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MONTHYEARRS-09-079, Request for Amendment to Technical Specifications Section 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation, to Eliminate Requirements for Main Steam Line Isolation on High Turbine Building Temperature2009-06-15015 June 2009 Request for Amendment to Technical Specifications Section 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation, to Eliminate Requirements for Main Steam Line Isolation on High Turbine Building Temperature Project stage: Request RS-09-077, Request for Processing an Amendment to Technical Specifications Section 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation, to Eliminate Requirements for Main Steam Line Isolation on High Turbine Building..2009-06-20020 June 2009 Request for Processing an Amendment to Technical Specifications Section 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation, to Eliminate Requirements for Main Steam Line Isolation on High Turbine Building.. Project stage: Request ML0917303892009-06-22022 June 2009 Emergency LAR RAI Project stage: Other RS-09-078, Response to Request for Additional Information Related to Technical Specification 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation2009-06-23023 June 2009 Response to Request for Additional Information Related to Technical Specification 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation Project stage: Response to RAI ML0917606182009-07-0202 July 2009 Request for Amendment to Technical Specifications Section 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation, to Eliminate Requirements for Main Steamline Isolation on High Turbine Building Temperature Project stage: Other ML0919005462009-07-10010 July 2009 Individual Notice of Consideration of Issuance of Amendment to Facility Operating License Ltr Project stage: Other ML0920305542009-07-31031 July 2009 RAI Related to Request for Amendment to TSs Section 3.3.6.1 Primary Containment and Drywell Isolation Instrumentation Project stage: RAI RS-09-105, Withdrawal of Request for Amendment to Technical Specifications Section 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation, to Eliminate Requirements for Main Steam Line Isolation on High Turbine Building Temperature2009-08-0404 August 2009 Withdrawal of Request for Amendment to Technical Specifications Section 3.3.6.1, Primary Containment and Drywell Isolation Instrumentation, to Eliminate Requirements for Main Steam Line Isolation on High Turbine Building Temperature Project stage: Withdrawal ML0923306642009-09-0202 September 2009 Withdrawal of License Amendment Request Primary Containment an Drywell Isolation Instrumentation Project stage: Withdrawal 2009-07-10
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Category:Letter type:RS
MONTHYEARRS-23-097, Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans2023-10-12012 October 2023 Constellation Energy Generation, LLC, Advisement of Leadership Changes and Submittal of Updated Standard Practice Procedures Plans RS-23-090, Annual Report of Emergency Core Cooling System Evaluation Model Changes and Errors for Clinton Power Station2023-09-0707 September 2023 Annual Report of Emergency Core Cooling System Evaluation Model Changes and Errors for Clinton Power Station RS-23-080, Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-264-A, Revision 0, 3.3.9 and 3.3.10 - Delete Flux Monitors Specific Overlap Requirement SRs2023-08-30030 August 2023 Constellation Energy Generation, LLC, Application to Revise Technical Specifications to Adopt TSTF-264-A, Revision 0, 3.3.9 and 3.3.10 - Delete Flux Monitors Specific Overlap Requirement SRs RS-23-081, Request for License Amendment to Revise Technical Specifications Related to Reactor Water Cleanup Isolation Instrumentation2023-08-21021 August 2023 Request for License Amendment to Revise Technical Specifications Related to Reactor Water Cleanup Isolation Instrumentation RS-23-085, Supplemental Information Related to Request for Partial Site Release2023-08-0303 August 2023 Supplemental Information Related to Request for Partial Site Release RS-23-077, Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations2023-06-16016 June 2023 Response to NRC Regulatory Issue Summary 2023-01, Preparation and Scheduling of Operator Licensing Examinations RS-23-073, Request for Partial Site Release2023-06-0707 June 2023 Request for Partial Site Release RS-23-042, Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling2023-05-25025 May 2023 Application to Revise Technical Specifications to Adopt TSTF-580, Provide Exception from Entering Mode 4 with No Operable RHR Shutdown Cooling RS-23-049, Constellation Energy Generation, LLC, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2023-03-23023 March 2023 Constellation Energy Generation, LLC, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations RS-23-039, Request for License Amendment to Revise Technical Specifications Section 3.8.3, Diesel Fuel Oil, Lube Oil, and Starting Air2023-03-0101 March 2023 Request for License Amendment to Revise Technical Specifications Section 3.8.3, Diesel Fuel Oil, Lube Oil, and Starting Air RS-23-045, Constellation Energy Generation, LLC Submittal of Fitness for Duty Performance Data Reports for 2022 Per 10 CFR 26.717(c) & 10 CFR 26.2032023-02-28028 February 2023 Constellation Energy Generation, LLC Submittal of Fitness for Duty Performance Data Reports for 2022 Per 10 CFR 26.717(c) & 10 CFR 26.203 RS-23-003, Constellation Energy Generation, LLC, Summary of Changes to Quality Assurance Topical Report, NO-AA-10, and Decommissioning Quality Assurance Program, NO-DC-102023-01-31031 January 2023 Constellation Energy Generation, LLC, Summary of Changes to Quality Assurance Topical Report, NO-AA-10, and Decommissioning Quality Assurance Program, NO-DC-10 RS-23-002, Application to Adopt TSTF-332, ECCS Response Time Testing2023-01-13013 January 2023 Application to Adopt TSTF-332, ECCS Response Time Testing RS-22-126, Constellation Energy Generation, LLC - Request to Use Provisions of a Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI2022-11-30030 November 2022 Constellation Energy Generation, LLC - Request to Use Provisions of a Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI RS-22-121, Notice of Intent to Pursue Subsequent License Renewal Applications2022-11-0909 November 2022 Notice of Intent to Pursue Subsequent License Renewal Applications RS-22-092, Nine and Quad Cities - Application to Revise Primary Containment Isolation Instrumentation Technical Specifications in Accordance with TSTF-306, Revision 2, Add Action to LCO 3.3.6.1 to Give Option to Isolate the Penetration2022-10-0303 October 2022 Nine and Quad Cities - Application to Revise Primary Containment Isolation Instrumentation Technical Specifications in Accordance with TSTF-306, Revision 2, Add Action to LCO 3.3.6.1 to Give Option to Isolate the Penetration RS-22-107, Annual Report of Emergency Core Cooling System Evaluation Model Changes and Errors for Clinton Power Station2022-09-29029 September 2022 Annual Report of Emergency Core Cooling System Evaluation Model Changes and Errors for Clinton Power Station RS-22-093, Advisement of Leadership Changes for Constellation Energy Generation, LLC and Submittal of Updated Standard Practice Procedures Plans2022-08-18018 August 2022 Advisement of Leadership Changes for Constellation Energy Generation, LLC and Submittal of Updated Standard Practice Procedures Plans RS-22-089, Additional Information Supporting Request for License Amendment to Revise the Secondary Containment Design Basis to Credit the Fuel Building Railroad Airlock2022-07-25025 July 2022 Additional Information Supporting Request for License Amendment to Revise the Secondary Containment Design Basis to Credit the Fuel Building Railroad Airlock RS-22-061, Request for License Amendment to Adopt TSTF-269, Revision 2, Allow Administrative Means of Position Verification for Locked or Sealed Valves2022-05-24024 May 2022 Request for License Amendment to Adopt TSTF-269, Revision 2, Allow Administrative Means of Position Verification for Locked or Sealed Valves RS-22-060, Request for License Amendment to Adopt TSTF-230, Revision 1, Add New Condition B to LCO 3.6.2.3, RHR Suppression Pool Cooling2022-05-24024 May 2022 Request for License Amendment to Adopt TSTF-230, Revision 1, Add New Condition B to LCO 3.6.2.3, RHR Suppression Pool Cooling RS-22-068, Constellation Radiological Emergency Plan Addendum Revision2022-05-19019 May 2022 Constellation Radiological Emergency Plan Addendum Revision RS-22-055, Submittal of Preliminary Decommissioning Cost Estimate and Spent Fuel Management Plan2022-04-18018 April 2022 Submittal of Preliminary Decommissioning Cost Estimate and Spent Fuel Management Plan RS-22-051, Constellation Energy Generation, LLC - Update to Correspondence Addressees and Service Lists2022-04-12012 April 2022 Constellation Energy Generation, LLC - Update to Correspondence Addressees and Service Lists RS-22-020, Request for License Amendment to Revise the Secondary Containment Design Basis to Credit the Fuel Building Railroad Airlock2022-04-0707 April 2022 Request for License Amendment to Revise the Secondary Containment Design Basis to Credit the Fuel Building Railroad Airlock RS-22-049, Constellation Energy Generation, LLC, Supplemental Information to Correct Typographical Errors in Constellation'S Application to Revise Technical Specifications to Adopt TSTF-541 Revision 2, Add Exceptions to Surveillance Requirements for2022-04-0404 April 2022 Constellation Energy Generation, LLC, Supplemental Information to Correct Typographical Errors in Constellation'S Application to Revise Technical Specifications to Adopt TSTF-541 Revision 2, Add Exceptions to Surveillance Requirements for V RS-22-045, Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2022-01, Preparation and Scheduling of Operator Licensing Examinations2022-03-25025 March 2022 Constellation Energy Generation, LLC, Response to NRC Regulatory Issue Summary 2022-01, Preparation and Scheduling of Operator Licensing Examinations RS-22-027, Constellation, Response to Request for Additional Information Regarding Application to Revise Technical Specifications to Adopt TSTF-541 Revision 2, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated2022-02-23023 February 2022 Constellation, Response to Request for Additional Information Regarding Application to Revise Technical Specifications to Adopt TSTF-541 Revision 2, Add Exceptions to Surveillance Requirements for Valves and Dampers Locked in the Actuated P RS-22-023, Constellation Energy Generation, LLC, Executed Trust Fund Agreement Amendment and Subordinate Trust Agreement2022-02-23023 February 2022 Constellation Energy Generation, LLC, Executed Trust Fund Agreement Amendment and Subordinate Trust Agreement RS-22-019, Constellation Energy Generation, LLC - Update to Correspondence Addressees and Service Lists2022-02-16016 February 2022 Constellation Energy Generation, LLC - Update to Correspondence Addressees and Service Lists RS-22-015, Notification of Completion of License Transfer and Request to Continue Processing Pending NRC Actions Previously Requested by Exelon Generation Company, LLC2022-02-0101 February 2022 Notification of Completion of License Transfer and Request to Continue Processing Pending NRC Actions Previously Requested by Exelon Generation Company, LLC RS-22-004, Supplement to Application to Adopt TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements2022-01-0404 January 2022 Supplement to Application to Adopt TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements RS-21-121, Proposed Changes to Decommissioning Trust Agreements and Master Terms2021-12-15015 December 2021 Proposed Changes to Decommissioning Trust Agreements and Master Terms RS-21-102, Annual Report of Emergency Core Cooling System Evaluation Model Changes and Errors2021-09-29029 September 2021 Annual Report of Emergency Core Cooling System Evaluation Model Changes and Errors RS-21-091, Implementation of Insider Threat Program Requirements Associated with the Voluntary Security Clearance Program and Advisement of Leadership Changes2021-09-13013 September 2021 Implementation of Insider Threat Program Requirements Associated with the Voluntary Security Clearance Program and Advisement of Leadership Changes RS-21-087, Additional Information Supporting Request for License Amendment to Revise Degraded Voltage Relay Allowable Values2021-08-31031 August 2021 Additional Information Supporting Request for License Amendment to Revise Degraded Voltage Relay Allowable Values RS-21-078, Response to Request for Additional Information for Application to Revise Technical Specification to Adopt TSTF-582, Reactor Pressure Vessel Water Inventory Control (RPV WIC) Enhancements, and TSTF-583-T, TSTF-582 Diesel2021-08-19019 August 2021 Response to Request for Additional Information for Application to Revise Technical Specification to Adopt TSTF-582, Reactor Pressure Vessel Water Inventory Control (RPV WIC) Enhancements, and TSTF-583-T, TSTF-582 Diesel RS-21-076, Application to Adopt TSTF-273, Safety Function Determination Program Clarifications2021-07-30030 July 2021 Application to Adopt TSTF-273, Safety Function Determination Program Clarifications RS-21-070, Proposed Alternative to Utilize Code Case N-8932021-06-30030 June 2021 Proposed Alternative to Utilize Code Case N-893 RS-21-063, Application to Adopt TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements2021-06-30030 June 2021 Application to Adopt TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements RS-21-069, Third Inservice Inspection Interval Relief Request I3R-182021-06-28028 June 2021 Third Inservice Inspection Interval Relief Request I3R-18 RS-21-054, Response to NRC Regulatory Issue Summary 2021-01, Preparation and Scheduling of Operator Licensing Examinations2021-04-29029 April 2021 Response to NRC Regulatory Issue Summary 2021-01, Preparation and Scheduling of Operator Licensing Examinations RS-21-039, Supplemental Information Regarding Application for Order Approving Transfers and Proposed Conforming License Amendments2021-03-25025 March 2021 Supplemental Information Regarding Application for Order Approving Transfers and Proposed Conforming License Amendments RS-21-037, Response to Request for Additional Information Regarding License Amendment Request to Adopt TSTF-505, Revision 22021-03-23023 March 2021 Response to Request for Additional Information Regarding License Amendment Request to Adopt TSTF-505, Revision 2 RS-21-028, Fitness for Duty Performance Data Reports - Annual 20202021-02-26026 February 2021 Fitness for Duty Performance Data Reports - Annual 2020 RS-21-032, Amended Decommissioning Trust Agreements2021-02-25025 February 2021 Amended Decommissioning Trust Agreements RS-21-014, License Amendment Request for One-Time Extension of the Containment Type a Integrated Leakage Rate Test Frequency2021-02-24024 February 2021 License Amendment Request for One-Time Extension of the Containment Type a Integrated Leakage Rate Test Frequency RS-21-030, Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations2021-02-24024 February 2021 Report on Status of Decommissioning Funding for Reactors and Independent Spent Fuel Storage Installations RS-21-005, Request for License Amendment to Revise Degraded Voltage Relay Allowable Values2021-01-20020 January 2021 Request for License Amendment to Revise Degraded Voltage Relay Allowable Values RS-21-001, Revised Proposed Alternative to Utilize Code Cases N-878 and N-880 for Carbon Steel Piping2021-01-0404 January 2021 Revised Proposed Alternative to Utilize Code Cases N-878 and N-880 for Carbon Steel Piping 2023-09-07
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Exelon~)
Exelon Nuclear 4300 Winfield Road www.exeloncorp.com Nuclear Warrenville, IL 60555 10 CFR 50.90 RS-09-077 June 20,2009 U. S. Nuclear Regulatory Commission ATIN: Document Control Desk Washington, D.C. 20555-0001 Clinton Power Station, Unit 1 Facility Operating License No. NPF-62 NRC Docket No. 50-461
Subject:
Request for Processing an Amendment to Technical Specifications Section 3.3.6.1, "Primary Containment and Drywellisolation Instrumentation," to Eliminate Requirements for Main Steam Line Isolation on High Turbine Building Temperature on an Emergency Basis
Reference:
Letter from P. R. Simpson (EGC) to U. S. NRC, "Request for Amendment to Technical Specifications Section 3.3.6.1, "Primary Containment and Drywell Isolation Instrumentation," to Eliminate Requirements for Main Steam Line Isolation on High Turbine Building Temperature, dated June 15, 2009 In the referenced letter, Exelon Generation Company, LLC (EGC), requested a change to the Technical Specifications (TS) of Facility Operating License No. NPF-62 for Clinton Power Station (CPS), Unit 1. The proposed change was requested to eliminate the requirement for main steam line (MSL) isolation on high Turbine Building temperatures from Technical Specifications (TS) Section 3.3.6.1, "Primary Containment and Drywelllsolation Instrumentation," Table 3.3.6.1-1 (l.e., Function 1.f). The proposed change was based on EGC's determination that the MSL Turbine Building Temperature - High isolation function does not meet the 10 CFR 50.36 criteria for inclusion in the CPS TS based on the following:
- The Turbine Building temperature sensors associated with the MSL isolation are used to detect a MSL leak equivalent to 25 gpm. This does not represent a significant degradation of the reactor coolant system pressure boundary.
- As stated in the CPS Updated Safety Analysis Report (USAR) Section 15.6.4, the pressure and temperature transients associated with a MSLB outside containment are insufficient to cause fuel damage.
- During a design basis MSLB outside containment, MSIV closure is assumed to occur due to high MSL flow.
- As stated in the CPS TS Bases, no credit is taken for these instruments in any transient or accident analysis.
Due to the recent increases in seasonal temperatures, Turbine Building temperatures at CPS have approached MSL isolation setpoints for the Turbine Building instruments. Outside air temperature and resulting Turbine Building temperature trends indicate that the trip setpoint may be exceeded in the near future, which would cause a MSL isolation and subsequent
June 20, 2009 U. S. Nuclear Regulatory Commission Page 2 reactor scram. The TS change included in the referenced letter will allow EGC to alleviate the potential for an avoidable plant transient.
Therefore, in accordance with 10 CFR 50.91, "Notice for public comment; State consultation,"
paragraph (a)(5), EGC is requesting that further processing of the license amendment request included in the referenced letter be completed on an emergency basis, since the failure to act in a timely way would result in shutdown of CPS, Unit 1. Approval of the referenced license amendment is requested by June 22, 2009. An explanation of the emergency situation and why it could not be avoided is included in the Attachment to this letter.
There are no regulatory commitments contained within this letter.
Should you have any questions concerning this letter, please contact Mr. Mitchel A. Mathews at (630) 657-2819.
I declare under penalty of perjury that the foregoing is true and correct. Executed on the 20th day of June 2009.
Respectfully, a.
Zl[2:nsen
J/,~c_)
Manager - Licensing Exelon Generation Company, LLC
Attachment:
Basis for Requesting an Emergency License Amendment
ATTACHMENT BASIS FOR REQUESTING AN EMERGENCY LICENSE AMENDMENT Explanation of Emergency Situation 10 CFR 50.91, "Notice for public comment; State consultation," paragraph (a)(5) states that where the NRC finds that an emergency situation exists, in that failure to act in a timely manner would result in derating or shutdown of a nuclear power plant, it may issue a license amendment involving no significant hazards consideration without prior notice and opportunity for a hearing or public comment. The regulation requires that a licensee requesting an emergency amendment explain why the emergency situation occurred and why the licensee could not avoid the situation.
In March 2009, Clinton Power Station (CPS) operators identified elevated temperatures in the Turbine Building. An investigation determined that eight Plant Chilled Water system (WO) area coolers were out of service contributing to the elevated temperatures. Additionally, two small steam leaks on the feedwater system were identified. A deep downpower from 97 percent to 28 percent reactor power was completed in May 2009 to attempt to repair one of the feedwater leaks and restore the WO area coolers that were known to be out of service. Attempts to repair the feedwater leakage were not successful, but through the use of temporary power under the station temporary modification process, five of the eight WO area coolers were restored to service. The remaining three area coolers were determined to have failed motors. These failed air coolers are located near the main steam lines (MSLs) in an approximately 1.5 rem per hour gamma field during full power operations. Repairs would take approximately four hours per fan, resulting in approximately 18 rem of dose for the station.
It has been determined that with a trip of a WO chiller or area coolers, there is very little operating margin between the normal operating temperatures and the Turbine Building main steam line (MSL) isolation setpoints. This condition could be exacerbated by minor steam leaks that are inaccessible during full power operation.
On June 15, 2009, Exelon Generation Company (EGC), LLC submitted a request for amendment to the CPS Technical Specifications (TS) in letter RS-09-079. Specifically, the proposed change was requested to eliminate the requirement for MSL isolation on high Turbine Building temperatures from TS Section 3.3.6.1, "Primary Containment and Drywell Isolation Instrumentation," Table 3.3.6.1-1 (l.e., Function 1.f). The proposed change was based on EGC's determination that the MSL Turbine Building Temperature - High isolation function does not meet the 10 CFR 50.36 criteria for inclusion in the CPS TS as follows:
- The Turbine Building temperature sensors associated with the MSL isolation are used to detect a MSL leak equivalent to 25 gpm. This does not represent a significant degradation of the reactor coolant system pressure boundary.
- As stated in the CPS Updated Safety Analysis Report (USAR) Section 15.6.4, the pressure and temperature transients associated with a MSLB outside containment are insufficient to cause fuel damage.
- During a design basis MSLB outside containment, MSIV closure is assumed to occur due to high MSL flow.
- As stated in the CPS TS Bases, no credit is taken for these instruments in any transient or accident analysis.
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ATTACHMENT BASIS FOR REQUESTING AN EMERGENCY LICENSE AMENDMENT In this amendment request, EGC stated that during operation in the summer months at CPS, the ambient temperatures within the Turbine Building trend up with increased outside air temperatures and approach the MSL isolation on Turbine BUilding temperature setpoints. The most limiting MSL isolation setpoint is 135 0 F in the Turbine Building. All discussions of Turbine Building temperature that follow are related to these instruments. The TS change was proposed in order to allow EGC to eliminate the potential for an avoidable plant transient.
Temperatures in the turbine building, including the turbine building heater bay, vary with the seasons. This results from variations in cooling system temperatures with lake temperatures and heating and cooling of the CPS structures. Generally, from the coldest winter months to the hottest late summer months, a variation of 12 0 F to 15 0 F is seen.
Since June 15, 2009, due to the recent increases in seasonal temperatures, and plant conditions, Turbine Building temperatures at CPS have risen to the point that a MSL isolation may occur due to reduced margins between the in-plant temperatures and the trip setpoints for the instruments. Outside air temperatures have risen, which has resulted in temperatures within the Turbine Building reaching a high of 128 0 F on June 19, 2009. This temperature is approaching levels that had been predicted as the highs for the summer.
Based on current weather forecasts, the outside air temperature at CPS is predicted to be approximately 95 0 F on June 22, 2009, followed by several days in the low 90 0 F range. With high temperatures for extended periods in the weather forecast, it is estimated that turbine building heater bay temperatures will reach or exceed 130 0 F on or about Monday, June 22, 2009, based on structure latent heat and minimal overnight cooling. This predicted temperature trend will result in further challenges to the margins to MSL Turbine Building Temperature - High isolation function setpoints in the very near term.
Historical temperature data has been reviewed to estimate the summer Turbine Building heater bay peak temperature based on current conditions. Based on current trends and historical data, a peak summer temperature of 135 0 F - 137 0 F is projected within the Turbine Building heater bay.
CPS Operations is monitoring and trending Turbine Building temperatures on an increased frequency (i.e., every four hours), to verify the performance of the Turbine Building ventilation and identify any vulnerabilities. Cameras have been installed in the Turbine Building heater bay to monitor the Feedwater leakage for degradation. Additional temporary air movers have been installed in the Turbine Building to reestablish cooling flow, and all ventilation filters have been replaced and are being monitored daily. Cooling loads for the WO system have been evaluated, and CPS has maximized cooling to the Turbine Building Heater Bays. The Turbine Building MSL Isolation instruments have been calibrated and the available margin between the as-left calibration settings and trip setpoints has been utilized.
A reevaluation of projected temperature trends indicates that the CPS MSL isolation trip setpoints will likely be exceeded in the near future, which would cause a MSL isolation and subsequent reactor scram. As discussed above, this emergency situation results from unforeseen adverse environmental conditions due to unseasonably high outside air temperatures in the area along with failure of equipment that is not accessible during full power Page 2 of 3
ATTACHMENT BASIS FOR REQUESTING AN EMERGENCY LICENSE AMENDMENT operation due to elevated dose rates in the Turbine Building heater bays. Under these conditions, EGC could not have reasonably applied for this emergency license amendment in advance of the event or in a more timely manner.
In addition, as demonstrated in EGC's June 15,2009, license amendment request, the proposed change does not involve a significant hazards consideration.
Based on the above, the requirements for an emergency situation as stipulated in 10 CFR 50.91(a)(5) have been met.
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