation of one of the systems listed in 10 CFR 50.73(a)(2)(iv)(B). At approximately 0637 EST on December 25, 2022, the 2B EDG inadvertently started and ran unloaded without a valid undervoltage or safety injection actuation signal. It was determined that this condition was caused by the failure of the emergency start button due to age-related degradation. The button is normally held depressed (closed) by the glass enclosure in standby. To start the EDG using the Emergency Start Button, the button is released (open) when the glass enclosure is broken, which sends a start signal to the EDG. During troubleshooting, the resistance across the button contacts was measured at zero volts DC, indicating the button had failed to an open state causing the EDG to start. The button fell apart when the glass enclosure was removed. The actuation was not initiated in response to actual plant conditions, it was not an intentional manual initiation, and there were no parameters satisfying the requirements for initiation of the emergency diesel generator. The NRC Resident Inspector has been notified. |
ENS 56355 | 6 February 2023 13:26:00 | Calvert Cliffs | NRC Region 1 | CE | The following information was provided by Constellation via email: On 02/06/2023 at 0416 EST, the Constellation Emergency Response Organization (ERO) Notification Database System uploaded data files into the Mass Notification System (Everbridge) which is used to notify ERO personnel when activated. At 0630, the individual reviewing the uploaded files discovered that the data files did not upload properly and that Everbridge may not notify all ERO individuals within the required 10 minutes of system initiation. Constellation resolved the issue by 0752. During the time period of 0416 to 0752, control room operators would have been unaware that the ERO notification was not successful. Therefore, this issue constitutes a loss of offsite communications capability and is reportable under 10 CFR 50.72(b)(3)(xiii), 'The licensee shall notify the NRC as soon as practical and in all cases within eight hours of the occurrence of any event that results in a major loss of emergency assessment capability, offsite response capability, or offsite communications capability (e.g., significant portion of control room indication, Emergency Notification System, or offsite notification system).' This loss of offsite communications capability affected all Constellation nuclear stations. There was no impact on the health and safety of the public or plant personnel. Each affected station NRC Resident Inspectors have been or will be notified. |